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  ID Date Author Target Materialdown Target Oven W.O# Source Status Subject
  23   Wednesday, May 25, 2011, 14:42 John WongUO2/CUCx-heatboat#1LP-SISDoneBatch#1: UO2/C mixing & carbonization

Before began the carbonization process, two cameras were setup in the hotlab for monitoring the evaporator and the power supply.  On duty ISAC Ops also helps to monitor on a regular basis and to grab the striptools + cameras (twice/shift) and put this information in the ISAC Logbook with subject header:  "UCx_2011_A 'date time'", for easy search.  


Wed May 25 14:39:31 2011:  UO2/C cast was dried in the fumehood over the weekend.  The cast was pilled off from the coated WD40 glass plate, rolled up and put in a target heating boat (/w TaC coating & sintered).   The boat was wrapped with 3 Ta-heat shields, then installed in the evaporator which is currently being pumped down.

Thu May 26 11:40:06 2011:  Vac @ 1.75e-6 torr, BP @ 0.032T.  TGHT stepped up to 30A/0.092V (panel @ 27A), ; TGHT has been held for over 10 mins, no change in vacuum yet.

Thu May 26 11:46:48 2011: TGHT @ 40A/0.123V (panel @ 37A), Vac 2.3e-6 Torr, BP@0.032T. 

Thu May 26 15:13:19 2011:  TGHT has been at 40A/0.123V for sometime.  Currently, Vac @ 4.39e-5 Torr, BP@ 0.27T.  (See Attachement#1)

Thu May 26 17:28:36 2011:  Auto ramping has begun.  (see attachment#2).  TGHT @ 40.60A, (panel @ 38A), vac @ 3.84 e-5 Torr.  

Wed Jun 1 13:28:58 2011:  TGHT currently at 395A/3.16V, vac @ 4.47e-5 Torr.  Heating sequence changed for the increment from 4.5e-5 Torr to 5.0e-5 Torr. 

Fri Jun 3 09:54:28 2011 :  The organics burnoff and the carbonization process are complete (see Attachment#3 for the striptool).  The cooling process will begin at a rate of 2A/min.  

Tue Jun 14 21:24:41 2011 :  The evaporator was about to be vented by argon on Jun 10 (Fri), but it was found that the argon cylinder was almost empty; a new one was replaced (see Attachment #4: Evaporator_Ar_flow).  After the argon cylinder was replaced,  the evaporator was purged with the gas and the vent valve was connected to the cylinder for venting of the evaporator.  The target oven was removed and stored in the hermetic transfer vessel, then transferred to the glove box.  (See attachment #5: UC2, Note: typo. Should read Ar gas, NOT N2).  The flakes were stored in the jar labelled "Stock# 2011_A", with total weight of 35g. 

Attachment 1: Screen_shot_2011-05-26_at_3.14.00_PM.png
Screen_shot_2011-05-26_at_3.14.00_PM.png
Attachment 2: auto_ramping.png
auto_ramping.png
Attachment 3: UCx_2011_A_carbonization.png
UCx_2011_A_carbonization.png
Attachment 4: Evaporator_Ar_flow.png
Evaporator_Ar_flow.png
Attachment 5: UC2.png
UC2.png
  24   Thursday, June 30, 2011, 12:42 John WongUO2/CUCx-heatboat#1LP-SISDoneBatch#2: UO2/C for carbonization

Before began the carbonization process, two cameras were setup in the hotlab for monitoring the evaporator and the power supply.  On duty ISAC Ops also helps to monitor on a regular basis and to grab the striptools + cameras (twice/shift) and put this information in the ISAC Logbook with subject header:  "UCx_2011_B 'date time'", for easy search.  

P/S camera: http://isaccamera1, user/pw = admin

Evaporator camera: http://isac-cam01, user =admin, pw=yield 


Thu Jun 30 12:24:31 2011

UO2 used = 50.29g 

Green UO2/C = 71.96g, rolled up /w graphite sheet (15cm x 12cm), and put in the target boat, then wrapped with 3 Ta-heat shields.  The target is installed in the evaporator and is being pumped down.

Thu Jun 30 12:45:39 2011: Currently Vac @ 3.75e-5, CG2 @ 0.045T.

Friday, July 01, 2011, 13:28:  Vac @ 2.2-6 Torr.  TGHT set at 10A yesterday.   

Friday, July 01, 2011, 13:42:  TGHT stepped up to 36A (panel 33A), 0.134V.  No change in vacuum,  2.38e-6 Torr, CG @33mT. 

Friday, July 01, 2011, 13:51:  TGHT stepped up to 50A (panel 47A), 0.194V.  Vac @ 5.7e-6 Torr, CG2 @ 33mT.  

Friday, July 01, 2011, 14:09 :  Vac was rising slowly.  TGHT stepped up to 57A and the pressure started to increase faster.  TGHT was brought back down to 30A, and vac is coming down gradually.  (See attachment 1#2: Startup Vac/Current)

Friday, July 01, 2011, 14:16 :  Auto ramping began.  0.1/min, max currently @ 525A. (see attachement #3: Parameter)

Monday, July 04, 2011, 12:33:  TGTH @ 146.20A, Vac @ 4.74e-5 Torr.  (see attachment#4: 3-day trend).  Increase auto ramping rate to 0.5/min. 

Monday, July 04, 2011, 13:01:   TGHT @ 148A, Vac @ 5.20e-5 torr.  Auto rampiing paused until vacuum goes down to 5.0e-5 torr.  (see attachment#4)

Monday, July 04, 2011, 17:34:  TGHT @ 220A, VAC started to come down, indicating the burning off organics was done.  Increased heating rate to 1A/min. 

Friday, July 08, 2011, 21:30:  As per Peter Kunz, "I started the target cooldown sequence for IEVAP:TGHT1 at 20:35. The pressure came down to 4e-6 torr. The ramp down rate is 2A/min. Please check if the target heater current comes down to 0A. Then it can cool off over the weekend."

Monday, July 11, 2011, 12:17:  Evap glove box flashed with Ar gas, set pressure ~100psi.  Chamber also vented with Ar, set pressure  @ ~5psi.


Attachment 1: startup_vac.jpg
startup_vac.jpg
Attachment 2: startup_current.jpg
startup_current.jpg
Attachment 3: parameter.jpg
parameter.jpg
Attachment 4: UCx_2011_b_3days.png
UCx_2011_b_3days.png
Attachment 5: grab.S13888.png
grab.S13888.png
  41   Thursday, September 29, 2011, 10:58 John WongUO2/CUCx-heatboat#2 DoneUCx#3: Batch#1 - UO2/C mixture of carbonization

Thursday, September 29, 2011, 10:54

UO2/C mixture was made on Tuesday Sept 27, casted on a piece of glass and let dried in the fume hood for ~2days. 

Dried UO2/C mass = 61.72g

Target material is wrapped /w graphite sheet and put on a new heatboat coated/sintered /w TaC.

Heat boat is wrapped with 3-Ta heat shields. 

Evaporator chamber is currently being pumped down. 


Friday, September 30, 2011, 10:01

Evaporator has been pumped down over night, IG currently @ 2.92e-6 Torr, BP @ 27mT.

TGHT will be stepped up to 40A and allow the pressure to slowly increase.  


Friday, September 30, 2011, 10:30  

TGHT is holding at 40A/0.139V  (local @ 37A), and pressure is slowly increasing, expect pressure to stabilize at ~4.5e-5 Torr before being auto-heating.

See attachment#1: TGHT_40A. 


Friday, September 30, 2011, 13:39

TGHT has been at 40A for more than 3 hrs.  Pressure went as high as 6.9e-5 Torr and it's now coming down.  (See attachment#2:  TGHT@40A_3hrs)

Auto-heating is initiating.  TGHT rate @ 0.1A/min to reach to max current of 525A.  (see attachment#3: parameter.jpg) 


Sunday, October 09, 2011, 10:44  

Target heater reached to 520A and held for a few hours.  

Evaporator was cooled down last night and TGHT is now at 0A.

(For the overall process, see Attachment#4: UCx#3_batch1.jpg) 

IG1 @ 5.7e-7 Torr.  Chamber will be vented with Ar on Tuesday. 

TGHT is off and water valve is shut.  


 Tuesday, October 11, 2011, 13:10

Evaporator glovebox was purged with Ar prior to venting the chamber with Ar.  

Layers of burnout marks were coated all around the inside of the evaporator (see attachment#5. Evpr_afterprocess.jpg), 

Before cleaning, the evaporator chamber had ~200,000 cpm. 

The heating boat containing UCx was removed from the evaporator and stored in the "orange" case, then transferred to the Ar-glove box.

Weight of UCx flasks:  47.15g (See attachment#6: UCx#3_batch1_mass.jpg)

The evaporator was thoroughly cleaned; the burnout marks were removed, and it will be used for UCx#3:batch#2 - UO2/C process.


 

 

Attachment 1: TGHT_40A.jpg
TGHT_40A.jpg
Attachment 2: TGHT@40A_3hrs.jpg
TGHT@40A_3hrs.jpg
Attachment 3: parameter.jpg
parameter.jpg
Attachment 4: UCx#3_batch1.jpg
UCx#3_batch1.jpg
Attachment 5: Evpr_afterprocess.jpg
Evpr_afterprocess.jpg
Attachment 6: UCx#3_batch1_mass.jpg
UCx#3_batch1_mass.jpg
  42   Thursday, October 06, 2011, 12:22 John WongUO2/CUCx-heatboat#2 DoneUCx#3: Batch#2 - UO2/C mixture of carbonization

 Thursday, October 06, 2011, 12:19

UO2/C mixture was made on Oct 4 and casted on a piece of glass costed with WD40, and let dried in the fume hood for 2days. 

Dried UO2/C mass = 64.95g

The batch is wrapped with a piece of graphite sheet and waiting to be heated in the evaporator.  

Currently, batch#1 is in the evaporator.


 Wednesday, October 12, 2011, 10:52

UO2/C mixture was loaded on a heatboat and wrapped with 3-Ta heat shields. 

Evaporator has been pumped down overnight, IG currently at 1.57e-6 Torr.

TGHT will be stepped up to 40A. 


Wednesday, October 12, 2011, 11:00  

TGHT @ 40A/0.128V, local @ 37A. IG @ 1.7e-6 Torr.  


Wednesday, October 12, 2011, 12:35 

TGHT tripped off @ 40A due to high vacuum (>8E-5 Torr).  See attachment#1

Vacuum has come down to 8.5e-6 Torr. 

Stepped up TGHT to 35A.


Wednesday, October 12, 2011, 15:19  

TGHT was held at 35A for 2.5 hrs.  IG @ 4.5e-5 Torr.

Initiated auto heating @ 0.1A/min, Max current @ 525A. 


 Thursday, October 20, 2011, 16:15

Vacuum suddenly increased to ~ 7.7e-5 Torr when TGHT @ 317A (see attachment#2).  There could be a shift in the material during the thermal reduction,

and caused a sudden spike in vacuum.

Currently, IG @ 5.2e-5 Torr, TGHT @ 316.7A.


TGHT reached to 525A and held for >4hrs before cooling down (see attachment#3)

UCx was removed from the evaporator and transferred to the Ar-glove box.  

The material looks great! 


 

 

 

 

Attachment 1: UCx#3_batch#2_tripped@40A.jpg
UCx#3_batch#2_tripped@40A.jpg
Attachment 2: UCx#3_batch#2_TGHT@317A.JPG
UCx#3_batch#2_TGHT@317A.JPG
Attachment 3: UO2_C_batch#2_Archive_overall_process.JPG
UO2_C_batch#2_Archive_overall_process.JPG
  49   Wednesday, June 06, 2012, 16:58 John WongUO2/CUCx-heatboat#2 DoneUC2 flakes for UCx#4: batch#01-04062012

Wednesday, June 06, 2012, 16:55

The UO2/C green was prepared on June 04, 2012. 

UO2 powder used = 50.26g

C-grv used = 10.14g. 

Dry UO2/C green mass = 61.71g.

The green was rolled and wrapped in a piece of graphite sheet.

The target boat was wrapped with 3 Ta-heat shield and installed in the Evap#1. 

The chamber is currently being pumped down.


 Tuesday, June 12, 2012, 11:42

Currently, IEVAPIG1= 1.83e-6 Torr, IEVAP:CG2= 48 mTorr.

Backing line pressure is slightly high.  Will get Edi to look into this.


 Tuesday, June 12, 2012, 14:38

The backing pump oil was changed (ISAC WP#2012-06-12-1).  IEVAP:CG2 is currently reading 27mTorr and IEVAPIG1 at 1.66e-6 Torr.


 Tuesday, June 12, 2012, 16:06

TGHT was tabbed up to 50A and stayed for 1.5 hrs.  Not much change in the pressure, currently at 1.8e-6 Torr, BP @ 25mTorr.  

Keep stepping up TGHT current...


 Tuesday, June 12, 2012, 16:37

TGHT at 65A.  Pressure is starting to rise.


 Tuesday, June 12, 2012, 16:46

Pressure at  6.8e-6 Torr and going up slowly. 

Initiated TGHT auto-ramping:

Max current = 525A,  rate @ 0.1A/min (see attachment #1)


 Wednesday, June 13, 2012, 13:22

TGHT has almost reached to 80A.  Pressure is limiting at 4.5e-6 Torr. (see attachment#2)


Thursday, June 14, 2012, 17:11

TGHT has reached to 95.40A, local @ 92A & 0.48V.  Pressure is still limiting at 4e-6 Torr.  (see attachment #3)

The TGHT current can not go up above 232A because it's voltage limiting at 1.953V (see attachment#4).  The carbon thermal-reduction process stops and the vacuum is going down to low 10e-6 Torr. 

The voltage can not be increased on EPICS; it has to be adjusted locally.  

Auto-ramping aborted.  

The TGHT current setpoint was lowered down to 228A.


Sunday, June 17, 2012, 12:03  

Asked ISAC Ops (Ed Parton) to help me increase the voltage locally.  The voltage nob was turned 1/4 clockwise, and the current was tapped up from 228 to 231A, and it was responding.  The voltage nob was further turned to 3/4 clockwise. 

Initiated auto-ramping. 

Currently, TGHT setpoint at 234.90A, local 231A/1.95V.  

Vacuum is responding and it's slowly going up (currently at 2.8e-6 Torr) - The carbon thermal reduction process continues... 


Monday, June 18, 2012, 00:20  

TGHT is going up slowly, currently at  285A.  The pressure is limiting as the carbonization process is under way (see attachment 5).


 Monday, June 25, 2012, 16:00

The EPICS control was down on Sunday night. So the auto-ramping was aborted.  

Control group fixed the problem, and the network is back online.

The auto-ramping has been re-initiated. 

TGHT is currently at 314.70A, local at 311/3.04V.  IG at 4.21e-5 Torr, BP at 15mTorr.


 Saturday, June 30, 2012, 23:08

The carbonization process has finished.

TGHT has reached to 520A and maintained at that current for about 5hrs. (see attachment #6).

Initiated auto-cool down.


Tuesday, July 03, 2012, 13:05 

TGHT is now at 0A.  The carbonization process is done.  

It took over 20 days for this process (see attachment #7), due to some control issues & power supply problem. Also the vacuum limit was set to 4.0e-5 Torrr; that might increase the pumping time.  

Next time, try setting the pressure limit to 5.0e-5 Torr.  

The chamber will be vented with Ar, and the UC2 flakes will be transferred to the Ar-glove box.  


 

Attachment 1: autoheating.GIF
autoheating.GIF
Attachment 2: TGHT_80A.GIF
TGHT_80A.GIF
Attachment 3: TGHT_95A.GIF
TGHT_95A.GIF
Attachment 4: vol_limiting.png
vol_limiting.png
Attachment 5: TGHT_285A.png
TGHT_285A.png
Attachment 6: TGHT_520A_max.png
TGHT_520A_max.png
Attachment 7: TGHT_0-520A.png
TGHT_0-520A.png
  50   Monday, June 11, 2012, 10:48 John WongUO2/CUCx-heatboat#2 ProblemsUC2 flakes - batch#01-04062012: broken seal & TGHT power supply

John Wong wrote:

Wednesday, June 06, 2012, 16:55

The UO2/C green was prepared on June 04, 2012. 

UO2 powder used = 50.26g

C-grv used = 10.14g. 

Dry UO2/C green mass = 61.71g.

The green was rolled and wrapped in a piece of graphite sheet.

The target boat was wrapped with 3 Ta-heat shield and installed in the Evap#1. 

The chamber is currently being pumped down.


 

 Monday, June 11, 2012, 10:31

Last week during the pump down of the chamber (vacuum got down to low 10e-5 Torr), the cooling was open in preparation of turning on the target heater.  A vacuum excursion was triggered (pressure went up to 300mTorr), and the system was tripped off.  It was suspected that there was some leaks. 

A leak test was performed - all the water connecters & joints are fine.  The seal for the chamber lid was found leaky (5e-8 atm cc/sec).  The seal was replaced and the vacuum was improved but no perfect.

The chamber has been pumped down over the weekend, pressure currently at 2.3e-6 Torr. 

Coincidentally, the TGHT power supply is broken.  The initial action was to turn on the power supply at 0A when the chamber vacuum had gone down to 10-6 Torr.  But the power supply did not regular and shot up to 1000A and caused a vacuum excursion.  Ray Dube will replaced it. 


 

  51   Tuesday, June 12, 2012, 11:38 John WongUO2/CUCx-heatboat#2 Problems resolvedUC2 flakes - batch#01-04062012: broken seal & TGHT power supply

John Wong wrote:

John Wong wrote:

Wednesday, June 06, 2012, 16:55

The UO2/C green was prepared on June 04, 2012. 

UO2 powder used = 50.26g

C-grv used = 10.14g. 

Dry UO2/C green mass = 61.71g.

The green was rolled and wrapped in a piece of graphite sheet.

The target boat was wrapped with 3 Ta-heat shield and installed in the Evap#1. 

The chamber is currently being pumped down.


 

 Monday, June 11, 2012, 10:31

Last week during the pump down of the chamber (vacuum got down to low 10e-5 Torr), the cooling was open in preparation of turning on the target heater.  A vacuum excursion was triggered (pressure went up to 300mTorr), and the system was tripped off.  It was suspected that there was some leaks. 

A leak test was performed - all the water connecters & joints are fine.  The seal for the chamber lid was found leaky (5e-8 atm cc/sec).  The seal was replaced and the vacuum was improved but no perfect.

The chamber has been pumped down over the weekend, pressure currently at 2.3e-6 Torr. 

Coincidentally, the TGHT power supply is broken.  The initial action was to turn on the power supply at 0A when the chamber vacuum had gone down to 10-6 Torr.  But the power supply did not regular and shot up to 1000A and caused a vacuum excursion.  Ray Dube will replaced it. 


 

 Tuesday, June 12, 2012, 11:37

Ray Dube repaired the TGHT power supply.  It is now operational.


 

  53   Sunday, June 24, 2012, 22:52 John WongUO2/CUCx-heatboat#2 ProblemsUC2 flakes - batch#01-04062012: IOC problems

John Wong wrote:

Wednesday, June 06, 2012, 16:55

The UO2/C green was prepared on June 04, 2012. 

UO2 powder used = 50.26g

C-grv used = 10.14g. 

Dry UO2/C green mass = 61.71g.

The green was rolled and wrapped in a piece of graphite sheet.

The target boat was wrapped with 3 Ta-heat shield and installed in the Evap#1. 

The chamber is currently being pumped down.


 Tuesday, June 12, 2012, 11:42

Currently, IEVAPIG1= 1.83e-6 Torr, IEVAP:CG2= 48 mTorr.

Backing line pressure is slightly high.  Will get Edi to look into this.


 Tuesday, June 12, 2012, 14:38

The backing pump oil was changed (ISAC WP#2012-06-12-1).  IEVAP:CG2 is currently reading 27mTorr and IEVAPIG1 at 1.66e-6 Torr.


 Tuesday, June 12, 2012, 16:06

TGHT was tabbed up to 50A and stayed for 1.5 hrs.  Not much change in the pressure, currently at 1.8e-6 Torr, BP @ 25mTorr.  

Keep stepping up TGHT current...


 Tuesday, June 12, 2012, 16:37

TGHT at 65A.  Pressure is starting to rise.


 Tuesday, June 12, 2012, 16:46

Pressure at  6.8e-6 Torr and going up slowly. 

Initiated TGHT auto-ramping:

Max current = 525A,  rate @ 0.1A/min (see attachment #1)


 Wednesday, June 13, 2012, 13:22

TGHT has almost reached to 80A.  Pressure is limiting at 4.5e-6 Torr. (see attachment#2)


Thursday, June 14, 2012, 17:11

TGHT has reached to 95.40A, local @ 92A & 0.48V.  Pressure is still limiting at 4e-6 Torr.  (see attachment #3)

The TGHT current can not go up above 232A because it's voltage limiting at 1.953V (see attachment#4).  The carbon thermal-reduction process stops and the vacuum is going down to low 10e-6 Torr. 

The voltage can not be increased on EPICS; it has to be adjusted locally.  

Auto-ramping aborted.  

The TGHT current setpoint was lowered down to 228A.


Sunday, June 17, 2012, 12:03  

Asked ISAC Ops (Ed Parton) to help me increase the voltage locally.  The voltage nob was turned 1/4 clockwise, and the current was tapped up from 228 to 231A, and it was responding.  The voltage nob was further turned to 3/4 clockwise. 

Initiated auto-ramping. 

Currently, TGHT setpoint at 234.90A, local 231A/1.95V.  

Vacuum is responding and it's slowly going up (currently at 2.8e-6 Torr) - The carbon thermal reduction process continues... 


Monday, June 18, 2012, 00:20  

TGHT is going up slowly, currently at  285A.  The pressure is limiting as the carbonization process is under way (see attachment 5).


 

Sunday, June 24, 2012, 22:51  

 

The Evaporator IOC has lost communication (see attachment #6).  The TGHT auto ramping was not responding to the vacuum limit and kept ramping up, so the program had to be aborted.  

On the live camera,  it showed that TGHT stopped at 311A/3.02V and the pressure was at 5.05e-5 Torr.  

An email has sent to Controls and hopefully things get resolved on Monday. 


 

 

Attachment 1: IOC_problem.png
IOC_problem.png
  54   Monday, June 25, 2012, 16:00 John WongUO2/CUCx-heatboat#2 Problems resolvedUC2 flakes - batch#01-04062012: Fiber converters failed

John Wong wrote:

John Wong wrote:

Wednesday, June 06, 2012, 16:55

The UO2/C green was prepared on June 04, 2012. 

UO2 powder used = 50.26g

C-grv used = 10.14g. 

Dry UO2/C green mass = 61.71g.

The green was rolled and wrapped in a piece of graphite sheet.

The target boat was wrapped with 3 Ta-heat shield and installed in the Evap#1. 

The chamber is currently being pumped down.


 Tuesday, June 12, 2012, 11:42

Currently, IEVAPIG1= 1.83e-6 Torr, IEVAP:CG2= 48 mTorr.

Backing line pressure is slightly high.  Will get Edi to look into this.


 Tuesday, June 12, 2012, 14:38

The backing pump oil was changed (ISAC WP#2012-06-12-1).  IEVAP:CG2 is currently reading 27mTorr and IEVAPIG1 at 1.66e-6 Torr.


 Tuesday, June 12, 2012, 16:06

TGHT was tabbed up to 50A and stayed for 1.5 hrs.  Not much change in the pressure, currently at 1.8e-6 Torr, BP @ 25mTorr.  

Keep stepping up TGHT current...


 Tuesday, June 12, 2012, 16:37

TGHT at 65A.  Pressure is starting to rise.


 Tuesday, June 12, 2012, 16:46

Pressure at  6.8e-6 Torr and going up slowly. 

Initiated TGHT auto-ramping:

Max current = 525A,  rate @ 0.1A/min (see attachment #1)


 Wednesday, June 13, 2012, 13:22

TGHT has almost reached to 80A.  Pressure is limiting at 4.5e-6 Torr. (see attachment#2)


Thursday, June 14, 2012, 17:11

TGHT has reached to 95.40A, local @ 92A & 0.48V.  Pressure is still limiting at 4e-6 Torr.  (see attachment #3)

The TGHT current can not go up above 232A because it's voltage limiting at 1.953V (see attachment#4).  The carbon thermal-reduction process stops and the vacuum is going down to low 10e-6 Torr. 

The voltage can not be increased on EPICS; it has to be adjusted locally.  

Auto-ramping aborted.  

The TGHT current setpoint was lowered down to 228A.


Sunday, June 17, 2012, 12:03  

Asked ISAC Ops (Ed Parton) to help me increase the voltage locally.  The voltage nob was turned 1/4 clockwise, and the current was tapped up from 228 to 231A, and it was responding.  The voltage nob was further turned to 3/4 clockwise. 

Initiated auto-ramping. 

Currently, TGHT setpoint at 234.90A, local 231A/1.95V.  

Vacuum is responding and it's slowly going up (currently at 2.8e-6 Torr) - The carbon thermal reduction process continues... 


Monday, June 18, 2012, 00:20  

TGHT is going up slowly, currently at  285A.  The pressure is limiting as the carbonization process is under way (see attachment 5).


 

Sunday, June 24, 2012, 22:51  

 

The Evaporator IOC has lost communication (see attachment #6).  The TGHT auto ramping was not responding to the vacuum limit and kept ramping up, so the program had to be aborted.  

On the live camera,  it showed that TGHT stopped at 311A/3.02V and the pressure was at 5.05e-5 Torr.  

An email has sent to Controls and hopefully things get resolved on Monday. 


 

 

 Monday, June 25, 2012, 15:57

The Control Support group investigated the problem and found out that the fiber converters on both ends failed.  They have been replaced with brand new switches with fiber connections.

 The Evap EPICS is back online. 


 

  56   Thursday, July 19, 2012, 17:14 John WongUO2/CTarget boat #2 DoneProcessing UC2 flakes for UCx#5 - (batch#02-13062012)

Thursday, July 19, 2012, 17:09

UO2/C green was prepared on June 13, 2012. 

UO2 powder used = 50.32g (Inventory R-00835A UO2 + bottle = 946.48g left)

Graphite powder used = 10.00g

The green was rolled and wrapped in a piece of graphite sheet.

The target boat was wrapped with 3 Ta-heat shield and installed in the Evap#1. 

The chamber is currently being pumped down.


 Friday, July 20, 2012, 09:50

IG1 currently at 6.2e-6 Torr, BP @ 31mTorr. 

The target will be ramped up to 520A at 0.1A/min. 

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.

TGHT tabbed up to 50A.  Not much of change in the vacuum.

Initiated autoramping..


Friday, July 20, 2012, 10:18  

TGHT tripped up at 51A due to high vacuum.  

Lowered TGHT to 30A and begin auto ramping.  Pressure is holding at 7e-5 Torr. 


 Wednesday, July 25, 2012, 11:57

TGHT has reached to 100A, and the vacuum is starting to come down from the high limit, 5e-5 Torr. (see attachment#1).  

The organic burn-off is almost to complete and the carbonization process will begin soon. 


Tuesday, August 07, 2012, 12:18

The carbonization process is completed.  The target heater reached to 520A (local 515A,5.17V), vacuum at 4.0 e-6 Torr. (see attachment #2)

Cooling down is in process at 2A/min.


 Tuesday, August 07, 2012, 17:44

TGHT has reached to 0A.  IG currently @ 1.3e-6 Torr, BP @ 34mTorr. 

The chamber will be vented with Ar gas tomorrow and the UC2 flakes will be transfer to the Ar-glove box.


 

Attachment 1: TGHT_100A.png
TGHT_100A.png
Attachment 2: UC2_flakes_0-520A.GIF
UC2_flakes_0-520A.GIF
  63   Tuesday, April 02, 2013, 17:46 John WongUO2/CTarget boat #2 DoneProcessing UC2 flakes for UCx#6 (batch#03 - 02042013)

Tuesday, April 02, 2013, 17:25

UO2/C green was prepared on Mar 11, 2013.

UO2 powder used = 50.32g (Inventory R-00835A UO2 + bottle = 896.16

Graphite powder used = 10.00g

The green was rolled and wrapped in a piece of graphite sheet

The target boat was wrapped with 3 -Ta heat shields and installed in the Evap#1.

The chamber is currently being pumped down.

The target will be ramped up to 520A at the rate of 0.1A/min. 

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Wednesday, April 03, 2013, 11:28

IG1 currently at 3.56e-6 Torr, BP at 28mTorr.

Tabbing up TGHT to 50A.

After 20 mins, IG got up to 7.5e-5 torr (tripping at 8e-5 Torr).  Lower TGHT to 20A. 

Initiated autoramping...


 Monday, April 15, 2013, 14:33

The domestic water will be shut off tomorrow, April 16 at 07:00 for ARIEL work.  The evaporator cooling water will be shut off; therefore the process must stop for now.

TGHT is current at 315.5A, IG1 at 5.2e-5 Torr. 

Cooling down at 1A/min.


 Tuesday, April 16, 2013, 16:28

The cooling water is back online.  The carbonization process will continue...

TGHT will be ramped up to 300A at 2A/min.  Then the ramping rate will changed to 0.1A/min to have TGHT reach to 520A.

IG is currently at 1.2e-6 Torr.


 Wednesday, April 17, 2013, 10:53

TGHT continues to ramp at 0.1A/min.


 Sunday, April 21, 2013, 22:11

The synthesis of UC2 is complete. 

Auto cooling is initiated.  Ramping down at 1A/min.

The chamber will be vented with Ar tomorrow.


 

  64   Monday, May 06, 2013, 14:34 John WongUO2/CTarget boat #2 DoneProcessing UC2 flakes (batch#04 - 05032013)

Monday, May 06, 2013, 14:29

UO2/C green was prepared on May 2, 2013 and let dry over the weekend.

UO2 powder used = 50.36g   (Inventory R-00835A UO2 + bottle = 896.30)

Graphite powder used = 10g

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-Ta heat shields and installed in the Evap#1

The chamber is currently being down down.

The target will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Tuesday, May 07, 2013, 11:12

Currently, IG @ 5.6e-6 Torr; BP @ 25mTorr.  Vacuum spikes intermittently...

Stepping up TGHT to 50A.  After about 15 min, vacuum climbed up to 5.5e-5 Torr. 

Lowered TGHT to 25A, and continue heating at that current...


 Tuesday, May 07, 2013, 12:18

Vacuum is coming down to 2.6e-5 Torr.

Auto-heating initiated...


 Friday, May 24, 2013, 14:19

The carbonization process has come the end.

TGHT has reached to 520A for ~14hrs. 

IG1 @ 6.34e-6 Torr, BP @ 25mTorr.

Autocooling is initiated; ramping rate @ 1A/min.

The chamber will be remained under vacuum, and will be vented in Ar next week.


 Monday, May 27, 2013, 14:11

The chamber was vented with Ar. 

UC2 was transfered to the Ar glovebox. 

Evap#1 is off.


 Wednesday, May 29, 2013, 17:14

See attachment#1 for TGHT vs IG1 data retrieval.


 

Attachment 1: UC2_flakes_batch#04-05032013.PNG
UC2_flakes_batch#04-05032013.PNG
  68   Tuesday, June 25, 2013, 14:49 Laura LambertUO2/CTarget boat #2 DoneProcessing UC2 flakes (batch#05 - 18062013)

 Tuesday, June 25, 2013, 14:35

UO2/C green was prepared on June 18, 2013 and let dry over the weekend.

UO2 powder used = 50.25g (Inventory R-00835A UO2 + bottle = 845.94g - before use)

Graphite powder used = 10.0g

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with a 3-Ta heat shields and installed in the Evap#1 on June 24, 2013

The chamber has been pumped down

IG1 currently at 4.6E-06 torr

 

 

Target will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0E-05 torr, backing off at 6.0E-05 torr


 

  69   Tuesday, June 25, 2013, 16:28 John WongUO2/CTarget boat #2 DoneProcessing UC2 flakes (batch#05 - 18062013)

Laura Lambert wrote:

 Tuesday, June 25, 2013, 14:35

UO2/C green was prepared on June 18, 2013 and let dry over the weekend.

UO2 powder used = 50.25g (Inventory R-00835A UO2 + bottle = 845.94g - before use)

Graphite powder used = 10.0g

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with a 3-Ta heat shields and installed in the Evap#1 on June 24, 2013

The chamber has been pumped down

IG1 currently at 4.6E-06 torr

 

 

Target will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0E-05 torr, backing off at 6.0E-05 torr


 

 Tuesday, June 25, 2013, 16:26

TGHT was stepped up to 30A for about 1hr and lowered to 20A before the pressure went up t0 ~ 1.5e-5 Torr.

Auto ramping initiated...


 

  70   Tuesday, July 02, 2013, 11:13 Peter Kunz UO2/CTarget boat #2 DoneProcessing UC2 flakes (batch#05 - 18062013)

 

1. stage - burning off organics complete

2. stage - carbonization began 1-8 am 2013/07/02

Attachment 1: UO2-C-01.png
UO2-C-01.png
  71   Thursday, July 11, 2013, 16:22 John WongUO2/CTarget boat #2 DoneProcessing UC2 flakes (batch#05 - 18062013)

Peter Kunz wrote:

 

1. stage - burning off organics complete

2. stage - carbonization began 1-8 am 2013/07/02

 Thursday, July 11, 2013, 16:11

EPICS was down and wiped out all the strip tools, but Evap stayed on.  Data archivers showed the system was down at around mid-night on July 10 - no data was archived for 12 hours. 

TGHT has stayed at 520A (max) for at least 4 hours since I started the Evap EPICS back.

Vacuum is currently at 7.7e-6 Torr. 

The carbonization process is complete.

Auto-cool down in process - at 1A/min.


 

  72   Monday, July 15, 2013, 09:45 John WongUO2/CTarget boat #2 DoneProcessing UC2 flakes (batch#05 - 18062013)

John Wong wrote:

Peter Kunz wrote:

 

1. stage - burning off organics complete

2. stage - carbonization began 1-8 am 2013/07/02

 Thursday, July 11, 2013, 16:11

EPICS was down and wiped out all the strip tools, but Evap stayed on.  Data archivers showed the system was down at around mid-night on July 10 - no data was archived for 12 hours. 

TGHT has stayed at 520A (max) for at least 4 hours since I started the Evap EPICS back.

Vacuum is currently at 7.7e-6 Torr. 

The carbonization process is complete.

Auto-cool down in process - at 1A/min.


 

 Monday, July 15, 2013, 09:43

The TGHT reached to zero on Friday and the chamber has been left under vacuum over the weekend, currently at 1.3e-6 Torr.

The chamber will be vented in Ar and the UC2 flakes will be transported into the Ar-glove box.

The process is complete


 

  75   Thursday, August 22, 2013, 18:00 John WongUO2/CTarget Boat #2 DoneProcessing UC2 flaskes (batch#06 - 08222013

Thursday, August 22, 2013, 17:31

1st attempt:

UO2/C green was prepared on Aug 14, 2013 (wed).  The slurry was cast on a piece of glass coated with WD40.

The cast was let dry until Aug 26 (Mon) - couldn't peel off from the glass. 

2nd attempt:

So, scrapped off cast, mixed with 30ml H20 in the WC jar, re-milled for 3 hrs, and cast/let dry over night  - SAME SHIT! couldn't peel off!  Don't understand why?!

3rd attempt:

scrapped off, added the additional compositions:

1g PEG400,1g Glycerol, 10g 7% PVA, 2ml n-butanol, 2ml methonal, 20ml DI H2O.

Re-milled for 3 hours, cast and let dry!  Wahlaa... it works! (See attachment#1: pretty uranium pancake!)

However... During this process, some lost of uranium was resulted.  The slurry was more viscous than normal.  Some material was stuck to the WC jar wall and the balls.

Initial UO2 powder used = 50.14g (Inventory R-00835A UO2 + bottle = 795.56 before use)

Graphite powder used = 10g.

1st attempt dried UO2/C + organic  mass = 55.75g

2nd attempt = didn't measure

3rd attempt + additional org mass = 44.5g  (expecting to loss more uranium from the scraping/sticking to jar/balls)

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-Ta layers of heat shield and installed in Evap1 on Aug 22, 2013.

Chamber is currently being pumped down. IG1 @ 2.4e-4 Torr.

Target will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr


 Monday, August 26, 2013, 11:28

Chamber has been pumped down over the weekend.  IG currently @ 5.2e-6 Torr, BP @ 38mTorr.

Stepped up TGHT to 30A/0.151V. 


 Monday, August 26, 2013, 12:28

TGHT has been at 30A for almost 50 min.  Pressure has gone up but stabled at ~ 3.7e-5 Torr.

Initiated auto-ramping...


 Monday, September 09, 2013, 15:35

The carbonization process has come to an end. 

TGHT is at 520A for almost a day; IG currently at 1.3e-5 Torr (coming down), see attachment #2.

Auto cooling initiated at 2A/min.

The chamber will be vented with Ar.


 

Attachment 1: UO2_C_cast.PNG
UO2_C_cast.PNG
Attachment 2: UCx_flakes.PNG
UCx_flakes.PNG
  76   Friday, August 23, 2013, 16:11 John WongUO2/CTarget Boat #2 Problems resolvedProcessing UC2 flaskes (batch#06 - 08222013

John Wong wrote:

Thursday, August 22, 2013, 17:31

1st attempt:

UO2/C green was prepared on Aug 14, 2013 (wed).  The slurry was cast on a piece of glass coated with WD40.

The cast was let dry until Aug 26 (Mon) - couldn't peel off from the glass. 

2nd attempt:

So, scrapped off cast, mixed with 30ml H20 in the WC jar, re-milled for 3 hrs, and cast/let dry over night  - SAME SHIT! couldn't peel off!  Don't understand why?!

3rd attempt:

scrapped off, added the additional compositions:

1g PEG400,1g Glycerol, 10g 7% PVA, 2ml n-butanol, 2ml methonal, 20ml DI H2O.

Re-milled for 3 hours, cast and let dry!  Wahlaa... it works! (See attachment#1: pretty uranium pancake!)

However... During this process, some lost of uranium was resulted.  The slurry was more viscous than normal.  Some material was stuck to the WC jar wall and the balls.

Initial UO2 powder used = 50.14g (Inventory R-00835A UO2 + bottle = 795.56 before use)

Graphite powder used = 10g.

1st attempt dried UO2/C + organic  mass = 55.75g

2nd attempt = didn't measure

3rd attempt + additional org mass = 44.5g  (expecting to loss more uranium from the scraping/sticking to jar/balls)

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-Ta layers of heat shield and installed in Evap1 on Aug 22, 2013.

Chamber is currently being pumped down. IG1 @ 2.4e-4 Torr.

Target will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr


 

 

 Friday, August 23, 2013, 15:08

The chamber wasn't pumping down well; there was a problem with the seal on the lid.

Rick M. replaced it. 

The chamber is currently being pumped down;  it seems OK!


 

  77   Tuesday, September 10, 2013, 12:20 Laura LambertUO2/CTarget Boat #2 DoneProcessing UC2 flaskes (batch#06 - 08222013

John Wong wrote:

John Wong wrote:

Thursday, August 22, 2013, 17:31

1st attempt:

UO2/C green was prepared on Aug 14, 2013 (wed).  The slurry was cast on a piece of glass coated with WD40.

The cast was let dry until Aug 26 (Mon) - couldn't peel off from the glass. 

2nd attempt:

So, scrapped off cast, mixed with 30ml H20 in the WC jar, re-milled for 3 hrs, and cast/let dry over night  - SAME SHIT! couldn't peel off!  Don't understand why?!

3rd attempt:

scrapped off, added the additional compositions:

1g PEG400,1g Glycerol, 10g 7% PVA, 2ml n-butanol, 2ml methonal, 20ml DI H2O.

Re-milled for 3 hours, cast and let dry!  Wahlaa... it works! (See attachment#1: pretty uranium pancake!)

However... During this process, some lost of uranium was resulted.  The slurry was more viscous than normal.  Some material was stuck to the WC jar wall and the balls.

Initial UO2 powder used = 50.14g (Inventory R-00835A UO2 + bottle = 795.56 before use)

Graphite powder used = 10g.

1st attempt dried UO2/C + organic  mass = 55.75g

2nd attempt = didn't measure

3rd attempt + additional org mass = 44.5g  (expecting to loss more uranium from the scraping/sticking to jar/balls)

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-Ta layers of heat shield and installed in Evap1 on Aug 22, 2013.

Chamber is currently being pumped down. IG1 @ 2.4e-4 Torr.

Target will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr


 

 

 Friday, August 23, 2013, 15:08

The chamber wasn't pumping down well; there was a problem with the seal on the lid.

Rick M. replaced it. 

The chamber is currently being pumped down;  it seems OK!


 

 Tuesday, September 10, 2013, 12:13

The TGHT reached zero on Monday and the chamber was left under vacuum overnight at 1.3e-6 Torr.

The chamber was accidentally vented in air until ~25mTorr for ~10min, then it was quickly pumped down again for ~10min before it was vented in Ar.

The chamber was vented in Ar and the UC2 flakes were transported into the Ar-glove box.

The process is complete 


 

  78   Thursday, September 19, 2013, 15:41 Laura LambertUO2/CTarget Boat #2 In progressProcessing UC2 flakes (batch #07 - 09192013)

Thursday, September 19, 2013, 15:35

UO2/C green was prepared on Aug 17, 2013. The slurry was cast on a piece of glass coated with WD40.

The cast was let dry until Aug 19, 2013.

Initial UO2 powder used = 49.97g (Inventory R-00835A UO2 + bottle = 745.42 before use)

Graphite powder used = 10.12g

Green cast dried UO2/C + organic mass = 59.62g

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-Ta layers of heat shield and installed in Evap1 on Sept 19, 2013.

Chamber is currently being pumped down. IG1 @ 9.97e-12T.

Target will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr


 

  79   Friday, September 20, 2013, 13:49 John WongUO2/CTarget Boat #2 DoneProcessing UC2Flk_00

Laura Lambert wrote:

Thursday, September 19, 2013, 15:35

UO2/C green was prepared on Aug 17, 2013. The slurry was cast on a piece of glass coated with WD40.

The cast was let dry until Aug 19, 2013.

Initial UO2 powder used = 49.97g (Inventory R-00835A UO2 + bottle = 745.42 before use)

Graphite powder used = 10.12g

Green cast dried UO2/C + organic mass = 59.62g

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-Ta layers of heat shield and installed in Evap1 on Sept 19, 2013.

Chamber is currently being pumped down. IG1 @ 9.97e-12T.

Target will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr


 

 Friday, September 20, 2013, 13:48

Chamber has been pumped down overnight.  IG at 6.2e-6 Torr, BP @ 32mT.

Stepping up TGHT to 30A.


 Friday, September 20, 2013, 15:12

TGHT auto ramping initiated.  


 Monday, October 07, 2013, 14:09

TGHT has reached to 520A/5.5V.

Vac at 7.7e-6 Torr. 

The carbonization process is complete.

Auto-cooling is initiated at 2A/min, and the chamber will be vented in Ar after the target is cooled.


 Thursday, October 09, 2014, 13:36

*update* RENAME: batch #07 - 09192013 to UC2Flk_00 used for UCx#11


 

  88   Wednesday, February 05, 2014, 14:29 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_01

 Wednesday, February 05, 2014, 14:13

1st attempt:

UO2/C green was prepared on Feb 4, 2014 [tues]. The slurry was cast on a piece of glass coated with WD40.

The cast was let dry until Feb 5, 2014 [wed] - the cast was cracked and too much WD40 was used because there were oil patches [see attached photo: cast1]; however, the cast peeled off the glass very nicely.

2nd attempt:

Due to cracked and oil patches, decided to re-mill and try again.

Scrapped off cast, added the additional compositions:

1g PEG400, 1g Glycerol, 14g 5% PVA, 2mL n-butanol, 2mL methanol, 20mL DI H2O

Re-milled for 3 hours and cast onto glass coated with slightly less WD40.

Before even allowing cast to dry, can see the slurry is far too thick. The slurry would not spread at all.

Will let dry overnight and attempt to scrape off and re-mill with more DI H2O tomorrow.


 Thursday, February 06, 2014, 10:57

Second cast was a lot thicker, but peeled off the glass nicely, will not re-cast. [see attached photo: cast2]

Some material was stuck to the WC jar wall and the balls, same as previously.

Initial UO2 powder used = 50.24g (Inventory R-00855A UO2 + bottle = 695.52g before use)

Graphite powder used = 10.05g

1st attempt = did not measure

2nd attempt dried UO2/C + organic mass = 46.56g (expecting to lose more uranium from re-casting a second time/ sticking to jar + balls)

The green was rolled up and wrapped in a piece of graphite sheet. [see attached photo: target boat]

The Ta-target boat was wrapped with 3-layers of heat shield and installed in EVAP1.

Chamber us currently being pumped down.

Target will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Friday, February 07, 2014, 10:15

Chamber has pumped down overnight. IG1 currently @ 2.4e-6 Torr.

 Stepped up TGHT to 35A/0.187V.


Friday, February 07, 2014, 12:02 

TGHT sat at 35A for 2hrs. Pressure took a while to fully stabilize, currently sitting at 1.9e-5 Torr [see attached photo: pre auto-ramp]

Initiating auto-ramping.


 Monday, February 24, 2014, 13:37

TGHT reached max setpoint of 520A on friday night.

Power = 5.45V

IGP1 = 3.2e-6 Torr.

Carbonization process is complete.

Initiating auto-cooling at 2.0A/min.


 Thursday, October 09, 2014, 13:41

update rename: batch #09 - 02062014 to UC2Flk_01


 

 

 

 

Attachment 1: UO2_cast1.jpg
UO2_cast1.jpg
Attachment 2: UO2_cast2.jpg
UO2_cast2.jpg
Attachment 3: UO2_target_boat.jpg
UO2_target_boat.jpg
Attachment 4: pre_auto-ramp.JPG
pre_auto-ramp.JPG
  92   Monday, March 24, 2014, 17:53 John WongUO2/C TARGET BOATDoneProcessing UC2Flk_02

 Monday, March 24, 2014, 17:50

UO2/C cast was prepared on March 21 and let dry over the weekend.  The cast looks pretty good, and it was rolled up and wrapped in a piece of graphite sheet. 

 

The Ta-target boat was wrapped with 3-layers of heat shield and installed in EVAP1.

Chamber is currently being pumped down.

Target will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Tuesday, March 25, 2014, 15:55

Chamber has been pumped down to 6.8e-6 Torr. BP 47mTorr.

Stepping up TGHT 35A/0.264V.  Vac stabilizing at 6.0e-5 Torr. 


Tuesday, March 25, 2014, 17:43

Auto-ramping initiated.


 Friday, April 11, 2014, 11:49

TGHT reached to max 520A.

Carbonization process is complete (see attachment)

IG at 9.3e-6 Torr.

 Cooling down TGHT at 2A/min

Will vent the chamber with Ar on Monday


 Monday, April 14, 2014, 16:41

UC2 flakes was removed from the chamber and transferred in to the Ar glovebox.

Evap off.


 

Attachment 1: UC2_flakes_batch#09-03242014.PNG
UC2_flakes_batch#09-03242014.PNG
  99   Tuesday, August 26, 2014, 15:27 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_03

 Tuesday, August 26, 2014, 11:54

UO2/C green was prepared Aug 20, 2014. The slurry was cast on a piece of glass coated with WD40 on Aug 21, 2014.

The cast peeled off the glass nicely Aug 22, 2014 and let dry until Aug 25, 2014.

Some materials were stuck on the WC jar wall and balls as always noted.

Initial UO2 powder used = 50.75g (Inventory R-00835A UO2 + bottle = 595.37g before use)

Graphite powder used = 10.78g

Green cast dried UO2/C + organic mass = 62.86g

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat is wrapped with 3-Ta layers of heat shield and installed in Evap1.

Chamber is currently being pumped down.

Target will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr


 Wednesday, August 27, 2014, 11:18

Chamber has pumped down overnight. IG1 = 6.4e-6 Torr

Stepped TGHT up to 35A.


 Wednesday, August 27, 2014, 14:41

Waited 1.5hrs for vacuum to fully stabilize, currently sitting at 2.2e-5 Torr.

Initiating auto-ramp.


 Friday, September 12, 2014, 14:09

TGHT reached max 520A/5.6V last night.

Carbonization process complete (see attachment: carbonization)

IG1 = 7.6e-6 Torr 

Initiating auto-cool at 2A/min

Will vent the chamber with Ar on Monday.


 Monday, September 22, 2014, 14:52

complete, UO2/C in glove box


 Thursday, October 09, 2014, 13:45

update rename: batch #11 - 08262014 to UC2Flk_03

Attachment 1: carbonization.JPG
carbonization.JPG
  100   Tuesday, September 23, 2014, 15:00 Laura LambertUO2/C40282-1TARGET BOATIn progressProcessing UC2Flk_04

 Tuesday, September 23, 2014, 14:54

UO2/C green was prepared Sept 18, 2014. The slurry was cast on a piece of glass coated with WD40 on Sept 19, 2014.

The cast was let dry over the weekend and peeled off the glass nicely Sept 22, 2014.

Some materials were stuck on the WC jar wall and balls as always noted.

Initial UO2 powder used = 50.04g (Inventory R-00835A UO2 + bottle = 544.51g before use)

Graphite powder used = 9.98g

Green cast dried UO2/C + organic mass = 59.35g

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber is currently being pumped down.

Target will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Wednesday, September 24, 2014, 11:27

Chamber pumped down overnight.

IGP1 = 2.3e-6 Torr

Manually stepping TGHT up to 30A


 Wednesday, September 24, 2014, 14:00

Vacuum stable.

IGP1 = 1.3e-5 Torr.

Initiating auto-ramp.


 

  101   Friday, October 10, 2014, 14:00 John WongUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_04

Laura Lambert wrote:

 Tuesday, September 23, 2014, 14:54

UO2/C green was prepared Sept 18, 2014. The slurry was cast on a piece of glass coated with WD40 on Sept 19, 2014.

The cast was let dry over the weekend and peeled off the glass nicely Sept 22, 2014.

Some materials were stuck on the WC jar wall and balls as always noted.

Initial UO2 powder used = 50.04g (Inventory R-00835A UO2 + bottle = 544.51g before use)

Graphite powder used = 9.98g

Green cast dried UO2/C + organic mass = 59.35g

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber is currently being pumped down.

Target will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Wednesday, September 24, 2014, 11:27

Chamber pumped down overnight.

IGP1 = 2.3e-6 Torr

Manually stepping TGHT up to 30A


 Wednesday, September 24, 2014, 14:00

Vacuum stable.

IGP1 = 1.3e-5 Torr.

Initiating auto-ramp.


 

 Friday, October 10, 2014, 13:51

TGHT has reached to 520A for over 20hrs;  Carbonization process is complete (see attachment).

Ramping down at 2A/min. 

As much as I like to come to work, Monday is a holiday.  So, the chamber will be kept under vacuum. 

On Tuesday, the chamber will be vent in Ar. 


Friday, October 17, 2014, 11:47  

Vented and taken out on tuesday.


 

Attachment 1: archiver_TGHT&VAC.PNG
archiver_TGHT&VAC.PNG
  107   Monday, January 26, 2015, 11:28 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_05

 Monday, January 26, 2015, 11:19

UO2/C green was prepared Jan 20, 2015. The slurry was cast on a piece of glass coated with WD40 on Jan 21, 2015.

The cast was let dry over the weekend and peeled off the glass nicely Jan 26, 2014. [see attached picture]

Some materials were stuck on the WC jar wall and balls, consistent with every time.

Initial UO2 powder used = 50.32g (Inventory R-00835A, UO2 + bottle = 494.52g before use)

Graphite powder used = 10.02g

Green cast dried UO2/C + organic mass = 60.33g

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber is currently being pumped down.

Target boat will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Wednesday, January 28, 2015, 11:33

change of plan.

there will be several interruptions over the course of the next month including a planned power outage and water shut off.

therefore UO2/C cannot be carbonized as these interruptions  will trip off the system when UO2/C would be at max temperature.

EVAP1 is now turned off and the flakes will be stored in the fume hood until further notice.


 Thursday, April 09, 2015, 16:03

EVAP1 has been cleaned.

Target boat has been reloaded into evap1 and currently pumping down.

Will initiate ramp up tomorrow.


 Friday, April 10, 2015, 08:05

IGP1 = 1.7e-6 Torr

Tapped up manually to 35A.

Waited ~2hrs, vacuum stable.

IGP1 = 9.7e-6 Torr.

Initiating auto-ramp.


 Monday, April 20, 2015, 11:20

TGHT reahed 520A, 5.78V on the weekend.

The boat has been sitting at max setpoint for 4.5hours.

Carbonization process is complete [See attachment].

IGP1 = 3.4e-6 Torr.

Initiating auto-cool at 2A/min.


 Tuesday, April 21, 2015, 16:20

Vented in Ar and opened up today.

Now in glove box.


 Monday, May 11, 2015, 11:58

UC2 flakes produced = 46.477g

Attachment 1: flk5.jpg
flk5.jpg
Attachment 2: striptool.JPG
striptool.JPG
  111   Monday, May 11, 2015, 11:49 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_06

 Monday, May 11, 2015, 11:45

UO2/C green was prepared May 6, 2015. The slurry was cast on a piece of glass coated with WD40 on May 7, 2015.

The cast peeled off the glass nicely May 8, 2014 and finished drying over the weekend. [see attached picture]

Some materials were stuck on the WC jar wall and balls, consistent with every time.

Initial UO2 powder used = 50.44g (Inventory R-00835A, UO2 + bottle = 444.23g before use)

Graphite powder used = 10.05g

Green cast dried UO2/C + organic mass = 61.23g

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber is currently being pumped down.

Target boat will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Tuesday, May 12, 2015, 08:40

IG1 = 3e-6 Torr

Tapping up manually to 35A...


Tuesday, May 12, 2015, 12:18

Waited ~2.5hrs.

Vacuum stable.

IG1 = 1.3e-5 Torr.

Initiating auto-ramp.


 Monday, May 25, 2015, 09:29

TGHT reached max setpoints on the 22nd.

IGP1 = 2.2e-6 Torr.

TGHT = 520A, 5.28V

Carbonization process is complete [see attachment].

Initiating auto-cool at 2.0A/min.


 Wednesday, May 27, 2015, 08:47

Vented in argon and opened up yesterday afternoon.

Uranium flakes in glove box.


 Wednesday, May 27, 2015, 16:09

UC2 flakes produced = 47.647g


 

Attachment 1: IMG_20150508_143957199_HDR.jpg
IMG_20150508_143957199_HDR.jpg
Attachment 2: striptool.JPG
striptool.JPG
Attachment 3: striptool-zoom.JPG
striptool-zoom.JPG
  116   Thursday, July 30, 2015, 17:19 John WongUO2/C40282-1TARGET BOATIn progressProcessing UC2_flk_07

 Thursday, July 30, 2015, 17:10

The mixture of UO2/C was prepared on July 13, 2015.  See screen shot for more info. 

The material is loaded into a target boat and wrapped with 3 layers of Ta-heat shield. 

 Chamber is currently being pumped down

Target boat will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Friday, July 31, 2015, 14:33

Chamber has been pumped down overnight, currently at 3.3e-6 Torr.

Manually stepping up to 35A.

Set auto ramping TGHT to 200A at 0.1A/min for over the long weekend.  This current should be safe to just burn off the organic binder but not to start the carbonization process. 


Wednesday, August 05, 2015, 11:05 
 
TGHT reached 200A about 5 hours ago.  Organic burn out is complete.  
Begin carbonization:  Increase TGHT to 520A at 0.1A/min rate. 

 

Attachment 1: IMG_20150714_145857963.jpg
IMG_20150714_145857963.jpg
  117   Tuesday, August 11, 2015, 10:23 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2_flk_07

John Wong wrote:

 Thursday, July 30, 2015, 17:10

The mixture of UO2/C was prepared on July 13, 2015.  See screen shot for more info. 

The material is loaded into a target boat and wrapped with 3 layers of Ta-heat shield. 

 Chamber is currently being pumped down

Target boat will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Friday, July 31, 2015, 14:33

Chamber has been pumped down overnight, currently at 3.3e-6 Torr.

Manually stepping up to 35A.

Set auto ramping TGHT to 200A at 0.1A/min for over the long weekend.  This current should be safe to just burn off the organic binder but not to start the carbonization process. 


Wednesday, August 05, 2015, 11:05 
 
TGHT reached 200A about 5 hours ago.  Organic burn out is complete.  
Begin carbonization:  Increase TGHT to 520A at 0.1A/min rate. 

 

 Tuesday, August 11, 2015, 08:38

IGP1 = 6.8e-6 Torr

TGHT = 520A, 5.5V

TGHT sat at max setpoint for ~15hours

Initiating auto-cool at 2.0A/min.


 Wednesday, August 12, 2015, 16:02

Vented in Argon and opened up this afternoon.

Transferred into glove box.


 

  118   Wednesday, August 19, 2015, 11:44 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_08

 Wednesday, August 19, 2015, 11:02

UO2/C green was prepared Aug 11, 2015. The slurry was cast on a piece of glass coated with WD40 on Aug 12, 2015.

The cast peeled off the glass nicely Aug 14, 2014 and finished drying over the weekend. [see attached picture]

Some materials were stuck on the WC jar wall and balls, consistent with every time.

Initial UO2 powder used = 50.34g (Inventory R-00835A, UO2 + bottle = 343.60g before use)

Graphite powder used = 10.14g

Green cast dried UO2/C + organic mass = 61.42g

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber has been pumped down overnight, currently at IG1 = 2.5e-6 Torr.

Manually stepping up to 35A.

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Wednesday, August 19, 2015, 14:05

Waited ~2.5hrs, vacuum stable.

IG1 = 1.2e-5 Torr.

Initiating auto-ramp.


 Monday, August 31, 2015, 09:38

EVAP 1 tripped off saturday 29th, due to a power outage with TGHT = ~450A at time of trip-off.

EVAP1 lost vacuum for ~4.5hrs [see archived photo]

Visual check performed of EVAP1 - OK.

IGP1 = 6.4e-7 Torr.

Re-initiating carbonization process.


 Monday, August 31, 2015, 10:05

Tapped up manually to 30A.

Vacuum stable.

Initiating auto-ramp at 2.0A/min to a final setpoint of 200A.


 Monday, August 31, 2015, 11:33

Increased max setpoint to 250A at 2.0A/min.

According to the archive, step 1 of the carbonization process was complete and vacuum dropped at ~TGHT = 250A

Vacuum still stable IGP1 = 2.7e-6 Torr.

Once 250A achieved, changed auto ramp to 0.2A/min with a final setpoint of 300A over lunch.

Will tap up manually after lunch.


 Monday, August 31, 2015, 13:07

IGP1 = 1.66e-6 Torr.

TGHT = 262A, 2.3V

Turning off auto-ramp, taking over manually...


 Monday, August 31, 2015, 16:15

Tapped up manually to TGHT = 355A, 3.5V

IGP1 = 5.8e-6 Torr.

Re-initiating auto-ramp at 0.1A/min with a final setpoint of 520A


 Wednesday, September 02, 2015, 09:04

IG1 = 7.5e-6 Torr

TGHT = 520A, 5.53V

TGHT remained at max setpoints ~12.5hours.

Carbonization process is complete.

Initiating auto-cool at 2.0A/min.


 Thursday, September 03, 2015, 11:55

UCx vented in Ar, removed from evap1 and currently in glove box this morning.

Will measure quantity obtained this afternoon.


 Thursday, September 03, 2015, 13:27

Attached are a few notable striptool screenshots from the entire carbonization process.

UCxflk_08 = 46.926g


 

Attachment 1: IMG_20150813_151855494.jpg
IMG_20150813_151855494.jpg
Attachment 2: vacuum_trip_off.JPG
vacuum_trip_off.JPG
Attachment 3: carbonization_pre-power_outage_trip-off.JPG
carbonization_pre-power_outage_trip-off.JPG
Attachment 4: entire_carbonization.JPG
entire_carbonization.JPG
Attachment 5: power_outage.JPG
power_outage.JPG
Attachment 6: round2_carbonization.JPG
round2_carbonization.JPG
Attachment 7: max_setpoints_-_round2_carbonization.JPG
max_setpoints_-_round2_carbonization.JPG
Attachment 8: final.jpg
final.jpg
  120   Monday, September 14, 2015, 15:31 John WongUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_09

 Monday, September 14, 2015, 15:28

Green cast dried UO2/C + organic mass = 61.31g

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber is NOT yet being pumped down due to the fume hood job in B2 level that will take place this week.  Once the job is complete the UC2Flk process will begin. 

 Wednesday, September 16, 2015, 17:55

The work in the B2 level is done; the nuclear ventilation for the evaporators is now operational. 

Tried to turn on the backing pump, but failed. 

Submitted an fault #8428 to vacuum group


 Thursday, September 17, 2015, 12:23

Vacuum group responded to the e-fault, and a new pump is installed.

Chamber is currently being pumped down.


 Friday, September 18, 2015, 14:12

Chamber pressure is at 3.0e-6 Torr.

TGHT stepped up to 30A.

Target boat will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Friday, September 18, 2015, 16:05

Pressure stabilized at 3.6e-5 Torr. 

Initiate autoramping


 Monday, September 21, 2015, 11:38

TGHT was found tripped off at 50A on Saturday at about 6am; the backing pump gauge went up to 150mTorr at the same time (see attachment)

Note that a refurbished backing pump was installed before starting this process.  It could be a leak somewhere; will let vacuum group to inspect this. 


 Monday, September 21, 2015, 15:34

Vacuum group took a look at the pump.  It was the bleeding valve that was not properly close while the pump was installed.  So after some period of running, the valve got loosen from the pump's vibration and caused the leak. 

The pump is now back to operational. 

Chamber is being pumped again.  Once the vacuum is good, TGHT will be stepped up to 50A and autoramping will be initiated once it's ready.


 Monday, September 21, 2015, 17:51

TGHT at 50A, IG at 3.6e-6 Torr.

Initiated autoramping.


 Wednesday, September 30, 2015, 10:11

TGHT has reached to 520A/5.36V.  The carbonization process is complete, vacuum at 3.29e-6 Torr, BP at 12mTorr. (see attachment#2)

Initiated auto-cooling at 2A/min.


 

Attachment 1: poor_backing_pump.PNG
poor_backing_pump.PNG
Attachment 2: current_pressure_plot.PNG
current_pressure_plot.PNG
  123   Friday, December 04, 2015, 15:06 Laura LambertUO2/C40282-1TARGET BOATDone1stepUCx project - round1

 Wednesday, December 02, 2015, 14:08

UO2/C was cast onto a graphite sheet in the fume hood and let dry.

Initial UO2 powder used = 25.11g (Inventory R-00835A, UO2 + bottle = 243.44g before use)

Graphite powder used = 5.16g

A 13mm punch was used to punch out discs from an 11mm wide strip.

5 discs were packed into one end of the graphite tube and a single 1cmx2cm strip was placed in the other end.

graphite tube = 4.57g

5 x UO2/C discs = 0.62g

2cm x 1cm strip = 0.21g

the graphite tube is placed inside a target boat.

The Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Pumping down overnight.


Thursday, December 03, 2015, 09:23 

IG1 = 5.7e-6 Torr.

Stepped up manually to 60A.

Waited ~1hr45, vacuum stable.

IG1 = 6.3e-6 Torr.

Initiating auto-ramp.

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Monday, December 07, 2015, 10:45

UO2/C reached 520A yesterday and has remained at max setpoint for 15hrs.

IG1 = 5.2e-6 Torr.

TGHT = 520A, 5.35V

Carbonization process is complete.

Initiating auto-cool at 2.0A/min.


 Wednesday, December 09, 2015, 10:09

Vented in argon and took the materials out yesterday.

Currently sitting in glove box.

All five discs and strip had fallen out of graphite tube and were sitting directly on the target boat.

^not sure if due to removal of heat shields [moving target boat around shook materials out of tube] or if this happened during carbonization process.

materials stuck to graphite foil fairly well, able to handle foils with tweezers and inspect without materials flaking off.

lightly scraped top of discs with spatula - no materials flaked off.

minor cracks are visible on discs.

graphite tube shows no visible changes.


 

 

  124   Thursday, December 10, 2015, 10:59 Laura LambertUO2/C40282-1TARGET BOATDone1stepUCx project - round2

 Thursday, December 10, 2015, 08:54

Filled graphite tube with 34 UO2/C discs cast onto graphite.

34 discs = 4.10g

graphite tube = 4.64g

IG1 = 2.8e-6 Torr.

Stepped up manually to 35A.

Waited ~1hr15, vacuum stable.

IG1 = 5.8e-6 Torr.

Initiating auto-ramp.

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Monday, December 14, 2015, 08:58

IG1 = 3.9e-6 Torr.

TGHT = 520A, 5.7

UO2/C reached 520A yesterday and has remained at max setpoint for ~12hrs.

Carbonization process is complete.

Initiating auto-cool at 2.0A/min.


 Friday, December 18, 2015, 15:37

Vented in argon and removed from evap1

Graphite tube appears golden in colour [ see photo attached]

Materials spilled out of graphite tube, could be partially due to movement of target boat between evaporator and glove box and removal of heat shields.

Black graphite tube in weigh boat behind target is the graphite tube from the first round in evap1, shows a comparison in colour difference between the two rounds.

The difference between round 1 and round2:

-round1 contained 5 single discs packed together and a single 1cm/2cm square on the other end

-round2 contained 34 discs packed together consuming the whole graphite tube

All other parameters ie. max setpoints, were the same.


 

Attachment 1: image.jpeg
image.jpeg
  128   Tuesday, March 08, 2016, 11:19 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_10

 Tuesday, March 08, 2016, 10:01

UO2/C green was prepared March 2, 2016.

This was the first time using the new rack built for holding multiple casts [see photo attached]

The cast peeled off the glass nicely March 3, 2014 and finished drying over the weekend. [see attached picture]

Some materials were stuck on the WC jar wall and balls, consistent with every time.

Initial UO2 powder used = 50.03g (Inventory R-00835A, UO2 + bottle = 218.54g before use)

Graphite powder used = 10.14g

Green cast dried UO2/C + organic mass = 60.08g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber has been pumped down overnight, currently at IG1 = 4.5e-6 Torr.

Manually stepping up to 35A...

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


Tuesday, March 08, 2016, 16:01

Waited ~3hrs, vacuum stable.

IG1 = 1.4e-5 Torr.

Initiating auto-ramp.


 Monday, March 21, 2016, 08:33

IG1 = 1.9e-6 Torr

TGHT = 520A, 5.13V

TGHT remained at max setpoints for ~63.5hrs [over the weekend].

Carbonization process is complete.

Initiating auto-cool at 2.0A/min.


 Thursday, March 24, 2016, 10:19

vented in argon and removed from evap1.

stored in glove box.

total flakes produced: 46.26g


 

Attachment 1: UCxFlk_10.jpg
UCxFlk_10.jpg
Attachment 2: UCxFlk_10(2).jpg
UCxFlk_10(2).jpg
Attachment 3: UCxFlk_10(3).jpg
UCxFlk_10(3).jpg
Attachment 4: UCxFlk_10-first_time_using_new_set_up.jpg
UCxFlk_10-first_time_using_new_set_up.jpg
Attachment 5: UCxFlk_10_carbonization.jpg
UCxFlk_10_carbonization.jpg
  129   Tuesday, April 05, 2016, 11:12 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_11

Tuesday, April 05, 2016, 10:58

UO2/C green was prepared March 31, 2016.

The cast peeled off the glass nicely April 1, 2016 and finished drying over the weekend. [see attached picture]

Some materials were stuck on the WC jar wall and balls, consistent with every time.

Initial UO2 powder used = 50.47g (Inventory R-00835A, UO2 + bottle = 168.33g before use)

Graphite powder used = 10.05g

Green cast dried UO2/C + organic mass = 59.50g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-layers of heat shield and installed in evap1 yesterday.

Chamber has been pumped down overnight, currently at IG1 = 3.7e-6 Torr.

Manually stepping up to 35A...

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


Tuesday, April 05, 2016, 15:04

Waited ~4hrs, vacuum stable.

IG1 = 8.5e-6 Torr.

Initiating auto-ramp.


 Friday, April 15, 2016, 13:50

IG1 = 3.2e-6 Torr

TGHT = 520A, 5.15V

TGHT remained at max setpoints for ~10hrs

Carbonization process is complete.

Initiating auto-cool at 2.0A/min.


 Monday, April 18, 2016, 11:08

vented in argon and removed from evap1.

stored in glove box.

will measure flakes produced tomorrow...


 Tuesday, April 19, 2016, 15:32

UC2 flakes produced = 45.99g


 

Attachment 1: UCxFlk_11.jpg
UCxFlk_11.jpg
  137   Friday, September 23, 2016, 16:09 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_12

Friday, September 23, 2016, 16:01

*Note: materials were scaled back small amount since only 48.5g of UO2 was left in bottle when usually 50g required to make slurry

UO2/C green was prepared September 22, 2016.

The cast peeled off the glass nicely September 23, 2016 and loaded into evap1.

Some materials were stuck on the WC jar wall and balls, consistent with every time.

Initial UO2 powder used = 48.52g (Inventory R-00835A, no more UO2 left in bottle! Empty bottle = 68.33g)

Graphite powder used = 9.78g

Green cast dried UO2/C + organic mass = 59.21g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-layers of heat shield and installed in evap1 today.

Chamber is currently pumping down, will remain under vacuum over weekend and initiate ramping process monday.

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


Monday, September 26, 2016, 13:52

IG1 = 1.56e-6 Torr

Tapped up to 35A

Waited ~1.5hrs, vacuum stable.

IG1 = 1.23e-5 Torr

Initiating auto-ramp


 Friday, October 07, 2016, 13:19

TGHT tripped off oct 5th at 7pm   alarm handlers were not on, so pager never went off

TGHT was at ~450A and vacuum stable when it tripped off

Reason for this is currently unknown

Ion gauge didn't trip off, neither did the water

Auto-ramping at 2.0A/min back up to 400A currently...


 Friday, October 07, 2016, 16:30

TGHT was ramped up to 420A at 2.0A/min today

IG1 = 4.9e-5 Torr

Changed ramping rate to 0.1A/min for the TGHT with a final setpoint of 520A

Alarm handlers on: if anything happens over weekend pager will go off


Tuesday, October 11, 2016, 10:30 

IG1 = 1.2e-6 Torr

TGHT = 520A, 5.35V

TGHT has remained at max setpoint for ~2.5days

Carbonization process is complete.

Initiating auto-cool at 2.0A/min.


 Wednesday, October 12, 2016, 16:23

Vented in Ar and opened up evap1 this morning.

Stored in glove box.

Flakes look good, ~45g produced.


 

  139   Monday, November 07, 2016, 13:34 Laura LambertUO2/C40282-1TARGET BOATIn progressProcessing UC2Flk_13

 Monday, November 07, 2016, 13:29

UO2/C green was prepared Nov 3rd, 2016.

This is the first cast made with the new batch of UO2 [but from the same purchase as the last batch]

The cast peeled off the glass nicely Nov 4th, 2016 and finished drying over the weekend.

Some materials were stuck on the WC jar wall and balls, consistent with every time.

Initial UO2 powder used = 50.16g (Inventory R-01032A, UO2 + bottle = 1078.15g before use)

Graphite powder used = 10.03g

Green cast dried UO2/C + organic mass = 60.91g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-layers of heat shield and installed in evap1 today.

Chamber is currently pumping down, IG1 = 2.4e-5 Torr.

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Tuesday, November 08, 2016, 07:43

IG1 = 2.4e-6 Torr

Tapped up to 35A, 0.50V

Waited ~50min, vacuum stable.

IG1 = 1.3e-5 Torr

Initiating auto-ramp


 

Attachment 1: UCxFlk_13[4].jpg
UCxFlk_13[4].jpg
Attachment 2: UCxFlk_13[1].jpg
UCxFlk_13[1].jpg
  140   Tuesday, November 15, 2016, 10:02 John WongUO2/C40282-1TARGET BOATIn progressProcessing UC2Flk_13

Laura Lambert wrote:

 Monday, November 07, 2016, 13:29

UO2/C green was prepared Nov 3rd, 2016.

This is the first cast made with the new batch of UO2 [but from the same purchase as the last batch]

The cast peeled off the glass nicely Nov 4th, 2016 and finished drying over the weekend.

Some materials were stuck on the WC jar wall and balls, consistent with every time.

Initial UO2 powder used = 50.16g (Inventory R-01032A, UO2 + bottle = 1078.15g before use)

Graphite powder used = 10.03g

Green cast dried UO2/C + organic mass = 61.91g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-layers of heat shield and installed in evap1 today.

Chamber is currently pumping down, IG1 = 2.4e-5 Torr.

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Tuesday, November 08, 2016, 07:43

IG1 = 2.4e-6 Torr

Tapped up to 35A, 0.50V

Waited ~50min, vacuum stable.

IG1 = 1.3e-5 Torr

Initiating auto-ramp


 

 Tuesday, November 15, 2016, 09:59

TGHT reached to 520A/5.12V; however the pressure was still remained high at the limit 5.0e-5 Torr which indicating that the carbonization process isn't complete yet.

Increase TGHT to 520A at a ramping rate of 0.1A/min.


 

  141   Wednesday, November 16, 2016, 16:41 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_13

John Wong wrote:

Laura Lambert wrote:

 Monday, November 07, 2016, 13:29

UO2/C green was prepared Nov 3rd, 2016.

This is the first cast made with the new batch of UO2 [but from the same purchase as the last batch]

The cast peeled off the glass nicely Nov 4th, 2016 and finished drying over the weekend.

Some materials were stuck on the WC jar wall and balls, consistent with every time.

Initial UO2 powder used = 50.16g (Inventory R-01032A, UO2 + bottle = 1078.15g before use)

Graphite powder used = 10.03g

Green cast dried UO2/C + organic mass = 61.91g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-layers of heat shield and installed in evap1 today.

Chamber is currently pumping down, IG1 = 2.4e-5 Torr.

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Tuesday, November 08, 2016, 07:43

IG1 = 2.4e-6 Torr

Tapped up to 35A, 0.50V

Waited ~50min, vacuum stable.

IG1 = 1.3e-5 Torr

Initiating auto-ramp


 

 Tuesday, November 15, 2016, 09:59

TGHT reached to 520A/5.12V; however the pressure was still remained high at the limit 5.0e-5 Torr which indicating that the carbonization process isn't complete yet.

Increase TGHT to 520A at a ramping rate of 0.1A/min.


 

 Wednesday, November 16, 2016, 11:55

*John increased maxTGHT setpoint to 530A not 520A

When the TGHT reached 520A, the vacuum was still at it's limit. Usually the vacuum starts to drop and stabilize slightly before the max setpoint is reached.

In the photo from UCx_flk10 at ~490A, the vacuum started to drop indicating the carbonization process was complete.

In the image posted from the current carbonization process one can see the vacuum was still at its limit when the TGHT reached its max set point of 520A meaning the carbonization process remains incomplete.


 Thursday, November 17, 2016, 07:36

Vacuum still high, carbonization remains incomplete.

Remained at 530A for ~18hrs

TGHT = 530A, 5.24V

IG1 = 3.8e-5 Torr

Increasing max setpoint to 540A.


 Thursday, November 17, 2016, 13:54

Vacuum remains high after ramping up to 540A, IG1 = 4.5e-5 Torr - still not fully carbonized

TGHT = 540A, 5.36V

Increasing max setpoint to 550A


 Thursday, November 17, 2016, 15:29

Vacuum still high

Increasing max setpoint to 580A

See excel to confirm this remains under 4kW

Wouldn't want to go much above 4kW otherwise container will break


 Friday, November 18, 2016, 13:14

Vacuum stable and decreasing - carbonization process complete.

Evap1 has remained at max setpoints for ~6.5hrs

IG1 = 5.6e-6 Torr

TGHT = 580A, 5.69V

Initiating auto-cool at 1.0A/min


 Monday, November 21, 2016, 16:20

Vented in Ar and opened up evap1 today.

Stored in glove box.

UC2 flakes produced = 47.23g


 

Attachment 1: UCxFlk_10_carbonization.jpg
UCxFlk_10_carbonization.jpg
Attachment 2: UCxFlk_13_not_done_carbonization_at_520A-see_vacuum.jpg
UCxFlk_13_not_done_carbonization_at_520A-see_vacuum.jpg
Attachment 3: UCxflk_13.xlsx
  142   Tuesday, November 29, 2016, 16:20 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_14

 Tuesday, November 29, 2016, 16:13

UO2/C green was prepared Nov 23rd, 2016.

The cast peeled off the glass nicely Nov 24th, 2016 and finished drying over the weekend.

Some materials were stuck on the WC jar wall and balls, consistent with every time.

Initial UO2 powder used = 50.61g (Inventory R-01032A, UO2 + bottle = 1028.05g before use)

Graphite powder used = 10.16g

Green cast dried UO2/C + organic mass = 61.94g 

The green was rolled up and wrapped in a piece of graphite sheet.

A new Ta target boat is being used due to the previous one being old and is now very expanded.

The last round of flakes being carbonized [UC2flk_13] showed a slight change in current and power from previous carbonization process', also indicating the target boat should be retired.

The new boat has only been used once in evap1 to sinter some endcaps earlier in the year.

This target boat is slightly different than the old one because both ends are open, no endcaps are attached to the boat.

The Ta-target boat was wrapped with 3-layers of heat shield and installed in evap1 today.

Chamber is currently pumping down...

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


Wednesday, November 30, 2016, 13:09

IG1 = 3.2e-6 Torr

Tapped up to 35A, 0.34V

Waited ~2hrs, vacuum stable.

IG1 = 8.7e-6 Torr

Initiating auto-ramp


 Monday, December 12, 2016, 09:15

Vacuum stable - carbonization process complete.

Evap1 remained at max setpoints over wknd

IG1 = 1.47e-6 Torr

TGHT = 520A, 5.12V

Initiating auto-cool at 1.0A/min


 Tuesday, December 13, 2016, 16:30

Vented in Ar and opened up evap1 today.

As previously mentioned this new target boat has no endcaps and one can see in the photo more materials have dispersed onto the sides of evap1

These materials appear to be mostly graphite since there are no visible holes through the graphite wrapping that surrounds the UC2 flakes.

Stored in glove box.


 

Attachment 1: UCxFlk_14[1].jpg
UCxFlk_14[1].jpg
Attachment 2: UC2flk_14_carbonized_in_new_boat.jpg
UC2flk_14_carbonized_in_new_boat.jpg
  145   Friday, March 03, 2017, 15:51 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_15

 Friday, March 03, 2017, 08:53

UO2/C green was prepared Feb 28th, 2017.

The cast peeled off the glass nicely March 2nd, 2017 and loaded into evap1.

Some materials were stuck on the WC jar wall and balls, consistent with every time.

Initial UO2 powder used = 50.08g (Inventory R-01032A, UO2 + bottle = 977.24g before use)

Graphite powder used = 10.05g

Green cast dried UO2/C + organic mass = 63.21g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-layers of heat shield and installed in evap1 today.

Chamber pumped down overnight.

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.

IG1 = 3.2e-6 Torr

Tapped up to 35A, 0.40V

Waited ~5hrs, vacuum stable.

IG1 = 6.8e-6 Torr

Initiating auto-ramp


 Monday, March 06, 2017, 08:47

Evap1 tripped off fri night.

See attached screenshot of strip tool.

Had continued to ramp up and was at ~340A, but since the power supply had tripped off this was not actually being applied.

TGHT set back to zero, auto-ramp turned off.

Will investigate further before re-starting...


 Tuesday, March 07, 2017, 09:50

Have not figured out reasoning behind power trip.

According to controls, there were no power bumps at that time.

Water was still on - had not tripped off.

Tapped back up manually to 40A yesterday morning.

Remained at 40A overnight.

IG1 = 4.46e-6 Torr this morning.

TGHT = 40A, 0.38V

Re-initiated auto-ramp.


 Monday, March 13, 2017, 15:46 by AM

IG1 = 5.2E-5 Torr

TGHT= 436A 4.28V


Thursday, March 16, 2017, 08:37 by AM

TGHT reached 520A @ 5.37V this morning. Vacuum  at 6.2E-6 Torr


Friday, March 17, 2017, 08:21 by AM

520A @ 5.37V this morning. Vacuum  at 2.2E-6 Torr

Ramping down


 Thursday, April 20, 2017, 11:44
 
John removed this while I was away - forgot to mark as done

 

Attachment 1: evap1_tripped_off_UCxFlk_15.jpg
evap1_tripped_off_UCxFlk_15.jpg
  147   Tuesday, May 23, 2017, 15:51 Laura LambertUO2/C40282-1TARGET BOATIn progressprocessing UC2Flk_16 - 1ST TEST CHANGING VACUUM LIMITS

 Tuesday, May 23, 2017, 14:42

UO2/C green was prepared May 16th, 2017.

The cast peeled off the glass nicely May 17th, 2017.

Initial UO2 powder used = 50.25g (Inventory R-01032A, UO2 + bottle = 876.80g before use)

Graphite powder used = 10.32g

Green cast dried UO2/C + organic mass = 61.70g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 1 long layer of heat shield and installed in evap1 today.

Chamber pumped down today.

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.

IG1 = 4.80e-6 Torr

Tapped up to 30A, 0.45V

Waited ~1hr, vacuum stable.

IG1 = 8.3e-6 Torr

Initiating auto-ramp


 Wednesday, May 24, 2017, 09:26

IG1 = 5.5e-5 Torr

TGHT = 64A, 0.72V

Vacuum currently yo-yo-ing.

Changing vacuum limits to attempt to speed up process.

Vacuum limit stop at 1.0e-4 Torr, backing off at 5.0e-4 Torr.

Once vacuum settles and vacuum starts to drop will adjust limits again accordingly.


 Wednesday, May 24, 2017, 11:17

IG1 = 1.2e-4 Torr

TGHT = 69A, 0.74V

TGHT direct readout = 66A, 0.73V

Thermometer attached to TP = 41.0C

Room temp = 24.0C


Wednesday, May 24, 2017, 13:16 

Vacuum going well.

Stable yo-yo-ing at current vacuum limit.

TP = 41.5C, RT = 23.9C

IG1 = 1.2e-4 Torr

TGHT = 71A, 0.77V

Increasing vacuum limit stop to 2.0e-4 Torr.


Thursday, May 25, 2017, 13:03

Vacuum has stabilized.

TGHT = 188A, 1.85V

IG1 = 2.2e-5 Torr.

Adjusting vacuum limits so when 2nd phase starts, vacuum does not spike.

Vacuum limit stop at 5.0e-5 Torr, backing off at 1.0e-4 Torr.


 

Attachment 1: UCxFlk_16_temp_readout.jpg
UCxFlk_16_temp_readout.jpg
  149   Friday, May 26, 2017, 15:23 Laura LambertUO2/C40282-1TARGET BOATProblemsprocessing UC2Flk_16 - 1ST TEST CHANGING VACUUM LIMITS

Laura Lambert wrote:

 Tuesday, May 23, 2017, 14:42

UO2/C green was prepared May 16th, 2017.

The cast peeled off the glass nicely May 17th, 2017.

Initial UO2 powder used = 50.25g (Inventory R-01032A, UO2 + bottle = 876.80g before use)

Graphite powder used = 10.32g

Green cast dried UO2/C + organic mass = 61.70g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 1 long layer of heat shield and installed in evap1 today.

Chamber pumped down today.

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.

IG1 = 4.80e-6 Torr

Tapped up to 30A, 0.45V

Waited ~1hr, vacuum stable.

IG1 = 8.3e-6 Torr

Initiating auto-ramp


 Wednesday, May 24, 2017, 09:26

IG1 = 5.5e-5 Torr

TGHT = 64A, 0.72V

Vacuum currently yo-yo-ing.

Changing vacuum limits to attempt to speed up process.

Vacuum limit stop at 1.0e-4 Torr, backing off at 5.0e-4 Torr.

Once vacuum settles and vacuum starts to drop will adjust limits again accordingly.


 Wednesday, May 24, 2017, 11:17

IG1 = 1.2e-4 Torr

TGHT = 69A, 0.74V

TGHT direct readout = 66A, 0.73V

Thermometer attached to TP = 41.0C

Room temp = 24.0C


Wednesday, May 24, 2017, 13:16 

Vacuum going well.

Stable yo-yo-ing at current vacuum limit.

TP = 41.5C, RT = 23.9C

IG1 = 1.2e-4 Torr

TGHT = 71A, 0.77V

Increasing vacuum limit stop to 2.0e-4 Torr.


Thursday, May 25, 2017, 13:03

Vacuum has stabilized.

TGHT = 188A, 1.85V

IG1 = 2.2e-5 Torr.

Adjusting vacuum limits so when 2nd phase starts, vacuum does not spike.

Vacuum limit stop at 5.0e-5 Torr, backing off at 1.0e-4 Torr.


 

 Friday, May 26, 2017, 13:40

Everything tripped off this morning at around 4:30am

This was not due to the vacuum spiking as one would expect.

No power bumps according to  ISAC controls.

Looking back on elogs  [see elog i.d. 145] evap1 had also tripped off during the last round of carbonizing UO2, however last time everything tripped off ~60A.

For last trip off the water valve remained open and on.

This time  WV1 showed yellow in the TGHT epics box, off under WV epics box, but black [open] in the WV epics box diagram [see screenshot for better understanding].

Water valves are closed - confirmed in person - water wheels not turning.

Trip-off occured ~275A.

Vacuum was stable at trip-off point; IG1 ~6e-6 Torr 

Reason: currently unknown.


 

 

 

Attachment 1: evap1_tripped_off_UCxFlk_16.jpg
evap1_tripped_off_UCxFlk_16.jpg
Attachment 2: evap1_tripped_off_UCxFlk_16(2).jpg
evap1_tripped_off_UCxFlk_16(2).jpg
Attachment 3: evap1_tripped_off_UCxFlk_16(3).jpg
evap1_tripped_off_UCxFlk_16(3).jpg
Attachment 4: evap1_tripped_off_UCxFlk_16_auto-ramp.jpg
evap1_tripped_off_UCxFlk_16_auto-ramp.jpg
Attachment 5: evap1_tripped_off_UCxFlk_16_water.jpg
evap1_tripped_off_UCxFlk_16_water.jpg
Attachment 6: evap1_tripped_off_UCxFlk_16(4).jpg
evap1_tripped_off_UCxFlk_16(4).jpg
  150   Friday, May 26, 2017, 16:09 Laura LambertUO2/C40282-1TARGET BOATIn progressprocessing UC2Flk_16 - 1ST TEST CHANGING VACUUM LIMITS

Laura Lambert wrote:

Laura Lambert wrote:

 Tuesday, May 23, 2017, 14:42

UO2/C green was prepared May 16th, 2017.

The cast peeled off the glass nicely May 17th, 2017.

Initial UO2 powder used = 50.25g (Inventory R-01032A, UO2 + bottle = 876.80g before use)

Graphite powder used = 10.32g

Green cast dried UO2/C + organic mass = 61.70g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 1 long layer of heat shield and installed in evap1 today.

Chamber pumped down today.

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.

IG1 = 4.80e-6 Torr

Tapped up to 30A, 0.45V

Waited ~1hr, vacuum stable.

IG1 = 8.3e-6 Torr

Initiating auto-ramp


 Wednesday, May 24, 2017, 09:26

IG1 = 5.5e-5 Torr

TGHT = 64A, 0.72V

Vacuum currently yo-yo-ing.

Changing vacuum limits to attempt to speed up process.

Vacuum limit stop at 1.0e-4 Torr, backing off at 5.0e-4 Torr.

Once vacuum settles and vacuum starts to drop will adjust limits again accordingly.


 Wednesday, May 24, 2017, 11:17

IG1 = 1.2e-4 Torr

TGHT = 69A, 0.74V

TGHT direct readout = 66A, 0.73V

Thermometer attached to TP = 41.0C

Room temp = 24.0C


Wednesday, May 24, 2017, 13:16 

Vacuum going well.

Stable yo-yo-ing at current vacuum limit.

TP = 41.5C, RT = 23.9C

IG1 = 1.2e-4 Torr

TGHT = 71A, 0.77V

Increasing vacuum limit stop to 2.0e-4 Torr.


Thursday, May 25, 2017, 13:03

Vacuum has stabilized.

TGHT = 188A, 1.85V

IG1 = 2.2e-5 Torr.

Adjusting vacuum limits so when 2nd phase starts, vacuum does not spike.

Vacuum limit stop at 5.0e-5 Torr, backing off at 1.0e-4 Torr.


 

 Friday, May 26, 2017, 13:40

Everything tripped off this morning at around 4:30am

This was not due to the vacuum spiking as one would expect.

No power bumps according to  ISAC controls.

Looking back on elogs  [see elog i.d. 145] evap1 had also tripped off during the last round of carbonizing UO2, however last time everything tripped off ~60A.

For last trip off the water valve remained open and on.

This time  WV1 showed yellow in the TGHT epics box, off under WV epics box, but black [open] in the WV epics box diagram [see screenshot for better understanding].

Water valves are closed - confirmed in person - water wheels not turning.

Trip-off occured ~275A.

Vacuum was stable at trip-off point; IG1 ~6e-6 Torr 

Reason: currently unknown.


 

 

 

 Friday, May 26, 2017, 15:43

Starting pumping down again this afternoon while trying to understand trip-off - no progress on that end.

IG1 = 4.9e-6 Torr

Tapped up to 40A, 0.24V

Vacuum spiked to 2e-5 Torr

Backed off to 35A, 0.20V

Showing lower voltage output than the last round that had tripped off...but ramping is so early on/ low current, hard to tell...

Vacuum stable.

IG1 = 5.4e-6 Torr

Target boat will be ramped up to 275A [trip-off point] at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.

 

TP = 37.9C, RT = 25.2C


 

  151   Monday, May 29, 2017, 08:54 Laura LambertUO2/C40282-1TARGET BOATProblemsprocessing UC2Flk_16 - 1ST TEST CHANGING VACUUM LIMITS

Laura Lambert wrote:

Laura Lambert wrote:

Laura Lambert wrote:

 Tuesday, May 23, 2017, 14:42

UO2/C green was prepared May 16th, 2017.

The cast peeled off the glass nicely May 17th, 2017.

Initial UO2 powder used = 50.25g (Inventory R-01032A, UO2 + bottle = 876.80g before use)

Graphite powder used = 10.32g

Green cast dried UO2/C + organic mass = 61.70g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 1 long layer of heat shield and installed in evap1 today.

Chamber pumped down today.

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.

IG1 = 4.80e-6 Torr

Tapped up to 30A, 0.45V

Waited ~1hr, vacuum stable.

IG1 = 8.3e-6 Torr

Initiating auto-ramp


 Wednesday, May 24, 2017, 09:26

IG1 = 5.5e-5 Torr

TGHT = 64A, 0.72V

Vacuum currently yo-yo-ing.

Changing vacuum limits to attempt to speed up process.

Vacuum limit stop at 1.0e-4 Torr, backing off at 5.0e-4 Torr.

Once vacuum settles and vacuum starts to drop will adjust limits again accordingly.


 Wednesday, May 24, 2017, 11:17

IG1 = 1.2e-4 Torr

TGHT = 69A, 0.74V

TGHT direct readout = 66A, 0.73V

Thermometer attached to TP = 41.0C

Room temp = 24.0C


Wednesday, May 24, 2017, 13:16 

Vacuum going well.

Stable yo-yo-ing at current vacuum limit.

TP = 41.5C, RT = 23.9C

IG1 = 1.2e-4 Torr

TGHT = 71A, 0.77V

Increasing vacuum limit stop to 2.0e-4 Torr.


Thursday, May 25, 2017, 13:03

Vacuum has stabilized.

TGHT = 188A, 1.85V

IG1 = 2.2e-5 Torr.

Adjusting vacuum limits so when 2nd phase starts, vacuum does not spike.

Vacuum limit stop at 5.0e-5 Torr, backing off at 1.0e-4 Torr.


 

 Friday, May 26, 2017, 13:40

Everything tripped off this morning at around 4:30am

This was not due to the vacuum spiking as one would expect.

No power bumps according to  ISAC controls.

Looking back on elogs  [see elog i.d. 145] evap1 had also tripped off during the last round of carbonizing UO2, however last time everything tripped off ~60A.

For last trip off the water valve remained open and on.

This time  WV1 showed yellow in the TGHT epics box, off under WV epics box, but black [open] in the WV epics box diagram [see screenshot for better understanding].

Water valves are closed - confirmed in person - water wheels not turning.

Trip-off occured ~275A.

Vacuum was stable at trip-off point; IG1 ~6e-6 Torr 

Reason: currently unknown.


 

 

 

 Friday, May 26, 2017, 15:43

Starting pumping down again this afternoon while trying to understand trip-off - no progress on that end.

IG1 = 4.9e-6 Torr

Tapped up to 40A, 0.24V

Vacuum spiked to 2e-5 Torr

Backed off to 35A, 0.20V

Showing lower voltage output than the last round that had tripped off...but ramping is so early on/ low current, hard to tell...

Vacuum stable.

IG1 = 5.4e-6 Torr

Target boat will be ramped up to 275A [trip-off point] at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.

 

TP = 37.9C, RT = 25.2C


 

 Monday, May 29, 2017, 08:21

Initially it looks like not enough time had been allowed for the vacuum to settle before initiating the auto-ramp resulting in the vacuum spiking and tripping off the system.

A closer look shows that is not the case.

Note: the vacuum limits were set to stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr. 

 

The TGHT started to back off when the vacuum was ~6e-6 Torr, this is considered a good vacuum and should not have caused the system to initiate backing off yet.

Over the course of ~1min, evap1 had backed off all the way down to 0A.

At this point the vacuum was now up to ~1.75e-5 Torr and still rising.

~34min after the TGHT had reached 0A, the vacuum eventually reached 8e-4 Torr and tripped off the evaporator.

See photos attached.


 

Attachment 1: evap1_tripped_off_roud2_UCxFlk_16.jpg
evap1_tripped_off_roud2_UCxFlk_16.jpg
Attachment 2: evap1_tripped_off_roud2_UCxFlk_16(2).jpg
evap1_tripped_off_roud2_UCxFlk_16(2).jpg
  152   Tuesday, May 30, 2017, 07:43 Laura LambertUO2/C40282-1TARGET BOATDoneprocessing UC2Flk_16 - 1ST TEST CHANGING VACUUM LIMITS

Laura Lambert wrote:

Laura Lambert wrote:

Laura Lambert wrote:

Laura Lambert wrote:

 Tuesday, May 23, 2017, 14:42

UO2/C green was prepared May 16th, 2017.

The cast peeled off the glass nicely May 17th, 2017.

Initial UO2 powder used = 50.25g (Inventory R-01032A, UO2 + bottle = 876.80g before use)

Graphite powder used = 10.32g

Green cast dried UO2/C + organic mass = 61.70g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 1 long layer of heat shield and installed in evap1 today.

Chamber pumped down today.

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.

IG1 = 4.80e-6 Torr

Tapped up to 30A, 0.45V

Waited ~1hr, vacuum stable.

IG1 = 8.3e-6 Torr

Initiating auto-ramp


 Wednesday, May 24, 2017, 09:26

IG1 = 5.5e-5 Torr

TGHT = 64A, 0.72V

Vacuum currently yo-yo-ing.

Changing vacuum limits to attempt to speed up process.

Vacuum limit stop at 1.0e-4 Torr, backing off at 5.0e-4 Torr.

Once vacuum settles and vacuum starts to drop will adjust limits again accordingly.


 Wednesday, May 24, 2017, 11:17

IG1 = 1.2e-4 Torr

TGHT = 69A, 0.74V

TGHT direct readout = 66A, 0.73V

Thermometer attached to TP = 41.0C

Room temp = 24.0C


Wednesday, May 24, 2017, 13:16 

Vacuum going well.

Stable yo-yo-ing at current vacuum limit.

TP = 41.5C, RT = 23.9C

IG1 = 1.2e-4 Torr

TGHT = 71A, 0.77V

Increasing vacuum limit stop to 2.0e-4 Torr.


Thursday, May 25, 2017, 13:03

Vacuum has stabilized.

TGHT = 188A, 1.85V

IG1 = 2.2e-5 Torr.

Adjusting vacuum limits so when 2nd phase starts, vacuum does not spike.

Vacuum limit stop at 5.0e-5 Torr, backing off at 1.0e-4 Torr.


 

 Friday, May 26, 2017, 13:40

Everything tripped off this morning at around 4:30am

This was not due to the vacuum spiking as one would expect.

No power bumps according to  ISAC controls.

Looking back on elogs  [see elog i.d. 145] evap1 had also tripped off during the last round of carbonizing UO2, however last time everything tripped off ~60A.

For last trip off the water valve remained open and on.

This time  WV1 showed yellow in the TGHT epics box, off under WV epics box, but black [open] in the WV epics box diagram [see screenshot for better understanding].

Water valves are closed - confirmed in person - water wheels not turning.

Trip-off occured ~275A.

Vacuum was stable at trip-off point; IG1 ~6e-6 Torr 

Reason: currently unknown.


 

 

 

 Friday, May 26, 2017, 15:43

Starting pumping down again this afternoon while trying to understand trip-off - no progress on that end.

IG1 = 4.9e-6 Torr

Tapped up to 40A, 0.24V

Vacuum spiked to 2e-5 Torr

Backed off to 35A, 0.20V

Showing lower voltage output than the last round that had tripped off...but ramping is so early on/ low current, hard to tell...

Vacuum stable.

IG1 = 5.4e-6 Torr

Target boat will be ramped up to 275A [trip-off point] at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.

 

TP = 37.9C, RT = 25.2C


 

 Monday, May 29, 2017, 08:21

Initially it looks like not enough time had been allowed for the vacuum to settle before initiating the auto-ramp resulting in the vacuum spiking and tripping off the system.

A closer look shows that is not the case.

Note: the vacuum limits were set to stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr. 

 

The TGHT started to back off when the vacuum was ~6e-6 Torr, this is considered a good vacuum and should not have caused the system to initiate backing off yet.

Over the course of ~1min, evap1 had backed off all the way down to 0A.

At this point the vacuum was now up to ~1.75e-5 Torr and still rising.

~34min after the TGHT had reached 0A, the vacuum eventually reached 8e-4 Torr and tripped off the evaporator.

See photos attached.


 

 Tuesday, May 30, 2017, 07:41

Still unsure as to why evap1 tripped off again.

Put evap1 back under vacuum/ turned turbo pump on and opened isolation valve yesterday afternoon.

Vacuum good this morning...nothing tripped off...


 Tuesday, May 30, 2017, 08:21

IG1 = 2.3e-6 Torr

Tapped up manually to 40A, 0.24V

Waited ~1hr

IG1 = 4.5e-6 Torr

Initiated auto-ramp at 0.2A/min up to a final setpoint of 250A


 Wednesday, May 31, 2017, 09:37

IG1 = 2.4e-6 Torr

TGHT = 250A, 2.57V

Increasing max setpoint to 275A [the trip off point] at a rate of 0.2A/min

Vacuum is currently stable and low; increasing limits to:

Vacuum limit stop at 1.0e-4 Torr, backing off at 5.0e-4 Torr.


 Wednesday, May 31, 2017, 13:39

IG1 = 3.7e-6 Torr

TGHT = 275A, 2.80V

Increasing max setpoint to final setpoint of 520A at a rate of 0.2A/min

Vacuum is currently stable and low; keeping  current limits.


Wednesday, May 31, 2017, 15:57

IG1 = 8.14e-6 Torr

TGHT = 300A, 3.08V

Vacuum stable.

Decreasing ramping rate to 0.1A/min for overnight heating.

turbo pump = 40.5C; room temp = 25.1C


 Thursday, June 01, 2017, 09:00

IG1 = 4.2e-5 Torr

TGHT = 396A, 4.06V

Vacuum stable.

Increasing ramping rate to 0.2A/min.

turbo pump = 41.6C; room temp = 24.3C


 Thursday, June 01, 2017, 13:18

IG1 = 1.25e-4 Torr

TGHT = 439A, 4.48V

Vacuum stable.

Changing vacuum limits.

Vacuum limit stop at 2.0e-4 Torr, backing off at 5.0e-4 Torr.

turbo pump = 42.3C; room temp = 24.6C


 Thursday, June 01, 2017, 15:48

IG1 = 1.95e-4 Torr

TGHT = 467A, 4.81V

Vacuum stable.

Changing vacuum limits and ramping rate for heating overnight.

Decreasing ramping rate to 0.1A/min

Vacuum limit stop at 1.0e-4 Torr, backing off at 5.0e-4 Torr.

turbo pump = 44.1C; room temp = 25.3C


 Friday, June 02, 2017, 07:19

IG1 = 1.26e-4 Torr

TGHT = 473A, 4.77V

Vacuum stable.

Changing vacuum limits and ramping rate.

Increasing ramping rate to 0.2A/min

Vacuum limit stop at 2.0e-4 Torr, backing off at 5.0e-4 Torr.


 Friday, June 02, 2017, 10:18

IG1 = 2.04e-4 Torr

TGHT = 498A, 5.08V

Vacuum stable.

Changing vacuum limits.

Vacuum limit stop at 3.0e-4 Torr, backing off at 5.0e-4 Torr.

Fan has been inserted - pointed at turbo pump, TP temp's have decreased.

tp = 32.1C; rt = 24.7C


 Friday, June 02, 2017, 13:22

IG1 = 2.4e-4 Torr

TGHT = 520A, 5.40V

Vacuum stable and decreasing.

Carbonization process almost complete.

Will remain at max setpoints over the weekend.

TP = 28.2C; RT = 24.5C


 Monday, June 05, 2017, 08:51

IG1 = 1.75e-6 Torr

TGHT = 520A, 5.29V

Carbonization process complete!

Remained at max setpoints over the weekend.

Initiating auto cool at 1.0A/min


 Tuesday, June 06, 2017, 15:56

Vented in Ar and removed today.

Currently in glove box.


 Monday, June 12, 2017, 11:44

Flakes produced: 48.00g


 

  154   Monday, June 12, 2017, 15:07 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_17

 Monday, June 12, 2017, 11:41

UO2/C green was prepared June 7th, 2017.

The cast peeled off the glass nicely June 8th, 2017.

Initial UO2 powder used = 50.10g (Inventory R-01032A, UO2 + bottle = 776.36g before use)

Graphite powder used = 10.06g

Green cast dried UO2/C + organic mass = 62.98g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 1 long layer of heat shield [reused from last carbonization] and installed in evap1 this morning.

Chamber pumped down.

Target boat will be ramped up to 520A.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.

IG1 = 1.58e-5 Torr

Tapped up to 30A, 0.21V

Waited ~1hr45, vacuum stable.

IG1 = 8.59e-6 Torr

Initiating auto-ramp at 0.1A/min


 Tuesday, June 13, 2017, 10:32

IG1 = 5.0e-5 Torr

TGHT = 65A, 0.47V

Vacuum currently yo-yo-ing, but stable.

Changing vacuum limits.

Vacuum limit stop at 2.0e-4 Torr, backing off at 5.0e-4 Torr.

Increasing ramping rate to 0.2A/min.


Thursday, June 15, 2017, 16:24  

IG1 = 1.96e-4 Torr

TGHT = 520A, 5.18V

TGHT has reached 520A, the vacuum remains at it's limit.

Vacuum usually drops and stabilizes slightly before the max setpoint is reached indicating carbonization process complete.

Since vacuum remains high, this indicates the carbonization remains incomplete.

Conditions have changed such as vacuum limits, which has greatly sped up the process.

This increase in speed could have an impact on the current at which the carbonization occurs.

Increasing max setpoint to 530A and re-initiating auto-ramp.


 Friday, June 16, 2017, 08:32

Vacuum stable, started decreasing when TGHT reached 530A - carbonization process complete.

Evap1 has remained at max setpoints for ~11hrs, but has remained at low vacuum for ~5hrs.

IG1 = 5.56e-6 Torr

TGHT = 530A, 5.31V

Initiating auto-cool at 1.0A/min

TP = 24.9C, RT = 24.3C

*note TP now has water cooling as well as fan pointed at it for this entire process


 Monday, June 19, 2017, 16:16

Vented in Ar and transferred from evap1 to glove box this a.m

UC2 flakes produced = 48.66g


 

Attachment 1: UC2Flk_17_entire_carbonization_process_using_new_vacuum_limits.JPG
UC2Flk_17_entire_carbonization_process_using_new_vacuum_limits.JPG
Attachment 2: UC2Flk_17_vac_vs._cur.JPG
UC2Flk_17_vac_vs._cur.JPG
Attachment 3: UC2Flk_17_vac_vs._volt.JPG
UC2Flk_17_vac_vs._volt.JPG
  164   Wednesday, August 23, 2017, 15:54 Laura LambertUO2/C40282-2TARGET BOATDoneCarbonizing UC2 discs for 1stepUCx in graphite sample container _#1

 Wednesday, August 23, 2017, 15:41

2 rounds of UO2/C were cast onto a graphite sheet in the fume hood and let dry.

For this round of samples, circles from cast 1 were used

Graphite powder used = 5.16g

A 14mm punch was used to punch out circles from a 16mm wide strip.

35 circles were packed into a graphite sample container.

graphite container [no endcap] = 3.37g

35 x UO2/C circles = 4.76g

graphite container+smpls = 8.13g

container+smpls+endcap = 10.08g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered - 1st use of newly sintered boat.

Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber currently pumping down.


 Friday, August 25, 2017, 09:59

IG1 = 3.45e-6 Torr.

Stepped up manually to 80A.

Vacuum stable.

IG1 = 3.0e-5 Torr.

Initiating auto-ramp.

Target boat will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 1.0e-4 Torr, backing off at 5.0e-4 Torr.


 Monday, August 28, 2017, 08:09

IG1 = 6.3e-6 Torr

TGHT = 455A, 4.65V

Vacuum stable.

Increasing ramping rate to 0.2A/min.


 Monday, August 28, 2017, 08:53

IG1 = 7.3e-6 Torr

TGHT = 465A, 4.75V

Vacuum stable.

Increasing ramping rate to 0.5A/min.


 Monday, August 28, 2017, 13:17

IG1 = 1.32e-5 Torr

TGHT = 520A, 5.44V

Vacuum still fairly high and not dropping very fast indicating carbonization incomplete.

Increasing max setpoint to 530A and restarting auto-ramp.


 Monday, August 28, 2017, 15:13

IG1 = 1.32e-5 Torr

TGHT = 530A, 5.58V

Vacuum still high, wavering up and down/ not dropping - carbonization remains incomplete.

Increasing max setpoint to 540A and restarting auto-ramp.


 Tuesday, August 29, 2017, 09:28

IG1 = 3.72e-6 Torr

TGHT = 540A, 5.66V

Carbonization complete.

Initiating auto-cool at 2.0A/min


 

Attachment 1: IMG_1768.JPG
IMG_1768.JPG
Attachment 2: IMG_1774.JPG
IMG_1774.JPG
  168   Wednesday, September 27, 2017, 12:05 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_18

 Wednesday, September 27, 2017, 09:25

UO2/C green was prepared Sept 20th, 2017.

The cast peeled off the glass Sept 22nd, 2017 - not quite enough 'special' ingredient.

UO2 stuck to glass around edges of cast - a lot of flakes produced while peeling off.

Initial UO2 powder used = 50.00g (Inventory R-01032A, UO2 + bottle = 726.38g before use)

Graphite powder used = 10.03g

Green cast dried UO2/C + organic mass = 60.38g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-layers of heat shield [reused from last 1stepUCx] and installed in evap1 yesterday afternoon.

Chamber pumped down overnight.

Target boat will be ramped up to 520A.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.

IG1 = 3.5e-6 Torr

Tapped up to 30A, 0.43V

Waited ~50min, vacuum stable.

IGP1 = 8.6e-6 Torr

Initiating auto-ramp at 0.1A/min


 Wednesday, September 27, 2017, 13:28

IGP1 = 1.4e-5 Torr

TGHT = 38.5A, 0.48V

Vacuum stable.

Changing vacuum limits and ramping rate.

Vacuum limit stop at 2.0e-4 Torr, backing off at 5.0e-4 Torr.

Increasing ramping rate to 0.2A/min.


 Thursday, September 28, 2017, 08:41

IGP1 = 3.26e-5 Torr

TGHT = 174A, 1.71V

Vacuum stable.

Increasing ramping rate to 0.5A/min.


 Thursday, September 28, 2017, 09:56

IGP1 = 4.85e-5 Torr

TGHT = 195A, 1.92V

Vacuum initially climbed a small amount with last increase, has started to decrease - vacuum stable.

Increasing ramping rate to 1.0A/min.


Thursday, September 28, 2017, 10:30  

IGP1 = 5.3e-5 Torr

TGHT = 220A, 2.18V

Vacuum increased slightly again with faster ramping rate.

Vacuum now dropping - stable.

Increasing ramping rate to 2.0A/min.


 Thursday, September 28, 2017, 11:07

IGP1 = 6.35e-5 Torr

TGHT = 302A, 3.09V

Vacuum increased slightly again with faster ramping rate.

Vacuum now dropping - stable.

Increasing ramping rate to 2.5A/min.


Thursday, September 28, 2017, 11:45

IGP1 = 1.67e-4 Torr

TGHT = 380A, 4.04V

Vacuum increased normally at slow rate for first half hour.

~30min into the 2.5A/min rate increase, vacuum started to climb much faster.

Paused auto-ramp for few min to allow vacuum to stabilize.

Vacuum decreasing - stable.

IGP1 = 1.4e-4 Torr

Decreasing ramping rate to 0.5A/min for next hour while unable to watch.


 Thursday, September 28, 2017, 13:20

IGP1 = 1.93e-4 Torr

TGHT = 425A, 4.58V

Vacuum stable.

Changing vacuum limits and ramping rate.

Increasing ramping rate 1.0A/min.

Vacuum limit stop at 3.0e-4 Torr, backing off at 6.0e-4 Torr.


 Thursday, September 28, 2017, 14:06

IGP1 = 3.1e-4 Torr

TGHT = 456A, 4.93V

Vacuum stable.

Changing vacuum limits and ramping rate.

Changing ramping rate to 0.5A/ 30sec.

Vacuum limit stop at 4.0e-4 Torr, backing off at 7.0e-4 Torr.


 Thursday, September 28, 2017, 14:44

IGP1 = 4.0e-4 Torr

TGHT = 468A, 5.07V

Vacuum stable.

Changing vacuum limits.

Vacuum limit stop at 5.0e-4 Torr, backing off at 8.0e-4 Torr.


 Thursday, September 28, 2017, 15:49

TP thermocouple = 28.1C

IGP1 = 5.0e-4 Torr

TGHT = 485A, 5.25V

Vacuum stable.

Changing ramping rate for overnight heating.

Decreasing ramping rate to 0.5A/min.


 Friday, September 29, 2017, 09:11

TP thermocouple = 26.1C

IGP1 = 5.0e-6 Torr

TGHT = 520A, 5.60V

Vacuum stable.

Carbonization process complete!

Evap1 has remained at max setpoints for ~13hrs

Initiating auto-cool at 1.0A/min


 Tuesday, October 03, 2017, 10:09

Vented in Ar and transferred from evap1 to glove box yesterday.


 

  169   Tuesday, October 10, 2017, 14:16 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_19

 Tuesday, October 10, 2017, 14:11

UO2/C green was prepared Oct 4th, 2017

The cast peeled off the glass nicely Oct 6th, 2017

Initial UO2 powder used = 50.26g (Inventory R-01032A, UO2 + bottle = 676.34g before use)

Graphite powder used = 10.12g

Green cast dried UO2/C + organic mass = 61.30g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-layers of heat shield [reused] and installed in evap1 this morning.

Chamber currently pumping down.

Target boat will be ramped up to 520A.

Vacuum limit stop at 3.0e-4 Torr, backing off at 6.0e-4 Torr.


 Wednesday, October 11, 2017, 09:06

IGP1 = 1.74e-6 Torr

Tapped up to 35A, 0.29V

Waited ~70min, vacuum stable.

IGP1 = 6.9e-6 Torr

Initiating auto-ramp at 0.2A/min


 Wednesday, October 11, 2017, 13:06

IGP1 = 3.1e-4 Torr

TGHT = 61A, 0.49V

Vacuum stable.

Changing vacuum limits.

Vacuum limit stop at 5.0e-4 Torr, backing off at 8.0e-4 Torr.


 Thursday, October 12, 2017, 08:31

IGP1 = 1.06e-5 Torr

TGHT = 275A, 2.55V

Vacuum stable.

Increasing ramping rate to 0.5A/min.


 Thursday, October 12, 2017, 09:03

IGP1 = 1.47e-5 Torr

TGHT = 290A, 2.70V

Vacuum stable.

Increasing ramping rate to 1.0A/ 30sec.


 Friday, October 13, 2017, 08:30

IGP1 = 5.8e-6 Torr

TGHT = 520A, 4.98V

Vacuum stable.

Carbonization process complete!

Evap1 has remained at max setpoints for ~17hrs

Initiating auto-cool at 1.0A/min


 Tuesday, October 17, 2017, 15:01

TGHT had sat at 0A for at least 24hrs.

At ~3:30-4am this morning everything tripped off. The only thing remained on was the roughing pump.

Power bump? Did someone accidentally turn it off? Will follow up on this...

Vacuum was sitting at ~3.5e-2Torr when I noticed today.

Most vacuum had been lost, but there was still a small vacuum - materials should be okay.

Purged and vented in Ar.

Transferred materials to glove box.


 

  173   Tuesday, November 14, 2017, 16:16 Laura LambertUO2/C40282-2TARGET BOATDoneCarbonizing UC2 discs for 1stepUCx in graphite sample container _#2

 Tuesday, November 14, 2017, 16:12

Circles from cast 1 were used, the same as the last round of 1stepUCx [see elog i.d. 164]

A 14mm punch was used to punch out circles from the cast.

35 circles were packed into a graphite sample container.

35 x UO2/C circles = 5.43g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber currently pumping down.


 Wednesday, November 15, 2017, 08:53

IGP1 = 1.6e-6 Torr

Tapping up manually...


 Wednesday, November 15, 2017, 11:59

IGP1 = 5.0e-5 Torr

Tapped up entire process manually to 520A in 3hrs!!!

TGHT = 520A, 4.98V

Vacuum coming down nicely indicating carbonization process complete 

Will remain at max setpoint for 4hrs to ensure full carbonization before cooling down later this afternoon.


 Wednesday, November 15, 2017, 15:16

IG1 = 8.65e-6 Torr

TGHT = 520A, 4.92V

Carbonization complete.

Initiating auto-cool at 2.0A/min


 Monday, November 20, 2017, 13:28

Evap1 was vented in argon and sample removed/ transfered to glove box on friday.

Discs look good, slightly lighter grayer compared to production UCx discs after second cast but before final carbonization.

Material seems to adhere to graphite backing foil well, no flakes coming off from just moving discs around.

Weight of 35 carbonized discs = 4.387g

Weight loss = 5.43g - 4.387g = 1.043g


 

Attachment 1: striptool.JPG
striptool.JPG
  175   Thursday, November 23, 2017, 13:39 Marla CervantesUO2/C40282-2 TARGET BOATDoneCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#3

 Thursday, November 23, 2017, 13:34

Circles from cast 1 were used, the same as the last round of 1stepUCx [see elog i.d. 164]

A 14mm punch was used to punch out circles from the cast.

35 circles were packed into a graphite sample container.

35 x UO2/C circles = 5.75 g

Graphite container = 5.38 g

Graphite container is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber currently pumping down.


 Friday, November 24, 2017, 12:48

IGP1=1.3e-6 Torr

TGHT = 520A, 4.98V 

Vacuum went down indicating carbonization.

Will remain at max setpoint for the weekend.


 Monday, November 27, 2017, 09:58

IG1 = 2.6e-6 Torr

TGHT = 520A, 5.1V

Carbonization complete in 3 hrs and 30 min.

Initiating auto-cool at 2.0A/min


 Wednesday, November 27, 2017, 13:10

 IEVAP was vented in argon and sample removed/transferred to glove box on Friday.

Attachment 1: 171124_1e-1.jpg
171124_1e-1.jpg
  176   Wednesday, January 10, 2018, 14:44 Marla CervantesUO2/C40282-1TARGET BOATIn progressCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#4

 Wednesday, January 10, 2018, 14:44

Circles from cast 1 were used, the same as the last round of 1stepUCx [see elog i.d. 164]

A 14mm punch was used to punch out circles from the cast.

35 circles were packed into a graphite sample container.

35 x UO2/C circles = 5.75 g

Graphite container = 5.38 g

Graphite container is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber currently pumping down.

  177   Friday, January 12, 2018, 07:46 Laura LambertUO2/C TARGET BOATIn progressCarbonizing UO2/C discs for 1stepUCx in graphite sample container_#4

Marla Cervantes wrote:

 Wednesday, January 10, 2018, 14:44

Circles from cast 1 were used, the same as the last round of 1stepUCx [see elog i.d. 164]

A 14mm punch was used to punch out circles from the cast.

35 circles were packed into a graphite sample container.

35 x UO2/C circles = 5.75 g

Graphite container = 5.38 g

Graphite container is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber currently pumping down.

 Friday, January 12, 2018, 07:43

IGP1 = 0.0266 Torr

TGHT = 520A, 5.92V

Voltage has been climbing consistently since it has reached it's max setpoint, gone up ~0.8V in ~18hrs

Carbonization complete.

Initiating auto-cool at 2.0A/min

Will update later with more information on this process.


 Friday, January 12, 2018, 09:47

Turned the turbo pump back on, to ensure safe cooling.


 

  178   Wednesday, January 17, 2018, 13:47 Marla CervantesUO2/C40282-1TARGET BOATDoneCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#5

 Monday, January 15, 2018, 13:37

35 circles of 14 mm diameter were packed into a graphite sample container.

35 x UO2/C circles = 5.58 g

Graphite container = 5.22 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 new Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


Tuesday, January 16, 2018, 13:41 

Initial IGP1 = 9x10e-7 Torr

Tapped up entire process manually to 520A in 1.5 hrs

TGHT = 525 A, 5.64 V

Vacuum coming down nicely indicating carbonization process complete 

Will remain at max setpoint overnight to ensure full carbonization before cooling down.


Wednesday, January 17, 2018, 10:30

Initiating auto-cool at 2.0A/min 


Wednesday, January 17, 2018, 4:30

Vented with Argon and removed form evaporator 1

Attachment 1: Carbonization-Batch5-180118.docx
  179   Thursday, January 18, 2018, 11:56 Marla CervantesUO2/C40282-2 TARGET BOATDoneCarbonizing UO2/C discs for 1stepUCx in graphite sample container TP1-off_#4

Laura Lambert wrote:

Marla Cervantes wrote:

 Wednesday, January 10, 2018, 14:44

Circles from cast 1 were used, the same as the last round of 1stepUCx [see elog i.d. 164]

A 14mm punch was used to punch out circles from the cast.

35 circles were packed into a graphite sample container.

35 x UO2/C circles = 5.75 g

Graphite container = 5.38 g

Graphite container is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber currently pumping down.

 Friday, January 12, 2018, 07:43

IGP1 = 0.0266 Torr

TGHT = 520A, 5.92V

Voltage has been climbing consistently since it has reached it's max setpoint, gone up ~0.8V in ~18hrs

Carbonization complete.

Initiating auto-cool at 2.0A/min

Will update later with more information on this process.


 Friday, January 12, 2018, 09:47

Turned the turbo pump back on, to ensure safe cooling.


 

 Monday, January 15, 2018, 10:00

Vented with Argon and removed from evap1


NB: The initial mass of the UO2/C discs was 5.9 g

 

 

       The final mass of the UCx discs was 4.614 g

Attachment 1: Carbonization-Batch4-110118-TP_off.docx
  180   Friday, January 19, 2018, 12:32 Marla CervantesUO2/C40282-2 TARGET BOATIn progressCarbonizing UO2/C discs for 1stepUCx in graphite sample container_#6

 Friday, January 19, 2018, 12:29

Circles from cast 1 were used, the same as the last round of 1stepUCx [see elog i.d. 164]

A 14mm punch was used to punch out circles from the cast.

35 circles were packed into a graphite sample container.

35 x UO2/C circles = 5.69 g

Graphite container = 6.84 g

Graphite container is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber currently pumping down.


 

  181   Monday, January 22, 2018, 15:51 Marla CervantesUO2/C40282-2 TARGET BOATProblemsCarbonizing UO2/C discs for 1stepUCx in graphite sample container_#6

Marla Cervantes wrote:

 Friday, January 19, 2018, 12:29

Circles from cast 1 were used, the same as the last round of 1stepUCx [see elog i.d. 164]

A 14mm punch was used to punch out circles from the cast.

35 circles were packed into a graphite sample container.

35 x UO2/C circles = 5.69 g

Graphite container = 6.84 g

Graphite container is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber currently pumping down.


 

 Monday, January 22, 2018, 15:48

A power outage on Sunday tripped off EVAP1.

  182   Monday, January 22, 2018, 16:20 Marla CervantesUO2/C40282-2 TARGET BOATProblems resolvedCarbonizing UO2/C discs for 1stepUCx in graphite sample container_#6

Marla Cervantes wrote:

Marla Cervantes wrote:

 Friday, January 19, 2018, 12:29

Circles from cast 1 were used, the same as the last round of 1stepUCx [see elog i.d. 164]

A 14mm punch was used to punch out circles from the cast.

35 circles were packed into a graphite sample container.

35 x UO2/C circles = 5.69 g

Graphite container = 6.84 g

Graphite container is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber currently pumping down.


 

 Monday, January 22, 2018, 9:00

A power outage on Sunday tripped off EVAP1.

 Monday, January 22, 2018, 10:00

Chamber pumping down.

Water flow turned on.


Monday, January 22, 2018, 13:30

IGP1 = 8e-6 Torr

Tapped up entire process manually to 520A in 45 min

TGHT = 520 A, 6.08 V 

Vacuum coming down indicating carbonization process complete

Will remain at max setpoint overnight.


 

Attachment 1: 180122-1e-1.jpg
180122-1e-1.jpg
  183   Tuesday, January 23, 2018, 12:49 Marla CervantesUO2/C40282-2 TARGET BOATDoneCarbonizing UO2/C discs for 1stepUCx in graphite sample container_#6

Marla Cervantes wrote:

Marla Cervantes wrote:

Marla Cervantes wrote:

 Friday, January 19, 2018, 12:29

Circles from cast 1 were used, the same as the last round of 1stepUCx [see elog i.d. 164]

A 14mm punch was used to punch out circles from the cast.

35 circles were packed into a graphite sample container.

35 x UO2/C circles = 5.69 g

Graphite container = 6.84 g

Graphite container is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers of heat shield and installed in Evap1.

Chamber currently pumping down.


 

 Monday, January 22, 2018, 9:00

A power outage on Sunday tripped off EVAP1.

 Monday, January 22, 2018, 10:00

Chamber pumping down.

Water flow turned on.


Monday, January 22, 2018, 13:30

IGP1 = 8e-6 Torr

Tapped up entire process manually to 520A in 45 min

TGHT = 520 A, 6.08 V 

Vacuum coming down indicating carbonization process complete

Will remain at max setpoint overnight.


 

 Tuesday, January 23, 2018, 9:30

Initiating auto-cool at 2 A/min


 Tuesday, January 23, 2018, 16:00

 EVAP1 was not vented, Ar tank has low level, Ar tank will be replaced.


Wednesday, January 24, 2018, 11:37

 EVAP1 was vented very carefully using the Ar remaining in the Ar tank.

Ar tank remaining gas: ~8 psi.


Wednesday, January 24, 2018, 15:42 

UCx was transferred to glove box.

Final mass 4.501 g

Attachment 1: Carbonization-Batch6-220118.docx
  184   Monday, January 29, 2018, 09:28 Marla CervantesUO2/C40282-2 TARGET BOATIn progressCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#7

 Monday, January 29, 2018, 09:26

35 circles of 14 mm diameter were packed into a graphite sample container.

35 x UO2/C circles = 4.94 g

Graphite container = 5.03 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 new Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


 

  185   Monday, January 29, 2018, 11:07 Marla CervantesUO2/C40282-2 TARGET BOATProblemsCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#7

Marla Cervantes wrote:

 Monday, January 29, 2018, 09:26

35 circles of 14 mm diameter were packed into a graphite sample container.

35 x UO2/C circles = 4.94 g

Graphite container = 5.03 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 new Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


 

 Monday, January 29, 2018, 11:06

A power outage around 10 am tripped off EVAP1.

  186   Monday, January 29, 2018, 14:25 Marla CervantesUO2/C40282-2 TARGET BOATProblems resolvedCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#7

Marla Cervantes wrote:

Marla Cervantes wrote:

 Monday, January 29, 2018, 09:26

35 circles of 14 mm diameter were packed into a graphite sample container.

35 x UO2/C circles = 4.94 g

Graphite container = 5.03 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 new Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


 

 Monday, January 29, 2018, 11:06

A power outage around 10 am tripped off EVAP1.

 Monday, January 29, 2018, 14:22

Water flow turned on.

Chamber set to pumping down. 


 

  187   Tuesday, January 30, 2018, 16:07 Marla CervantesUO2/C40282-2 TARGET BOATDoneCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#7

Marla Cervantes wrote:

Marla Cervantes wrote:

Marla Cervantes wrote:

 Monday, January 29, 2018, 09:26

35 circles of 14 mm diameter were packed into a graphite sample container.

35 x UO2/C circles = 4.94 g

Graphite container = 5.03 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 new Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


 

 Monday, January 29, 2018, 11:06

A power outage around 10 am tripped off EVAP1.

 Monday, January 29, 2018, 14:22

Water flow turned on.

Chamber set to pumping down. 


 

 Tuesday, January 30, 2018, 16:06

Initial IGP1 = 9.4x10e-7 Torr

Tapped up entire process manually to 520A in 32 min

TGHT = 520 A, 5.45 V

Vacuum coming down indicating carbonization process complete 

Will remain at max setpoint for 4 hrs to ensure full carbonization before cooling down.


 Tuesday, January 30, 2018, 18:40

 Initiating auto-cool at 2.0 A/min 


 Wednesday, January 31, 2018, 14:00

Ar tank was changed.


Thursday, February 01, 2018, 12:58 

EVAP1 was vented with Argon and UCx was removed form evaporator 1.

 

Attachment 1: Carbonization-Batch7-300118.docx
  188   Thursday, February 01, 2018, 13:15 Marla CervantesUO2/C40282-1TARGET BOATDoneCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#8

 Thursday, February 01, 2018, 12:59

35 circles of 14 mm diameter were packed into a graphite sample container.

28 discs corresponded to cats#1 and 7 discs to cast#2

35 x UO2/C circles = 3.42 g

Graphite container = 6.96 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 new Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


 Friday, February 02, 2018, 13:18

Initial IGP1 = 4.82x10e-7 Torr

Tapped up entire process manually to 520A in 30 min

TGHT = 520 A, 5.63 V

Vacuum coming down nicely indicating carbonization process complete 

Will remain at max setpoint for 4 hrs to ensure full carbonization before cooling down.


 Friday, February 02, 2018, 16:57

Initiating auto-cool at 2.0 A/min 


Monday, February 05, 2018, 17:23 

Vented with Argon and removed form evaporator 1

Attachment 1: Carbonization-Batch8-020218.docx
  189   Monday, February 05, 2018, 17:26 Marla CervantesUO2/C40282-1TARGET BOATDoneCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#9

Monday, February 05, 2018, 17:24

35 circles from cast#2 of 14 mm diameter were packed into a graphite sample container.

35 x UO2/C circles = 4.59 g

Graphite container = 5.3 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 new Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


 Tuesday, February 06, 2018, 10:59

Initial IGP1 = 4.79e-7 Torr

Tapped up entire process manually to 520A in 30 min

TGHT = 520 A, 5.32 V

Vacuum coming down indicating carbonization process complete.  

Will remain at max setpoint for 4 hrs to ensure full carbonization before cooling down.


 Tuesday, February 06, 2018, 14:44

Initiating auto-cool at 2.0 A/min 


 Thursday, February 08, 2018, 10:43

Vented with Ar and removed from EVAP1


 

Attachment 1: Carbonization-Batch9-060218.docx
  190   Thursday, February 08, 2018, 14:51 Marla CervantesUO2/C40282-2 TARGET BOATProblemsCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#10

 Thursday, February 08, 2018, 14:50

35 circles from cast#2 of 14 mm diameter were packed into a graphite sample container.

35 x UO2/C circles = 4.76 g

Graphite container = 5.3 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 new Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


 Friday, February 09, 2018, 10:40

Initial IGP1 = 4.54e-7 Torr

Tapped up entire process manually to 520A in 25 min

TGHT = 520 A, 5.49 V

Vacuum coming down indicating carbonization process complete.  

Current suddenly tripped off from 520 A to 0 A.

There was not a power outage.

There was good vacuum.

Water cooling did not trip off 


 

  191   Friday, February 09, 2018, 16:57 Marla CervantesUO2/C40282-2 TARGET BOATProblems resolvedCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#10

Marla Cervantes wrote:

 Thursday, February 08, 2018, 14:50

35 circles from cast#2 of 14 mm diameter were packed into a graphite sample container.

35 x UO2/C circles = 4.76 g

Graphite container = 5.3 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 new Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


 Friday, February 09, 2018, 10:40

Initial IGP1 = 4.54e-7 Torr

Tapped up entire process manually to 520A in 25 min

TGHT = 520 A, 5.49 V

Vacuum coming down indicating carbonization process complete.  

Current suddenly tripped off from 520 A to 0 A.

There was not a power outage.

There was good vacuum.

Water cooling did not trip off 


 

 Friday, February 09, 2018, 16:49

The power supply was tested and its working normally.

Apparently a glitch on EPICS caused the tripped off.


 

  192   Friday, February 09, 2018, 17:04 Marla CervantesUO2/C40282-2 TARGET BOATDoneCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#10

Marla Cervantes wrote:

Marla Cervantes wrote:

 Thursday, February 08, 2018, 14:50

35 circles from cast#2 of 14 mm diameter were packed into a graphite sample container.

35 x UO2/C circles = 4.76 g

Graphite container = 5.3 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 new Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


 Friday, February 09, 2018, 10:40

Initial IGP1 = 4.54e-7 Torr

Tapped up entire process manually to 520A in 25 min

TGHT = 520 A, 5.49 V

Vacuum coming down indicating carbonization process complete.  

Current suddenly tripped off from 520 A to 0 A.

There was not a power outage.

There was good vacuum.

Water cooling did not trip off 


 

 Friday, February 09, 2018, 16:49

The power supply was tested and its working normally.

Apparently a glitch on EPICS caused the tripped off.


 

 Friday, February 09, 2018, 17:00

Target remained in EVAP1 for 2 hours at 0 A to ensure cooling.

EVAP1 was vented with Ar and the target was removed from EVAP1.

Graphite container seems unbroken.

Ta boat looks unbroken.

Attachment 1: 20180209_153539.jpg
20180209_153539.jpg
Attachment 2: 20180209_153728.jpg
20180209_153728.jpg
Attachment 3: 20180209_153817.jpg
20180209_153817.jpg
Attachment 4: Carbonization-current_trippoff.JPG
Carbonization-current_trippoff.JPG
Attachment 5: Carbonization-Batch10-090218.docx
  193   Tuesday, February 13, 2018, 11:44 Marla CervantesUO2/C40282-1TARGET BOATProblemsCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#11

 Tuesday, February 13, 2018, 11:39

35 circles of 14 mm diameter were packed into a graphite sample container.

35 x UO2/C circles = 5.74 g

Graphite container = 5.20 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 used Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


 Tuesday, February 13, 2018, 15:30

Initial IGP1 = 2.73x10e-6 Torr

Tapped up entire process manually to 520 A in 30 min

TGHT = 520 A, 5.41 V

Vacuum coming down nicely indicating carbonization process complete.

Current trip off after 5 min of being at 520 A.


 Wednesday, February 14, 2018, 15:32

EVAP1 vented with Argon and the target was removed.

Target was transferred to glove box.

Ta boat and graphite container look unbroken.

Attachment 1: Carbonization-current_trippoff2.JPG
Carbonization-current_trippoff2.JPG
Attachment 2: Ta-Boat.jpg
Ta-Boat.jpg
Attachment 3: C-Container.jpg
C-Container.jpg
  195   Friday, March 02, 2018, 16:35 Marla CervantesUO2/C40282-1TARGET BOATProblems resolvedCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#11

Marla Cervantes wrote:

 Tuesday, February 13, 2018, 11:39

35 circles of 14 mm diameter were packed into a graphite sample container.

35 x UO2/C circles = 5.74 g

Graphite container = 5.20 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 used Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


 Tuesday, February 13, 2018, 15:30

Initial IGP1 = 2.73x10e-6 Torr

Tapped up entire process manually to 520 A in 30 min

TGHT = 520 A, 5.41 V

Vacuum coming down nicely indicating carbonization process complete.

Current trip off after 5 min of being at 520 A.


 Wednesday, February 14, 2018, 15:32

EVAP1 vented with Argon and the target was removed.

Target was transferred to glove box.

Ta boat and graphite container look unbroken.

 Friday, March 02, 2018, 16:31

A test was performed in EVAP1 (see log ID 194):

- A Ta boat without Ta shielding was submitted to 520 A and it remained at that current point overnight.

-No trip off

  196   Friday, March 02, 2018, 16:35 Marla CervantesUO2/C40282-1TARGET BOATDoneCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#11

Marla Cervantes wrote:

Marla Cervantes wrote:

 Tuesday, February 13, 2018, 11:39

35 circles of 14 mm diameter were packed into a graphite sample container.

35 x UO2/C circles = 5.74 g

Graphite container = 5.20 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 used Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


 Tuesday, February 13, 2018, 15:30

Initial IGP1 = 2.73x10e-6 Torr

Tapped up entire process manually to 520 A in 30 min

TGHT = 520 A, 5.41 V

Vacuum coming down nicely indicating carbonization process complete.

Current trip off after 5 min of being at 520 A.


 Wednesday, February 14, 2018, 15:32

EVAP1 vented with Argon and the target was removed.

Target was transferred to glove box.

Ta boat and graphite container look unbroken.

 Friday, March 02, 2018, 16:31

A test was performed in EVAP1 (see log ID 194):

- A Ta boat without Ta shielding was submitted to 520 A and it remained at that current point overnight.

-No trip off

 

  197   Monday, March 12, 2018, 11:14 Marla CervantesUO2/C40282-2 TARGET BOATDoneCarbonizing UO2/C discs for 1stepUCx in graphite sample container _#12

 Monday, March 12, 2018, 9:13

35 circles from cast#2 of 14 mm diameter were packed into a graphite sample container.

35 x UO2/C circles = 5.21 g

Graphite container = 6.85 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


 Monday, March 12, 2018, 13:57

Initial IGP1 = 4.79e-7 Torr

Tapped up entire process manually to 520A in 30 min

TGHT = 520 A, 5.32 V

Vacuum coming down indicating carbonization process complete.  

Will remain at max setpoint for 1 hrs to ensure full carbonization before cooling down.


 Monday, March 12, 2018, 14:57 

Cooling down rate used 3 A/10s.


 Tuesday, March 13, 2018, 18:22

Vented with Ar and removed from EVAP1

  199   Wednesday, March 28, 2018, 11:46 Laura LambertUO2/C40282-2TARGET BOATIn progressCarbonizing first full length 1step UCx target

 Wednesday, March 28, 2018, 11:35

D-shaped discs were cut from cast 2, the same as the last sample of 1stepUCx [see elog i.d. 197]

A 13mm punch was used to punch out discs from pre-cut strips using the old method.

The target consists of 195 discs with 8.1cm in length - all single discs, no packs.

195 x UO2/C discs = 19.79g

Graphite insert is placed inside a target boat with both endcaps on.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers of heat shield and installed in evap1 yesterday afternoon.

Chamber pumped down overnight.


 Wednesday, March 28, 2018, 13:33

IGP1 = 4.03e-7 Torr

Tapped up TGHT manually to 80A, 0.83V - waited 50min, vacuum started to drop/stabilize.

Continued to tap up manually to 430A, 4.22V

Started out slow with a rate of ~10A/5min, and slowly increased to a rate of ~10A/min as vacuum stabilized, slowing down again when reaching carbonization outgassing.

Auto ramp at 0.2A/min from 430A-520A.


Thursday, March 29, 2018, 10:04

Reached 520A around 2am.

TGHT = 520A, 5.13V

IGP1 = 1.74e-6 Torr

Initiated auto-cool this morning at a rate of 1.0A/min.


 

  200   Monday, April 09, 2018, 16:51 Laura LambertUO2/C40282-2TARGET BOATProblemsCarbonizing first full length 1step UCx target

Laura Lambert wrote:

 Wednesday, March 28, 2018, 11:35

D-shaped discs were cut from cast 2, the same as the last sample of 1stepUCx [see elog i.d. 197]

A 13mm punch was used to punch out discs from pre-cut strips using the old method.

The target consists of 195 discs with 8.1cm in length - all single discs, no packs.

195 x UO2/C discs = 19.79g

Graphite insert is placed inside a target boat with both endcaps on.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers of heat shield and installed in evap1 yesterday afternoon.

Chamber pumped down overnight.


 Wednesday, March 28, 2018, 13:33

IGP1 = 4.03e-7 Torr

Tapped up TGHT manually to 80A, 0.83V - waited 50min, vacuum started to drop/stabilize.

Continued to tap up manually to 430A, 4.22V

Started out slow with a rate of ~10A/5min, and slowly increased to a rate of ~10A/min as vacuum stabilized, slowing down again when reaching carbonization outgassing.

Auto ramp at 0.2A/min from 430A-520A.


Thursday, March 29, 2018, 10:04

Reached 520A around 2am.

TGHT = 520A, 5.13V

IGP1 = 1.74e-6 Torr

Initiated auto-cool this morning at a rate of 1.0A/min.


 

 Monday, April 09, 2018, 16:00

ISAC controls performed a PLC switch over compromising the nuclear ventilation controls WITHOUT NOTIFYING ME  

This is the 2nd time in a month this has happened without being notified.

Evap1 has therefore tripped.

During this switch there was a problem which caused the turn over to take even longer.

Sat here tapping reset until nuclear ventilation was 'back on'.

Vacuum proceeded to drop once the tests were complete, then started to spike again, nuc vent remained not ok after tests were done nuc vent ok.


 

Attachment 1: evap1_trip.JPG
evap1_trip.JPG
Attachment 2: evap1_trip_archive.JPG
evap1_trip_archive.JPG
  201   Monday, April 09, 2018, 16:53 Laura LambertUO2/C40282-2TARGET BOATProblems resolvedCarbonizing first full length 1step UCx target

Laura Lambert wrote:

Laura Lambert wrote:

 Wednesday, March 28, 2018, 11:35

D-shaped discs were cut from cast 2, the same as the last sample of 1stepUCx [see elog i.d. 197]

A 13mm punch was used to punch out discs from pre-cut strips using the old method.

The target consists of 195 discs with 8.1cm in length - all single discs, no packs.

195 x UO2/C discs = 19.79g

Graphite insert is placed inside a target boat with both endcaps on.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers of heat shield and installed in evap1 yesterday afternoon.

Chamber pumped down overnight.


 Wednesday, March 28, 2018, 13:33

IGP1 = 4.03e-7 Torr

Tapped up TGHT manually to 80A, 0.83V - waited 50min, vacuum started to drop/stabilize.

Continued to tap up manually to 430A, 4.22V

Started out slow with a rate of ~10A/5min, and slowly increased to a rate of ~10A/min as vacuum stabilized, slowing down again when reaching carbonization outgassing.

Auto ramp at 0.2A/min from 430A-520A.


Thursday, March 29, 2018, 10:04

Reached 520A around 2am.

TGHT = 520A, 5.13V

IGP1 = 1.74e-6 Torr

Initiated auto-cool this morning at a rate of 1.0A/min.


 

 Monday, April 09, 2018, 16:00

ISAC controls performed a PLC switch over compromising the nuclear ventilation controls WITHOUT NOTIFYING ME  

This is the 2nd time in a month this has happened without being notified.

Evap1 has therefore tripped.

During this switch there was a problem which caused the turn over to take even longer.

Sat here tapping reset until nuclear ventilation was 'back on'.

Vacuum proceeded to drop once the tests were complete, then started to spike again, nuc vent remained not ok after tests were done nuc vent ok.


 

 Monday, April 09, 2018, 16:52

Turns out I wasn't on a list of ppl who need to know about this test when I should be

They also didn't reset the alarms locally outside the hot lab so nuc vent remained not ok until this was reset.

IGP1 reached 0.027 Torr before nuc vent was ok and pumps were able to be turned back on 

Pumps back on IGP1 = 1.86e-5 Torr and still pumping down


 

  202   Tuesday, April 10, 2018, 14:49 Laura LambertUO2/C40282-2TARGET BOATDoneCarbonizing first full length 1step UCx target

Laura Lambert wrote:

Laura Lambert wrote:

Laura Lambert wrote:

 Wednesday, March 28, 2018, 11:35

D-shaped discs were cut from cast 2, the same as the last sample of 1stepUCx [see elog i.d. 197]

A 13mm punch was used to punch out discs from pre-cut strips using the old method.

The target consists of 195 discs with 8.1cm in length - all single discs, no packs.

195 x UO2/C discs = 19.79g

Graphite insert is placed inside a target boat with both endcaps on.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers of heat shield and installed in evap1 yesterday afternoon.

Chamber pumped down overnight.


 Wednesday, March 28, 2018, 13:33

IGP1 = 4.03e-7 Torr

Tapped up TGHT manually to 80A, 0.83V - waited 50min, vacuum started to drop/stabilize.

Continued to tap up manually to 430A, 4.22V

Started out slow with a rate of ~10A/5min, and slowly increased to a rate of ~10A/min as vacuum stabilized, slowing down again when reaching carbonization outgassing.

Auto ramp at 0.2A/min from 430A-520A.


Thursday, March 29, 2018, 10:04

Reached 520A around 2am.

TGHT = 520A, 5.13V

IGP1 = 1.74e-6 Torr

Initiated auto-cool this morning at a rate of 1.0A/min.


 

 Monday, April 09, 2018, 16:00

ISAC controls performed a PLC switch over compromising the nuclear ventilation controls WITHOUT NOTIFYING ME  

This is the 2nd time in a month this has happened without being notified.

Evap1 has therefore tripped.

During this switch there was a problem which caused the turn over to take even longer.

Sat here tapping reset until nuclear ventilation was 'back on'.

Vacuum proceeded to drop once the tests were complete, then started to spike again, nuc vent remained not ok after tests were done nuc vent ok.


 

 Monday, April 09, 2018, 16:52

Turns out I wasn't on a list of ppl who need to know about this test when I should be

They also didn't reset the alarms locally outside the hot lab so nuc vent remained not ok until this was reset.

IGP1 reached 0.027 Torr before nuc vent was ok and pumps were able to be turned back on 

Pumps back on IGP1 = 1.86e-5 Torr and still pumping down


 

 Tuesday, April 10, 2018, 14:46

Glove box fixed!

Vented in Argon and transferred to glove box.

Graphite insert has moved to within 1mm of the end of the left side of the boat.

This could have happened during removal from evap1, hard to tell.

Either way, clearly a looser fit of the graphite insert in the boat indicating possible shrinkage of graphite insert.


 

  203   Tuesday, April 17, 2018, 12:45 Laura LambertUO2/C40282-2TARGET BOATDoneProcessing UC2Flk_20

 Tuesday, April 17, 2018, 10:30

UO2/C green was prepared April 12th, 2018

The cast peeled off the glass nicely April 13th, 2018

Initial UO2 powder used = 50.56g (Inventory R-01032A, UO2 + bottle = 626.28g before use)

Graphite powder used = 10.38g

Green cast dried UO2/C + organic mass = 61.40g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-layers of heat shield [1 reused, 2 new] and installed in evap1 yesterday.

Chamber pumped down overnight.

IGP1 = 8.4e-7 Torr

Tapped up to 35A, 0.46V

Waited ~135min, vacuum stable.

IGP1 = 1.6e-5 Torr

Initiating auto-ramp at 0.2A/min

Target boat will be ramped up to 520A.

Vacuum limit stop at 3.0e-4 Torr, backing off at 6.0e-4 Torr.


 Wednesday, April 18, 2018, 09:21

IGP1 = 9.6e-6 Torr

TGHT = 245A, 2.10V

Vacuum stable, increasing ramping rate to 0.5A/min.


 Thursday, April 19, 2018, 08:35

IGP1 = 3.21e-6 Torr

Materials have finished carbonizing.

TGHT = 520A, 4.97V

Evap1 has remained at max setpoints for ~6.5hrs

Initiating auto-cool at 1.0A/min


 Thursday, May 10, 2018, 10:33

Materials were vented in Ar and transferred to glove box on April 20th


 

  205   Friday, May 18, 2018, 18:38 Marla CervantesUO2/C40282-1TARGET BOATDoneCarbonizing UO2/C discs for 1stepUCx in graphite sample container #13

 Friday, May 18, 2018, 18:32

35 circles of 14 mm diameter of cast #3 were packed into a graphite sample container.

40 x UO2/C circles = 4.58 g

Graphite container mass = 6.95 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 used Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


Saturday, May 19, 2018, 07:30 

Initial IGP1 = 6.27e-7 Torr

 Tapped to 80A at 10A/10s with 20 s waiting period each 10 A

 Waited 4 min for vacuum to stabilize.

 Tapped to 100 A at 10A/10s with 20 s waiting period each 10 A

 Waited 12 min for vacuum

Tapped to 400 A at 25A/30s with 30 s waiting period each 25 A

Tapped to 520 A at 20A/30s with 30 s waiting period each 20 A

Pressure dropping indicates carbonization complete.

Current tripped off, vacuum was ok, water cooling was ok.

Saturday, May 19, 2018, 10:00 

Current was returned to 520 A manually

Tapped to 100 A at 10A/10s with 20 s waiting period each 10 A 

Tapped to 400 A at 25A/30s with 30 s waiting period each 25 A

Tapped to 520 A at 20A/30s with 30 s waiting period each 20 A

The discs will stay at max current for 4 hrs


 Saturday, May 19, 2018, 18:31

Vented with Argon and removed form evaporator 1

Attachment 1: 180519-B13-Current_trip_off.JPG
180519-B13-Current_trip_off.JPG
  206   Friday, May 25, 2018, 15:38 Marla CervantesUO2/C40282-1TARGET BOATDoneCarbonizing full length 1-step UCx target #2

Friday, May 25, 2018, 15:34 

D-shaped discs were cut from cast 3

A 13mm punch was used to punch out discs from pre-cut strips using the old method.

The target consists of 205 discs with 10 cm in length - all single discs, no packs.

205 x UO2/C discs = 22.04 g

Graphite insert with caps is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers of heat shield and installed in evap1.

Chamber is pumping down.


 Saturday, May 26, 2018, 10:39

Current tapped manually to 80 A at 1A/s in 10 A blocks with a waiting period of 20 s between each increment

18 min waiting for pressure stabilization

Current tapped to 100 A in same rate


Saturday, May 26, 2018, 10:51 

After 9 min current was reduced to 60 A to reduce pressure.

Cuerrent was tapped to 100 A

After 10 min the rate was increased to 25 A each 20 s until 450 A

The rate was changed to 10 A each 2 min until 500 A

Last 20 A were tapped after 1 min 


Saturday, May 26, 2018, 15:41 

After 4hrs the current was reduced in a rate of 10 A /min


Monday, May 28, 2018, 12:45 

EVAPI was vented with Ar and UCx was transferred to glove box.

  208   Wednesday, June 13, 2018, 10:20 Marla CervantesUO2/C40282-1TARGET BOATIn progressCarbonizing UO2/C discs for 1stepUCx in graphite sample container #14

 Tuesday, June 12, 2018, 18:20

35 circles of 14 mm diameter of cast #4 were packed into a graphite sample container.

30 x UO2/C circles = 4.07 g

Graphite container mass = 5.3 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 used Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


Wednesday, June 13, 2018, 10:29 

Initial IGP1 = 6.43e-7 Torr

Tapped to 80A at 10A/10s with 20 s waiting period each 10 A

Waited 5 min for vacuum to stabilize.

Tapped to 90 A at 10A/10s with 20 s waiting period each 10 A

Waited 5 min to tap to 100 A 

Waited 14 min for vacuum to stabilize

Tapped to 400 A at 25A/30s with 30 s waiting period each 25 A

Tapped to 520 A at 20A/30s with 30 s waiting period each 20 A

Max pressure ~0.06 Torr 

  209   Wednesday, June 13, 2018, 11:09 Marla CervantesUO2/C40282-1TARGET BOATProblemsCarbonizing UO2/C discs for 1stepUCx in graphite sample container #14

Marla Cervantes wrote:

 Tuesday, June 12, 2018, 18:20

35 circles of 14 mm diameter of cast #4 were packed into a graphite sample container.

30 x UO2/C circles = 4.07 g

Graphite container mass = 5.3 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 used Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


Wednesday, June 13, 2018, 10:29 

Initial IGP1 = 6.43e-7 Torr

Tapped to 80A at 10A/10s with 20 s waiting period each 10 A

Waited 5 min for vacuum to stabilize.

Tapped to 90 A at 10A/10s with 20 s waiting period each 10 A

Waited 5 min to tap to 100 A 

Waited 14 min for vacuum to stabilize

Tapped to 400 A at 25A/30s with 30 s waiting period each 25 A

Tapped to 520 A at 20A/30s with 30 s waiting period each 20 A

Max pressure ~0.06 Torr 

 Wednesday, June 13, 2018, 11:08

Pressure was dropping indicating full carbothermal reduction but the current tripped off to 0 A.

  210   Wednesday, June 13, 2018, 12:25 Marla CervantesUO2/C40282-1TARGET BOATDoneCarbonizing UO2/C discs for 1stepUCx in graphite sample container #14

Marla Cervantes wrote:

Marla Cervantes wrote:

 Tuesday, June 12, 2018, 18:20

35 circles of 14 mm diameter of cast #4 were packed into a graphite sample container.

30 x UO2/C circles = 4.07 g

Graphite container mass = 5.3 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 used Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


Wednesday, June 13, 2018, 10:29 

Initial IGP1 = 6.43e-7 Torr

Tapped to 80A at 10A/10s with 20 s waiting period each 10 A

Waited 5 min for vacuum to stabilize.

Tapped to 90 A at 10A/10s with 20 s waiting period each 10 A

Waited 5 min to tap to 100 A 

Waited 14 min for vacuum to stabilize

Tapped to 400 A at 25A/30s with 30 s waiting period each 25 A

Tapped to 520 A at 20A/30s with 30 s waiting period each 20 A

Max pressure ~0.06 Torr 

 Wednesday, June 13, 2018, 11:08

Pressure was dropping indicating full carbothermal reduction but the current tripped off to 0 A.

 Wednesday, June 13, 2018, 12:23

The problem was reported to controls group

After 1 hour at 0 A, the autoramp was set to 4 A/min up to 520 A

The current and voltage are increasing accordingly.

The material will stay 4 hours at max point.


Thursday, June 14, 2018, 09:14 

After 4 hours the auto ramp was set to -1A/min to 0 A


Thursday, June 14, 2018, 14:47 

The IEVAP  was vented with Ar and the UCx was trasnferred to the glove box.

  211   Tuesday, June 19, 2018, 15:39 Marla CervantesUO2/C40282-1TARGET BOATDoneCarbonizing UO2/C discs for 1stepUCx in graphite sample container #15

 Friday, June 15, 2018, 16:39

35 circles of 14 mm diameter of cast #3 were packed into a graphite sample container.

35 x UO2/C circles = 4.07 g

Graphite container mass = 5.3 g

Graphite tube is placed inside a target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3 used Ta foils for heat shielding and the boat was installed in Evap1.

Chamber currently pumping down.


 Saturday, June 16, 2018, 15:00

Tapped to 80A at 10A/10s with 20 s waiting period each 10 A

Waited 5 min for vacuum to stabilize.

Tapped to 90 A at 10A/10s with 20 s waiting period each 10 A

Waited 14 min for vacuum to stabilize

Tapped to 100 A at 10A/10s with 20 s waiting period each 10 A

Tapped to 400 A at 25A/25s with 20 s waiting period each 25 A

Tapped to 520 A at 20A/20s with 20 s waiting period each 20 A


 Tuesday, June 19, 2018, 15:51 

 The material will be in the evap for a week

Wednesday, June 27, 2018, 09:53 

 The IEVAP  was vented with Ar and the UCx was trasnferred to the glove box.

  214   Wednesday, July 11, 2018, 17:44 John WongUO2/C TARGET BOATDoneProcessing UC2Flk_21

Wednesday, July 11, 2018, 17:41

Cast prepared by Marla (see note in Hotlab)

Target boat contained about 50g UO2 powder. 

TGHT will be ramped up to 520A.

Vacuum limit stop at 3.0 e-4 Torr, backing off at 6.0e-4 Torr. 

Chamber is currently being pumped down


 Thursday, July 12, 2018, 10:45

Pressure at 8.9e-7 Torr. 

Initiate auto ramping TGHT at 0.1A/min to reach 580A (will monitor vacuum to ensure complete carbonization)


 Wednesday, July 18, 2018, 10:23

TGTH at 369A/3.7V, carbonization in progress. 

Pressure limited was set to 5.0e-5 Torr; change limit to 6e-4 Torr (as indicated above)

Increase ramping rate to 0.2A/min.


 Thursday, July 19, 2018, 12:12

Completion of the U-carbonization has been reached. 

Cooling down TGHT at 2A/min

Chamber will be vented in Ar and materials will be transferred to Ar glovebox


 

  219   Saturday, September 29, 2018, 19:04 John WongUO2/C TARGET BOATIn progressProcessing UC2_flk_22

Saturday, September 29, 2018, 18:52

Cast is from Jar#1.  (see process sheet for details)

Target boat contains about 50g UO2 powder. 

TGHT will be ramped up to 520A; fast tapping can be done, see elog#211, or set to autoramping with higher vacuum limit (1setup UCx process with pressure up to 60mTorr, see elog #210)

Chamber is currently being pumped down


 Saturday, September 29, 2018, 21:21

Pressure at 2.6e-5 Torr.

Tapping up TGHT in process


 Saturday, September 29, 2018, 21:32

Tapped to 80A/0.65V.  Wait for vacuum to stabilize.


 Saturday, September 29, 2018, 21:42

Pressure stabilized at 2.5mTorr.

Tapping up to 90A/0.701V


Saturday, September 29, 2018, 21:44

Pressure stabilized at 2.7m Torr; tapping up to 100A/0.77V


Saturday, September 29, 2018, 23:57

TGHT at 520A/4394V (see attachment for striptool capture).  Pressure at 163mTorr and coming down.


 Sunday, September 30, 2018, 12:56

At around midnight, pressure was coming down from 160 mTorr to 21 mTorr before TGHT tripped off (see attachment#2).

I suspect the TP was working too hard causing it to trip.

Pressure at 2.1e-6 Torr. 

Using auto-ramping.  Set good vac at 2.0e-4 Torr, bad vac at 5.0e-4 Torr.  Ramping TGHT at 2A/min to reah 520A.


 Sunday, September 30, 2018, 17:11

Pressure limiting at 0.2 mTorr as TGHT slowly ramping up, currently at 442A;  (see attachment#3).


 Monday, October 01, 2018, 21:15

TGHT was held at 520A for at least a day.  Vac at 3.7e-6 Torr.  Ramping down TGHT at 2A/min.


 

Attachment 1: striptool_capture.JPG
striptool_capture.JPG
Attachment 2: TGHT_tripped.JPG
TGHT_tripped.JPG
Attachment 3: pressure_limiting.JPG
pressure_limiting.JPG
  222   Monday, October 22, 2018, 17:58 Marla CervantesUO2/C27252-1TARGET BOATProblemsProcessing UC2Flk_22

Monday, October 22, 2018, 17:55 

UO2/C green was prepared , September 24, 2018

Initial UO2 powder used = 50.11 g (Inventory R-01032A, UO2 + bottle = 374.03 g before use)

Graphite powder used = 10.13 g

Green cast dried UO2/C + organic mass = 62.45 g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-layers of heat shield [2 reused, 1 new] and installed in evap1.

Currently pumping down.


 Tuesday, October 23, 2018, 15:38

IGP1 = 2.44e-6 Torr,

Tapped to 60 A at 10A/10s with 20 s waiting every 10 A,

Waited 28 min to vacuum to stabilize,

tapped to 80 A at 10A/10s with 20 s waiting every 10 A,

max pressure 7x10-3 Torr, waited 50 min to vacuum to drop

Tapped to 100 A at 10A/10s with 20 s waiting every 10 A,

max pressure 4x10-2 Torr, tapped current to 80 A,

The pressure was dropping, when it was at 2x10-2 Torr, the current tripped off.

IGP1 = 1x10-4 Torr

Tapped back to 60 A at 10A/10s with 20 s waiting every 10 A,

waited 5 min to tap to 80 A at same rate

waited 5 min to tap to 100 A at same rate

waited 25 min to vacuum to drop from 2e-2 Torr to 8e-4Torr

Tapped to 110 A at same rate

waited 3 min  to tap to 120 A at same rate

waited 1 min  to tap to 130 A at same rate

waited 1 min  to tap to 140 A at same rate
 
waited 15 min to pressure to drop from 6e-2 Torr to 7e-4 Torr
 
Changing manual rate to 10A/10s with waiting periods of 1 min, current was increased from 140 A to 260 A with this rate.
 
Changing manual rate to 20A/10s with waiting periods of 30 s, current was increased from 260 A to 480 A with this rate.
 
Waiting 4 min for the pressure to increase.
 
Changing the rate to 5A/30s, tapped until 510 A,
 
Changing the waiting period to 1 min, kept tapping to 530 A,
 
The pressure was dropping, when it was at 2x10-2 Torr, the current tripped off
 
The vacuum limit is 5e-1 Torr, and the pressure was dropping, there was no reason for the current to trip.
 
The pumps seems to be fine in the hot lab.
Attachment 1: current-trip-1.jpg
current-trip-1.jpg
Attachment 2: current-trip-2.jpg
current-trip-2.jpg
  226   Wednesday, October 24, 2018, 20:01 Marla CervantesUO2/C27252-1TARGET BOATProblemsProcessing UC2Flk_22

Marla Cervantes wrote:

Monday, October 22, 2018, 17:55 

UO2/C green was prepared , September 24, 2018

Initial UO2 powder used = 50.11 g (Inventory R-01032A, UO2 + bottle = 374.03 g before use)

Graphite powder used = 10.13 g

Green cast dried UO2/C + organic mass = 62.45 g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-layers of heat shield [2 reused, 1 new] and installed in evap1.

Currently pumping down


 Tuesday, October 23, 2018, 15:38

IGP1 = 2.44e-6 Torr,

Tapped to 60 A at 10A/10s with 20 s waiting every 10 A,

Waited 28 min to vacuum to stabilize,

tapped to 80 A at 10A/10s with 20 s waiting every 10 A,

max pressure 7x10-3 Torr, waited 50 min to vacuum to drop

Tapped to 100 A at 10A/10s with 20 s waiting every 10 A,

max pressure 4x10-2 Torr, tapped current to 80 A,

The pressure was dropping, when it was at 2x10-2 Torr, the current tripped off.

IGP1 = 1x10-4 Torr

Tapped back to 60 A at 10A/10s with 20 s waiting every 10 A,

waited 5 min to tap to 80 A at same rate

waited 5 min to tap to 100 A at same rate

waited 25 min to vacuum to drop from 2e-2 Torr to 8e-4Torr

Tapped to 110 A at same rate

waited 3 min  to tap to 120 A at same rate

waited 1 min  to tap to 130 A at same rate

waited 1 min  to tap to 140 A at same rate
 
waited 15 min to pressure to drop from 6e-2 Torr to 7e-4 Torr
 
Changing manual rate to 10A/10s with waiting periods of 1 min, current was increased from 140 A to 260 A with this rate.
 
Changing manual rate to 20A/10s with waiting periods of 30 s, current was increased from 260 A to 480 A with this rate.
 
Waiting 4 min for the pressure to increase.
 
Changing the rate to 5A/30s, tapped until 510 A,
 
Changing the waiting period to 1 min, kept tapping to 530 A,
 
The pressure was dropping, when it was at 2x10-2 Torr, the current tripped off
 
The vacuum limit is 5e-1 Torr, and the pressure was dropping, there was no reason for the current to trip.
 
The pumps seems to be fine in the hot lab.

 Wednesday, October 24, 2018, 17:51

Rod from controls checked on the system, seems that the controls are not the cause of the trip

Rod suggested that the power supply might be overheating, 

thermocouples were installed on the surface of the power supply to register the temperature during the process

Tapping the current up again at accelerated rate see spread sheet for details.

Since pressure was not decreasing the current was increased to 595 A (rate 1A/min) [see figure CT-2]

The power supply's maximum temperature was 32.7 C which is a difference of 9.7 degrees with respect to the initial temperature. 

The target will remain at maximum temperature overnight.

Attachment 1: PowerSupply-TempLog.xlsx
Attachment 2: CT-2.jpg
CT-2.jpg
  227   Thursday, October 25, 2018, 09:10 Marla CervantesUO2/C27252-1TARGET BOATDoneProcessing UC2Flk_22

Marla Cervantes wrote:

Marla Cervantes wrote:

Monday, October 22, 2018, 17:55 

UO2/C green was prepared , September 24, 2018

Initial UO2 powder used = 50.11 g (Inventory R-01032A, UO2 + bottle = 374.03 g before use)

Graphite powder used = 10.13 g

Green cast dried UO2/C + organic mass = 62.45 g 

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-layers of heat shield [2 reused, 1 new] and installed in evap1.

Currently pumping down.


 Tuesday, October 23, 2018, 15:38

IGP1 = 2.44e-6 Torr,

Tapped to 60 A at 10A/10s with 20 s waiting every 10 A,

Waited 28 min to vacuum to stabilize,

tapped to 80 A at 10A/10s with 20 s waiting every 10 A,

max pressure 7x10-3 Torr, waited 50 min to vacuum to drop

Tapped to 100 A at 10A/10s with 20 s waiting every 10 A,

max pressure 4x10-2 Torr, tapped current to 80 A,

The pressure was dropping, when it was at 2x10-2 Torr, the current tripped off.

IGP1 = 1x10-4 Torr

Tapped back to 60 A at 10A/10s with 20 s waiting every 10 A,

waited 5 min to tap to 80 A at same rate

waited 5 min to tap to 100 A at same rate

waited 25 min to vacuum to drop from 2e-2 Torr to 8e-4Torr

Tapped to 110 A at same rate

waited 3 min  to tap to 120 A at same rate

waited 1 min  to tap to 130 A at same rate

waited 1 min  to tap to 140 A at same rate
 
waited 15 min to pressure to drop from 6e-2 Torr to 7e-4 Torr
 
Changing manual rate to 10A/10s with waiting periods of 1 min, current was increased from 140 A to 260 A with this rate.
 
Changing manual rate to 20A/10s with waiting periods of 30 s, current was increased from 260 A to 480 A with this rate.
 
Waiting 4 min for the pressure to increase.
 
Changing the rate to 5A/30s, tapped until 510 A,
 
Changing the waiting period to 1 min, kept tapping to 530 A,
 
The pressure was dropping, when it was at 2x10-2 Torr, the current tripped off
 
The vacuum limit is 5e-1 Torr, and the pressure was dropping, there was no reason for the current to trip.
 
The pumps seems to be fine in the hot lab.

 Wednesday, October 24, 2018, 17:51

Rod from controls checked on the system, seems that the controls are not the cause of the trip

Rod suggested that the power supply might be overheating, 

thermocouples were installed on the surface of the power supply to register the temperature during the process

Tapping the current up again at accelerated rate see spread sheet for details.

Since pressure was not decreasing the current was increased to 595 A (rate 1A/min) [see figure CT-2]

The power supply's maximum temperature was 32.7 C which is a difference of 9.7 degrees with respect to the initial temperature. 

The target will remain at maximum temperature overnight.

 Thursday, October 25, 2018, 09:07

Carbothermal reduction completed

IGP1 =  1.22e-5 Torr

Maximum power supply's temperature 33.3 C

Ramping current down at 2 A/min.


Monday, October 29, 2018, 12:30

Transferring  UCx to glove box

Mass = 48.384 g

  231   Thursday, November 22, 2018, 17:32 Marla CervantesUO2/C40202-1TARGET BOATProblemsUCx Fully loaded graphite insert - UCx26

 Thursday, November 22, 2018, 17:25

D-shaped discs were cut from cast #26

A 13mm punch was used to punch out discs from pre-cut strips

The target consists of 236 discs of 10 cm in length - all single discs, no packs.

236 x UO2/C discs = 22.66 g

Graphite insert with caps = 11.74 g

The loaded inser is placed on target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers (2 new one used) of heat shield and installed in evap1.

Chamber is pumping down.


 Friday, November 23, 2018, 08:53

Vacuum limits:

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

IGP1 = 4.12 e-6 Torr

Current tapped manually to 100 A at 1A/s in 10 A blocks with a waiting period of 20 s between each increment.

Initial IGP1 = 5.31 e-6 Torr

Max  IGP1 = 0.066 Torr

Waited 20 min for pressure to rise and drop.

The current tripped off, when the 0.013 torr  (Fig. Nov23-CurrentTrip1).

Increasing the current to 100 A again.


IGP1 = 7.00e-5 Torr

Rate was increased to 25 A each 20 s until 200 A

The pressure increased and IV1 opened, current was dropped to 100 A

Pressure after 5 min 4e-4 Torr

Rate was increased again to 25 A each 20 s until 200 A

The current was reduced to 110 A because the pressure was rising to fast

Rate was increased again to 25 A each 20 s until 300 A

Pressure was ok and current tripped off  (Fig. Nov23-CurrentTrip2).

The automatic ramp was set to 20 A/ min from 0 to 300 A

The automatic ramp was changed to 10A/2min to 450 A

IGP1 = 2.15e-5 Torr

After 1.5 hour, the automatic ramp was set to 20 A/ min from 450 to 500 A

After 4hrs, the automatic ramp was set to -2 A/ min from 500 to 0 A

Attachment 1: Nov23-CurrenTrip1.jpg
Nov23-CurrenTrip1.jpg
Attachment 2: Nov23-CurrenTrip2.jpg
Nov23-CurrenTrip2.jpg
  232   Monday, November 26, 2018, 17:06 Marla CervantesUO2/C40202-1TARGET BOATDoneUCx Fully loaded graphite insert - UCx26

Marla Cervantes wrote:

 Thursday, November 22, 2018, 17:25

D-shaped discs were cut from cast #26

A 13mm punch was used to punch out discs from pre-cut strips

The target consists of 236 discs of 10 cm in length - all single discs, no packs.

236 x UO2/C discs = 22.66 g

Graphite insert with caps = 11.74 g

The loaded inser is placed on target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers (2 new one used) of heat shield and installed in evap1.

Chamber is pumping down.


 Friday, November 23, 2018, 08:53

Vacuum limits:

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

IGP1 = 4.12 e-6 Torr

Current tapped manually to 100 A at 1A/s in 10 A blocks with a waiting period of 20 s between each increment.

 

Initial IGP1 = 5.31 e-6 Torr

Max  IGP1 = 0.066 Torr

Waited 20 min for pressure to rise and drop.

The current tripped off, when the 0.013 torr. Increasing the current to 100 A again.


IGP1 = 7.00e-5 Torr

Rate was increased to 25 A each 20 s until 200 A

The pressure increased and IV1 opened, current was dropped to 100 A

Pressure after 5 min 4e-4 Torr

Rate was increased again to 25 A each 20 s until 200 A

The current was reduced to 110 A because the pressure was rising to fast

Rate was increased again to 25 A each 20 s until 300 A

Pressure was ok and current tripeed off

The automatic ramp was set to 20 A/ min from 0 to 300 A

The automatic ramp was changed to 10A/2min to 450 A

IGP1 = 2.15e-5 Torr

After 1.5 hour, the automatic ramp was set to 20 A/ min from 450 to 500 A

After 4hrs, the automatic ramp was set to -2 A/ min from 500 to 0 A

 Monday, November 26, 2018, 17:00

 The UCx was transferred to the glove box and loaded in  tantalum container  42218-3.

Attachment 1: CR-UCx26.png
CR-UCx26.png
  239   Monday, June 17, 2019, 08:58 Marla CervantesUO2/C TARGET BOATDoneUCx#27 Carbothermal reduction

Friday, June 14, 2019, 17:10

A 14 mm die was used to cut out discs from strips

The target consists of 236 discs of 10 cm in length - all single discs, no packs.

231 x UO2/C discs = 25.76 g

12 UO2 discs for measurements = 1.49 g

Graphite insert without caps= 11.59 g

The loaded insert is placed on target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers (2 new one used) of heat shield and installed in evap1.

Chamber is pumping down.


Monday, June 17, 2019, 08:56 

Pressure limits:

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

IGP1 = 6.600777e-7 Torr

Current tapped manually to 80 A at 1A/s in 10 A blocks with a waiting period of 20 s between each increment.

Initial IGP1 = 5.31 e-6 Torr


Monday, June 17, 2019, 10:03

After 42 minutes the pressure started dropping and the current rate was changed to 1A/s with for 20 second intervals followed by 20 second wait while monitoring pressure.


Monday, June 17, 2019, 14:41

Current was tapped to 100A but the pressure increased too rapidly; therefore, the current was tapped down to 75A.

After pressure stabilized, the current was tapped up to 100 A @1A/s in 20A segments and 20 second pauses.

Continued tapping up at the above rate until 160A, at which point the pressure shot up and tripped the system.

The pressure stabilized within 18 minutes.


The wait interval on the heater ramps control was changed to 1s

The current increment was set to 0.2A with a final value of 200A

At 170A the autoramp was stopped and the current manually tapped down to 160A to prevent rapid pressure buildup.

5 minutes later the pressure had stabilized and autramp was restarted.


At 160A we changed the waiting interval to 10s and the current increment to 2A.

At 200A we stopped autoramp and manually tapped at 1A/s in 20A segments with 10s pauses. 

At 360A, we changed the current increment to 1A while keeping the wait interval at 10s.

At 440A the autoramp was stopped to change the current increment to 0.5A while the waiting interval was kept at 10s.

The autoramp final current was set to 500A.

At 495A the autoramp was stopped because the pressure was dropping significantly.

The Target was left for 3 hours at 495A.


Pre-cooling conditions:

TGHT = 494A, 4.8V

IGP1 = 6.7e-6 Torr

Cooling rate = -2A/min

 

 

 

  240   Tuesday, July 30, 2019, 10:27 Marla CervantesUO2/C TARGET BOATDoneUCx#28 Carbothermal reduction

Friday, June 26, 2019, 17:10

A 13 mm die was used to cut out discs from strips

The target consists of 264 discs of 10 cm in length - all single discs, no packs.

231 x UO2/C discs = 25.76 g

10 UO2 discs for measurements = 1.49 g

Graphite insert without caps= 17.44 g

The loaded insert is placed on target boat.

Boat previously coated with TaC and sintered.

Ta-target boat is wrapped with 3-layers (3 used) of heat shield and installed in evap1.

Chamber is pumping down. 


Tuesday, July 30, 2019, 09:45

Pressure limits:

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

Initial vacuum IGP1 = 5.94e-7 Torr

Current tapped manually to 85 A at 1A/s in 5 A blocks with a waiting period of 25 s between each increment. 


Tuesday, July 30, 2019, 10:53

After 30 min, the pressure started stabilizing around 0.0013 g

The current rate was changed to 1 A/2min to 88 A

The current rate was changed to 1 A/min to 90 A


The current rate was changed to 1 A/30s to 100 A

The final pressure obtained was 0.0011 Torr


The current rate was changed to 2 A each 10 s to 170 A

The final pressure obtained was 0.04 Torr


The current rate was changed to 1 A each 10 s to 180 A

The final pressure obtained was 0.008 Torr


The current rate was changed to 2 A each 10 s to 200 A

The final pressure obtained was 0.002 Torr

The current rate was changed to 3.2 A each 10 s to 292 A

The final pressure was 0.001 Torr

The current was tapped manually to 400 A in intervals of 10 A at 1 A/s each 10 s


The autoramp was set to 1 A each 10 s to 450 A

Then the current was increased manually at 1 a each 20 s until 475 A

The current was increased in this manner until 480 A to make sure the pressure was not rising 


Tuesday, July 30, 2019, 12:00

After the pressure stabilized and started reducing the current was reduced to 480 A

After 3 hours at 475 A the autoramp was set to -2A/min

Attachment 1: UCx28.JPG
UCx28.JPG
  246   Wednesday, October 02, 2019, 11:10 Marla CervantesUO2/C TARGET BOATDoneUCx#29 Carbothermal reduction

 Wednesday, October 02, 2019, 11:09

A graphite cartridge loaded with UO2/C foils, wrapped with three Ta heat shields was placed in the EVAP1.

The EVAP1 is currently pumping down.


 Thursday, October 03, 2019, 09:40

Pressure limits:

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

Initial vacuum IGP1 = 9.54e-7 Torr

Current tapped manually to 80 A at 1A/s in 5 A blocks with a waiting period of 25 s between each increment. 


Thursday, October 03, 2019, 10:36

The pressure started decreasing after 45 min and the auto ramp was set to 1 A each 30 s to 86 A 

The autoramp was set to 2 A each 10 s to 180 A

The autoramp was set to 3.2 A each 10 s to 300 A

The autoramp was re start at 3.2 A each 10 s to 400 A 

The autoramp was set to 1 A each 10 s to 430 A 

The autoramp was set to 2 A each 10 s to 450 A 

The autoramp was set to 2 A each 10 s to 480 A 

Autoramp at 2 A per min to 500 A

Manually tapped to 545 A.

After 48 hrs at maximum temperature, the target was cooled done at -2 A/min 

Attachment 1: CarbothermalReduction-UCx29.JPG
CarbothermalReduction-UCx29.JPG
  248   Monday, October 28, 2019, 11:23 Marla CervantesUO2/C TARGET BOATIn progressUCx#30 Carbothermal Reduction

Monday, October 28, 2019, 10:29

A loaded graphite cartridge was set in a tantalum boated and wrapped with 3 tantalum sheets

The set up was installed in the EVAP1 and pumped dwon during the weekend.

IGP1 = 1.10 e-6 Torr


Monday, October 28, 2019, 10:31

Good vacuum = 1e-1 Torr

Bad vaccum = 5e-1 Torr

The current ramp is 1 A each 10 s from 0 A to 100 A


Monday, October 28, 2019, 11:13 

After 18 min the pressure started dropped.


Monday, October 28, 2019, 11:22 

When the pressure reduced to 5e-4 Torr the current ramp was changed to 3.3 A each 10 s to 480 A, the vacuum limits stayed the same.


Monday, October 28, 2019, 11:45

The limit was set to 500 A with same ramp


Monday, October 28, 2019, 11:48 

The ramp was changed to 1A/10s to 550 A


 Monday, October 28, 2019, 11:55

At 520 A the pressure reach 1e-1 Torr and the autoramp stopped


Monday, October 28, 2019, 13:39

the current was increased manually at aprox. 1A/30 s 

The current dropped suddenly even though the pressure was under the limits and the ramping was in the limits.

Autoramp was set to 3 A/ 10 s from to to 500 A

Then it was changed to 1 A  /30s from 500 to 506 A

Finally it was changed to 1 A/ 10 s from 506 to 520 A

Manually tapped to 530 A


Monday, October 28, 2019, 15:40

At 13:45 the current reached 530 A. 

Attachment 1: UCx30-CarbothramlReduction.JPG
UCx30-CarbothramlReduction.JPG
Attachment 2: UCx30-CurrentDrop.JPG
UCx30-CurrentDrop.JPG
  249   Thursday, October 31, 2019, 13:59 Marla CervantesUO2/C TARGET BOATProblemsUCx#30 Carbothermal Reduction

Marla Cervantes wrote:

Monday, October 28, 2019, 10:29

A loaded graphite cartridge was set in a tantalum boated and wrapped with 3 tantalum sheets

The set up was installed in the EVAP1 and pumped dwon during the weekend.

IGP1 = 1.10 e-6 Torr


Monday, October 28, 2019, 10:31

Good vacuum = 1e-1 Torr

Bad vaccum = 5e-1 Torr

The current ramp is 1 A each 10 s from 0 A to 100 A


Monday, October 28, 2019, 11:13 

After 18 min the pressure started dropped.


Monday, October 28, 2019, 11:22 

When the pressure reduced to 5e-4 Torr the current ramp was changed to 3.3 A each 10 s to 480 A, the vacuum limits stayed the same.


Monday, October 28, 2019, 11:45

The limit was set to 500 A with same ramp


Monday, October 28, 2019, 11:48 

The ramp was changed to 1A/10s to 550 A


 Monday, October 28, 2019, 11:55

At 520 A the pressure reach 1e-1 Torr and the autoramp stopped


Monday, October 28, 2019, 13:39

the current was increased manually at aprox. 1A/30 s 

The current dropped suddenly even though the pressure was under the limits and the ramping was in the limits.

Autoramp was set to 3 A/ 10 s from to to 500 A

Then it was changed to 1 A  /30s from 500 to 506 A

Finally it was changed to 1 A/ 10 s from 506 to 520 A

Manually tapped to 530 A


Monday, October 28, 2019, 15:40

At 13:45 the current reached 530 A. 

The final pressure was IGP1 = 3.3e-6 Torr 

After 18 hrs at maximum temperature the autoramp was set to -2 A/min to 0 A.

  254   Thursday, January 30, 2020, 09:37 Marla CervantesUO2/CP2N-02 In progressP2N target material carbothermal reduction

Wednesday, January 29 2020, 05:55  

A P2N container  with heat shields, and with a UO2/C loaded graphite container was installed in the EVAP1

Chamber is currently being evacuated.


Thursday, January 30, 2020, 08:56

Pressure limits:

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

Initial pressure: 

IGP1=1.52e-6Torr

Current ramp set to 1A/min to 10 A, voltage is stable.

Current ramp increased to 1A/10s to 100 A. The pressure started raising around 80 A.

Current was kept 5min at at 100 A, voltage was stable


Thursday, January 30, 2020, 09:32 

Current ramp set to 1A/20s to 150 A (same pressure limits)

Pressure keep increasing during heating


Thursday, January 30, 2020, 09:53 

Current was kept at 150 min during 5 min, the voltage is stable, pressure started to stabilize:

IGP1 = 0.027 Torr

TGHT = 0.418 V

Ramp set to 1A/min to 200 A.


Thursday, January 30, 2020, 10:02

Pressure decreasing:

TGHT= 153 A 

  255   Thursday, January 30, 2020, 10:15 Marla CervantesUO2/CP2N-02 ProblemsP2N target material carbothermal reduction

Marla Cervantes wrote:

Wednesday, January 29 2020, 05:55  

A P2N container  with heat shields, and with a UO2/C loaded graphite container was installed in the EVAP1

Chamber is currently being evacuated.


Thursday, January 30, 2020, 08:56

Pressure limits:

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

Initial pressure: 

IGP1=1.52e-6Torr

Current ramp set to 1A/min to 10 A, voltage is stable.

Current ramp increased to 1A/10s to 100 A. The pressure started raising around 80 A.

Current was kept 5min at at 100 A, voltage was stable


Thursday, January 30, 2020, 09:32 

Current ramp set to 1A/20s to 150 A (same pressure limits)

Pressure keep increasing during heating


Thursday, January 30, 2020, 09:53 

Current was kept at 150 min during 5 min, the voltage is stable, pressure started to stabilize:

IGP1 = 0.027 Torr

TGHT = 0.418 V

Ramp set to 1A/min to 200 A.


Thursday, January 30, 2020, 10:02

Pressure decreasing:

TGHT= 153 A 

 Thursday, January 30, 2020, 10:15

At 155 A while pressure decreasing, the power supply tripped off,

Controls has been notified, waiting for instructions.

 
  256   Thursday, January 30, 2020, 11:53 Marla CervantesUO2/CP2N-02 Problems resolvedP2N target material carbothermal reduction

Marla Cervantes wrote:

Marla Cervantes wrote:

Wednesday, January 29 2020, 05:55  

A P2N container  with heat shields, and with a UO2/C loaded graphite container was installed in the EVAP1

Chamber is currently being evacuated.


Thursday, January 30, 2020, 08:56

Pressure limits:

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

Initial pressure: 

IGP1=1.52e-6Torr

Current ramp set to 1A/min to 10 A, voltage is stable.

Current ramp increased to 1A/10s to 100 A. The pressure started raising around 80 A.

Current was kept 5min at at 100 A, voltage was stable


Thursday, January 30, 2020, 09:32 

Current ramp set to 1A/20s to 150 A (same pressure limits)

Pressure keep increasing during heating


Thursday, January 30, 2020, 09:53 

Current was kept at 150 min during 5 min, the voltage is stable, pressure started to stabilize:

IGP1 = 0.027 Torr

TGHT = 0.418 V

Ramp set to 1A/min to 200 A.


Thursday, January 30, 2020, 10:02

Pressure decreasing:

TGHT= 153 A 

 Thursday, January 30, 2020, 10:15

At 155 A while pressure decreasing, the power supply tripped off,

Controls has been notified, waiting for instructions.

 

 Thursday, January 30, 2020, 11:51

Controls respond "It looks like the power supplies were tripped by either the pirani gauge (IEVAP:IGP1) or the Nuclear vent or by both. But, it did not look like that the interlock tree latched the bad condition when the power supplies tripped. I modified the PLC to properly latch the cause of the trip." and gave green light to restart the carbothermal reduction.

  257   Thursday, January 30, 2020, 13:11 Marla CervantesUO2/CP2N-02 ProblemsP2N target material carbothermal reduction

Marla Cervantes wrote:

Marla Cervantes wrote:

Marla Cervantes wrote:

Wednesday, January 29 2020, 05:55  

A P2N container  with heat shields, and with a UO2/C loaded graphite container was installed in the EVAP1

Chamber is currently being evacuated.


Thursday, January 30, 2020, 08:56

Pressure limits:

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

Initial pressure: 

IGP1=1.52e-6Torr

Current ramp set to 1A/min to 10 A, voltage is stable.

Current ramp increased to 1A/10s to 100 A. The pressure started raising around 80 A.

Current was kept 5min at at 100 A, voltage was stable


Thursday, January 30, 2020, 09:32 

Current ramp set to 1A/20s to 150 A (same pressure limits)

Pressure keep increasing during heating


Thursday, January 30, 2020, 09:53 

Current was kept at 150 min during 5 min, the voltage is stable, pressure started to stabilize:

IGP1 = 0.027 Torr

TGHT = 0.418 V

Ramp set to 1A/min to 200 A.


Thursday, January 30, 2020, 10:02

Pressure decreasing:

TGHT= 153 A 

 Thursday, January 30, 2020, 10:15

At 155 A while pressure decreasing, the power supply tripped off,

Controls has been notified, waiting for instructions.

 

 Thursday, January 30, 2020, 11:51

Controls respond "It looks like the power supplies were tripped by either the pirani gauge (IEVAP:IGP1) or the Nuclear vent or by both. But, it did not look like that the interlock tree latched the bad condition when the power supplies tripped. I modified the PLC to properly latch the cause of the trip." and gave green light to restart the carbothermal reduction.

 Thursday, January 30, 2020, 13:09

IGP1=5.9e-6Torr

Ramp set to 1A/10s to 200 A

Pressure rising too fast at 200 A, current reduced manually to 190 A

Pressure start dropping and system tripped, notify to controls again, "The strip tool shows the vacuum level shoot down to 0 then shoot back up for a quick second but that is enough to tell the PLC that IGP is “bad”"


Thursday, January 30, 2020, 15:58 

Restarting process to try to trip the system on purpose 

Initial pressure IGP1 = 2.7e-6Torr

Ramp set to 1/A/10s to 200 A, 0.59 V

Ramp set to 2A/10s to 300 A

Max pressure during process IGP1 = 0.03 Torr

Voltage increased and stabilized (see voltage rising).

Ramp kept at 2A/10s to 400 A


Thursday, January 30, 2020, 16:48 

TGHT = 1.54 V, 399.744 A

IGP1 = 0.00016 Torr and going down

Ramp set to 2A/10s to 500 A


Thursday, January 30, 2020, 17:02 

TGHT= 1.9V, 499.2 A

IGP1 = 0.00014 Torr

Ramp set to 2A/10s to 600 A

Ramp set to 0.5 A/min to 700 A, ramp stopped at 680 A

Manually tapped to 697 A

Pressure dropping indicated that carbothermal reduction is done.

Unfortunately, the system did not trip. 

Contact Gelo for the  next run, such that he can monitor the system and we can spot the problem.

Attachment 1: voltage-rising.JPG
voltage-rising.JPG
  258   Friday, January 31, 2020, 15:36 Marla CervantesUO2/CP2N-02 DoneP2N target material carbothermal reduction

Marla Cervantes wrote:

Marla Cervantes wrote:

Marla Cervantes wrote:

Marla Cervantes wrote:

Wednesday, January 29 2020, 05:55  

A P2N container  with heat shields, and with a UO2/C loaded graphite container was installed in the EVAP1

Chamber is currently being evacuated.


Thursday, January 30, 2020, 08:56

Pressure limits:

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

Initial pressure: 

IGP1=1.52e-6Torr

Current ramp set to 1A/min to 10 A, voltage is stable.

Current ramp increased to 1A/10s to 100 A. The pressure started raising around 80 A.

Current was kept 5min at at 100 A, voltage was stable


Thursday, January 30, 2020, 09:32 

Current ramp set to 1A/20s to 150 A (same pressure limits)

Pressure keep increasing during heating


Thursday, January 30, 2020, 09:53 

Current was kept at 150 min during 5 min, the voltage is stable, pressure started to stabilize:

IGP1 = 0.027 Torr

TGHT = 0.418 V

Ramp set to 1A/min to 200 A.


Thursday, January 30, 2020, 10:02

Pressure decreasing:

TGHT= 153 A 

 Thursday, January 30, 2020, 10:15

At 155 A while pressure decreasing, the power supply tripped off,

Controls has been notified, waiting for instructions.

 

 Thursday, January 30, 2020, 11:51

Controls respond "It looks like the power supplies were tripped by either the pirani gauge (IEVAP:IGP1) or the Nuclear vent or by both. But, it did not look like that the interlock tree latched the bad condition when the power supplies tripped. I modified the PLC to properly latch the cause of the trip." and gave green light to restart the carbothermal reduction.

 Thursday, January 30, 2020, 13:09

IGP1=5.9e-6Torr

Ramp set to 1A/10s to 200 A

Pressure rising too fast at 200 A, current reduced manually to 190 A

Pressure start dropping and system tripped, notify to controls again, "The strip tool shows the vacuum level shoot down to 0 then shoot back up for a quick second but that is enough to tell the PLC that IGP is “bad”"


Thursday, January 30, 2020, 15:58 

Restarting process to try to trip the system on purpose 

Initial pressure IGP1 = 2.7e-6Torr

Ramp set to 1/A/10s to 200 A, 0.59 V

Ramp set to 2A/10s to 300 A

Max pressure during process IGP1 = 0.03 Torr

Voltage increased and stabilized (see voltage rising).

Ramp kept at 2A/10s to 400 A


Thursday, January 30, 2020, 16:48 

TGHT = 1.54 V, 399.744 A

IGP1 = 0.00016 Torr and going down

Ramp set to 2A/10s to 500 A


Thursday, January 30, 2020, 17:02 

TGHT= 1.9V, 499.2 A

IGP1 = 0.00014 Torr

Ramp set to 2A/10s to 600 A

Ramp set to 0.5 A/min to 700 A, ramp stopped at 680 A

Manually tapped to 697 A

Pressure dropping indicated that carbothermal reduction is done.

Unfortunately, the system did not trip. 

Contact Gelo for the  next run, such that he can monitor the system and we can spot the problem.

 Friday, January 31, 2020, 15:35

The EVP1 was vent with Ar and the P2N target was transferred to the glove box.

Attachment 1: P2N-Carbothermal_reduction.JPG
P2N-Carbothermal_reduction.JPG
  259   Tuesday, May 26, 2020, 20:44 Darwin Ortiz RosalesUO2/C TARGET BOATDoneUCx#33 Carbothermal Reduction

 Tuesday, May 26, 2019, 18:20

A loaded graphite cartridge was set in a tantalum boated and wrapped with 3 tantalum sheets (Friday May 22, 2020)

The set up was installed in the EVAP1 and pumped down during the weekend.

IGP1 = 7.10 e-7 Torr

Good vacuum = 1e-1 Torr

Bad vacuum = 5e-1 Torr

Current ramp is 1A per 10s from 0A to 120A


Tuesday, May 26, 2020, 19:15
 
Heater (TGHT) tripped after being at 120A about approximately 10 min.
The pressure was below 500 mTorr when the trip occured (around 20 mTorr) .  Pressure did not appear to have gone past 200 mTorr but was dropping fast at the time of trip.  
Will try again tomorrow after consulting with Gelo.
 

 
 Wednesday, May 27, 2020, 10:26
 
Trying again while monitoring Power Supply reading ( Darwin Remotely and Marla onsite)

IGP1 = 7.7 e-7 Torr

Good vacuum = 1e-1 Torr

Bad vacuum = 5e-1 Torr

Current ramp is 1A per 10s from 0A to 120A


 Wednesday, May 27, 2020, 10:49

Reached 120A on TGHT

TGHT= 0.92V 

IGP1 = 3.6 e-06 Torr and rising


Wednesday, May 27, 2020, 12:46

TGHT =  120.2 A, 0.98V

IGP1 = 6.85e-6 Torr

Starting ramp at 3A per 10s up to 550 A or up to pressure drop start


Wednesday, May 27, 2020, 14:21

Heater tripped again at around 0.14 Torr and approx 440 A

Will start again hoping pressure stable enough to not trip heater.


Wednesday, May 27, 2020, 14:22

IGP1= 1.05e-6 Torr

Ramping to 120 A at 1 A per 10 s



Wednesday, May 27, 2020, 15:12 

Starting ramp on TGHT at 3A per 10s up to 550A or pressure dip.


Wednesday, May 27, 2020, 15:35

Changed vacuum settings (paused ramp and restarted) 

Good vacuum 1e-2

bad vacuum 5e-1


Wednesday, May 27, 2020, 16:30

TGHT = 549.4 A, 5.35V

IGP1= 2.1e-5 Torr

Reached 550 at approx 4 pm 


Thursday, May 28, 2020, 00:31

IGP1= 3.31e-6Torr

TGHT = 549.3 A, 5.45V

Initiate ramp down  at 2 A/min to 0A

Reduced cartridge was dismounted Friday, May 29, 2020 and transferred to Glove box.

 


 

 

  262   Wednesday, June 03, 2020, 08:10 Darwin Ortiz RosalesUO2/C TARGET BOATDoneUCx#34 Carbothermal Reduction

Wednesday, June 03, 2020, 08:11 

A loaded graphite cartridge was set in a tantalum boated and wrapped with 3 tantalum sheets (Friday May 29, 2020)

The set up was installed in the EVAP1 then IEVAP:IGP1 was replaced (elogs 260 and 261).  

Vacuum was turned on after Ion Gauge swap.

IGP1 = 3.6 e-5 Torr

Good vacuum = 5e-2 Torr

Bad vacuum = 5e-1 Torr

Current ramp is 1A per 10s from 0A to 120A


Wednesday, June 03, 2020, 09:59 

After about 20 minutes at 120 A, TGHT tripped again exactly as before.

Will restart ramp at 1A per 10s from 0A to 120A .  Will set good vacuum to 1e-2 Torr

IGP1= 4.3e-05 Torr


Wednesday, June 03, 2020, 10:57

IGP1 =  9e-4 Torr

Pressure peaked around 4e-3 Torr and now trending down

TGHT =120 A


Wednesday, June 03, 2020, 11:23

IGP1=9.5e-5 Torr

Good Vacuum 1e-02 Torr

Bad Vacuum 5e-1 Torr

Starting TGHT ramp to 550 A at 3A per 10s  


Wednesday, June 03, 2020, 14:41

ramp up was good.  TGHT at 550 A since 12:30 pm.  TGHT did not trip. *note adjusted good vacuum.  Ramping takes a little longer but doesn't trigger TGHT shutdown.


Wednesday, June 03, 2020, 22:55

IGP1 =  3.5e-5 Torr

TGHT = 249.4 A, 5.7 V

Start ramp down at -2A per minute to 0 A


 

  263   Thursday, August 13, 2020, 14:37 Marla CervantesUO2/CP2N-02 ProblemsP2N target material carbothermal reduction

Marla Cervantes wrote:

Marla Cervantes wrote:

Marla Cervantes wrote:

Marla Cervantes wrote:

Marla Cervantes wrote:

Wednesday, January 29 2020, 05:55  

A P2N container  with heat shields, and with a UO2/C loaded graphite container was installed in the EVAP1

Chamber is currently being evacuated.


Thursday, January 30, 2020, 08:56

Pressure limits:

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

Initial pressure: 

IGP1=1.52e-6Torr

Current ramp set to 1A/min to 10 A, voltage is stable.

Current ramp increased to 1A/10s to 100 A. The pressure started raising around 80 A.

Current was kept 5min at at 100 A, voltage was stable


Thursday, January 30, 2020, 09:32 

Current ramp set to 1A/20s to 150 A (same pressure limits)

Pressure keep increasing during heating


Thursday, January 30, 2020, 09:53 

Current was kept at 150 min during 5 min, the voltage is stable, pressure started to stabilize:

IGP1 = 0.027 Torr

TGHT = 0.418 V

Ramp set to 1A/min to 200 A.


Thursday, January 30, 2020, 10:02

Pressure decreasing:

TGHT= 153 A 

 Thursday, January 30, 2020, 10:15

At 155 A while pressure decreasing, the power supply tripped off,

Controls has been notified, waiting for instructions.

 

 Thursday, January 30, 2020, 11:51

Controls respond "It looks like the power supplies were tripped by either the pirani gauge (IEVAP:IGP1) or the Nuclear vent or by both. But, it did not look like that the interlock tree latched the bad condition when the power supplies tripped. I modified the PLC to properly latch the cause of the trip." and gave green light to restart the carbothermal reduction.

 Thursday, January 30, 2020, 13:09

IGP1=5.9e-6Torr

Ramp set to 1A/10s to 200 A

Pressure rising too fast at 200 A, current reduced manually to 190 A

Pressure start dropping and system tripped, notify to controls again, "The strip tool shows the vacuum level shoot down to 0 then shoot back up for a quick second but that is enough to tell the PLC that IGP is “bad”"


Thursday, January 30, 2020, 15:58 

Restarting process to try to trip the system on purpose 

Initial pressure IGP1 = 2.7e-6Torr

Ramp set to 1/A/10s to 200 A, 0.59 V

Ramp set to 2A/10s to 300 A

Max pressure during process IGP1 = 0.03 Torr

Voltage increased and stabilized (see voltage rising).

Ramp kept at 2A/10s to 400 A


Thursday, January 30, 2020, 16:48 

TGHT = 1.54 V, 399.744 A

IGP1 = 0.00016 Torr and going down

Ramp set to 2A/10s to 500 A


Thursday, January 30, 2020, 17:02 

TGHT= 1.9V, 499.2 A

IGP1 = 0.00014 Torr

Ramp set to 2A/10s to 600 A

Ramp set to 0.5 A/min to 700 A, ramp stopped at 680 A

Manually tapped to 697 A

Pressure dropping indicated that carbothermal reduction is done.

Unfortunately, the system did not trip. 

Contact Gelo for the  next run, such that he can monitor the system and we can spot the problem.

 Friday, January 31, 2020, 15:35

The EVP1 was vent with Ar and the P2N target was transferred to the glove box.

 Thursday, August 13, 2020, 14:33

XRD analysis of the P2N material showed that the carbothermal reduction was not completed

The material was loaded again in its oven, new Ta caps where secured to the edges, the body remained the same

The oven was set in the EVAP1 using Ar to avoid oxidation of the P2N material

Currently pumping down.


 Saturday, August 15, 2020, 14:45 

Vacuum is having a strange behavior, pressure shows that is going from 8e-11 to 4e-6 Torr (fig. 200815-Vaccum_P2N)

Proceeded to turn off turbo pump


Tuesday, August 18, 2020, 10:38

The IGP1 head was replaced with the EVAP1's IGP1 head

The vacuum will be started again

Attachment 1: 200815-Vacuum_P2N.PNG
200815-Vacuum_P2N.PNG
  265   Tuesday, August 18, 2020, 20:45 Marla CervantesUO2/CP2N-02 Problems resolvedP2N target material carbothermal reduction

Marla Cervantes wrote:

Marla Cervantes wrote:

Marla Cervantes wrote:

Marla Cervantes wrote:

Marla Cervantes wrote:

Marla Cervantes wrote:

Wednesday, January 29 2020, 05:55  

A P2N container  with heat shields, and with a UO2/C loaded graphite container was installed in the EVAP1

Chamber is currently being evacuated.


Thursday, January 30, 2020, 08:56

Pressure limits:

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

Initial pressure: 

IGP1=1.52e-6Torr

Current ramp set to 1A/min to 10 A, voltage is stable.

Current ramp increased to 1A/10s to 100 A. The pressure started raising around 80 A.

Current was kept 5min at at 100 A, voltage was stable


Thursday, January 30, 2020, 09:32 

Current ramp set to 1A/20s to 150 A (same pressure limits)

Pressure keep increasing during heating


Thursday, January 30, 2020, 09:53 

Current was kept at 150 min during 5 min, the voltage is stable, pressure started to stabilize:

IGP1 = 0.027 Torr

TGHT = 0.418 V

Ramp set to 1A/min to 200 A.


Thursday, January 30, 2020, 10:02

Pressure decreasing:

TGHT= 153 A 

 Thursday, January 30, 2020, 10:15

At 155 A while pressure decreasing, the power supply tripped off,

Controls has been notified, waiting for instructions.

 

 Thursday, January 30, 2020, 11:51

Controls respond "It looks like the power supplies were tripped by either the pirani gauge (IEVAP:IGP1) or the Nuclear vent or by both. But, it did not look like that the interlock tree latched the bad condition when the power supplies tripped. I modified the PLC to properly latch the cause of the trip." and gave green light to restart the carbothermal reduction.

 Thursday, January 30, 2020, 13:09

IGP1=5.9e-6Torr

Ramp set to 1A/10s to 200 A

Pressure rising too fast at 200 A, current reduced manually to 190 A

Pressure start dropping and system tripped, notify to controls again, "The strip tool shows the vacuum level shoot down to 0 then shoot back up for a quick second but that is enough to tell the PLC that IGP is “bad”"


Thursday, January 30, 2020, 15:58 

Restarting process to try to trip the system on purpose 

Initial pressure IGP1 = 2.7e-6Torr

Ramp set to 1/A/10s to 200 A, 0.59 V

Ramp set to 2A/10s to 300 A

Max pressure during process IGP1 = 0.03 Torr

Voltage increased and stabilized (see voltage rising).

Ramp kept at 2A/10s to 400 A


Thursday, January 30, 2020, 16:48 

TGHT = 1.54 V, 399.744 A

IGP1 = 0.00016 Torr and going down

Ramp set to 2A/10s to 500 A


Thursday, January 30, 2020, 17:02 

TGHT= 1.9V, 499.2 A

IGP1 = 0.00014 Torr

Ramp set to 2A/10s to 600 A

Ramp set to 0.5 A/min to 700 A, ramp stopped at 680 A

Manually tapped to 697 A

Pressure dropping indicated that carbothermal reduction is done.

Unfortunately, the system did not trip. 

Contact Gelo for the  next run, such that he can monitor the system and we can spot the problem.

 Friday, January 31, 2020, 15:35

The EVP1 was vent with Ar and the P2N target was transferred to the glove box.

 Thursday, August 13, 2020, 14:33

XRD analysis of the P2N material showed that the carbothermal reduction was not completed

The material was loaded again in its oven, new Ta caps where secured to the edges, the body remained the same

The oven was set in the EVAP1 using Ar to avoid oxidation of the P2N material

Currently pumping down.


 Saturday, August 15, 2020, 14:45 

Vacuum is having a strange behavior, pressure shows that is going from 8e-11 to 4e-6 Torr (fig. 200815-Vaccum_P2N)

Proceeded to turn off turbo pump


Tuesday, August 18, 2020, 10:38

The IGP1 head was replaced with the EVAP1's IGP1 head

The vacuum will be started again

 Tuesday, August 18, 2020, 20:44

The pressure reading are normal after swapping the IGP1's gauge head

  266   Wednesday, August 19, 2020, 07:49 Marla CervantesUO2/CP2N-02 DoneP2N carbothermal reduction (#2)

Wednesday, August 19, 2020, 07:47 

XRD analysis of the P2N material showed that the carbothermal reduction was not completed

The material was loaded again in its oven, new Ta caps where secured to the edges, the body remained the same

The oven was set in the EVAP1 using Ar to avoid oxidation of the P2N material

See elog 263


Wednesday, August 19, 2020, 07:47

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

IGP1 = 4.11e-6 Torr

Autoramp set to 1A/10s to 150 A.


Wednesday, August 19, 2020, 10:00

TGHT = .45 V, 149.8 A

IGP1 = 9.1e-5 Torr

 Autoramp set to 1A/10s to 200 A.


Wednesday, August 19, 2020, 10:13

TGHT = 0.6 V, 200.2 A

IGP1 = 3e-4 Torr and increasing

After 6 min:

good vacuum =  5e-2 Torr

bad vacuum = 1e-1 Torr

autoramp set to 1A/30s to 250 A

Since the pressure was decreasing, the ramp was changed to  1A/10s to 250 A, vacuum limits remained the same


Wednesday, August 19, 2020, 10:28

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

IGP1 = 1.7e-4 Torr

TGHT =  0.78 V, 250.1 A

Autoramp set to 2.5 A/10 s to 700 A


Wednesday, August 19, 2020, 11:17

 Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

IGP1 = 2e-4 Torr

TGHT = 2.64 V, 699 A

Autoramp set to 2 A/10 s to 800 A


 Wednesday, August 19, 2020, 11:29

 Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

IGP1 = 5.2e-5 Torr

TGHT = 3.1 V, 798.8 A

Note: Voltage starts to become unstable, an power is around 2.3 kW, pressure has not increased enough to indicate reduction with certainty

In order to reach 3 kW autoramp set to 1A/10 s to 900 A


Wednesday, August 19, 2020, 12:18

The current was increased to 1000 A expecting to see a high peak in pressure but there was not an increase in preasure.

The target is being ramped down to 850 A 

Attachment 1: P2N.PNG
P2N.PNG
  267   Tuesday, September 08, 2020, 20:45 Marla CervantesUO2/CP2N-02 DoneP2N-2 carbothermal reduction

 Tuesday, September 08, 2020, 20:44

A P2N oven with three heat shields, loaded with a graphite container filled with UO2/C ring-discs was set in the EVAP1

EVAP1 is currently being evacuated.


Wednesday, September 09, 2020, 10:11

IGP1 = 4.7e-6 Torr

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

Autoramp set to 1A/10s to 150 A.


Wednesday, September 09, 2020, 10:50 

TGHT = .32 V, 149.8 A

IGP1 = 6.5e-5 Torr

Autoramp set to 1A/10s to 200 A 


Wednesday, September 09, 2020, 11:00

TGHT =0.46 V, 200 A

IGP1 =  6e-4 Torr and going up

good vacuum =  5e-2 Torr

bad vacuum = 1e-2 Torr

autoramp set to 1A/10s to 250 A

autoramp stopped at 215 A, since pressure kept increasing, the current was manually decreased to 180 A.


 Wednesday, September 09, 2020, 11:16

TGHT = 0.4 V, 179.7 A,

IGP1 = 8.5e-4 Torr an going down

good vacuum =  5e-2 Torr

bad vacuum = 1e-2 Torr

autoramp set to 1A/30s to 200 A


Wednesday, September 09, 2020, 11:32

TGHT = 0.46 V, 200.2 A,

IGP1 = 3e-3 Torr an going down

good vacuum =  5e-2 Torr

bad vacuum = 1e-2 Torr

autoramp set to 1A/30s to 300 A


Wednesday, September 09, 2020, 11:38

IGP1 = 1e-3 Torr 

Since the pressure was decreasing, the ramp was stopped at 210 and changed to  1A/10s to 300 A, vacuum limits remained the same


Wednesday, September 09, 2020, 11:53

The pressure reached the bad vacuum limit 1e-2 Torr and stopped

After ~8min the pressure limits were changed to:

good vacuum =  5e-2 Torr

bad vacuum = 1e-1 Torr


Wednesday, September 09, 2020, 12:05 

IGP1 = 1.15e-3 Torr

Autoramp set to 2.5 A/10 s to 700 A


Wednesday, September 09, 2020, 12:36

Pressure increased! and ramp paused at 685 A

re-started autoramp to 700 A at 1A/10s


Wednesday, September 09, 2020, 13:56

Pressure kept increasing after 700 A, so autoramp was set to 750 A at  1A/10s

Pressure kept increasing

At 750 A pressure started reducing, autoramp was set to 760 A at 1A/10 s

System tripped suddenly (Gelo was notified)


The carbothermal reduction seemed complete 

Attachment 1: P2N-2-CR-1.PNG
P2N-2-CR-1.PNG
  268   Thursday, September 10, 2020, 14:07 Marla CervantesUO2/CP2N-02 DoneP2N-2 Conditioning

 Thursday, September 10, 2020, 14:01

A P2N target was carbothermal reduced but at the maximum current, the power supply tripped (elog. 267)

Therefore, the target was not hot long enough to fully outgas, that is why it will be reheated.

Desired current 650 A


Thursday, September 10, 2020, 14:07 

IGP1 =  3.3e-6 Torr

Autoramp set to 650 A at 1 A/10 s 


Thursday, September 10, 2020, 16:06

Ramp reached desired current

TGHT = 2.4 V, 649 A

IGP1 = 3e-3 Torr 


 Friday, September 11, 2020, 11:17

TGHT = 2.24 V, 649.2 A

IGP1 = 3.7e-6 Torr


Friday, September 11, 2020, 12:55 

 TGHT = 2.2 V, 648.8 A

IGP1 = 3.7e-6 Torr

Autoramp set to 700 A at 1 A/10 s,

No more gas was released, the system was ramped down to 0 A at 2 A/min


Friday, September 11, 2020, 18:17

TGHT = 0.35 V, 133 A

IGP1 = 2.7e-6 Torr


 Friday, September 11, 2020, 20:01

TGHT = 0 V, 2.56 A

IGP1 = 2.6e-6 Torr


Monday, September 14, 2020, 16:19

EVAP1 was vented with Ar and the P2N material was transferred to the preparatory glove box. 

  269   Tuesday, March 30, 2021, 16:04 Marla CervantesUO2/CP2N-02 DoneP2N-3 carbothermal reduction

Green target material characteristics  (elog 105)

#discs = 49

Average disc thickness = 0.453mm

Empty cartridge weight = 9.42 g

Full cartridge weight = 39.86 g

UO2+C weight = 30.44 g 


Tuesday, March 30, 2021, 16:04

The target material was loaded in a P2N oven, wrapped with three heat shields, and set in the EVAP1

EVAP1 is currently being evacuated.


Wednesday, March 31, 2021, 09:42

IGP1 = 3.24e-6 Torr

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

Autoramp set to 1A/10s to 150 A. 


Wednesday, March 31, 2021, 10:17

TGHT = .54 V, 149.88 A

IGP1 = 6.3e-4 Torr and increasing

Max pressure = 0.06 Torr


Wednesday, March 31, 2021, 10:33 

IGP1= 0.004 Torr

Autoramp set to 1A/10s to 200 A


Wednesday, March 31, 2021, 10:43

Maximum pressure 0.03 Torr and going down

Autoramp set to 1A/10s to 250 A


Wednesday, March 31, 2021, 11:04 

TGHT = 1.1 V, 299.9 A

IGP1 = 6e-4 Torr and going down

Autoramp set to 2.5 A/10 s to 700 A


Wednesday, March 31, 2021, 11:35

Ramp stopped at 690 A

TGHT = 2.9V, 689.1A

IGP1 = 0.127 Torr 


Wednesday, March 31, 2021, 11:37

Autoramp  set to 700 A at 1A/20s

Manually ramped to 740 A (3V) to make sure carbothermal reduction is done.


 Wednesday, March 31, 2021, 12:00

The power supply tripped, Gelo was monitoring the heating process.



Wednesday, March 31, 2021, 14:33

The target will be heated for 4 hours to get read of impurities.

IGP1 = 6e-6 Torr 

Autoramp set to 650 at 1A/10s 


Wednesday, March 31, 2021, 20:37

TGHT = 2.77 V, 669.6A 

IGP1 = 8.5e-6 Torr

EVAP1 ramped down to 0 A at 2 A/min

  272   Wednesday, June 30, 2021, 13:35 Darwin Ortiz RosalesUO2/C TARGET BOATDoneUCx#34 conditioning

Target #34 was installed in the EVAP1 and pumped down (Tuesday June 29, 2021).

Target #34 is going to be conditioned on a Ta boat wrapped with 3 Ta foils.

IGP1 = 1.85e-6 Torr

Good vacuum = 1e-1 Torr

Bad vacuum = 5e-1 Torr

Power desired 1.6kW. This is the second target conditioned this way. 

Subsequent targets should be conditioned following thermal reduction.


 Thursday, July 01, 2021, 06:05

IGP1= 1.35e-06 Torr

Start autoramp @2A/30s to 400A


Thursday, July 01, 2021, 07:59

Pressure increase was observed near 400A 

will ramp to 450A and  keep for 8 hours

IGP1= 1.4 e-05 Torr


450A and 4.0V reached at 8:14 am on Thursday July 01, 2021

Rampdown @-2A/min was started at 4.14 pm on Thursday July 01, 2021 IGP1 stable at 2.7e-06Torr

Cannot transfer into glovebox yet because moisture is a bit high after regeneration.  Moisture is dropping. Will wait until moisture is sufficiently low.


Monday, July 05, 2021, 20:43

Cartridge was removed and placed in bag inside glovebox

Removed 10 discs for analysis but might place them back inside depending on final decision.  We had previously removed 10 discs after thermal reduction.

 

  273   Wednesday, July 07, 2021, 12:40 Darwin Ortiz RosalesUO2/C TARGET BOATDoneUCx Provisional ID= 200229 conditioning

 Wednesday, July 07, 2021, 14:39

Target Provisional ID = 200929 was installed in the EVAP1 and pumped down (Tuesday July 7, 2021).

Target is going to be thermally reduced for 8 hours and then conditioned for an additional 8 hours

IGP1 = 2.0 e-6 Torr

Good vacuum = 1e-1 Torr

Bad vacuum = 5e-1 Torr

Power desired 1.6kW.

10 extra discs included for analysis


Wednesday, July 07, 2021, 14:49 

Ramping up TGHT at 6A/min [wait interval = 10 s at increments of 1A]


Wednesday, July 07, 2021, 15:58

IGP1= 5.7 e-5 Torr and trending down.  Will start ramp up to 450A at  18A/min [wait interval 10s at 3A increments]

 


Wednesday, July 07, 2021, 16:20 

IGP1= 2.2e-3 Torr

Will continue ramping TGHT to 500A and watch pressure


Wednesday, July 07, 2021, 16:26

Continue ramping to 550 at 3A/10s


 Wednesday, July 07, 2021, 16:29

holding at 550A, 5.1V for 8 hours 


Wednesday, July 07, 2021, 23:41 

TGHT = 550A, 5.7 V

begin ramp down at -2A/min to 450A and leave for 8 hours


Thursday, July 08, 2021, 08:20

 IGP1= 2.7 e-06 Torr

TGHT = 450A, 4.5V

Will start ramp down at -2A/min to 0A 


 

 

  275   Thursday, September 23, 2021, 07:03 Darwin Ortiz RosalesUO2/C TARGET BOATDoneUCx#35 C reduction

 Thursday, September 23, 2021, 06:55

A loaded graphite cartridge was set in a tantalum boated and wrapped with 3 tantalum sheets (Wednesday September 22)

IGP1 = 3.6 e-5 Torr

Good vacuum = 5e-2 Torr

Bad vacuum = 5e-1 Torr

Current ramp is 2A per min from 0A to 120A and 1A/10s from 120A to (450-550A)


Thursday, September 23, 2021, 07:09 

IGP1 = 1.84 e-06 Torr

Start Autoramp to 120A @ 2A/min 


Thursday, September 23, 2021, 10:25

Start Autoramp to 550A @ 1A/10s

 IGP1= 1.05e-05 Torr

TGHT= 120 A, 1.06 V


Thursday, September 23, 2021, 11:57 

Pressure drop observed at 530A.  Start 4 hour count.  


Thursday, September 23, 2021, 15:57 

IGP1= 9.1e-06 Torr

After 4 hour reduction started rampdown to 400A at 2A/30s.

8 hour conditioning to start at 16:15 pm


Friday, September 24, 2021, 00:16

TGHT= 399.8 A, 3.5V

IGP1= 2.4 e-06 Torr 

Start ramp down at 2A/min


 

  281   Wednesday, June 01, 2022, 08:42 Darwin Ortiz RosalesUO2/CTarget Boat DoneUO2 reduction Provisional ID C211209-1

Wednesday, June 01, 2022, 08:39

A loaded graphite cartridge was set in a tantalum boated and wrapped with 3 tantalum sheets (previous day)

IGP1 = 1.6 e-6 Torr

Good vacuum = 5e-2 Torr

Bad vacuum = 5e-1 Torr

Current ramp is 1A per 10s from 0A to 40A then continue to 80A at 1A/10s.  Then at 1A/min to 120 A and allow degas and then autoramp 1A/10s from 120A to (450-550A)

 


Wednesday, June 01, 2022, 09:51

IGP1= 3.0e-4 Torr

TGHT = 120A, 1.0V

Start autoramp at 1A/10s to 420A


Wednesday, June 01, 2022, 10:02

Increased ramp rate to 3A/10 s as per SOP to 440 A then will slow down the ramp to observe pressure behavior.


Wednesday, June 01, 2022, 10:19

At 430 A, autoramp set to 1A/10s to 500A as pressure was increasing. 

Will observe behavior of pressure curve then leave for 4 hours


Wednesday, June 01, 2022, 11:04

Pressure started dropping at 520A.  Stopped ramping and will leave for 4 hours.


Wednesday, June 01, 2022, 14:48

Autoramp to 400 A at 2A/30s and leave for 8 hour treatment


Wednesday, June 01, 2022, 23:00

IGP1= 2.1e-6 Torr

TGHT= 400A

Ramping down @-2A/min to 0A


Thursday, June 02, 2022, 10:09

IGP1= 6.7e-7 Torr

Ready to dismount

  282   Friday, June 03, 2022, 06:21 Darwin Ortiz RosalesUO2/C42218-4LP-IG-LISDoneUCx#39 reduction

Friday, June 03, 2022, 06:24

A loaded graphite cartridge was set in a tantalum boated and wrapped with 3 tantalum sheets (previous day)

IGP1 = 1.4 e-6 Torr

Good vacuum = 5e-2 Torr

Bad vacuum = 5e-1 Torr

Current ramp is 1A per 10s from 0A  to 80A at 1A/10s.  Then at 1A/min to 120 A, allow degas and then autoramp 1A/10s from 120A to (450-550A)


Friday, June 03, 2022, 06:52

starting autoramp at 1A/min to 120A


Friday, June 03, 2022, 07:30

note*: At approximately 108A the pressure did not rise again but was stable.


Friday, June 03, 2022, 07:46

started autoramp at 1A/10s to 450A 


Friday, June 03, 2022, 09:29

start autoramp to 500A at 1A/min


Friday, June 03, 2022, 09:40

pressure keeps stable as ramping continues. 

increased ramp rate to 2A/min


Friday, June 03, 2022, 09:56

Drop in pressure observed as current increased at 2A/min.

Final current is 490A.  Will keep at this current for 4 hours. 


Friday, June 03, 2022, 14:05

Start auroramp to 400A at -2A/30s

will keep at 400A for 8 hours


Friday, June 03, 2022, 22:06

Start autoramp down at -2A/min to 0A

IGP1= 1.6e-06 Torr

TGHT= 400A, 3.6 V

  283   Tuesday, June 07, 2022, 07:09 Darwin Ortiz RosalesUO2/CTarget Boat DoneUO2 reduction ID C220510-1

Tuesday, June 07, 2022, 07:05

A loaded graphite cartridge was set in a tantalum boated and wrapped with 3 tantalum sheets (previous day)

IGP1 = 1.2 e-6 Torr

Good vacuum = 5e-2 Torr

Bad vacuum = 5e-1 Torr

Current ramp is 1A per 10s from 0A to 80A at 1A/10s.  Then at 1A/min to 120 A and allow degas and then autoramp 1A/10s from 120A to (450-550A)


Tuesday, June 07, 2022, 08:28

IGP1=9.8e-5 Torr

TGHT = 120A, 0.85V

Start autoramp at 1A/10s to 420A


Tuesday, June 07, 2022, 08:45

Increased ramp rate to 3A/10 s as per SOP to 450 A then will slow down the ramp to observe pressure behavior.


Tuesday, June 07, 2022, 09:04

slowed autoramp to 2A/min to observe (1A/30s)

some erratic pressure oscillations observed then stabilized. 


Tuesday, June 07, 2022, 09:32

At TGHT = 495A pressure started dropping even while current ramping up.  Stopped ramp.  Will keep for 4 hours.

TGHT = 495.6A, 4.7V


Tuesday, June 07, 2022, 13:30

TGHT = 495.6 A, 4.7V

IGP1= 8.5 e-6 Torr

Start rampdown to 400A at 2A/30s and leave for 8 hour treatment

 

  284   Friday, October 07, 2022, 08:14 Darwin Ortiz RosalesUO2/C LP-SISDoneC-220928UCx conditioning experiments

Friday, October 07, 2022, 07:55

Cartridge-220928UCx was installed in the EVAP1 and pumped down yesterday.

Material will be reduced in LP-SIS wrapped with 3 Ta foils.

IGP1 = 2.1e-6 Torr

a cap was installed to collect material coming out from the ionizer tube

The initial weight of the cap 1 + small bag was recorded to be: 2.82 g   Final weight of cap1 + small bag = 2.84g (see attached picture)

Good vacuum = 5e-4 Torr

Bad vacuum = 5e-2 Torr

Power desired 1900W as approximate power used online. 

Will autoramp @2A/min to 30A, then slow down ramp to 1A/min to 120A.

After first pressure bump cleared, will ramp up to 400 A @ 2A/20s to 425A on TGHT.  TBHT will be topped off at 230A. 

from 425A, TGHT will be ramped at 1A/min and monitored for pressure behaeviour. 

sytem will be left at reduction current for 4 hours.  Then, the current will be dropped to 1900W and allow to run for 8 hours.

The cup will be collected and the system will be run again in increments of two hours. 

*slight change from test plan to save time*

 


Friday, October 07, 2022, 21:55

A true pressure max was not observed.  A max while current still rising.  stopped at 560A on TGHT and 5.3V

will leave at the above conditions for 4 hours.

Suspect that the thinner Ta shields make a difference.  Suggest to add a fourth shield and process the previous cartridge in a tube rather than a boat.  Treat for four hours (pressure max) and then test increasing the current to see if there is a pressure bump.  If no pressure bump then lower current to deposit 1900W for 8 additional hours. 

 


After 4 hours at max current, the current was dropped to 450A (TGHT) and left for 8 hours.

 


Saturday, October 08, 2022, 09:26

start autoramp down @-2A/min for TGHT and -1A/min for TBHT

Cap+ bag = 2.82 g

final cap +bag = 2.84 g


Tuesday, October 11, 2022, 10:15

Today will switch end-cup.  Will weigh new end-cup and place inside the evap1 glovebox.  Then will remove used end-cap and install new end-cap.  Used end-cup will be weighed on same balance as before.  All mass measurements will be done with the same balance. Note, that a makeshift balance air isolation container was built to allow balance to not be affected by air currents.

 Cap 2+bag initial weight = 2.80 g +/- 0.01 g

Cap 2+bag final weight = 2.81g +/- 0.01 g

No visible deposition on cap


Wednesday, October 12, 2022, 07:51

 

Start ramp up at 2A/min.  TGHT to 450A, TBHT to 230A

IGP1= 6.7e-07Torr


Wednesday, October 12, 2022, 09:47

Ramping up @ 4A/min to same final settings: TGHT = 450A and TBHT = 230A

 


Wednesday, October 12, 2022, 11:15

@10:45am 450A, 4.15V were reached on TGHT

Will leave for 2 hours at 450A then ramp down, then switch cap. 


Monday, October 17, 2022, 09:40

The second cap was taken out over the weekend  (attachment number 2).

The final weight of this cap with bag = 2.81 +/- 0.01 g

Installed a nex cap (3) with initial weigh of cap +bag = 2.74 g

Allowed vacuum to settle over Sunday and will start ramping today

Will ramp to 470 A and hold for 2 hours.  Ramp rate  2A /30s

IGP1= 4.6e-07 Torr


 Monday, October 17, 2022, 11:39

ramping with no issues.  will finish ramp around 12:03 pm and will start rampdown @ around 2:05 pm.

 


Monday, October 17, 2022, 12:03

TGHT= 470A, 4.5V

TBHT= 228A, 2.9V

IGP1= 5.6e-06 Torr


Monday, October 17, 2022, 14:05

Start rampdown at 2A/min TGHT and 1A/min TBHT to zero amp

current IGP1= 2.6e-06 Torr

TGHT = 470A, 4.5V

TBHT= 228.3A, 2.9V

 


Tuesday, October 18, 2022, 09:39

IGP1=4.4e-7 Torr

ready to dismount


Tuesday, October 18, 2022, 13:50

Cap 3 + bag initial weight = 2.74 g

Final weight of cap+bag = 2.74 g (no change)

no visible deposition on cap either

Attachment 1: Cap_1_221011.png
Cap_1_221011.png
Attachment 2: Cap_2.png
Cap_2.png
Attachment 3: cap3.png
cap3.png
  286   Monday, November 28, 2022, 05:59 Darwin Ortiz RosalesUO2/C LP-SISDoneC221125experiment

Monday, November 28, 2022, 05:58

Left weekend to pump down

current IGPI= 7.23e-7 Torr

 

Material will be reduced in LP-SIS wrapped with 3 Ta foils.

a cap was installed to collect material coming out from the ionizer tube

Initial weight of target material plus cartridge was recorded

All relevant data and findings will be reported and added to docushare as document :

 

Good vacuum = 5e-4 Torr

Bad vacuum = 5e-2 Torr

Power desired 1900W as approximate power used online. 

Will autoramp @2A/min to 30A, then slow down ramp to 1A/min to 120A.

After first pressure bump cleared, will ramp up to 400 A @ 2A/20s to 425A on TGHT.  TBHT will be topped off at 230A. 

from 425A, TGHT will be ramped at 1A/min and monitored for pressure behaeviour. 

sytem will be left at reduction current for 4 hours.  Then, the current will be dropped to 425 A and allow to run for 8 hours.

The cup will be collected and the system will be run again for two hours. at the same current until no material visible on cap.  Then it will be run at 450A for increments of two hours until no significant mass change of target material.

 


Monday, November 28, 2022, 06:05

started initial heating to 30A at 2A/min on both TGHT and TBHT.


Monday, November 28, 2022, 08:46

was ramping at 6A/min (2A/20s) on both tGHT and TBHT but aborted due to pressure spike.  will allow pressure to stabilize.

TGHT = 162A, 1.35V

TBH 162A, 1.9V


Monday, November 28, 2022, 08:51

Restarting the heating at 6A/min (2A/20s)


Monday, November 28, 2022, 09:21

Pausing heating @ TGHT= 323 A 3.0V

Allow pressure to stabilize to better spot reduction current


Monday, November 28, 2022, 09:49

Started heating TGHT at 2A/min so reduction current can be better resolved


Monday, November 28, 2022, 10:12

heating aborted to allow pressure to stabilize

IGP1> 5.0e-4 Torr


Monday, November 28, 2022, 11:31

IGP1= 1.5e-4 Torr start autoramp TGHT @1A/min


Monday, November 28, 2022, 11:51

paused heating.  Second peak has been passed.  Will let pressure drop before starting heating again to try and better observe reduction peak.


Monday, November 28, 2022, 12:46

start autoramp at 2A/min from 389A on TGHT

IGP1- 6.4e-6 Torr


Monday, November 28, 2022, 14:21

Pressure starts to drop at around 535A, but large bump observed around 386A. 

Will leave four hours. 

TGHT= 539A, 4.98V

TBHT= 229A, 2.9V

 


Monday, November 28, 2022, 18:19

Ramping down at 4A/min to 425A

Currently IGP1= 6.2e-6 Torr

TGHT = 539A, 4.98 V

TBHT= 230A, 2.98V

 


Monday, November 28, 2022, 22:23

425 A on TGHT reached at 6:50 pm.  Will ramp down at 2:50 am .  -2A/min TGHT and -1A/min TBHT


Tuesday, November 29, 2022, 09:34

Final IGP1 when TGHT and TBHT = 0A  is 5.0e-7 Torr


Tuesday, November 29, 2022, 14:08

Weighed materials and reloaded

Currently at 1.1 e-05 Torr

Will initiate heat ramp at 2A/min to 425 A

@241A increase ramp rate to 4A/min on TGHT


Wednesday, November 30, 2022, 12:44

heating B finished and cartridge loading for heating C

Current pressure = 2.09 E-05 Torr.  Will ramp up to 450A at 4A/min and regulate as needed.

Will heat at 450A TGHT for 2 hours, TBHT max= 230A


Wednesday, November 30, 2022, 16:30

Starting rampdown @-2A/min TGHT and -1A/min TBHT

Final heating was @ 450A, 4.0V TGHT and 230A, 2.7V TBHT

 


Friday, December 02, 2022, 09:00

IGP1= 7.2 e-07 Torr

Starting ramp at 2A/min to 450A on TGHT and 230A on TBHT

 


Friday, December 02, 2022, 10:02

pressure stated dropping.  Will increase ramp to 4A/min (2A/30s)


Friday, December 02, 2022, 15:35

Starting ramp down at -2A/min TGHT and -1A/min TBHT

IGP1= 2.6 e-06 Torr

TGHT 450A   4.2V

TBHT  230A  2.9V

 

Attachment 1: Data_summary.png
Data_summary.png
  287   Monday, December 19, 2022, 10:45 Darwin Ortiz RosalesUO2/C LP TUBEDoneC-221207 Reduction

Monday, December 19, 2022, 10:38

Cartridge with 175 discs (including 5 analysis discs) loaded into a graphite cartridge. 

To be reduced inside a Ta container tube.  Tube wrapped in 3 Ta foil heatshields

Will keep at reducing current for 4 hours and then 10 hours @ 425A

Good Vacuum: 5.0e-04 Torr

Bad Vacuum: 5.0e-02 Torr

Initial pressure was 6.36 e-07 Torr

Autoramped to 56A @ 1A/30s

Outgassing bump observed starting at 50A and at 56A the maximum pressure was ~1.9e-05 Torr


Monday, December 19, 2022, 10:47

started autoramping at 1A/30s to 90A


Monday, December 19, 2022, 10:50

observed that pressure not increasing radically, therefore ramping up faster.  2A/30s


Monday, December 19, 2022, 10:58

Second pressure bump observed at 90A, 1.0V

leaving at this current until pressure drops


Monday, December 19, 2022, 17:15

ramped to 280A and left at 280 until pressure started dropping

ramping again to 500A @ 2A/30s

 


Monday, December 19, 2022, 17:26

Stopped at 330A due to pressure hike.  Will allow pressure to drop then continue ramp.


Monday, December 19, 2022, 18:00

restarting ramp @ 2A/30s


Monday, December 19, 2022, 18:11

Pressure started dropping around 350A corresponding to additive gas-off.  Will rampt to 500A @ 2A/30 seconds and then at 1A/30s to 530A


Final current was 548A, 6.7 V.  Will test increasing current after 4 hours (11 pm)


Monday, December 19, 2022, 23:10

ramping down @ 2A/min to 425A .  should be done by 12:00 am and cooling at9:00 am (includes 1 hour ramp down to 425).


Ramping down to zero @ -2A/min


Wednesday, December 21, 2022, 10:47

Final IGP1= 3.7e-07 Torr

  288   Thursday, January 19, 2023, 10:02 Darwin Ortiz RosalesUO2/C LP TUBEDoneC230105 Reduction

Thursday, January 19, 2023, 09:57

Cartridge #8 loaded with 198 discs

To be reduced inside a Ta container tube.  Tube wrapped in 3 Ta foil heatshields.

Reduction for 4 hours and then 10 hours @ 425A

Good Vacuum: 5.0e-04 Torr

Bad Vacuum: 5.0e-02 Torr

Initial pressure is 1.41e-06 Torr


Thursday, January 19, 2023, 10:02 Auto ramping to 120A @ 1A/min

 


Thursday, January 19, 2023, 18:58

Autoramping to  300A @ 4/min (2A/30s)

IGP1=3.34e-06 Torr

 


Friday, January 20, 2023, 07:37

left at 300 A for 8 hours and pressure dropped.  Restarted autoramp at 2A/30s and pressure was increasing until 425A where it peaked.  Reduced autoramp to 1A/min and observed slow but definite pressure drop.  Will go to 450A and leave there for 4 hours. 

Currently 440A, 5.3V on TGHT and 1.28e-05 Torr on IGP1


Friday, January 20, 2023, 12:06

After 4 hours at 450A IGP1= 3.49e-06 Torr

TGHT = 450A 5.4V

Will drop to 425A and leave for 10 hours

 


Friday, January 20, 2023, 21:53

TGHT 425A, 5.2V

IGP1= 1.81e-06 Torr

autoramping to 0 A @ -2A/min

  289   Wednesday, March 22, 2023, 22:29 Darwin Ortiz RosalesUO2/C LP TUBEDone230316 Reduction

Wednesday, March 22, 2023, 22:29

Cartridge #9 loaded with 213 plus 3 analysi discs

To be reduced inside a Ta container tube.  Tube wrapped in 3 Ta foil heatshields.

Reduction for 4 hours and then 8 hours @ 450A

Good Vacuum: 5.0e-04 Torr

Bad Vacuum: 5.0e-02 Torr

Initial pressure is 3.71e-06 Torr

 


Wednesday, March 22, 2023, 22:33

Autoramping to 400A @ 1A/min


Thursday, March 23, 2023, 06:57

Starting heating at 2A/min

Currently at 400A and 4.5V

IGP1= 9.6e-06 Torr


At around 500A, the reduction was observed.  Current manually increased to 508 A and left there for remainder of four hours.  4 hours will be done at 1210 pm, then will ramp down to 450 and 8 hours


Thursday, March 23, 2023, 12:01

IGP1= 7.6 e-06 Torr

508 A, 6.0 V TGHT

Start rampdown to 450 @ -2A/min


Thursday, March 23, 2023, 20:27

IGP1= 2.36e-06 Torr

TGHT = 452A, 5.3A

Starting ramp down @-2A/min

 

 

  290   Wednesday, October 11, 2023, 10:06 Darwin Ortiz RosalesUO2/C LP TUBEDoneTUCx-231005 reduction & conditioning

Wednesday, October 11, 2023, 9:36

Cartridge #10 loaded with 213 plus 3 analysi discs

To be reduced inside a Ta container tube.  Tube wrapped in 3 Ta foil heatshields.

Reduction for 4 hours and then 8 hours @ 450A

Good Vacuum: 5.0e-04 Torr

Bad Vacuum: 5.0e-02 Torr

Initial pressure is 2.4 e-06 Torr


 Wednesday, October 11, 2023, 10:56

Starting heat ramp at 2A/min to 60A

First pressure bump observed at 60A

Allowing pressure to restabilize


Wednesday, October 11, 2023, 13:12

IGP1=2.6 e-5 Torr

continuing to heat at 2A/min


Wednesday, October 11, 2023, 13:35

another pressure bump observed around 90A (should go slowly in these current range).  Aborted ramp, waiting for pressure to stabilize.

pressure rose to around 2.5e-02 Torr (close to our bad pressure)


Wednesday, October 11, 2023, 13:52

IGP1=5.4e-04 Torr Start ramp at 2A/min


Wednesday, October 11, 2023, 17:53

Pressure has started to drop so increased ramp to 4A/min

 


 Wednesday, October 11, 2023, 18:18

 Second small pressure bump observed at 482A and 5.0 V.  Pressure falling.  Will leave at 500A for 4 hours . 

 


 Wednesday, October 11, 2023, 22:00

IGP1= 8.0 e-06 Torr

TGHT=500A, 5.2V

Initiate rampdown to 450A and will leave there for 8 hours


Thursday, October 12, 2023, 07:02

Initiate rampdown to zero.  IGP1=3.21e-06 Torr

TGHT= 450A, 4.6V

  292   Thursday, September 12, 2024, 06:23 Darwin Ortiz RosalesUO2/C LP TUBEDoneUCx240904 reduction

Thursday, September 12, 2024, 06:19

Cartridge #19 loaded with 232 discs including 5 analysis discs

To be reduced inside a Ta container tube.  Tube wrapped in 3 Ta foil heatshields.

Reduction for 4 hours and then 8 hours @ 450A

Good Vacuum: 5.0e-04 Torr

Bad Vacuum: 5.0e-02 Torr

Initial pressure is 3.12 e-06 Torr


Thursday, September 12, 2024, 06:20

Starting step one in ramping

 

Wait interval (s)

Current increment (A)

Initial value (A)

Final value (A)

60

2

0

60

60

1

60

90

30

2

90

550*

 


Thursday, September 12, 2024, 09:12  

Pressure lowered after passing outgas peak. 

IGP1= 2.5e-05 Torr

will continue with step 2 of ramping

 Thursday, September 12, 2024, 14:46

At 115A outgas peak observed and current ramped down from 120A t 115A.  Allowing pressure to drop before continuing ramp.

 

 

Roughing pump issue.  Cooling, turning pumps off until vacuum group can take a look.


Friday, September 13, 2024, 14:39

Roughing pump seems ok.  Restarting ramp at 1A/min to 115A


Friday, September 13, 2024, 17:38

Starting ramp up at 2A/min to 520A (will monitor pump and outgassing)


Saturday, September 14, 2024, 07:44

inflection point at aroung 450A


Saturday, September 14, 2024, 07:48

pressure started dropping at 466A, but some sporadic peaks observed.  Will heat to 488A and leave for 4 hours


Saturday, September 14, 2024, 20:23  

 ramping down after 8 hour conditioning

IGP1= 2.45e-06 Torr

 
  293   Tuesday, September 17, 2024, 06:49 Darwin Ortiz RosalesUO2/C LP TUBEDoneUCx240916 reduction

Tuesday, September 17, 2024, 06:45

Cartridge #20 loaded with 224 discs plus 3 analysis discs

To be reduced inside a Ta container tube.  Tube wrapped in 3 Ta foil heatshields.

Reduction for 4 hours and then 8 hours @ 450A

Good Vacuum: 5.0e-04 Torr

Bad Vacuum: 5.0e-02 Torr

Initial pressure is 1.5 e-06 Torr


Tuesday, September 17, 2024, 06:47

Starting initial ramp @ 2A/min to 60A


Tuesday, September 17, 2024, 10:05

Started ramp at 1A/min to 90A

 


Wednesday, September 18, 2024, 07:05

Reduction at 480A held for 4 hours then 8 hours at 450A

Tested by increasing 10A and significant increase in pressure observed (no real peak). 

Started rampdown at -2Amin

 

  294   Thursday, September 19, 2024, 22:48 Darwin Ortiz RosalesUO2/Cconditioning oven#3LP TUBEDoneUCx240917 reduction

Thursday, September 19, 2024, 22:44

 

Cartridge #21 loaded with 211 discs including 3 analysis discs

To be reduced inside a Ta container tube.  Tube wrapped in 3 Ta foil heatshields.

Reduction for 4 hours and then 8 hours @ 450A

Good Vacuum: 5.0e-04 Torr

Bad Vacuum: 5.0e-02 Torr

Initial pressure is 1.6 e-06 Torr


Friday, September 20, 2024, 08:47

ramped to 300 A and allowed pressure to drop. Pressure stable around 5.0 e-5 Torr.  Will continue ramp at 2A/min


Friday, September 20, 2024, 12:30

At 500A the pressure stops rising.  Will leave for 4 hours. 


Tuesday, September 24, 2024, 15:46

reduced for 4 hours then ramped down to 450A at -2A/min

After 8 hours ramped down to zero A at -2A/min

  295   Tuesday, January 14, 2025, 16:28 Darwin Ortiz RosalesUO2/Cconditioning oven#3LP TUBEIn progressUCx250113 reduction

Tuesday, January 14, 2025, 16:26

 

Cartridge #22 loaded with 211 discs including 3 analysis discs

To be reduced inside a Ta container tube.  Tube wrapped in 3 Ta foil heatshields.

Reduction for 4 hours and then 8 hours @ 450A (see docushare 177267)

Good Vacuum: 5.0e-04 Torr

Bad Vacuum: 5.0e-02 Torr

Initial pressure is 1.6 e-06 Torr


Tuesday, January 14, 2025, 16:27

Left system to pump down earlier in the day. 


Wednesday, January 15, 2025, 10:23

Earlier started initial ramp to 60A at 2A/min

Initial pressure IGP1 was 2.65e-06 Torr

Pressure stable now at 2.40e-5 Torr

Starting ramp to 90 A at 1A/min

  45   Tuesday, February 14, 2012, 21:56 John WongUO238481-9LP-FEBIADDoneUO2/Nb sintering process

 Tuesday, February 14, 2012, 20:58

Evaporator is setup for UO2/Nb sintering process.  

Target oven filled with 402 discs of UO2/Nb, 5.0cm in length with tot mass of 61.49g. 

The chamber has been pumped down for 7 hrs, vac is currently at 4.6e-6 Torr. 

Parament set as follow, see attachment 1. 

 TGHT ramped up to 57A.  Pressure is stabilizing at 3.8e-5 Torr.  

Auto heating initiated.  0.1A/min.  Max TGHT = 500A. 


Sunday, February 19, 2012, 11:41 

TGHT has stayed at 500A for >10hrs,  Vac levels at 2.9e-6 Torr.

Target cool down initiated @ 2A/min.


 Monday, February 20, 2012, 10:23

Target has been cooled down over the weekend.  Vac currently at 5.77e-7 Torr.  

See attachment#2: UO2_Nb_1_striptool.jpg 

Chamber  vented in atmosphere.   


Monday, February 20, 2012, 16:23 

Pumps/ power supplies off. 


 

Attachment 1: Screen_shot_2012-02-14_at_9.00.04_PM.png
Screen_shot_2012-02-14_at_9.00.04_PM.png
Attachment 2: UO2_Nb_1_striptool.jpg
UO2_Nb_1_striptool.jpg
  291   Tuesday, April 09, 2024, 14:43 Darwin Ortiz RosalesUO2 LP TUBEDoneUCx240408 reduction

 Tuesday, April 09, 2024, 14:42

Cartridge #16 loaded with 213 plus 3 analysi discs

To be reduced inside a Ta container tube.  Tube wrapped in 3 Ta foil heatshields.

Reduction for 4 hours and then 8 hours @ 450A

Good Vacuum: 5.0e-04 Torr

Bad Vacuum: 5.0e-02 Torr

Initial pressure is 2.4 e-06 Torr


Tuesday, April 09, 2024, 14:42

Start ramp @2A/min to 120A then wait for pressure drop to continue.


Tuesday, April 09, 2024, 16:51

Set ramp to 2A/30s to 480A


Wednesday, April 10, 2024, 00:02

Ramping down to 450 A


Thursday, April 11, 2024, 09:56

Cool down Wednesday morning

Will be left under vacuum in EVAP1 due to hotlab closure.


 

  26   Wednesday, July 27, 2011, 13:02 John WongUC238634-3LP-SISProblemsUCx#2 conditioning

Wednesday, July 27, 2011, 12:58: 

Target length = 11.2cm

Total UC2/C foils = 245 discs

Total U/cm2 = 15.27g

Target has been pumped down over night,  Vac currently @ 1.64e-6 Torr.  BP @ 38mT.

TGHT @ 76A/0.27V.  Vacuum went up slowly to 4.8e-5 Torr.  TGHT brought back down to 68A, vacuum is holding at 4.8e-5 Torr. 

Wednesday, July 27, 2011, 14:43: Vac @ 2.3e-5 Torr.  Start auto-heating.  0.5A/min, TGHT max = 525A.

Sunday, July 31, 2011, 10:43:  TGHT has reached to 525A.  The pressure came down when the heater was stable at that current (see attachment: striptool_july 31); this implies that more power is needed to finish the carbonization process.  Peter Kunz was informed, and we decided to increase the target heater to 580A.  I will continue to monitor this from home. 

-----------------------------------

On Aug 01, Peter and I agreed to increase the TGHT to 600A (see attachment: striptool_july31_600A) .  Based on the heating curve with 3 Ta-heat shield @ 600A, the would give ~ 2050C/3700W (300C/1600W more than UCx#2).  By looking at the striptool, the pressure came down soon after.  More power might be needed to finish the carbonization process; however as per Peter the graphite vapour pressure increases above 2000C, and we don't know what will happen above that temperature.  So, we will keep it at 600A until the pressure comes down to low 10e-6 Torr.  Then I will being the auto cooling.  Anyway, we are running at 580A online.  On the safe side, 600A may be enough for the conditioning.   

-----------------------------------

 Tuesday, August 02, 2011, 11:19:  TGHT has reached to zero current (see attachment: UCx#2_conditioning).  The evaporator will be vented with Ar.

 


 Friday, August 05, 2011, 10:49

Unfortunately, after the evaporator was vented with Ar, the target was found be be broken into 3 segments. More details later...

 

 

 

 

 

 

 

Attachment 1: striptool_july31.png
striptool_july31.png
Attachment 2: Target_with_3_heat_shields.jpg
Target_with_3_heat_shields.jpg
Attachment 3: striptool_july31_600A.jpg
striptool_july31_600A.jpg
Attachment 4: UCx#2-conditioning.jpg
UCx#2-conditioning.jpg
  28   Thursday, August 04, 2011, 17:46 John WongUC238634-8LP-SISProblems resolvedRepacking UCx in new target oven

Thursday, August 04, 2011, 17:44:  All the UCx material from target oven 38634-3 was recovered and repacked in this new oven.  Total mass recovered = 45.911g and packed in 10.7cm length.  Target is currently being pumped down. 

Thursday, August 04, 2011, 20:23:  Current vac 5.6e-6 Torr.  Stepping up TGHT to 104A, vac increasing slowly.  Being auto heating @ 2A/min to 200A. 

Thursday, August 04, 2011, 21:32 THGT @ 200A,( see attachment1: 200A.jpg)

Friday, August 05, 2011, 09:04:  TGHT reached to 520A, and was cool down last night by ISAC Ops.  (See attachment2: re-conditioning).  Target looks good! 

Attachment 1: 200A.jpg
200A.jpg
Attachment 2: reconditioning.jpg
reconditioning.jpg
  43   Thursday, November 03, 2011, 09:24 John WongUC238634-10LP-SISDoneUCx#3: Final conditioning

 Thursday, November 03, 2011, 08:59

Target was previously coated/sintered with TaC & wrapped with 3 Ta-heat shields, including the back-block. 

Target was loaded with 365 UC2 discs + 3 samples for analysis. 

One regular endcap and one D-cap on the other end where the 3 samples sit. 

Evaporator has been pumped down since last night.  Currently vac @ 2.0e-6 Torr.  

For this final conditioning, here are the instructions: 

1.  Slowly stepping up TGHT  to 100A to burn off the organic binder.  Vacuum is expected to rise to the limit and stay at the plateau for a few days.  

2.  Once the vacuum has come down, the target will be cooldown and the chamber will be vented with Ar.  The cup-holder may be filled with the organic binder and needed to be clean.

3.  Pump back down the evaporator; step up TGHT to 100A and wait for the reaction. 

4.  Initial TGHT auto ramping.  Set TGHT to 520A @ rate of 0.1A/min.  

5.  Allow TGHT to held at 520A for 4 hours, then cool down. 

6.  Remove target from the chamber and store in the air-tight box and transferred to the Ar-glove box. 


Thursday, November 03, 2011, 09:13 

TGHT reached to 55A, and vacuum slowly to rise. Vac @ 5.7e-6 Torr. 

Wil stay at 55A for now... 


 Thursday, November 03, 2011, 09:51

A spike in vacuum and triggered the alarm handler but didn't tripped the TGHT.

Brought TGHT back down to 50A.

Initiated Auto-heating.  Set TGHT to 100A @ 0.1A/min. 


Thursday, November 03, 2011, 18:25  

I just found out that the target heater did not reach to 100A.  The auto-heating was running to bring up TGHT to 100, but the readback stayed at 50A.  Peter K. was contacted.  We stopped the auto-heating program and instantly the target heating jumped to 100A.  Quickly, we brought down the heater to 50A.  (see attachment1 for the stiptool).  Not sure what was happening.  

I stepped up the TGHT manually to 61A, and the pressure is slowing increasing.  


Thursday, November 03, 2011, 19:26  

Something is wrong with the TGHT power supply.  I stepped it up from 55 to 63A, and found the readback stuck at 58 (local @ 56).  So, I tapped the TGHT down to 58A and then the readback followed the setpoint.

I tried again to bring it up to 63 and it stuck at 60A, and tapping down and up the slider triggered the readback to follow the setpoint.  This is a fault in the system. 

Peter was informed, and is taking over this for now.  We need to bring up the THGT up to 100A to burn off the organic binder.  I don't know what we should do from here.  I need a break! 


Friday, November 04, 2011, 15:46  

As per Jane,  there is a problem with the network issue that controls the target heater power supply.  The power supply current is not regulating proper.  (see attachment #2)

TGHT was ramped down from 85A to 0A for Control to work on the problem since this morning.  

See e-fault#5672, WP#2011-11-04-5. 


 Monday, November 07, 2011, 11:12

 Control has fixed the network issue.  

Stepped up to 10A, local read 8A.

 Initiated autoramping, setp TGHT to 20A at 1A/min.  TGHT did reach to 20A with no problem.  

Stepped up further to 30A, local at 28A.  

I conclude that the power supply is now regulating properly.  

Conditioning of UCx#3 continues... 


 Monday, November 07, 2011, 12:14

TGHT at 84.5A, locat @ 82A.  Vacuum hovering at 7.2e-5 Torr.  

Initiated auto-ramping: TGHT set to 100A, at 0.1A/min.  Incrementing current if vac < 5.0e-5 Torr and backing off if vac >6.0e-5 Torr. 


Monday, November 14, 2011, 11:03 

TGHT reached to 175A on Nov 11, 2011 to finish off the organics burnout process. 

Then TGHT was cool down @ 2A/min until TGHT reached to zero.

Evaporator was vented with Ar and the chamber was open.

The target was removed from the evaporator; the organic binder was condensed out from the D-endcap and some from the ionizer tube (See attachment 3 & 4).

One of the samples was retrieved for analysis, and the D-endcap was put back.

The target was installed back, and the chamber was pumped down. 

The sintering and thermal reduction processes continued with TGHT ramped up to 520A.  Heating rate @ 0.1/min. 

Target has been heated at 520A for ~5hrs, vac @ 5.35e-6 Torr. (see attachment 5). 


Wednesday, November 16, 2011, 13:42

 Target looks good.  It has been installed in the heatshield, and it's being stored in the Ar-golve box. 

Evaporator is now off.  


 

Attachment 1: auto_heating_failed.jpg
auto_heating_failed.jpg
Attachment 2: Evap1_TGHT_problem.jpg
Evap1_TGHT_problem.jpg
Attachment 3: Evpr_org_burnout_01.jpg
Evpr_org_burnout_01.jpg
Attachment 4: Evpr_org_burnout.jpg
Evpr_org_burnout.jpg
Attachment 5: archive_overall_process.JPG
archive_overall_process.JPG
  44   Monday, November 14, 2011, 11:56 Peter Kunz UC238634-10LP-SISDoneUCx03: Conditioning up to 175A

Evaporator was cleaned Nov 11 from after target was conditioned up to 175A. There was significant condensation of oily fluid on the left side where the target container was open (D-shaped end cap). There were also deposits in the hole for the ionizer, but the ionizer itself seemed to be clean.

Attachment 1: 0--0009.jpg
0--0009.jpg
Attachment 2: 0--0011.jpg
0--0011.jpg
  55   Tuesday, July 10, 2012, 12:54 John WongUC238634-9LP-SISDoneUCx#4 final conditioning completed

Tuesday, July 10, 2012, 12:44

Target contains 230 discs of UCx (material from UC2 flakes, batch#01-04062012). 

Total UCx mass (UC2 + C-grv extra + C-foil + Org.) = 38.564g

Total length = 8.0 cm

Target was previously contained with TaC and sintered;  it's wrapped with 3 layers of Ta-heat shield, including the back-block.

A regular TaC-coated endcap is inserted on one end and the other is inserted with a D-cap with two samples  (Marked sample #1 & #2).

The chamber is currently being pumped down.


 Tuesday, July 10, 2012, 19:06

IG currently at 9.1e-6 Torr, BP @ 22mTorr.  

Set TGHT auto-ramping parameters:  

Vacuum limit 5.0 e-6 Torr, (max 6.0 e-6 Torr)

rate = 0.25A/min

TGHT = 55A  

Initiated auto-ramping...


 Tuesday, July 10, 2012, 23:20

TGHT reached to 55A and stayed for about 55min.  The pressure was at 2.5e-5 Torr.

Increases TGHT auto-ramping to 175A to allow burning off most of the organic binder, and the chamber will be vented and cleaned before ramping 

up the heater to 520A.

Ramping rate set to 0.1A/min.


Monday, July 16, 2012, 09:44 

TGHT reached to 175A.  It has taken almost 6 days to burn off the organic binder. (see attachment #1).  

Auto-cool down has initiated.  The chamber will be vented with Ar gas and it will be opened for cleaning of the burn-off binder. 


 Monday, July 16, 2012, 14:20

The chamber was vented with Ar, and the target was removed for cleaning.  There was quite a bit of organic gunge filled the ionizer holder-base plate and condensation out the D-cap (as usual).

The chamber was cleaned and the target was installed back.  It's currently being pumped down.

Once the vacuum reached to 10e- Torr.  The heater will be ramped up to max 520A to finish the sintering process.


 Monday, July 16, 2012, 17:01

Pressure has reached to 9.1e-6 Torr. 

Initiated auto-heating at 1A/min.  Set TGHT = 175A.


 Monday, July 16, 2012, 20:00

TGHt reached to 175A.  Pressure stable at 2.2e-5 Torr.  

Increase target heater to 520A; autoramping at 0.1A/min. 


 Thursday, July 19, 2012, 10:27

TGHT reached to 520A, 5.47V (local 516A, 5.36V) and has stayed for about 4 hours.  IG1 = 9.58e-6 Torr and coming down.  BP=29mTorr.


Thursday, July 19, 2012, 10:29

Auto-cooling down in process...  2A/min for TGHT --> 0A.


 Thursday, July 19, 2012, 16:52

The chamber was vented with Ar gas, and the target was transported to the Ar-glove box. 

The samples were removed from the target.

A new TaC-sintered end-cap was inserted.

The target looks good!

Total time for the conditioning process = 9 days.

See attachment#2 for the overall heating/pressure curves.


 

Attachment 1: TGHT_0-175_orgburnoff.GIF
TGHT_0-175_orgburnoff.GIF
Attachment 2: UCx#4_final_conditioning_0-520A.PNG
UCx#4_final_conditioning_0-520A.PNG
  57   Friday, August 24, 2012, 16:44 John WongUC239165-5LP-SISIn progressConditioning UCx#5

Friday, August 24, 2012, 16:40

Target is loaded with 245 discs of UCx (material from batch#02-13062012),

Tot length = 9.1 cm. 

The container is wrapped with 3 layers of Ta-heat shield, including the back block. 

A regular TaC-coated endcap is inserted on one end and the other is inserted with a D-cap

The chamber is currently begin pumped down.


 Instructions (while I'm on vacation)

1.  TGHT will need to heat up to ~175A to burn off the organics. 

      Parameter setup:  5.0e-5 good vac, 6.0-5 bad vac.  The auto-ramping rate is set to 0.1A/min.

2.  Once the organics have burnt off, ramp down the TGHT to 0A at 2A/min.

3.  Purge the glovebox with argon gas for at least 5 mins. 

4.  Vent the chamber with Ar gas.  Close the valve when it is completely vented.

5.  Remove the target.  Be careful the left end (view from the top) is open with the D-cap. 

6.  Clean the chamber with TCE and remove all the gunge.

7.  Install the target back

8.  Pump down the chamber to at least low 10e-6 Torr before begin the final carbonization process.

9.  Auto-ramp the TGHT current to 175A at 1A/min.

10.  Once the TGHT reach to 175A.  Auto-ramp TGHT to 520A at 0.1A/min.

11.  At 520A, keep heating the target for at least 4-5 hours.

12.  Auto ramp TGHT to 0A at 2A/min.

13.  Purge the glovebox with argon for at least 5 min

14.  Vent the chamber with argon gas.  Close the vavle when it is completely vented.

15.  Remove the target from the chamber and put in the "orange box" and transport to the Ar-glove box.

Done!


 Monday, August 27, 2012, 11:26

The chamber has been pumped down over the weekend.  Vac is currently at 3.45e-6 Torr. 

Auto-ramping TGHT to 55A at 0.25A/min.


 Monday, August 27, 2012, 16:24

TGHT reached to 55A and stayed for about 2 hours.  Vacuum went up to 1.9e-5 Torr and it's slowly coming down. 

Increase auto ramping to 175A at 0.1A/min.


 

  58   Monday, September 03, 2012, 02:56 Peter Kunz UC239165-5LP-SISIn progressConditioning UCx05
Organic/volatile burnoff complete at TGHT = 190A. Rampdown initiated.
  59   Tuesday, September 04, 2012, 17:26 Peter Kunz UC239165-5LP-SISIn progressConditioning UCx05
Organic gunk cleaned out. Beginning 2nd phase of conditioning.
  60   Friday, September 07, 2012, 17:21 Peter Kunz UC239165-5LP-SISIn progressConditioning UCx05
Target 6h at 520A. IEVAP:IG1 8.4e-6 Torr. Cool down sequence initiated.
  61   Monday, September 10, 2012, 11:00 Peter Kunz UC239165-5LP-SISIn progressConditioning UCx05
Plot of conditioning run: IEVAP:IG1, TGHT
Attachment 1: UC2_05_conditioning.png
UC2_05_conditioning.png
  65   Thursday, May 30, 2013, 16:25 John WongUC239165-6LP-SISDoneConditioning UCx#06

Thursday, May 30, 2013, 16:16

The target container was previously coated with TaC and sintered in Evap 2.

The target is loaded with 250 discs of UCx (material from batch#03_02042013)

Total length = 8.9cm

The container is wrapped with 3 layers of Ta-heat shield, including the back block.

A regular TaC coated/sintered endcap is inserted on left, wrt to the ionizer tube pointing out of the page.  The right end is open with no cap. 

(Did not use a D-cap... trying out this method.  Need to be careful when handling the target!)

The chamber is dumping down.


 Instructions for conditioning the UCx target:

1.  TGHT will need to heat up to ~175A to burn off the organics. 

      Parameter setup:  5.0e-5 good vac, 6.0-5 bad vac.  The auto-ramping rate is set to 0.1A/min.

2.  Once the organics have burnt off, ramp down the TGHT to 0A at 2A/min.

3.  Purge the glovebox with argon gas. 

4.  Vent the chamber with Ar gas.  Close the valve when it is completely vented.

5.  Remove the target.  Be careful the left end (view from the top) is open with the D-cap. 

6.  Clean the chamber with TCE and remove all the gunge.

7.  Install the target back

8.  Pump down the chamber to at least low 10e-6 Torr before begin the final carbonization process.

9.  Auto-ramp the TGHT current to 175A at 1A/min.

10.  Once the TGHT reach to 175A.  Auto-ramp TGHT to 520A at 0.1A/min.

11.  At 520A, keep heating the target for at least 4-5 hours.

12.  Auto ramp TGHT to 0A at 2A/min.

13.  Purge the glovebox with argon for at least 5 min

14.  Vent the chamber with argon gas.  Close the vavle when it is completely vented.

15.  Remove the target from the chamber and put in the "orange box" and transport to the Ar-glove box.

Done!


 Friday, May 31, 2013, 18:17

Chamber has pumped down to 6.7e-6 Torr. 

Ramping up TGHT to 175A.


 Wednesday, June 05, 2013, 11:14

TGHT reached to 227A/1.99V. (see attachment#1)

TGHT is ramping down to 0A  to clean up the chamber before continue with the conditioning.


 

 

Attachment 1: UCx#6_conditioning_stage1.PNG
UCx#6_conditioning_stage1.PNG
  66   Wednesday, June 05, 2013, 16:52 Laura LambertUC239165-6LP-SISDoneConditioning UCx#06

John Wong wrote:

Thursday, May 30, 2013, 16:16

The target container was previously coated with TaC and sintered in Evap 2.

The target is loaded with 250 discs of UCx (material from batch#03_02042013)

Total length = 8.9cm

The container is wrapped with 3 layers of Ta-heat shield, including the back block.

A regular TaC coated/sintered endcap is inserted on left, wrt to the ionizer tube pointing out of the page.  The right end is open with no cap. 

(Did not use a D-cap... trying out this method.  Need to be careful when handling the target!)

The chamber is dumping down.


 Instructions for conditioning the UCx target:

1.  TGHT will need to heat up to ~175A to burn off the organics. 

      Parameter setup:  5.0e-5 good vac, 6.0-5 bad vac.  The auto-ramping rate is set to 0.1A/min.

2.  Once the organics have burnt off, ramp down the TGHT to 0A at 2A/min.

3.  Purge the glovebox with argon gas. 

4.  Vent the chamber with Ar gas.  Close the valve when it is completely vented.

5.  Remove the target.  Be careful the left end (view from the top) is open with the D-cap. 

6.  Clean the chamber with TCE and remove all the gunge.

7.  Install the target back

8.  Pump down the chamber to at least low 10e-6 Torr before begin the final carbonization process.

9.  Auto-ramp the TGHT current to 175A at 1A/min.

10.  Once the TGHT reach to 175A.  Auto-ramp TGHT to 520A at 0.1A/min.

11.  At 520A, keep heating the target for at least 4-5 hours.

12.  Auto ramp TGHT to 0A at 2A/min.

13.  Purge the glovebox with argon for at least 5 min

14.  Vent the chamber with argon gas.  Close the vavle when it is completely vented.

15.  Remove the target from the chamber and put in the "orange box" and transport to the Ar-glove box.

Done!


 Friday, May 31, 2013, 18:17

Chamber has pumped down to 6.7e-6 Torr. 

Ramping up TGHT to 175A.


 Wednesday, June 05, 2013, 11:14

TGHT reached to 227A/1.99V. (see attachment#1)

TGHT is ramping down to 0A  to clean up the chamber before continue with the conditioning.


 

 

 Wednesday, June 05, 2013, 16:45

Glove box purged with Ar, ~30min

Chamber vented with Ar

Target removed. chamber cleaned with TCE.

Chamber pumped back down

IG1 currently at 1.4E-4 torr

See attachment 1 before chamber was cleaned


 


 

Thursday, June 06, 2013, 11:38

Chamber has been pumped down overnight

IG1 currently at 4.7E-06 Torr, BP at 30 mTorr

TGHT will be ramped up to 220A at 1A/min


 

Attachment 1: UCx#6_conditioningstage1.PNG
UCx#6_conditioningstage1.PNG
  67   Thursday, June 06, 2013, 16:56 John WongUC239165-6LP-SISDoneConditioning UCx#06

Laura Lambert wrote:

John Wong wrote:

Thursday, May 30, 2013, 16:16

The target container was previously coated with TaC and sintered in Evap 2.

The target is loaded with 250 discs of UCx (material from batch#03_02042013)

Total length = 8.9cm

The container is wrapped with 3 layers of Ta-heat shield, including the back block.

A regular TaC coated/sintered endcap is inserted on left, wrt to the ionizer tube pointing out of the page.  The right end is open with no cap. 

(Did not use a D-cap... trying out this method.  Need to be careful when handling the target!)

The chamber is dumping down.


 Instructions for conditioning the UCx target:

1.  TGHT will need to heat up to ~175A to burn off the organics. 

      Parameter setup:  5.0e-5 good vac, 6.0-5 bad vac.  The auto-ramping rate is set to 0.1A/min.

2.  Once the organics have burnt off, ramp down the TGHT to 0A at 2A/min.

3.  Purge the glovebox with argon gas. 

4.  Vent the chamber with Ar gas.  Close the valve when it is completely vented.

5.  Remove the target.  Be careful the left end (view from the top) is open with the D-cap. 

6.  Clean the chamber with TCE and remove all the gunge.

7.  Install the target back

8.  Pump down the chamber to at least low 10e-6 Torr before begin the final carbonization process.

9.  Auto-ramp the TGHT current to 175A at 1A/min.

10.  Once the TGHT reach to 175A.  Auto-ramp TGHT to 520A at 0.1A/min.

11.  At 520A, keep heating the target for at least 4-5 hours.

12.  Auto ramp TGHT to 0A at 2A/min.

13.  Purge the glovebox with argon for at least 5 min

14.  Vent the chamber with argon gas.  Close the vavle when it is completely vented.

15.  Remove the target from the chamber and put in the "orange box" and transport to the Ar-glove box.

Done!


 Friday, May 31, 2013, 18:17

Chamber has pumped down to 6.7e-6 Torr. 

Ramping up TGHT to 175A.


 Wednesday, June 05, 2013, 11:14

TGHT reached to 227A/1.99V. (see attachment#1)

TGHT is ramping down to 0A  to clean up the chamber before continue with the conditioning.


 

 

 Wednesday, June 05, 2013, 16:45

Glove box purged with Ar, ~30min

Chamber vented with Ar

Target removed. chamber cleaned with TCE.

Chamber pumped back down

IG1 currently at 1.4E-4 torr

See attachment 1 before chamber was cleaned


 


 

Thursday, June 06, 2013, 11:38

Chamber has been pumped down overnight

IG1 currently at 4.7E-06 Torr, BP at 30 mTorr

TGHT will be ramped up to 220A at 1A/min


 

 Thursday, June 06, 2013, 16:53

TGHT has reached to 220A; continue ramping up to 520A at 0.1A/min rate.


 Monday, June 10, 2013, 12:28

TGHT has reached to 520A; target has been heated at the current over the weekend.

IG is stabilizing at 3.7e-6 Torr. 

Initiating auto-cooling to 0A at 2A/min.

Chamber will be vented in Ar tomorrow.


 Monday, June 10, 2013, 17:50

TGHT reached to 0A. See attachment #1 for the overall process. 


 

Attachment 1: UCx#6_final_conditioning.PNG
UCx#6_final_conditioning.PNG
  73   Friday, August 02, 2013, 11:06 Laura LambertUC238634-7LP-SISIn progressConditioning UCx # 07

Thursday, August 01, 2013, 16:16

The target container was previously coated with TaC and sintered in Evap 2.

The target is loaded with 210 discs of UCx (material from batch # 04 - 05032013)

Total length = 7.2cm

The container is wrapped with 3 layers of Ta-heat shield, including the back block.

A regular TaC coated / sintered endcap is inserted on left, wrt the ionizer tube pointing out of the page. The right end is open with no cap.

The chamber is pumping down.


Instructions for conditioning the UCx target:

1. TGHT will need to heat up to ~ 175A to burn off the organics.

    Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac. The auto-ramping rate is set to 0.1A/min.

2. Once the organics have burnt off, ramp down the TGHT to 0A at 2A/min.

3. Purge the glovebox with argon gas.

4. Vent the chamber with Ar gas. Close the valve when it is completely vented.

5. Remove the target. Be careful the left end (view from the top) is open with the D-cap.

6. Clean the chamber with TCE and remove all the gunge.

7. Install the target back

8. Pump down the chamber to at least low 10e-6 Torr before begin the final carbonization process.

9. Auto-ramp the TGHT current to 175A at 1A/min.

10. Once the TGHT reach to 175A. Auto-ramp TGHT to 520A at 0.1A/min.

11. At 520A, keep heating the target for at least 4-5 hours.

12. Auto ramp TGHT to 0A at 2A/min.

13. Purge the glovebox with argon for at least 5 min.

14. Vent the chamber with argon gas. Close the valve when it is completely vented.

15. Remove the target from the chamber and put in the "orange james bond box" and transport to the Ar-glove box.

Done!


  74   Monday, August 05, 2013, 07:52 John WongUC238634-7LP-SISDoneConditioning UCx # 07

Laura Lambert wrote:

Thursday, August 01, 2013, 16:16

The target container was previously coated with TaC and sintered in Evap 2.

The target is loaded with 210 discs of UCx (material from batch # 04 - 05032013)

Total length = 7.2cm

The container is wrapped with 3 layers of Ta-heat shield, including the back block.

A regular TaC coated / sintered endcap is inserted on left, wrt the ionizer tube pointing out of the page. The right end is open with no cap.

The chamber is pumping down.


Instructions for conditioning the UCx target:

1. TGHT will need to heat up to ~ 175A to burn off the organics.

    Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac. The auto-ramping rate is set to 0.1A/min.

2. Once the organics have burnt off, ramp down the TGHT to 0A at 2A/min.

3. Purge the glovebox with argon gas.

4. Vent the chamber with Ar gas. Close the valve when it is completely vented.

5. Remove the target. Be careful the left end (view from the top) is open with the D-cap.

6. Clean the chamber with TCE and remove all the gunge.

7. Install the target back

8. Pump down the chamber to at least low 10e-6 Torr before begin the final carbonization process.

9. Auto-ramp the TGHT current to 175A at 1A/min.

10. Once the TGHT reach to 175A. Auto-ramp TGHT to 520A at 0.1A/min.

11. At 520A, keep heating the target for at least 4-5 hours.

12. Auto ramp TGHT to 0A at 2A/min.

13. Purge the glovebox with argon for at least 5 min.

14. Vent the chamber with argon gas. Close the valve when it is completely vented.

15. Remove the target from the chamber and put in the "orange james bond box" and transport to the Ar-glove box.

Done!


 Monday, August 05, 2013, 07:51

Chamber has been pumped down over the weekend.  IG1 currently at 2.65e-6 Torr,

Stepped up TGHT to 20A. 


Monday, August 05, 2013, 08:01  

Vacuum seems stable.  

Initiated auto-ramping for TGHT to reach 175A at 1A/min. 


 Sunday, August 11, 2013, 21:23

TGHT has reached to 175A; target has heated at that current for ~28hours.  

Vacuum is currently at 2.9e-6 Torr, BP @ 31mTorr. 

Cooling target down to 0A at 2A/min. 

The chamber will be vented in Ar tomorrow for cleaning. 


 Monday, August 12, 2013, 17:37 (Interesting day....Close call )

Early this morning, the target was removed from the chamber.  As it was transferred to the "orange" seal-box, half the length of the UCx discs fell out from the opening end of the container. 

The discs and the target were transferred to the Ar-glove box.  Tried to fill back the discs but only a few could get in; most of the discs were cracked;

Used the recently prepared UC flakes from Batch#5-18062013 to fill up the target. 

Total length remained the same ~7.2 cm.

The chamber was cleaned;

The target is now installed back in the chamber, and it's currently being pumped down.

The right end remains open (wrt. the ionizier pointing out of the page). 

TGHT will be ramped up to 520A at the rate of 0.1A/min for the full conditioning.


Tuesday, August 13, 2013, 07:51  

Chamber has pumped down to 5.1e-6 Torr. 

Stepping up TGHT to 50A, monitoring pressure... 


Tuesday, August 13, 2013, 08:08  

Vac @ 8.6e-6 Torr and slowly going up. 

Increase TGHT to 80A. 


Tuesday, August 13, 2013, 08:38  

Pressure reached to 6.4e-5 Torr and came down. 

Initiated auto heating.  TGHT max to 520A at 0.1A/min. 


 Monday, August 19, 2013, 10:56

TGHT has reached to max current @ 520A, and heated over the weekend. (See attachment #1)

IG1 currently @ 4.5e-6 Torr, BP @ 33mTorr

Cooling down in progress, rate @ 2A/min.


 Thursday, August 22, 2013, 17:27

Target was removed from the chamber yesterday. 

It looks good and the assembly is underway....

This process is completed.


 

Attachment 1: UC#7_final_conditioning.PNG
UC#7_final_conditioning.PNG
  81   Friday, October 11, 2013, 18:10 John WongUC239814-IVLP-IG-LISDoneUCx#8 - Final Conditioning

 Friday, October 11, 2013, 18:00

 

The target container was previously coated with TaC and sintered in Evap 2.

The target is loaded with ??? discs of UCx (material from batch #???)

Total length = ???

The container is wrapped with 3 layers of Ta-heat shield, including the back block.

A regular TaC coated / sintered endcap is inserted on left, wrt the ionizer tube pointing out of the page. The right end is open with no cap.

The chamber is pumping down.


Instructions for conditioning the UCx target:

1. TGHT will need to heat up to ~ 175A to burn off the organics.

    Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac. The auto-ramping rate is set to 0.1A/min.

2. Once the organics have burnt off, ramp down the TGHT to 0A at 2A/min.

3. Purge the glovebox with argon gas.

4. Vent the chamber with Ar gas. Close the valve when it is completely vented.

5. Remove the target. Be careful the left end (view from the top) is open with the D-cap.

6. Clean the chamber with TCE and remove all the gunge.

7. Install the target back

8. Pump down the chamber to at least low 10e-6 Torr before begin the final carbonization process.

9. Auto-ramp the TGHT current to 175A at 1A/min.

10. Once the TGHT reach to 175A. Auto-ramp TGHT to 520A at 0.1A/min.

11. At 520A, keep heating the target for at least 4-5 hours.

12. Auto ramp TGHT to 0A at 2A/min.

13. Purge the glovebox with argon for at least 5 min.

14. Vent the chamber with argon gas. Close the valve when it is completely vented.

15. Remove the target from the chamber and put in the "orange james bond box" and transport to the Ar-glove box.


Friday, October 11, 2013, 18:03 
 
Chamber has been pumping down, IG1 currently at 1.58e-6 Torr.
 
TGHT stepped up to 25A and auto ramping initiated... 

 Monday, October 21, 2013, 11:29
 
TGHT to max current at 520A and heated for about 2 days (over the weekend).
 
IG came down to 4.6 e-6 Torr.
 
Cooling down initiated at 2A/min.

 

 

  93   Wednesday, April 30, 2014, 14:58 John WongUC239165-9LP-SISDoneConditioning UCx#9

Wednesday, April 30, 2014, 14:50

The target container was previously coated with TaC and sintered in Evap 2.

The target is loaded with 250 discs of UCx (material from batch#09_06022014)

Total length = 9.3cm

The container is wrapped with 3 layers of Ta-heat shield, including the back block.

A regular TaC coated/sintered endcap is inserted on left, wrt to the ionizer tube pointing out of the page, so the right end is open with no cap to allow out-gassing.

(Did not use a D-cap... This worked for UCx#8. Need to be careful when handling the target!)

The chamber is being dumping down.

TGHT will be ramped up to 520A - keep heating at that current for ~4 to 5 hours.

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac. The auto-ramping rate is set to 0.1A/min.


 Wednesday, April 30, 2014, 16:41

Vacuum at 1.5 e-5 Torr.  Stepped up TGHT to 25A.


 Wednesday, April 30, 2014, 17:42

Pressure 9.2 e-6 Torr.  Initiate auto-heating.


 Friday, May 16, 2014, 16:02

Conditioning complete. (see attachment)

End-caps need to be expended before assembly.


 

Attachment 1: UCx#9_final_conditioning.PNG
UCx#9_final_conditioning.PNG
  94   Wednesday, May 21, 2014, 11:41 John WongUC2 TARGET BOATIn progressTests: Sintering carbon Mesh coated with UC2

Tuesday, May 20, 2014, 16:01

Target boat contains one pellet of carbon mesh coated with UC2.  The sample was prepared in the Ar-glove box and the container is wrapped with 2 layer of Ta foil (it wasn't easy to do the wrapping).

Chamber is currently being pumped down.

TGHT will be heated up to 600A. 


Wednesday, May 21, 2014, 11:40

Chamber has been pumped down overnight, vac @ 6.7e-6 Torr.


Tuesday, May 27, 2014, 10:51 

TGHT was heated up to 600A and stayed for 12hrs before cooled down (see attachment).

EDX/SEM/XRD will be done soon...

More information about this sample structure can be found here: https://www.dropbox.com/sh/hirm808pgjwzg71/AAB1-kP399IbIa8AGdI-OMGua


 Friday, June 13, 2014, 14:57

Chamber was vented and cleaned for UCx target production. 

Will re-visit this later...


 

Attachment 1: Vac_Cur_plot.PNG
Vac_Cur_plot.PNG
  95   Friday, June 13, 2014, 15:21 John WongUC239165-10LP-SISDoneConditioning UCx#10

Friday, June 13, 2014, 15:02

Target container was previously coated and sintered with TaC.  It's wrapped with 3-layers of Ta heat shield, including the center block.

The target consists of 280 discs of UCx with 9cm in length.

A regular TaC coated/sintered endcap is inserted on right, wrt to the ionizer tube pointing down, so the left end is open with no cap to allow out-gassing.

The chamber is being dumping down.

TGHT will be ramped up to 520A - keep heating at that current for ~4 to 5 hours.

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac. The auto-ramping rate is set to 0.1A/min.


 Friday, June 13, 2014, 16:26

Pressure at 1.9e-5 Torr. 

Initiate auto-ramping- stepping up from 0A at 0.1A/min - leaving for the weekend.


 Wednesday, June 25, 2014, 11:45

TGHT has reached 520A and target has been conditioned at that current for 13hrs. 

Auto-cooling initiated at 2A/min.

Once the target is cooled, the chamber will be vented in Ar.


 Friday, July 04, 2014, 10:06

Process is complete.  Target is stored in the Ar-glove box and ready for assembly.


 

  102   Friday, October 17, 2014, 11:55 Laura LambertUC240282-5LP-SISIn progressConditioning UCx #11

 Friday, October 17, 2014, 11:47

Target container was previously coated with TaC spray and sintered.

It's is wrapped with 3 layers of Ta-heat shield, including the center block.

The target consists of 255 discs of UCx with 10.5cm in length.

A regular TaC coated endcap is inserted right, wrt the ionizer tube pointing down, so the left is open with a removable half-cap to allow out-gassing.

The chamber was pumped down overnight.

TGHT will be ramped up to 520A - keep heating the current for 4-5 hours.

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.

Auto ramp at 0.1A/min.


 Friday, October 17, 2014, 13:25

IG1 = 2.6e-6 Torr

Manually stepped up to 35A

Waited ~1hr15

IG1 = 4.2e-6 Torr

Initiating auto-ramp.


 

  103   Monday, October 20, 2014, 16:22 John WongUC240282-5LP-SISDoneConditioning UCx #11

Laura Lambert wrote:

 Friday, October 17, 2014, 11:47

Target container was previously coated with TaC spray and sintered.

It's is wrapped with 3 layers of Ta-heat shield, including the center block.

The target consists of 255 discs of UCx with 10.5cm in length.

A regular TaC coated endcap is inserted right, wrt the ionizer tube pointing down, so the left is open with a removable half-cap to allow out-gassing.

The chamber was pumped down overnight.

TGHT will be ramped up to 520A - keep heating the current for 4-5 hours.

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.

Auto ramp at 0.1A/min.


 Friday, October 17, 2014, 13:25

IG1 = 2.6e-6 Torr

Manually stepped up to 35A

Waited ~1hr15

IG1 = 4.2e-6 Torr

Initiating auto-ramp.


 

 Monday, October 20, 2014, 14:10

There were two big power bumps occurred on Saturday Oct 18 and wiped all the IOC/PLC on the Evaporators.   All the system, including TGHT/pumps/EPICS/Alarm handlers were found off.  The ion gauge was turned on this morning and showed the pressure was around 16mTorr. (see attachment).

The pump has been turned back on; pressure is currently at 3.5e-6 Torr.

Ramping up TGHT...


 Monday, November 03, 2014, 12:05

TGHT has reached to 580A and the target has conditioned at that current for about 3 days. 

Cooling down at 2A/min.


 Wednesday, November 05, 2014, 16:40

UCx conditioning complete.

Target is now in the Ar-glove box.  End caps are inserted but need to be expanded.

Need to insert Re foil prior to assembly.


 

Attachment 1: power_bump.PNG
power_bump.PNG
  104   Monday, November 10, 2014, 13:50 Laura LambertUC240282-5LP-SISDoneConditioning UCx #11

John Wong wrote:

Laura Lambert wrote:

 Friday, October 17, 2014, 11:47

Target container was previously coated with TaC spray and sintered.

It's is wrapped with 3 layers of Ta-heat shield, including the center block.

The target consists of 255 discs of UCx with 10.5cm in length.

A regular TaC coated endcap is inserted right, wrt the ionizer tube pointing down, so the left is open with a removable half-cap to allow out-gassing.

The chamber was pumped down overnight.

TGHT will be ramped up to 520A - keep heating the current for 4-5 hours.

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.

Auto ramp at 0.1A/min.


 Friday, October 17, 2014, 13:25

IG1 = 2.6e-6 Torr

Manually stepped up to 35A

Waited ~1hr15

IG1 = 4.2e-6 Torr

Initiating auto-ramp.


 

 Monday, October 20, 2014, 14:10

There were two big power bumps occurred on Saturday Oct 18 and wiped all the IOC/PLC on the Evaporators.   All the system, including TGHT/pumps/EPICS/Alarm handlers were found off.  The ion gauge was turned on this morning and showed the pressure was around 16mTorr. (see attachment).

The pump has been turned back on; pressure is currently at 3.5e-6 Torr.

Ramping up TGHT...


 Monday, November 03, 2014, 12:05

TGHT has reached to 580A and the target has conditioned at that current for about 3 days. 

Cooling down at 2A/min.


 Wednesday, November 05, 2014, 16:40

UCx conditioning complete.

Target is now in the Ar-glove box.  End caps are inserted but need to be expanded.

Need to insert Re foil prior to assembly.


 

 Monday, November 10, 2014, 13:48

UCx was being assembled, but as one of the endcaps was being expanded, the target container broke [friday nov 7th].

attempting to recover the materials and re-load into a new container now...


 Monday, November 10, 2014, 15:52

new target materials weight total [incl graphite] = 23.368g

(33.994g of materials taken out of broken target)


 

  109   Friday, March 20, 2015, 15:21 Laura LambertUC241177-2LP-SISDoneConditioning UCx #12

Friday, March 20, 2015, 15:17 

Target container was previously coated with TaC spray and sintered.

It's is wrapped with 3 layers of Ta-heat shield, including the center block.

The target consists of 225 discs of UCx with 9.2cm in length.

Packing step was skipped for first time, loaded singular discs into target container, no binder holding discs together.

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down, so the right is open.

The chamber is currently pumping down.

TGHT will be ramped up to 520A - keep heating the current for 4-5 hours.

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.

Auto ramp at 0.1A/min.


 Monday, March 23, 2015, 09:09

IOC has been rebooted.

Ion gauge won't turn on - goes into drive, then times out...


 Monday, March 23, 2015, 15:06

Both filaments in IG1 are burnt out.

EVAP1 will be vented tomorrow morning.

UCx will be placed in the pelican case under argon while the filaments are being replaced in the morning.


 Tuesday, March 24, 2015, 11:27

Vented in argon and placed target in pelican case.

Ion gauge replaced this morning.

Continued purging evap1 and re-installed UCx back into evap1.

Currently pumping back down.


 Wednesday, March 25, 2015, 09:38

IG1 = 8.65e-7 Torr

Tapped up evap1 manually to 40A.

Waited ~20min.

Vaccuum stable.

IGP1 = 7.75e-7 Torr.

Initiating auto-ramp.


 Wednesday, April 01, 2015, 15:07

TGHT has reached 520A, 5.82V - YAY!

Will continue to heat overnight and initiate ramp-down/ cooling tomorrow morning.

Slightly shorter time frame to reach max setpoints than normal - possibly due to lack of binder/ skipping packing process.

Great timing before the long weekend 


 Thursday, April 02, 2015, 09:20

Target has been conditioned at max setpoints for 20hours.

Auto-cooling ramp down initiated at 2.0A/min.


 Thursday, April 09, 2015, 16:02

Vented in argon and removed from evap1 tuesday.

Appears as though some discs may be slightly displaced, pictures to follow...


 

  112   Tuesday, June 30, 2015, 13:31 Laura LambertUC240860-1LP-IG-LISIn progressConditioning UCx #13

 Tuesday, June 30, 2015, 13:28

Target container was previously coated with TaC spray and sintered.

It's is wrapped with 3 layers of Ta-heat shield, including the center block.

The target consists of 221 discs of UCx with 7.3cm in length.

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down, so the right is open - discs are held on with Ta wire spring.

The chamber is currently pumping down.

TGHT will be ramped up to 520A at 0.1A/min

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


 Tuesday, June 30, 2015, 14:43

IG1 = 1.8e-5 Torr.

Tapped up manually to 30A.

Vacuum stable; IG1 = 1.2e-5 Torr.

Initiating auto-ramp.


 Thursday, July 02, 2015, 08:41

EVAP1 was tripped off due to backflow preventer test this morning.

IG1 - 4.2e-6 Torr.

Tapping back-up manually before re-initiating auto-ramp.


 Thursday, July 02, 2015, 11:49

Tapped up manually to 85A, 0.65V

IG1 = 3.6e-6 Torr.

Initiating auto-ramp.


 Friday, July 03, 2015, 14:47

All water valves look good, flow is good.

WV turned back on, TGHT turned back on. 

Tapped back up manually to 20A.

IG1 = 2.3e-6 Torr

Initiating auto-ramp at 0.1A/min with a max setpoint of 150A over the weekend.

Will continue to ramp up monday.

Approved by Peter Kunz.


 

  113   Thursday, July 02, 2015, 13:01 John WongUC240860-1LP-IG-LISIn progressConditioning UCx #13

Laura Lambert wrote:

 Tuesday, June 30, 2015, 13:28

Target container was previously coated with TaC spray and sintered.

It's is wrapped with 3 layers of Ta-heat shield, including the center block.

The target consists of 221 discs of UCx with 7.3cm in length.

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down, so the right is open - discs are held on with Ta wire spring.

The chamber is currently pumping down.

TGHT will be ramped up to 520A at 0.1A/min

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


 Tuesday, June 30, 2015, 14:43

IG1 = 1.8e-5 Torr.

Tapped up manually to 30A.

Vacuum stable; IG1 = 1.2e-5 Torr.

Initiating auto-ramp.


 Thursday, July 02, 2015, 08:41

EVAP1 was tripped off due to backflow preventer test this morning.

IG1 - 4.2e-6 Torr.

Tapping back-up manually before re-initiating auto-ramp.


 Thursday, July 02, 2015, 11:49

Tapped up manually to 85A, 0.65V

IG1 = 3.6e-6 Torr.

Initiating auto-ramp.


 

 Thursday, July 02, 2015, 12:58

NOTE:  Before venting the EVAP1 chamber, the Ar line must disconnect from Peter's sampling chamber (inside the fumehood) and connect back to the EVAP. 


 

  114   Friday, July 03, 2015, 13:45 Laura LambertUC240860-1LP-IG-LISIn progressConditioning UCx #13

John Wong wrote:

Laura Lambert wrote:

 Tuesday, June 30, 2015, 13:28

Target container was previously coated with TaC spray and sintered.

It's is wrapped with 3 layers of Ta-heat shield, including the center block.

The target consists of 221 discs of UCx with 7.3cm in length.

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down, so the right is open - discs are held on with Ta wire spring.

The chamber is currently pumping down.

TGHT will be ramped up to 520A at 0.1A/min

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


 Tuesday, June 30, 2015, 14:43

IG1 = 1.8e-5 Torr.

Tapped up manually to 30A.

Vacuum stable; IG1 = 1.2e-5 Torr.

Initiating auto-ramp.


 Thursday, July 02, 2015, 08:41

EVAP1 was tripped off due to backflow preventer test this morning.

IG1 - 4.2e-6 Torr.

Tapping back-up manually before re-initiating auto-ramp.


 Thursday, July 02, 2015, 11:49

Tapped up manually to 85A, 0.65V

IG1 = 3.6e-6 Torr.

Initiating auto-ramp.


 

 Thursday, July 02, 2015, 12:58

NOTE:  Before venting the EVAP1 chamber, the Ar line must disconnect from Peter's sampling chamber (inside the fumehood) and connect back to the EVAP. 


 

 Friday, July 03, 2015, 13:42

water valve tripped off at ~1pm, which subsequently tripped off the TGHT [see photo]

currently trying to figure out what caused this to occur before re-starting....


 Friday, July 03, 2015, 14:47

All water valves look good, flow is good.

WV turned back on, TGHT turned back on. 

Tapped back up manually to 20A.

IG1 = 2.3e-6 Torr

Initiating auto-ramp at 0.1A/min with a max setpoint of 150A over the weekend.

Will continue to ramp up monday.

 

Approved by Peter Kunz.


 Monday, July 06, 2015, 09:29

TGHT reached 150A 1.5hrs ago.

Vacuum stable.

IG1 = 2.7e-5 Torr.

Re-starting auto-ramp at 0.1A/min with a max setpoint of 520A.


 

Attachment 1: evap1_trip_off_july_3rd.JPG
evap1_trip_off_july_3rd.JPG
  115   Wednesday, July 08, 2015, 10:52 John WongUC240860-1LP-IG-LISDoneConditioning UCx #13

Laura Lambert wrote:

John Wong wrote:

Laura Lambert wrote:

 Tuesday, June 30, 2015, 13:28

Target container was previously coated with TaC spray and sintered.

It's is wrapped with 3 layers of Ta-heat shield, including the center block.

The target consists of 221 discs of UCx with 7.5cm in length.

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down, so the right is open - discs are held on with Ta wire spring.

The chamber is currently pumping down.

TGHT will be ramped up to 520A at 0.1A/min

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


 Tuesday, June 30, 2015, 14:43

IG1 = 1.8e-5 Torr.

Tapped up manually to 30A.

Vacuum stable; IG1 = 1.2e-5 Torr.

Initiating auto-ramp.


 Thursday, July 02, 2015, 08:41

EVAP1 was tripped off due to backflow preventer test this morning.

IG1 - 4.2e-6 Torr.

Tapping back-up manually before re-initiating auto-ramp.


 Thursday, July 02, 2015, 11:49

Tapped up manually to 85A, 0.65V

IG1 = 3.6e-6 Torr.

Initiating auto-ramp.


 

 Thursday, July 02, 2015, 12:58

NOTE:  Before venting the EVAP1 chamber, the Ar line must disconnect from Peter's sampling chamber (inside the fumehood) and connect back to the EVAP. 


 

 Friday, July 03, 2015, 13:42

water valve tripped off at ~1pm, which subsequently tripped off the TGHT [see photo]

currently trying to figure out what caused this to occur before re-starting....


 Friday, July 03, 2015, 14:47

All water valves look good, flow is good.

WV turned back on, TGHT turned back on. 

Tapped back up manually to 20A.

IG1 = 2.3e-6 Torr

Initiating auto-ramp at 0.1A/min with a max setpoint of 150A over the weekend.

Will continue to ramp up monday.

 

Approved by Peter Kunz.


 Monday, July 06, 2015, 09:29

TGHT reached 150A 1.5hrs ago.

Vacuum stable.

IG1 = 2.7e-5 Torr.

Re-starting auto-ramp at 0.1A/min with a max setpoint of 520A.


 

 Wednesday, July 08, 2015, 10:44

The carbonization process is complete; chamber vacuum is stabilizing at 9.5e-6 Torr. 

Currently TGHT is at 430A.  Increased TGHT ramping rate to 1A/min.  Target should be at max current (520A) in 1.5 hours, so TGHT can be ramped down around 4:30pm today. 


 Wednesday, July 08, 2015, 16:36

TGHT at 520A/5.884V for over 4 hours.  Pressure coming down, currently at 1.42e-5 Torr. 

Initiated cooling at -2A/min. 

Chamber can be vented in Ar tomorrow and the target will be inspected.


Thursday, July 09, 2015, 17:08  

The target was taken out from the evaporator and inspected. 

Some "burnt" marks on the ionization legs can be observed and also the centre support leg is bent.  (see photos#1)

Not sure if the centre leg came in bent after machining or it happened during the carbonization process??  Do not have photos of the container before the process to compare.  

A few things to note…  During the process, the power supply did tripped off twice due to the cooling water valve shut off. (see photo#2).  An assumption is that sudden cool down of the hot target might have caused the quenching effect. 

No other visible damage.  

End caps are inserted and ready for assembly.

Link to photos:  https://www.dropbox.com/sh/c1ake0fu4x7lckc/AAD0F8TVRrpCbbHquEvSkyYIa?dl=0

 

 

 

Attachment 1: Screen_Shot_2015-07-09_at_5.20.37_PM.png
Screen_Shot_2015-07-09_at_5.20.37_PM.png
Attachment 2: pressure_current_plot.PNG
pressure_current_plot.PNG
  121   Thursday, October 15, 2015, 16:05 John WongUC241077-5LP-SISIn progressConditioning UCx#14

Thursday, October 15, 2015, 15:52

Target container previously sintered with TaC in Evap#2 - Target current at 440A, temp measured at 1900C.  A few tests on the temp measured were done (see Evap#2 elog #251 & 252). 
Note:  This is the new design container with a small back block.

Container is loaded with 245 discs of UC2; measured disc length 7.5 cm

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down, so the right is open - discs are held on with Ta wire spring.

3 layers of Ta-heat shield is used. 

Target heater will be ramped up to 440A (according to the achieved temperature from Evap#2). 

Ramping rate at 0.1A/min.

Monitor closely on the vacuum around 400A to see if the carbonization process is complete. 

Chamber is currently being pumped down. 


 Friday, October 16, 2015, 10:33

Chamber has pumped down to 2e-6 Torr. 

Stepping up TGHT to 70A/0.23V. 


 Friday, October 16, 2015, 14:55

TGHT stepped up to 70A, pressure went to max 5.7e-5 Torr and it's coming down.

Initated autoramping.  (good vac at 5e-5 Torr, bad at 6.0e-5 Torr)


 Thursday, October 22, 2015, 12:26

TGHT has reached 440A/4.403V and stablized for about 5 hours. 

Pressure started coming down at around 370A which indicated the ending of the carbonization process. 

Currently vacuum is at 5.6e-6 torr. 

Initiated cooling down process at 2A/min.


 

  122   Monday, October 26, 2015, 16:20 Laura LambertUC241077-5LP-SISDoneConditioning UCx#14

John Wong wrote:

Thursday, October 15, 2015, 15:52

Target container previously sintered with TaC in Evap#2 - Target current at 440A, temp measured at 1900C.  A few tests on the temp measured were done (see Evap#2 elog #251 & 252). 
Note:  This is the new design container with a small back block.

Container is loaded with 245 discs of UC2; measured disc length 7.5 cm

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down, so the right is open - discs are held on with Ta wire spring.

3 layers of Ta-heat shield is used. 

Target heater will be ramped up to 440A (according to the achieved temperature from Evap#2). 

Ramping rate at 0.1A/min.

Monitor closely on the vacuum around 400A to see if the carbonization process is complete. 

Chamber is currently being pumped down. 


 Friday, October 16, 2015, 10:33

Chamber has pumped down to 2e-6 Torr. 

Stepping up TGHT to 70A/0.23V. 


 Friday, October 16, 2015, 14:55

TGHT stepped up to 70A, pressure went to max 5.7e-5 Torr and it's coming down.

Initated autoramping.  (good vac at 5e-5 Torr, bad at 6.0e-5 Torr)


 Thursday, October 22, 2015, 12:26

TGHT has reached 440A/4.403V and stablized for about 5 hours. 

Pressure started coming down at around 370A which indicated the ending of the carbonization process. 

Currently vacuum is at 5.6e-6 torr. 

Initiated cooling down process at 2A/min.


 

 Monday, October 26, 2015, 16:18

Target vented in argon, taken out and currently in glove box.

Target looks good, last one of the year! 

Endcaps inserted and need to be expanded, Rh foil still needs to be added.


 

  125   Thursday, February 18, 2016, 15:42 Laura LambertUC241077-1LP-SISIn progressConditioning UCx#15

 Thursday, February 18, 2016, 15:34

Target container was previously coated with TaC spray and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block - same method as for sintering TaC coating [new wrapping method-see elog112 eva2].

The target consists of 244 discs of UCx with 7.8cm in length.

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down, so the right is open

The chamber is currently pumping down.

TGHT will be ramped up to 520A at 0.1A/min

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


 Friday, February 19, 2016, 08:28

IG1 = 4.7e-6 Torr

Tapped up manually to 35A.

Waited ~1hr, vacuum stable

IG1 = 3.8e-6 Torr.

Initiating auto-ramp.


 

  126   Friday, February 26, 2016, 10:27 John WongUC241077-1LP-SISIn progressConditioning UCx#15

Laura Lambert wrote:

 Thursday, February 18, 2016, 15:34

Target container was previously coated with TaC spray and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block - same method as for sintering TaC coating [new wrapping method-see elog112 eva2].

The target consists of 244 discs of UCx with 7.8cm in length.

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down, so the right is open

The chamber is currently pumping down.

TGHT will be ramped up to 520A at 0.1A/min

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


 Friday, February 19, 2016, 08:28

IG1 = 4.7e-6 Torr

Tapped up manually to 35A.

Waited ~1hr, vacuum stable

IG1 = 3.8e-6 Torr.

Initiating auto-ramp.


 

 Friday, February 26, 2016, 10:26

Target has been heated at 520A for 10 hrs.

Vacuum at 5.3e-6 Torr. 

Initiated cool down at 1A/min. 

Remember to vent with Ar. 


 

  127   Monday, February 29, 2016, 16:16 Laura LambertUC241077-1LP-SISDoneConditioning UCx#15

John Wong wrote:

Laura Lambert wrote:

 Thursday, February 18, 2016, 15:34

Target container was previously coated with TaC spray and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block - same method as for sintering TaC coating [new wrapping method-see elog112 eva2].

The target consists of 244 discs of UCx with 7.8cm in length.

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down, so the right is open

The chamber is currently pumping down.

TGHT will be ramped up to 520A at 0.1A/min

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


 Friday, February 19, 2016, 08:28

IG1 = 4.7e-6 Torr

Tapped up manually to 35A.

Waited ~1hr, vacuum stable

IG1 = 3.8e-6 Torr.

Initiating auto-ramp.


 

 Friday, February 26, 2016, 10:26

Target has been heated at 520A for 10 hrs.

Vacuum at 5.3e-6 Torr. 

Initiated cool down at 1A/min. 

Remember to vent with Ar. 


 

 Monday, February 29, 2016, 16:15

Vented in Ar.

Target removed from evap1 this morning.

Currently sitting in glovebox.

Weird red discharge on the end of the right side, inside the container [wrt ionizer tube into page] - same side with no endcap during carbonization.

Materials look good, both endcaps inserted.

Rh foil still needs to be implanted.


 Wednesday, March 02, 2016, 10:13

The discoloration appears to be a simple change in the morphology of the TaC coating, future tests would need to be done to confirm this estimation.

This should not effect the container/ target.

See photo attached.

Attachment 1: UCx_15.jpg
UCx_15.jpg
  130   Tuesday, April 19, 2016, 10:48 Laura LambertUC2*** Done***ALL FUTURE UCx TARGETS***

 Tuesday, April 19, 2016, 09:47

Temperature measurements have been taken in evap2 on target containers. 

Previously all UCx targets have been conditioned in evap1 at 520A. The respective target containers TaC coating was sintered in evap2 at a different current.

All future UCx targets will now be conditioned in evap1 at the same current required to reach 1900C in evap2 when sintering the TaC coating on the container to be used for the respective target.

ie. If a container is being sintered in evap2 at 450A [1900C], this same container is used for UCx - then that specific UCx target will be conditioned in evap1 at 450A.

Confirm full carbonization has been achieved by following with the vacuum on the strip tool and make sure the final vacuum comes down at the end of the whole process.


 

  132   Wednesday, May 18, 2016, 15:15 Laura LambertUC240860-2LP-IG-LISDoneConditioning UCx#16

 Wednesday, May 18, 2016, 15:05

Target container was previously coated with TaC spray and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block - new wrapping method-see elog112 evap2

The target consists of 200 discs of UCx with 7.4cm in length [4 packs of 5 + 180 single discs].

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down.

The right side is open with a TaC coated spring to help hold materials in.

The chamber is currently pumping down.

TGHT will be ramped up to 460A at 0.1A/min [same current used to reach 1900C in evap2 when sintering TaC coating - elog291 evap2]

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


 Thursday, May 19, 2016, 09:25

IG1 = 3.4e-6 Torr

Tapped up manually to 35A

Vacuum stable.

IG1 = 3.5e-6 Torr.

Initiating auto-ramp.


 Wednesday, May 25, 2016, 13:05

Target has been heated at 460A, 4.5V for 5 hrs.

Vacuum at 6.4e-6 Torr. 

Initiated cool down at 1A/min. 


 Friday, May 27, 2016, 11:14

UCx done.

Vented in Ar and put in glove box yesterday.

Looked inside before inserting 2nd endcap - clean view all the way through the materials to the endcap/ not much visible shifting.

Ta coated spring helped hold materials in place.

Slightly darker markings on legs of container on side that was open in evap1.

2nd endcap put in.

Ready for assembly.


 

  133   Monday, July 11, 2016, 16:00 Laura LambertUC241790-3LP-SISDoneConditioning UCx#17

Monday, July 11, 2016, 15:54

Target container was previously coated with TaC spray and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block - new wrapping method-see elog112 evap2

The target consists of 216 discs of UCx with 7.6cm in length [4 packs of 5 + 196 single discs].

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down.

The right side is open with a TaC coated spring to help hold materials in.

The chamber is currently pumping down.

TGHT will be ramped up to 410A at 0.1A/min [same current used to reach 1900C in evap2 when sintering TaC coating - elog308 evap2]

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


 Tuesday, July 12, 2016, 08:50

IG1 = 5.3e-6 Torr

Tapped up manually to 35A

Vacuum stable.

IG1 = 5.25e-6 Torr.

Initiating auto-ramp.


 Friday, July 15, 2016, 16:59

With evap2 not working, water was turned off to check valves...this tripped off evap1 since this also turned off the water to evap1.

TGHT was ~115A when evap1 tripped off.

Vacuum stable = 2.9e-6 Torr.

Tapped back up manually to 115A, 1.08V

Vacuum stable = 2.8e-6 Torr.

Restarting auto ramp at 0.1A/min.


 Friday, July 22, 2016, 16:25

Target has remained at max setpoints for 4.5days.

TGHT = 410A, 3.99V

IG1 = 2.5e-6 Torr

Voltage has wavered a small amount, between 3,91V-4.02V; this can be seen in the photo attached of the screenshot of the striptool.

Conditioning process is now complete.

Initiating auto-cool at 1.0A/min


 Tuesday, July 26, 2016, 16:48

Vented in Ar and currently transfering into glove box

will update elog tomorrow...


 Wednesday, July 27, 2016, 14:56

had a few problems with the transfer chamber in the glove box, but managed to get the target into the glove box okay last night.

was exposed to oxygen for minimal amount of time - transfer chamber wasnt flushing properly/ leak in james bond box


 

Attachment 1: trip-off.JPG
trip-off.JPG
Attachment 2: snapshot_of_striptool.JPG
snapshot_of_striptool.JPG
  138   Wednesday, October 19, 2016, 16:52 Laura LambertUC241790-6LP-SISDoneConditioning UCx#18

 Wednesday, October 19, 2016, 16:47

Target container was previously coated with TaC spray and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block using one single foil/ layer

The target consists of 165 discs of UCx with 5.4cm in length

Materials: 4 packs of 5 {all made with 'modified' UC2cast} + 145 single discs{20 from 'modified cast'}

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down.

The right side is open with a TaC coated spring to help hold materials in.

The chamber is currently pumping down.

TGHT will be ramped up to 430A at 0.1A/min [same current used to reach 1900C in evap2 when sintering TaC coating - elog327 evap2]

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


Thursday, October 20, 2016, 10:11

Tapped up manually to 40A

Vacuum stable.

IG1 = 4.45e-6 Torr.

Initiating auto-ramp.


 Monday, October 24, 2016, 11:19

TGHT = 254A, 2.46V

Still ramping up...~half way to final setpoint

Vacuum dropped, looks good, IG1 = 6.77e-6 Torr


 Wednesday, October 26, 2016, 09:38

Target has remained at max setpoints for ~16hrs.

TGHT = 430A, 4.25V

IG1 = 2.3e-6 Torr

Conditioning/ re-carbonization process is now complete.

Initiating auto-cool at 1.0A/min


 Thursday, October 27, 2016, 15:35

UCx done.

Vented in Ar and transferred to glove box.

Looked inside before inserting 2nd endcap - clean view all the way through the materials to the endcap/ no visible shifting.

Ta coated spring helped hold materials in place, materials expanded minimally ~0.5cm

Pushed materials back to desired length.

Successfully removed a single disc for further analysis.

Second endcap now in with 2x graphite foils.

Both endcaps need expanding.

Ready for assembly.

Requires Rh foil - to be inserted during assembly.


 

  144   Thursday, February 16, 2017, 15:09 Laura LambertUC242218-12LP-SISDoneConditioning UCx#19

 Thursday, February 16, 2017, 15:04

Target container was previously coated with TaC spray and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block

The target consists of 200 discs of UCx with 7.3cm in length [6 packs of 5 + 170 single discs].

Discs in target are arranged as follows: 5singles / 1pack / 40singles / 1pack / 40singles / 2packs / 40singles / 1pack / 40singles / 1pack / 5singles

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down.

The right side is open with a TaC coated spring to help hold materials in.

The chamber is currently pumping down.

TGHT will be ramped up to 475A at 0.1A/min [same current used to reach 1900C in evap2 when sintering TaC coating - elog340 evap2]

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.

NOTE: small bug in evap1 IOC. when current is tapped up 1A, it auto-taps back down 0.01A. should be OK, but will keep an eye on evaporator during conditioning process and acct for changes.


 Friday, February 17, 2017, 09:56

IG1 = 1.56e-6 Torr

Tapped up manually to 35A

Vacuum stable.

IG1 = 1.56e-6 Torr.

Initiating auto-ramp.


 Friday, February 24, 2017, 15:09

Local TGHT 473 A 4.63 V


Monday, February 27, 2017, 09:06 

Target has remained at max setpoints for 20+hrs [epics problems and archives currently not working so unable to find out exact time]

TGHT = 475A, 4.67V

IG1 = 1.48e-6 Torr

Conditioning process is now complete.

Initiating auto-cool at 1.0A/min


 Tuesday, February 28, 2017, 12:00

UCx conditioning process complete.

Vented in Ar and transferred to glove box this morning.


 Tuesday, April 11, 2017, 09:44

A few photos taken of the target post-conditioning.

Note a few flakes came out from one end - end disc from 'open' side flaked off.


 

Attachment 1: IMG_1578.JPG
IMG_1578.JPG
Attachment 2: IMG_1587.JPG
IMG_1587.JPG
Attachment 3: IMG_1594.JPG
IMG_1594.JPG
Attachment 4: IMG_1598.JPG
IMG_1598.JPG
  146   Thursday, April 20, 2017, 11:41 Laura LambertUC242218-1LP-IG-LISDoneConditioning UCx#20

 Thursday, April 20, 2017, 11:31

Target container was previously coated with TaC spray and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block

The target consists of 220 discs of UCx with 7.55cm in length [6 packs of 5 + 190 single discs].

Discs in target are arranged as follows: 1pack / 45singles / 1pack / 50singles / 2packs / 50singles / 1pack / 45singles / 1pack

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down.

The right side is open with a TaC coated spring to help hold materials in.

The chamber is currently pumping down.

TGHT will be ramped up to 490A at 0.1A/min [same current used to reach 1900C in evap2 when sintering TaC coating - elog350 evap2]

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


 Friday, April 21, 2017, 10:14

IG1 = 2.47e-6 Torr

Tapped up manually to 35A.

Waited ~1.5hrs, vacuum stable IG1 = 2.37e-6 Torr

Initiating auto-ramp.


 Thursday, April 27, 2017, 09:19

IG1 = 4.611e-6 Torr

TGHT = 490A, 4.93V

Target has remained at max setpoints for ~9hrs.

Initiating auto-cool at 1.0A/min


 Tuesday, May 16, 2017, 13:21

Update: 

Target looks good, see photos attached post sintering.

Gold tint on container commonly seen with the Uranium targets.

Orange colouring on inside of container end - also common.

Both endcaps in and handed off to assembly yesterday.


 

Attachment 1: 20170420_103410.jpg
20170420_103410.jpg
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20170420_103516.jpg
Attachment 3: 20170420_103154_Richtone(HDR).jpg
20170420_103154_Richtone(HDR).jpg
Attachment 4: 20170508_150816_Richtone(HDR).jpg
20170508_150816_Richtone(HDR).jpg
Attachment 5: 20170512_101150_Richtone(HDR).jpg
20170512_101150_Richtone(HDR).jpg
Attachment 6: 20170512_101348_Richtone(HDR).jpg
20170512_101348_Richtone(HDR).jpg
  155   Wednesday, July 12, 2017, 17:07 Laura LambertUC242218-15LP-SISIn progressConditioning UCx#21

 Wednesday, July 12, 2017, 17:06

Target container was previously coated with TaC and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block

The target consists of 400 discs of UCx with 13.60cm in length [8 packs of 5 + 360 single discs/ 2.6cm on left side, 2.8cm on right side wrt ionizer into page].

Discs in target are arranged as follows: 1pack / 60singles / 1pack / 60singles / 1pack / 60singles / 2packs / 60singles / 1pack / 60singles / 1pack / 60singles / 1pack

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down.

The right side is open with a TaC coated spring to help hold materials in.

The chamber is currently pumping down.

TGHT will be ramped up to 450A at 0.1A/min [same current used to reach 1900C in evap2 when sintering TaC coating - elog373 evap2]

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


Thursday, July 13, 2017, 12:49

Tapped up manually to 35A.

Waited ~2hrs, vacuum stable: IG1 = 2.64e-6 Torr

Initiating auto-ramp.


 

  157   Thursday, July 13, 2017, 14:50 Laura LambertUC242218-15LP-SISProblemsConditioning UCx#21

Laura Lambert wrote:

 Wednesday, July 12, 2017, 17:06

Target container was previously coated with TaC and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block

The target consists of 400 discs of UCx with 13.60cm in length [8 packs of 5 + 360 single discs/ 2.6cm on left side, 2.8cm on right side wrt ionizer into page].

Discs in target are arranged as follows: 1pack / 60singles / 1pack / 60singles / 1pack / 60singles / 2packs / 60singles / 1pack / 60singles / 1pack / 60singles / 1pack

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down.

The right side is open with a TaC coated spring to help hold materials in.

The chamber is currently pumping down.

TGHT will be ramped up to 450A at 0.1A/min [same current used to reach 1900C in evap2 when sintering TaC coating - elog373 evap2]

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


Thursday, July 13, 2017, 12:49

Tapped up manually to 35A.

Waited ~2hrs, vacuum stable: IG1 = 2.64e-6 Torr

Initiating auto-ramp.


 

 Thursday, July 13, 2017, 14:48

Update: auto-ramp not started.

With recent updates to evap1 epics, not everything was uploaded correctly.

TGHT auto-ramp system not working: parameter boxes have white outline indicating locked.

No parameters can be inputed and therefore unable to start auto-ramp.


 Friday, July 14, 2017, 15:56

Problems still not fixed.

Have tapped up manually to 50A, 0.59V

Vacuum stable; IG1 = 5.26e-6 Torr.

Will remain at setpoints over weekend before continuing to ramp up manually...


 Monday, July 17, 2017, 15:10

New problems:

Paddle wheels for evap2 need replacing asap [see elog evap2 i.d.378]

In order to replace, supply/ return need to be turned off and a full purge; therefore, evap1 must be off otherwise it will trip off from no water.

Evap2 needs to be fixed asap and cannot wait for this process to be complete.

Evap1 had been tapped up manually to 60A.

Tapping down manually to 0A so one can start the paddle wheel replacement work tomorrow.


 Tuesday, July 18, 2017, 15:31

Paddle wheels for evap2 replaced and up and running again.

IG1 = 1.2e-6 Torr.

Starting to tap back-up manually...


 

  158   Wednesday, July 19, 2017, 14:15 Laura LambertUC242218-15LP-SISProblems resolvedConditioning UCx#21

Laura Lambert wrote:

Laura Lambert wrote:

 Wednesday, July 12, 2017, 17:06

Target container was previously coated with TaC and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block

The target consists of 400 discs of UCx with 13.60cm in length [8 packs of 5 + 360 single discs/ 2.6cm on left side, 2.8cm on right side wrt ionizer into page].

Discs in target are arranged as follows: 1pack / 60singles / 1pack / 60singles / 1pack / 60singles / 2packs / 60singles / 1pack / 60singles / 1pack / 60singles / 1pack

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down.

The right side is open with a TaC coated spring to help hold materials in.

The chamber is currently pumping down.

TGHT will be ramped up to 450A at 0.1A/min [same current used to reach 1900C in evap2 when sintering TaC coating - elog373 evap2]

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


Thursday, July 13, 2017, 12:49

Tapped up manually to 35A.

Waited ~2hrs, vacuum stable: IG1 = 2.64e-6 Torr

Initiating auto-ramp.


 

 Thursday, July 13, 2017, 14:48

Update: auto-ramp not started.

With recent updates to evap1 epics, not everything was uploaded correctly.

TGHT auto-ramp system not working: parameter boxes have white outline indicating locked.

No parameters can be inputed and therefore unable to start auto-ramp.


 Friday, July 14, 2017, 15:56

Problems still not fixed.

Have tapped up manually to 50A, 0.59V

Vacuum stable; IG1 = 5.26e-6 Torr.

Will remain at setpoints over weekend before continuing to ramp up manually...


 Monday, July 17, 2017, 15:10

New problems:

Paddle wheels for evap2 need replacing asap [see elog evap2 i.d.378]

In order to replace, supply/ return need to be turned off and a full purge; therefore, evap1 must be off otherwise it will trip off from no water.

Evap2 needs to be fixed asap and cannot wait for this process to be complete.

Evap1 had been tapped up manually to 60A.

Tapping down manually to 0A so one can start the paddle wheel replacement work tomorrow.


 Tuesday, July 18, 2017, 15:31

Paddle wheels for evap2 replaced and up and running again.

IG1 = 1.2e-6 Torr.

Starting to tap back-up manually...


 

 Wednesday, July 19, 2017, 14:12

TGHT auto-ramp fixed.

Since TBHT isn't hooked up yet, epics thinks TBHT has tripped off.

Currently during auto-ramp, every time steps up: states TBHT tripped off.

This is not the case but not a big deal as we will soon have TBHT hooked up and this won't be an issue.

Also it only states it, doesn't stop auto-ramp and therefore technically works fine/ will go with this for now...

Note: Might be a few spikes on striptool from past hour when IOC was rebooted.


 

  159   Wednesday, July 19, 2017, 14:17 Laura LambertUC242218-15LP-SISIn progressConditioning UCx#21

Laura Lambert wrote:

Laura Lambert wrote:

Laura Lambert wrote:

 Wednesday, July 12, 2017, 17:06

Target container was previously coated with TaC and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block

The target consists of 400 discs of UCx with 13.60cm in length [8 packs of 5 + 360 single discs/ 2.6cm on left side, 2.8cm on right side wrt ionizer into page].

Discs in target are arranged as follows: 1pack / 60singles / 1pack / 60singles / 1pack / 60singles / 2packs / 60singles / 1pack / 60singles / 1pack / 60singles / 1pack

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down.

The right side is open with a TaC coated spring to help hold materials in.

The chamber is currently pumping down.

TGHT will be ramped up to 450A at 0.1A/min [same current used to reach 1900C in evap2 when sintering TaC coating - elog373 evap2]

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


Thursday, July 13, 2017, 12:49

Tapped up manually to 35A.

Waited ~2hrs, vacuum stable: IG1 = 2.64e-6 Torr

Initiating auto-ramp.


 

 Thursday, July 13, 2017, 14:48

Update: auto-ramp not started.

With recent updates to evap1 epics, not everything was uploaded correctly.

TGHT auto-ramp system not working: parameter boxes have white outline indicating locked.

No parameters can be inputed and therefore unable to start auto-ramp.


 Friday, July 14, 2017, 15:56

Problems still not fixed.

Have tapped up manually to 50A, 0.59V

Vacuum stable; IG1 = 5.26e-6 Torr.

Will remain at setpoints over weekend before continuing to ramp up manually...


 Monday, July 17, 2017, 15:10

New problems:

Paddle wheels for evap2 need replacing asap [see elog evap2 i.d.378]

In order to replace, supply/ return need to be turned off and a full purge; therefore, evap1 must be off otherwise it will trip off from no water.

Evap2 needs to be fixed asap and cannot wait for this process to be complete.

Evap1 had been tapped up manually to 60A.

Tapping down manually to 0A so one can start the paddle wheel replacement work tomorrow.


 Tuesday, July 18, 2017, 15:31

Paddle wheels for evap2 replaced and up and running again.

IG1 = 1.2e-6 Torr.

Starting to tap back-up manually...


 

 Wednesday, July 19, 2017, 14:12

TGHT auto-ramp fixed.

Since TBHT isn't hooked up yet, epics thinks TBHT has tripped off.

Currently during auto-ramp, every time steps up: states TBHT tripped off.

This is not the case but not a big deal as we will soon have TBHT hooked up and this won't be an issue.

Also it only states it, doesn't stop auto-ramp and therefore technically works fine/ will go with this for now...

Note: Might be a few spikes on striptool from past hour when IOC was rebooted.


 

 Wednesday, July 19, 2017, 14:16

Tapped up manually to 30A yesterday.

Continued manual tap up today and reached 60A.

Initiated auto-ramp.

IG1 = 4.4e-6 Torr


 

  160   Thursday, July 20, 2017, 15:00 Laura LambertUC242218-15LP-SISProblemsConditioning UCx#21

Laura Lambert wrote:

Laura Lambert wrote:

Laura Lambert wrote:

Laura Lambert wrote:

 Wednesday, July 12, 2017, 17:06

Target container was previously coated with TaC and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block

The target consists of 400 discs of UCx with 13.60cm in length [8 packs of 5 + 360 single discs/ 2.6cm on left side, 2.8cm on right side wrt ionizer into page].

Discs in target are arranged as follows: 1pack / 60singles / 1pack / 60singles / 1pack / 60singles / 2packs / 60singles / 1pack / 60singles / 1pack / 60singles / 1pack

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down.

The right side is open with a TaC coated spring to help hold materials in.

The chamber is currently pumping down.

TGHT will be ramped up to 450A at 0.1A/min [same current used to reach 1900C in evap2 when sintering TaC coating - elog373 evap2]

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


Thursday, July 13, 2017, 12:49

Tapped up manually to 35A.

Waited ~2hrs, vacuum stable: IG1 = 2.64e-6 Torr

Initiating auto-ramp.


 

 Thursday, July 13, 2017, 14:48

Update: auto-ramp not started.

With recent updates to evap1 epics, not everything was uploaded correctly.

TGHT auto-ramp system not working: parameter boxes have white outline indicating locked.

No parameters can be inputed and therefore unable to start auto-ramp.


 Friday, July 14, 2017, 15:56

Problems still not fixed.

Have tapped up manually to 50A, 0.59V

Vacuum stable; IG1 = 5.26e-6 Torr.

Will remain at setpoints over weekend before continuing to ramp up manually...


 Monday, July 17, 2017, 15:10

New problems:

Paddle wheels for evap2 need replacing asap [see elog evap2 i.d.378]

In order to replace, supply/ return need to be turned off and a full purge; therefore, evap1 must be off otherwise it will trip off from no water.

Evap2 needs to be fixed asap and cannot wait for this process to be complete.

Evap1 had been tapped up manually to 60A.

Tapping down manually to 0A so one can start the paddle wheel replacement work tomorrow.


 Tuesday, July 18, 2017, 15:31

Paddle wheels for evap2 replaced and up and running again.

IG1 = 1.2e-6 Torr.

Starting to tap back-up manually...


 

 Wednesday, July 19, 2017, 14:12

TGHT auto-ramp fixed.

Since TBHT isn't hooked up yet, epics thinks TBHT has tripped off.

Currently during auto-ramp, every time steps up: states TBHT tripped off.

This is not the case but not a big deal as we will soon have TBHT hooked up and this won't be an issue.

Also it only states it, doesn't stop auto-ramp and therefore technically works fine/ will go with this for now...

Note: Might be a few spikes on striptool from past hour when IOC was rebooted.


 

 Wednesday, July 19, 2017, 14:16

Tapped up manually to 30A yesterday.

Continued manual tap up today and reached 60A.

Initiated auto-ramp.

IG1 = 4.4e-6 Torr


 

 Thursday, July 20, 2017, 14:48

TGHT tripped off yesterday evening 

Auto-ramping was fixed but a few more glitches in the system caused the TGHT to trip.

Please refer to photos.

When auto-ramp is running and vacuum reaches the parameter set for 'Good Vacuum', the auto-ramp should stop until the vacuum drops below the good vacuum at which point it can then continue to auto-ramp.

When auto-ramp is running and vacuum reaches the parameter set for 'Bad Vacuum', the auto-ramp should initiate auto-cool/ramp-down until the vacuum drops to the good vacuum parameter at which point it can then proceed with the 'Good Vacuum' requirement.

With this scenario, the auto-ramp system ignored the parameters set for good and bad vacuum, proceeded past both points and continued to ramp until the vacuum eventually reached it's trip off vacuum causing the TGHT to trip.

The TGHT current was at ~90A when it tripped off, so the target should be OK.


 

Attachment 1: Capture.JPG
Capture.JPG
Attachment 2: Capture3.JPG
Capture3.JPG
  161   Thursday, July 20, 2017, 15:35 Laura LambertUC242218-15LP-SISProblems resolvedConditioning UCx#21

Laura Lambert wrote:

Laura Lambert wrote:

Laura Lambert wrote:

Laura Lambert wrote:

Laura Lambert wrote:

 Wednesday, July 12, 2017, 17:06

Target container was previously coated with TaC and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block

The target consists of 400 discs of UCx with 13.60cm in length [8 packs of 5 + 360 single discs/ 2.6cm on left side, 2.8cm on right side wrt ionizer into page].

Discs in target are arranged as follows: 1pack / 60singles / 1pack / 60singles / 1pack / 60singles / 2packs / 60singles / 1pack / 60singles / 1pack / 60singles / 1pack

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down.

The right side is open with a TaC coated spring to help hold materials in.

The chamber is currently pumping down.

TGHT will be ramped up to 450A at 0.1A/min [same current used to reach 1900C in evap2 when sintering TaC coating - elog373 evap2]

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


Thursday, July 13, 2017, 12:49

Tapped up manually to 35A.

Waited ~2hrs, vacuum stable: IG1 = 2.64e-6 Torr

Initiating auto-ramp.


 

 Thursday, July 13, 2017, 14:48

Update: auto-ramp not started.

With recent updates to evap1 epics, not everything was uploaded correctly.

TGHT auto-ramp system not working: parameter boxes have white outline indicating locked.

No parameters can be inputed and therefore unable to start auto-ramp.


 Friday, July 14, 2017, 15:56

Problems still not fixed.

Have tapped up manually to 50A, 0.59V

Vacuum stable; IG1 = 5.26e-6 Torr.

Will remain at setpoints over weekend before continuing to ramp up manually...


 Monday, July 17, 2017, 15:10

New problems:

Paddle wheels for evap2 need replacing asap [see elog evap2 i.d.378]

In order to replace, supply/ return need to be turned off and a full purge; therefore, evap1 must be off otherwise it will trip off from no water.

Evap2 needs to be fixed asap and cannot wait for this process to be complete.

Evap1 had been tapped up manually to 60A.

Tapping down manually to 0A so one can start the paddle wheel replacement work tomorrow.


 Tuesday, July 18, 2017, 15:31

Paddle wheels for evap2 replaced and up and running again.

IG1 = 1.2e-6 Torr.

Starting to tap back-up manually...


 

 Wednesday, July 19, 2017, 14:12

TGHT auto-ramp fixed.

Since TBHT isn't hooked up yet, epics thinks TBHT has tripped off.

Currently during auto-ramp, every time steps up: states TBHT tripped off.

This is not the case but not a big deal as we will soon have TBHT hooked up and this won't be an issue.

Also it only states it, doesn't stop auto-ramp and therefore technically works fine/ will go with this for now...

Note: Might be a few spikes on striptool from past hour when IOC was rebooted.


 

 Wednesday, July 19, 2017, 14:16

Tapped up manually to 30A yesterday.

Continued manual tap up today and reached 60A.

Initiated auto-ramp.

IG1 = 4.4e-6 Torr


 

 Thursday, July 20, 2017, 14:48

TGHT tripped off yesterday evening 

Auto-ramping was fixed but a few more glitches in the system caused the TGHT to trip.

Please refer to photos.

When auto-ramp is running and vacuum reaches the parameter set for 'Good Vacuum', the auto-ramp should stop until the vacuum drops below the good vacuum at which point it can then continue to auto-ramp.

When auto-ramp is running and vacuum reaches the parameter set for 'Bad Vacuum', the auto-ramp should initiate auto-cool/ramp-down until the vacuum drops to the good vacuum parameter at which point it can then proceed with the 'Good Vacuum' requirement.

With this scenario, the auto-ramp system ignored the parameters set for good and bad vacuum, proceeded past both points and continued to ramp until the vacuum eventually reached it's trip off vacuum causing the TGHT to trip.

The TGHT current was at ~90A when it tripped off, so the target should be OK.


 

 Thursday, July 20, 2017, 15:14

Turns out the auto-ramp was reading the vacuum of 'IGP1' which is what the old ion gauge used to be called for evap1 and is currently one on evap2

AKA attempting to take a vacuum reading from one that doesn't exist for evap1

This ion gauge is now labelled 'IGP' and the auto-ramp system now uses 'IGP' for the vacuum parameter confirmations.

Changed a few things in the auto-ramp system:

-Updated messages.

-Auto-ramp aborts when TGHT/TBHT trips off.

-Displays setpoint it is ramping up to for next step

-Confirms which ion gauge it is reading

-Displays final setpoint and increment on message board

-No longer displays TBHT as 'tripped off' when not running.

System updated.


 

  162   Thursday, July 20, 2017, 15:57 Laura LambertUC242218-15LP-SISDoneConditioning UCx#21

Laura Lambert wrote:

Laura Lambert wrote:

Laura Lambert wrote:

Laura Lambert wrote:

Laura Lambert wrote:

Laura Lambert wrote:

 Wednesday, July 12, 2017, 17:06

Target container was previously coated with TaC and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block

The target consists of 400 discs of UCx with 13.60cm in length [8 packs of 5 + 360 single discs/ 2.6cm on left side, 2.8cm on right side wrt ionizer into page].

Discs in target are arranged as follows: 1pack / 60singles / 1pack / 60singles / 1pack / 60singles / 2packs / 60singles / 1pack / 60singles / 1pack / 60singles / 1pack

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down.

The right side is open with a TaC coated spring to help hold materials in.

The chamber is currently pumping down.

TGHT will be ramped up to 450A at 0.1A/min [same current used to reach 1900C in evap2 when sintering TaC coating - elog373 evap2]

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


Thursday, July 13, 2017, 12:49

Tapped up manually to 35A.

Waited ~2hrs, vacuum stable: IG1 = 2.64e-6 Torr

Initiating auto-ramp.


 

 Thursday, July 13, 2017, 14:48

Update: auto-ramp not started.

With recent updates to evap1 epics, not everything was uploaded correctly.

TGHT auto-ramp system not working: parameter boxes have white outline indicating locked.

No parameters can be inputed and therefore unable to start auto-ramp.


 Friday, July 14, 2017, 15:56

Problems still not fixed.

Have tapped up manually to 50A, 0.59V

Vacuum stable; IG1 = 5.26e-6 Torr.

Will remain at setpoints over weekend before continuing to ramp up manually...


 Monday, July 17, 2017, 15:10

New problems:

Paddle wheels for evap2 need replacing asap [see elog evap2 i.d.378]

In order to replace, supply/ return need to be turned off and a full purge; therefore, evap1 must be off otherwise it will trip off from no water.

Evap2 needs to be fixed asap and cannot wait for this process to be complete.

Evap1 had been tapped up manually to 60A.

Tapping down manually to 0A so one can start the paddle wheel replacement work tomorrow.


 Tuesday, July 18, 2017, 15:31

Paddle wheels for evap2 replaced and up and running again.

IG1 = 1.2e-6 Torr.

Starting to tap back-up manually...


 

 Wednesday, July 19, 2017, 14:12

TGHT auto-ramp fixed.

Since TBHT isn't hooked up yet, epics thinks TBHT has tripped off.

Currently during auto-ramp, every time steps up: states TBHT tripped off.

This is not the case but not a big deal as we will soon have TBHT hooked up and this won't be an issue.

Also it only states it, doesn't stop auto-ramp and therefore technically works fine/ will go with this for now...

Note: Might be a few spikes on striptool from past hour when IOC was rebooted.


 

 Wednesday, July 19, 2017, 14:16

Tapped up manually to 30A yesterday.

Continued manual tap up today and reached 60A.

Initiated auto-ramp.

IG1 = 4.4e-6 Torr


 

 Thursday, July 20, 2017, 14:48

TGHT tripped off yesterday evening 

Auto-ramping was fixed but a few more glitches in the system caused the TGHT to trip.

Please refer to photos.

When auto-ramp is running and vacuum reaches the parameter set for 'Good Vacuum', the auto-ramp should stop until the vacuum drops below the good vacuum at which point it can then continue to auto-ramp.

When auto-ramp is running and vacuum reaches the parameter set for 'Bad Vacuum', the auto-ramp should initiate auto-cool/ramp-down until the vacuum drops to the good vacuum parameter at which point it can then proceed with the 'Good Vacuum' requirement.

With this scenario, the auto-ramp system ignored the parameters set for good and bad vacuum, proceeded past both points and continued to ramp until the vacuum eventually reached it's trip off vacuum causing the TGHT to trip.

The TGHT current was at ~90A when it tripped off, so the target should be OK.


 

 Thursday, July 20, 2017, 15:14

Turns out the auto-ramp was reading the vacuum of 'IGP1' which is what the old ion gauge used to be called for evap1 and is currently one on evap2

AKA attempting to take a vacuum reading from one that doesn't exist for evap1

This ion gauge is now labelled 'IGP' and the auto-ramp system now uses 'IGP' for the vacuum parameter confirmations.

Changed a few things in the auto-ramp system:

-Updated messages.

-Auto-ramp aborts when TGHT/TBHT trips off.

-Displays setpoint it is ramping up to for next step

-Confirms which ion gauge it is reading

-Displays final setpoint and increment on message board

-No longer displays TBHT as 'tripped off' when not running.

System updated.


 

Thursday, July 20, 2017, 15:57

Tapped up manually to 35A, 0.45V

IG1 = 5.26e-6 Torr

Re-initiated auto-ramp at 0.1A/min.


 Friday, July 21, 2017, 13:50

TGHT = 81A, 0.92V

IG1 = 5.2e-5 Torr

Vacuum currently yo-yo-ing, but stable.

Changing vacuum limits.

Vacuum limit stop at 1.0e-4 Torr, backing off at 5.0e-4 Torr.

TP = 28.4C, RT = 27.3C


 Thursday, July 27, 2017, 09:02

TGHT = 431A, 4.37V

IG1 = 1.32e-5 Torr

Vacuum stable.

Increasing ramping rate to 0.2A/min

TP = 26.7C, RT = 22.0C


 Friday, July 28, 2017, 09:35

TGHT = 450A, 4.59V

IG1 = 5.4e-6 Torr

Target has remained at max setpoint for 23hrs.

TP = 25.9C, RT = 19.5C

Initiating auto-cool at 1.0A/min


 Friday, August 04, 2017, 13:59

Evap1 was vented in Ar and transferred to the glove box on monday.

A few discs on opened end had slightly shifted [see photo], discs moved back in place - can see down into target.

Discoloration of Ta container to gold in some spots - this is normal as seen with most UCx targets

Target looks good.

Still requires 2nd endcap to be inserted.


 Monday, August 21, 2017, 11:13

Both endcaps in.

No Rh foil inserted.

Endcaps require expanding.


 

Attachment 1: IMG_3249.JPG
IMG_3249.JPG
Attachment 2: IMG_3251.JPG
IMG_3251.JPG
Attachment 3: IMG_3257.JPG
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Attachment 5: IMG_3260.JPG
IMG_3260.JPG
  198   Tuesday, March 20, 2018, 14:52 Laura LambertUC242218-13LP-SISDoneConditioning UCx#22

 Tuesday, March 20, 2018, 14:43

Target container was previously coated with TaC and sintered.

Container is wrapped with 3 layers of Ta-heat shield, including the center block

The target consists of 230 discs of UCx with 7.28cm in length [6 packs of 5 + 200 single discs].

Discs in target are arranged as follows: 1pack / 55singles / 1pack / 50singles / 2packs / 50singles / 1pack / 45singles / 1pack

A regular TaC coated endcap is inserted left, wrt the ionizer tube pointing down.

The right side is open with a TaC coated spring to help hold materials in.

An extra 5 single discs are loaded on the right side on top of the last pack, these discs will be removed after conditioning and analysed using SEM and XRD

The chamber is currently pumping down.

TGHT will be ramped up to 445A and TBHT will be ramped up to 230A [same parameters used to reach 1900C in evap2 when sintering TaC coating - elog402 evap2]

NOTE: This will be the first UCx target to go online using the TBHT in evap1 after the target is loaded with materials.


 Wednesday, March 21, 2018, 09:37

IGP1 = 2.47e-6 Torr

Tapped up manually to 40A.

TGHT = 40A, 0.61V

TBHT = 40A, 0.78V

Waited ~1hr, vacuum stable IG1 = 9.3e-6 Torr

Initiating auto-ramp for TGHT at a rate of 0.2A/min

Initiating auto-ramp for TBHT at a rate of 0.1A/min

Parameter setup: 5.0e-5 good vac, 8.0e-5 bad vac.


Wednesday, March 21, 2018, 13:02

TGHT = 57A, 0.72V

TBHT = 48A, 0.85V

IG1 = 5.8e-5 Torr

Vacuum stable.

Changing vacuum limits.

Vacuum limit stop at 3.0e-4 Torr, backing off at 6.0e-4 Torr.


 Monday, March 26, 2018, 09:32

TGHT = 450A, 4.54V

TBHT = 230A, 2.75V

IGP1 = 8.99e-7 Torr

Target has remained at max setpoint over weekend.

Initiating auto-cool at 1.0A/min for the TGHT and 0.5A/min for the TBHT.


 Wednesday, March 28, 2018, 11:31

Evap1 was vented in Ar and transferred to the glove box yesterday.

Inspection of target still required as well as 2nd endcap to be inserted.


 

  204   Friday, May 11, 2018, 12:36 Marla CervantesUC241369-2LP-SISDoneUCx Fully loaded graphite insert thermal test - FL#1

 Thursday, May 10, 2018, 16:00 

Graphite insert fully loaded with UCx was loaded into previously TaC coated target container.

No end caps on Ta target container.

Weight of graphite tube + UCx discs = 27 g

Currently pumping down in evap1.


Friday, May 11, 2018, 11:41 

IGP1 = 1.13e-6 Torr

Good vac at 3.0e-4, bad vac at 6.0e-4 Torr.

Tapped up manually to 100A.

Pressure increased to ~2e-5 Torr

Vacuum stabilized after 40 min

IGP1 = 1e-5 Torr

Initiating auto ramp for TGHT @ 20 A/min to a max setpoint of 520 A

Initiating auto ramp for TBHT @ 10 A/min to a max setpoint of 245 A

Preassure increased o 1e-4 Torr and the auto ramp was aborted

After 8 min IGP1 = 3e-5 Torr

Initiating auto ramp for TGHT @ 10 A/min to a max setpoint of 520 A

Initiating auto ramp for TBHT @ 5 A/min to a max setpoint of 245 A

The vacuum is more stable.

TBHT reached 230 A at 13:00

TGHT reached 520 A at 13:24

Final pressure 1.15e-4 Torr

Target will stay at max current point for a week.


 Friday, May 18, 2018, 13:01
 
IGP1 = 8.03e-7 Torr
 
TGHT 5.67 V, 519.3 A
 
TBHT 2.59 V, 228.3 A
 
Initiation auto cool at  TGHT  -5 A/min
 
Initiation auto cool at  TBHT  -2 A/min
 
Friday, May 18, 2018, 13:58
 
Accelerating auto cool   TGHT  -10 A/min
 
Accelerating auto cool at  TBHT  -5 A/min

 Friday, May 18, 2018, 18:31

Evap1 was vented in Ar and UCx target was transferred to the glove box

Attachment 1: 180511-FL1_520A.png
180511-FL1_520A.png
  207   Monday, June 04, 2018, 11:29 Marla CervantesUC240282-1TARGET BOATDoneConditioning B13 and 2sc

 Friday, June 01, 2018, 11:20

Target boat was previously coated with TaC and sintered.

Two small C-inserts of ~2cm length were placed on Ta boat

Sample 1-sc: 15 discs of cast 3 made with 1-step cast method (UCx+foil 1.437 g)

Sample 2-sc: 24 discs from rejected discs of 2-step casting (UCx+foil 1.585 g)

Ta boat was wrapped with 3 layers of Ta-heat shield

The chamber is currently pumping down.

TGHT will be ramped up to 495A [same parameters used to reach 1910C in evap2 when sintering TaC coating - elog410 evap2]


Monday, June 04, 2018, 11:27 

IG1 = 4e-7 Torr

Tapped up manually to 35A

Waited 1hr

Vacuum stable.

IG1 = 8.02e-7 Torr.

Initiating auto-ramp (0.1 A/min) up to 80 A


 Tuesday, June 07, 2018, 15:47

Vacuum stable

IG1 = 7.02e-7 Torr.

Changing auto-ramp to 0.02 A/min up to 140 A


Thursday, June 07, 2018, 15:49 

Vacuum stable 5.5e-7 Torr

Current 139 A, voltage 1.25 V

Changing auto-ramp to 0.1 A/min up to 495 


Saturday, June 9, 2018, 10:41 

The material stayed 4 hours at 495 A

Auto-ramp set to -1 A/min down to 0 A 


Monday, June 11, 2018, 17:43 

EVAPI was vented with Ar and UCx was transferred to glove box

 

 

 

  213   Thursday, July 05, 2018, 13:43 John WongUC2 HP-FEBIAD-CTLDoneConditioning UCx#23

Thursday, July 05, 2018, 13:24

Target container was previously coated and sintered with TaC, also wrapped with Ta heat shields (see Evap2 elog# 410).

Loaded 201 discs of UCx with 7.27 cm in length + 5 extra discs for QC samples. 

One end-cap (coated/sintered TaC) inserted right, wrt the ionizer tube pointing down.

Left side is OPEN; a spring is inserted to hold the discs in place.

Chamber is currently being pumped down. 

TGHT will be ramped up to 495A/8.85V and TBHT to 230A/3.26V (same parameters used for sintering the container, evap2 elog#410).

 

Vacuum initial setting:

Good Vac = 5.0 e-5 Torr, Bad vac = 8.0 e-5 Torr.

pressure level will be monitored accordingly...

 

Auto-ramping setting

TGHT: 60 wait time, 0.2A/min, final 495A

TGHT: 60 wait time, 0.2A/min, final 230A.

 


 Thursday, July 05, 2018, 16:50

Tapping up TGHT to 40 A/0.49 V and TGHT to 40A/0.64V.

Vac slowly increasing from 5.0 e-6 Torr. 

Initiate auto-heating


 Tuesday, July 10, 2018, 10:46

Holding TGHT at 495A/5.3V for over 25 hours.  Pressure at 2.9e-6 Torr.

Initiate autocooling TGHT at 2A/min, TBHT 1.0A/min


 Wednesday, July 11, 2018, 17:12

Target was removed from the Evap; it is now in the Ar glovebox.  End cap is inserted. 

Target is ready for installation.


 

  215   Friday, August 03, 2018, 17:49 John WongUC2 LP-SISIn progressConditioning UCx#24

Friday, August 03, 2018, 17:44

Target consists of 230 UCx discs, total packing length of 7.1cm. 

Container was previously coated/sintered with TaC (see elog #415) in Evap#2 with TGHT set to 450A/7.5V and TBHT 230A/4.2

Vacuum initial setting:

Good Vac = 5.0 e-5 Torr, Bad vac = 8.0 e-5 Torr.

pressure level will be monitored accordingly...

 

Auto-ramping setting

TGHT: 60 wait time, 0.2A/min, final 450A

TGHT: 60 wait time, 0.2A/min, final 230A.

 

Chamber is currently being pumped down.Good


 Monday, August 06, 2018, 00:04

Pressure at 3.6e-6 Torr. 

Initiate autoramping.


 Friday, August 10, 2018, 11:02

TGHT/TBHT have been at 450A(4.5V)/230A(2.9) for over 15 hours.

Pressure is stabilized at 5.2e-6 Torr. 

Initiated auto-cooling at 2A/min for TGHT and 1A/min for TBHT.


 

  216   Friday, August 17, 2018, 11:23 Marla CervantesUC2NA DoneUCx 1-step casting -Oxidation test

 Friday, August 17, 2018, 11:17

Four discs of UCx produced with the 1-step casting method were placed in a glass jar.

The mass of the discs was 0.400 g.

The glass jar with the discs were placed in the heating chamber of the IEVAP.

Currently IEVAP is pumping down until vacuum is in the order of  ~10^-6 Torr.


Friday, August 17, 2018, 16:28 

Final vacuum: 9.5x10^-6 Torr

IEVAP's heating chamber will be vented with air and the materials will be taken out.


 Friday, August 17, 2018, 17:27

Material was transferred to the glove box


 

  217   Tuesday, September 04, 2018, 10:18 Marla CervantesUC241369-2 In progressUCx Fully loaded graphite insert thermal test - FL#1.2

 Monday, September 03, 2018, 10:17

Graphite insert fully loaded with UCx was loaded into previously TaC coated target container.

No end caps on Ta target container.

Weight of graphite tube + UCx discs = 27.118 g

Currently pumping down in evap1.


Tuesday, September 04, 2018, 10:17 

IGP1 = 4.02e-6 Torr

Tapped up TBHT and TGHT manually to 100 A @1 A/s with pauses of 20 s.

Wait for 40 min to pressure to stabilize.

Max pressure 1.38e-4 Torr.

Final pressure 5.93e-5 Torr.


Tuesday, September 04, 2018, 11:46 

Good vacuum 5e-1 Torr

Bad vacuum 8e-1 Torr

Initiating auto ramp for TGHT @ 10 A/min to a max setpoint of 520 A

Initiating auto ramp for TBHT @ 5 A/min to a max setpoint of 245 A


 Tuesday, September 04, 2018, 12:54

 After achieving 520 A with auto ramp, manually tapped to 599 A.

Manually tapped back to 550 A.

 

Attachment 1: 180904-UCxFL1-T2-2.png
180904-UCxFL1-T2-2.png
  218   Friday, September 21, 2018, 10:22 Anders MjosUC241369-2 DoneUCx Fully loaded graphite insert thermal test - FL#1.2

Marla Cervantes wrote:

 Monday, September 03, 2018, 10:17

Graphite insert fully loaded with UCx was loaded into previously TaC coated target container.

No end caps on Ta target container.

Weight of graphite tube + UCx discs = 27.118 g

Currently pumping down in evap1.


Tuesday, September 04, 2018, 10:17 

IGP1 = 4.02e-6 Torr

Tapped up TBHT and TGHT manually to 100 A @1 A/s with pauses of 20 s.

Wait for 40 min to pressure to stabilize.

Max pressure 1.38e-4 Torr.

Final pressure 5.93e-5 Torr.


Tuesday, September 04, 2018, 11:46 

Good vacuum 5e-1 Torr

Bad vacuum 8e-1 Torr

Initiating auto ramp for TGHT @ 10 A/min to a max setpoint of 520 A

Initiating auto ramp for TBHT @ 5 A/min to a max setpoint of 245 A


 Tuesday, September 04, 2018, 12:54

 After achieving 520 A with auto ramp, manually tapped to 599 A.

Manually tapped back to 550 A.

 

 Friday, September 21, 2018, 10:21

Ramping down heaters at 2 A/min and 1 A/min for TGHT and TBHT.

  220   Saturday, September 29, 2018, 20:53 John WongUC241369-2 DoneUCx Fully loaded graphite insert thermal test - FL#1.2

Marla Cervantes wrote:

 Monday, September 03, 2018, 10:17

Graphite insert fully loaded with UCx was loaded into previously TaC coated target container.

No end caps on Ta target container.

Weight of graphite tube + UCx discs = 27.118 g

Currently pumping down in evap1.


Tuesday, September 04, 2018, 10:17 

IGP1 = 4.02e-6 Torr

Tapped up TBHT and TGHT manually to 100 A @1 A/s with pauses of 20 s.

Wait for 40 min to pressure to stabilize.

Max pressure 1.38e-4 Torr.

Final pressure 5.93e-5 Torr.


Tuesday, September 04, 2018, 11:46 

Good vacuum 5e-1 Torr

Bad vacuum 8e-1 Torr

Initiating auto ramp for TGHT @ 10 A/min to a max setpoint of 520 A

Initiating auto ramp for TBHT @ 5 A/min to a max setpoint of 245 A


 Tuesday, September 04, 2018, 12:54

 After achieving 520 A with auto ramp, manually tapped to 599 A.

Manually tapped back to 550 A.

 

 Saturday, September 29, 2018, 20:52

Target is taken out from the chamber and transferred to the Ar glove box.


 

  221   Thursday, October 11, 2018, 18:13 John WongUC2 LP-SISIn progressConditioning UCx#25

Thursday, October 11, 2018, 18:06

Target consists of 284 UCx discs, total packing length of 8.0 cm. 

Container was previously coated/sintered with TaC (see elog #417) in Evap#2 with TGHT set to 400A and TBHT 230A, but there was a problem with the readback.  Will ramp up TGHT to 400A to see if the carbonization is complete; if not, additional 50A on TGHT can be applied.

One end-cap is inserted on the right, wrt to the ionizer, and left end is open. 

Vacuum initial setting:

Good Vac = 5.0 e-5 Torr, Bad vac = 8.0 e-5 Torr.

pressure level will be monitored accordingly...

Auto-ramping setting

TGHT: 60 wait time, 0.2A/min, final 400A (or addtional of 50 A if required as mentioned above)

TGHT: 60 wait time, 0.2A/min, final 230A.

 Chamber is currently being pumped down.


 Friday, October 12, 2018, 15:35

Chamber has pumped down to 1.8e-6 Torr. 

Stepping up TGHT and TBHT to 40A.


 Friday, October 12, 2018, 17:07

TGHT/TBTH was held at 40A reaching max pressure of 1.7e-5 before slowly coming down. 

Initiated autoramping.


 Thursday, October 18, 2018, 11:10

TGHT reached to 400A/3.98V, pressure is coming down from the upper limit at around 320A which indicated the carbonization is approaching to completion (see attachment#1).  However, two more out-gassing steps are typically observed as TGHT reached around 450 A (see previous UCx conditioning process).  Currently the pressure is at 1.04 e-5 torr. 

Auto-ramping TGHT to 450A at 1A/min, continue to observe the vacuum...


 Thursday, October 18, 2018, 12:57

TGHT reached to 450A/4.6V. Pressure is coming down from 1.6 e-5 Torr. (see attachment#2).  Will remain at this heating current until pressure reached to mid 10-6 torr.


 

Attachment 1: UC#25_conditioning.JPG
UC#25_conditioning.JPG
Attachment 2: UC#25_conditioning-450A.JPG
UC#25_conditioning-450A.JPG
  223   Tuesday, October 23, 2018, 10:24 Marla CervantesUC2 LP-SISProblemsConditioning UCx#25

John Wong wrote:

Thursday, October 11, 2018, 18:06

Target consists of 284 UCx discs, total packing length of 8.0 cm. 

Container was previously coated/sintered with TaC (see elog #417) in Evap#2 with TGHT set to 400A and TBHT 230A, but there was a problem with the readback.  Will ramp up TGHT to 400A to see if the carbonization is complete; if not, additional 50A on TGHT can be applied.

One end-cap is inserted on the right, wrt to the ionizer, and left end is open. 

Vacuum initial setting:

Good Vac = 5.0 e-5 Torr, Bad vac = 8.0 e-5 Torr.

pressure level will be monitored accordingly...

Auto-ramping setting

TGHT: 60 wait time, 0.2A/min, final 400A (or addtional of 50 A if required as mentioned above)

TGHT: 60 wait time, 0.2A/min, final 230A.

 Chamber is currently being pumped down.


 Friday, October 12, 2018, 15:35

Chamber has pumped down to 1.8e-6 Torr. 

Stepping up TGHT and TBHT to 40A.


 Friday, October 12, 2018, 17:07

TGHT/TBTH was held at 40A reaching max pressure of 1.7e-5 before slowly coming down. 

Initiated autoramping.


 Thursday, October 18, 2018, 11:10

TGHT reached to 400A/3.98V, pressure is coming down from the upper limit at around 320A which indicated the carbonization is approaching to completion (see attachment#1).  However, two more out-gassing steps are typically observed as TGHT reached around 450 A (see previous UCx conditioning process).  Currently the pressure is at 1.04 e-5 torr. 

Auto-ramping TGHT to 450A at 1A/min, continue to observe the vacuum...


 Thursday, October 18, 2018, 12:57

TGHT reached to 450A/4.6V. Pressure is coming down from 1.6 e-5 Torr. (see attachment#2).  Will remain at this heating current until pressure reached to mid 10-6 torr.


 

 Friday, October 19, 2018, 10:00

TRIUMF had a total power outage, the TBHT  and TGHT current had been ramped down already.


 

  224   Tuesday, October 23, 2018, 10:49 Marla CervantesUC2 LP-SISProblems resolvedConditioning UCx#25

Marla Cervantes wrote:

John Wong wrote:

Thursday, October 11, 2018, 18:06

Target consists of 284 UCx discs, total packing length of 8.0 cm. 

Container was previously coated/sintered with TaC (see elog #417) in Evap#2 with TGHT set to 400A and TBHT 230A, but there was a problem with the readback.  Will ramp up TGHT to 400A to see if the carbonization is complete; if not, additional 50A on TGHT can be applied.

One end-cap is inserted on the right, wrt to the ionizer, and left end is open. 

Vacuum initial setting:

Good Vac = 5.0 e-5 Torr, Bad vac = 8.0 e-5 Torr.

pressure level will be monitored accordingly...

Auto-ramping setting

TGHT: 60 wait time, 0.2A/min, final 400A (or addtional of 50 A if required as mentioned above)

TGHT: 60 wait time, 0.2A/min, final 230A.

 Chamber is currently being pumped down.


 Friday, October 12, 2018, 15:35

Chamber has pumped down to 1.8e-6 Torr. 

Stepping up TGHT and TBHT to 40A.


 Friday, October 12, 2018, 17:07

TGHT/TBTH was held at 40A reaching max pressure of 1.7e-5 before slowly coming down. 

Initiated autoramping.


 Thursday, October 18, 2018, 11:10

TGHT reached to 400A/3.98V, pressure is coming down from the upper limit at around 320A which indicated the carbonization is approaching to completion (see attachment#1).  However, two more out-gassing steps are typically observed as TGHT reached around 450 A (see previous UCx conditioning process).  Currently the pressure is at 1.04 e-5 torr. 

Auto-ramping TGHT to 450A at 1A/min, continue to observe the vacuum...


 Thursday, October 18, 2018, 12:57

TGHT reached to 450A/4.6V. Pressure is coming down from 1.6 e-5 Torr. (see attachment#2).  Will remain at this heating current until pressure reached to mid 10-6 torr.


 

 Friday, October 19, 2018, 10:00

TRIUMF had a total power outage, the TBHT  and TGHT current had been ramped down already.


 

  Sunday, October 21, 2018, 1:00 pm

the pumps went out, and the communication with the IEVAP was recovered on Sunday, the vacuum was 160 mTorr,

the pumps were turned on again.


 

  225   Tuesday, October 23, 2018, 10:55 Marla CervantesUC2 LP-SISDoneConditioning UCx#25

Marla Cervantes wrote:

Marla Cervantes wrote:

John Wong wrote:

Thursday, October 11, 2018, 18:06

Target consists of 284 UCx discs, total packing length of 8.0 cm. 

Container was previously coated/sintered with TaC (see elog #417) in Evap#2 with TGHT set to 400A and TBHT 230A, but there was a problem with the readback.  Will ramp up TGHT to 400A to see if the carbonization is complete; if not, additional 50A on TGHT can be applied.

One end-cap is inserted on the right, wrt to the ionizer, and left end is open. 

Vacuum initial setting:

Good Vac = 5.0 e-5 Torr, Bad vac = 8.0 e-5 Torr.

pressure level will be monitored accordingly...

Auto-ramping setting

TGHT: 60 wait time, 0.2A/min, final 400A (or addtional of 50 A if required as mentioned above)

TGHT: 60 wait time, 0.2A/min, final 230A.

 Chamber is currently being pumped down.


 Friday, October 12, 2018, 15:35

Chamber has pumped down to 1.8e-6 Torr. 

Stepping up TGHT and TBHT to 40A.


 Friday, October 12, 2018, 17:07

TGHT/TBTH was held at 40A reaching max pressure of 1.7e-5 before slowly coming down. 

Initiated autoramping.


 Thursday, October 18, 2018, 11:10

TGHT reached to 400A/3.98V, pressure is coming down from the upper limit at around 320A which indicated the carbonization is approaching to completion (see attachment#1).  However, two more out-gassing steps are typically observed as TGHT reached around 450 A (see previous UCx conditioning process).  Currently the pressure is at 1.04 e-5 torr. 

Auto-ramping TGHT to 450A at 1A/min, continue to observe the vacuum...


 Thursday, October 18, 2018, 12:57

TGHT reached to 450A/4.6V. Pressure is coming down from 1.6 e-5 Torr. (see attachment#2).  Will remain at this heating current until pressure reached to mid 10-6 torr.


 

 Friday, October 19, 2018, 10:00

TRIUMF had a total power outage, the TBHT  and TGHT current had been ramped down already.


 

  Sunday, October 21, 2018, 1:00 pm

the pumps went out, and the communication with the IEVAP was recovered on Sunday, the vacuum was 160 mTorr,

the pumps were turned on again.


 

 Monday, October 22, 2018, 9:00

The target was transferred to the Ar glove box.


 Tuesday, October 23, 2018, 10:19

Target was inspected:

- Discs were in place

- Orange coating formed on the open end of target container

Spring was removed, two graphite discs were introduced, end cap was placed.

Attachment 1: OrangeCoat.jpg
OrangeCoat.jpg
Attachment 2: IonizerTube.jpg
IonizerTube.jpg
Attachment 3: ClosedSide.jpg
ClosedSide.jpg
  228   Tuesday, October 30, 2018, 10:17 Marla CervantesUC243044-7 LP-SISIn progressUCx Fully loaded graphite insert thermal test - FL#1

 Tuesday, October 30, 2018, 10:12

A new LP-SIS was coated and syntered (e-log 420 Evaporator_2) 

The container was loaded with a graphite insert loaded with UCx

Graphite insert + UCx mass = 26.927 g

A current of 440 A TGHT and 230 A TBHT will be inputed to the contianer


IGP1 = 8.72e-7 Torr

 The current was tapped manually to 440 A TGHT and 230 A TBHT (see fig. Heatinf test)

Maximum pressure during heating = 1.7e-3 Torr.

Target will stay at maximum current for 1 week.

 

Attachment 1: Heat_test.JPG
Heat_test.JPG
  229   Wednesday, October 31, 2018, 10:30 Marla CervantesUC243044-7 LP-SISProblemsUCx Fully loaded graphite insert thermal test - FL#1

Marla Cervantes wrote:

 Tuesday, October 30, 2018, 10:12

A new LP-SIS was coated and syntered (e-log 420 Evaporator_2) 

The container was loaded with a graphite insert loaded with UCx

Graphite insert + UCx mass = 26.927 g

A current of 440 A TGHT and 230 A TBHT will be inputed to the contianer


IGP1 = 8.72e-7 Torr

 The current was tapped manually to 440 A TGHT and 230 A TBHT (see fig. Heating test)

Maximum pressure during heating = 1.7e-3 Torr.

Target will stay at maximum current for 1 week.

 Wednesday, October 31, 2018, 10:09

The current tripped off,  around 5:00 am, the pressure was below 1e-5 Torr (see fig. current-trip_off).

On a previous test, we measured the maximum temperature of the power supply = 33.3 C (e-log 227).

Power supply overheating doesn't seem to be the problem.

EPICS windows are half withe and not answering correctly.

Also, TBHT says that IGP1 < 500 mTorr, and its interlock needs reset (see figure EPICS).

Attachment 1: current-trip_off.JPG
current-trip_off.JPG
Attachment 2: epics.JPG
epics.JPG
  230   Wednesday, October 31, 2018, 15:23 Marla CervantesUC243044-7 LP-SISDoneUCx Fully loaded graphite insert thermal test - FL#1

Marla Cervantes wrote:

Marla Cervantes wrote:

 Tuesday, October 30, 2018, 10:12

A new LP-SIS was coated and syntered (e-log 420 Evaporator_2) 

The container was loaded with a graphite insert loaded with UCx

Graphite insert + UCx mass = 26.927 g

A current of 440 A TGHT and 230 A TBHT will be inputed to the contianer


IGP1 = 8.72e-7 Torr

 The current was tapped manually to 440 A TGHT and 230 A TBHT (see fig. Heating test)

Maximum pressure during heating = 1.7e-3 Torr.

Target will stay at maximum current for 1 week.

 Wednesday, October 31, 2018, 10:09

The current tripped off,  around 5:00 am, the pressure was below 1e-5 Torr (see fig. current-trip_off).

On a previous test, we measured the maximum temperature of the power supply = 33.3 C (e-log 227).

Power supply overheating doesn't seem to be the problem.

EPICS windows are half withe and not answering correctly.

Also, TBHT says that IGP1 < 500 mTorr, and its interlock needs reset (see figure EPICS).

 Wednesday, October 31, 2018, 15:20

The problem was reported to controls, it will be also reported to power supply group.

In the meantime, the target will be ramp-up again with the auto ramp at:

TGHT = 20 A/min to 440 A

TBHT = 10 A/min to 230 A 

The pressure before heating is 4.07e-7 Torr


Wednesday, October 31, 2018, 19:24

The maximum pressure during heating was 6.57e-6 Torr.

Current pressure 3.00e-6Torr


Wednesday, November 07, 2018, 18:37

IGP1 = 9.7e-7 Torr

 TGHT = -2 A/min to 0A

TBHT = -1 A/min to 0A 


 Thursday, November 08, 2018, 16:16

EVAP1 was vented with Ar, and target was transferred to glove box.

The mass of the loaded graphite insert changed to 26.854 g

That is a difference of 0.075 g

The tantalum container "cathode" crystalized (see fig)

The rest of the tantalum container did not change.

Attachment 1: Ta-container.png
Ta-container.png
  241   Wednesday, September 18, 2019, 09:57 Marla CervantesUC244062-4LP-SISDoneUCx28 Conditioning #1

Wednesday, September 18, 2019, 07:48

A TaC coated target container  was loaded with a graphite cartridge with UCx

The target container has 3 heat shields


IGP1 = 9.3e-6 Torr

Autoramp set up to:

TGHT= 0.2 A/min to 438 A (same current used to reach 1900C in evap2 when sintering TaC coating - elog-455 evap2)

TBHT= 0.1 A/min 230 A

The limits are:

Good vacuum 5e-5 Torr

Bad vacuum 8e-5 Torr


Wednesday, September 18, 2019, 09:55

The autoramp where changed to 1 A/min on both the TGHt and the TGHT.


 Wednesday, September 18, 2019, 21:06

After 4 hours at TGHT = 4.15 V, 437.76 A and TBHT = 2.77 V, 228.31 A (and pressure of 1.07e-5 Torr)

The autoramp was set to TGHT = - 1 A/min and TBHT = -0.5 Torr


Tuesday, September 29, 2019, 14:05

 The EVAP1 was vented with Ar and the target was removed, 

The target was directly assembled after removing it from EVAP1

Finally, the assembly was transferred to the glove box

  242   Tuesday, September 24, 2019, 06:53 Marla CervantesUC244062-4LP-SISDoneUCx28 Conditioning #2

 Tuesday, September 24, 2019, 06:52

The target UCx28 that was previously conditioned e-log 241, was set again in the EVAP1 for re-conditioning,

the reason was to get rid of all the material that could evaporate from the target and has the potential of clogging the ionizer.

The heating conditions are the same as the previous conditioning:

TGHT= 1 A/min to 438 A (same current used to reach 1900C in evap2 when sintering TaC coating - elog-455 evap2)

TBHT= 1 A/min 230 A

IGP1 = 2.91e-6 Torr


 Wednesday, September 24, 2019, 18:30

IGP1 = 5.77e-6 Torr

The cooling conditions are the same as the previous conditioning:

TGHT= -1 A/min 

TBHT= -0.5 A/min


 Wednesday, September 25, 2019, 13:56

EVAP1 was vented with Ar,

The target container was removed to look at the Ta cap

The Ta cap was coated.


Wednesday, September 25, 2019, 13:58 

A new Ta cap was set in the transfer tube hole and the target container was installed again.

  243   Wednesday, September 25, 2019, 14:00 Marla CervantesUC244062-4LP-SISDoneUCx28 Conditioning #3

Wednesday, September 25, 2019, 14:00 

The target UCx28 that was previously conditioned , was set again in the EVAP1 for re-conditioning,

the reason was to get rid of all the material that could evaporate from the target and has the potential of clogging the ionizer.

EVAP1 currently pumping down.


Thursday, September 26, 2019, 07:09 

The heating conditions are the same as the previous conditioning:

TGHT= 1 A/min to 438 A (same current used to reach 1900C in evap2 when sintering TaC coating - elog-455 evap2)

TBHT= 1 A/min 230 A

IGP1 = 1.51e-6 Torr


Friday, September 26, 2019, 12:56

The cooling conditions are the same as the previous conditioning:

TGHT= -1 A/min 

TBHT= -0.5 A/min


Friday, September 27, 2019, 17:59

EVAP1 was vented with Ar, the target was removed from the heating chamber to exchange the Ta cap for a new one.

The old Ta cap was not fully coated and it presented a different coloration with respect to the 2 previous caps used for conditioning.

  244   Friday, September 27, 2019, 18:04 Marla CervantesUC244062-4LP-SISDoneUCx28 Conditioning #4

Friday, September 27, 2019, 18:03

The target UCx28 that was previously conditioned , was set again in the EVAP1 for re-conditioning,

the reason was to get rid of all the material that could evaporate from the target and has the potential of clogging the ionizer.

EVAP1 currently pumping down.


Saturday, September 28, 2019, 09:33 

The heating conditions are the same as the previous conditioning:

TGHT= 1 A/min to 438 A (same current used to reach 1900C in evap2 when sintering TaC coating - elog-455 evap2)

TBHT= 1 A/min 230 A

IGP1 = 1.419e-6 Torr

The ramping started at 9:36 am on Septemper 28th 


Sunday, September 29, 2019, 12:30

The cooling conditions are the same as the previous conditioning:

TGHT= -1 A/min 

TBHT= -0.5 A/min


Monday, September 30, 2019, 11:40 

After 23 hours being heated, the target was cooled down and EVAP1 was vented with Ar

The target was removed form EVAP1 and placed in the fumehood.

The tantalum cap used to collect the outgassed material from the target container was not fully coated.


The heat shields of the target container were removed and the target container was inspected,

the ends of the Ta container were crystallized, the area above the graphite cartridge does not have signs of crystallization. 

Attachment 1: IMG_1393.JPG
IMG_1393.JPG
  245   Wednesday, October 02, 2019, 11:07 Marla CervantesUC244062-4LP-SISDoneUCx28 Conditioning #5

Monday, September 30, 2019, 10:54 

After being exposed to air for 1.5 hours,

the target UCx28 that was previously conditioned , was set again in the EVAP1 for re-conditioning.

The UCx28 was wrapped with 3 new Ta-heat shields and placed in the EVAP1, 

EVAP1 is currently pumping down.


Tuesday, October 1, 2019, 08:33

The heating conditions are:

TGHT= 1 A/min to 430 A 

TBHT= 1 A/min 230 A

Initial vacuum IGP1 = 1.22193-6 Torr

 


Since the ends of the target container are crystallized and the voltage is starting to vary, the target was heated only for 3 hours instead of 4.

The cooling conditions are the same as the previous conditioning:

TGHT= -1 A/min 

TBHT= -0.5 A/min


Wednesday, October 02, 2019, 11:01 

EVAP1 was vented with Ar and the target was removed form EVAP1 and assembled,

the assembly was placed in the glove box.

The tantalum cap used to collect the outgassed material from the target container was not fully coated.

  247   Tuesday, October 08, 2019, 09:53 Marla CervantesUC244062-6LP-SISDoneUCx29 Conditioning

Monday, October 07, 2019, 09:51 

A TaC coated target container  was loaded with a graphite cartridge with UCx

The target container has 3 heat shields


Tuesday, October 08, 2019, 09:51 

IGP1 = 1.9596e-6 Torr

Autoramp set up to:

TGHT= 1 A/min to 425 A (same current used to reach 1900C in evap2 when sintering TaC coating - e-log 241 evap2)

TBHT= 1 A/min 230 A

The limits are:

Good vacuum 5e-5 Torr

Bad vacuum 8e-5 Torr


Wednesday, October 09, 2019, 13:58

After 4 hours at maximum current, the current was ramped down at 1 A/min for both.


Wednesday, October 09, 2019, 14:00

EVAP1 was vented with Ar, and the target oven was removed to access the Ta cap.

The Ta cap difference in mass was 0.002 g

  251   Wednesday, November 06, 2019, 11:48 Marla CervantesUC244062-3 LP-SISDoneUCx#30 Conditioning

 Tuesday, November 05, 2019, 16:43

A TaC coated target container  was loaded with a graphite cartridge with UCx

The target container has 3 heat shields

EVAP1 pumping down


Wednesday, November 06, 2019, 11:46 

IGP1 = 2.09e-6 Torr

Good vacuum 5e-5 Torr

Bad vacuum 8e-5 Torr

Autoramp set up to:

TGHT= 1 A/min to 465 A (same current used to reach 1865 C in evap2 when sintering TaC coating - e-log 464 evap2)

TBHT= 1 A/min 230 A


 Thursday, November 07, 2019, 10:15

After approximately 4 hours at maximum temperature the pressure was 5.85e-6 Torr and the autoramp was set to:

TGHT -1 A/min

TBHT -0.5 A/min

After 4 hours that the current stayed at 0 A, EVAP1 was vented with argon and the target was removed; before transferring the target to the preparatory glove box, the tantalum cap to collect deposits from the target was inspected, there was not deposits on it so it was determined that the conditioning was successful and the target was transferred to the preparatory glove box.

  271   Saturday, June 05, 2021, 09:14 Marla CervantesUC2 TARGET BOATIn progressUCx#33 Conditioning

 Saturday, June 05, 2021, 08:57

Target #33 was installed in the EVAP1 and pumped down yesterday (Friday 4).

Target #33 is going to be conditioned on a Ta boat wrapped with 3 Ta foils.

IGP1 = 3.85e-6 Torr

Good vacuum = 1e-1 Torr

Bad vacuum = 5e-1 Torr

Power desired 1.6kW. This is the first target conditioned this way, 


Saturday, June 05, 2021, 09:13

Current ramp is 2A/30s to 400 A


Saturday, June 05, 2021, 10:59

TGHT = 3.5V, 399.7 A, 1.4 kW

IGP1 = 4.4e-5 Torr


Saturday, June 05, 2021, 11:00  

Current ramp is 2A/30s to 450 A


Saturday, June 05, 2021, 11:14

 TGHT = 4.06 V, 451.584 A, 1.4 kW

IGP1 = 4.86e-5 Torr


Saturday, June 05, 2021, 11:15 

Current ramp is 2A/30s to 500 A


Saturday, June 05, 2021, 11:23

TGHT = 4.23 V, 467.2 A, 1.97 kW pressure was still increasing a little at 1.6kW

IGP1 = 4.86e-5 Torr


Saturday, June 05, 2021, 19:10

 TGHT = 4.08 V, 459.52 A, 

IGP1 = 6.4e-6 Torr

Initiate ramp down  at 2 A/min to 0A

  274   Wednesday, September 15, 2021, 07:19 Marla CervantesUC2 TARGET BOATDoneConditioning 2sc samples

Wednesday, September 14, 2021, 21:14

Boat is wrapped with 2 layers of Ta-heat shield

The samples consists of 15 discs of UCx of 14mm diameter

The chamber is currently pumping down.

TGHT will be ramped up to 450 A


Wednesday, September 15, 2021, 07:17

IGP1 = 6.75e-6 Torr

Tapped up manually to 40A.

TGHT = 60 A, 2.39 V

Vacuum stable IG1 = 7.25e-6 Torr

Initiating auto-ramp for TGHT at a rate of 0.2A/min to 445 A

Parameter setup: 5.0e-5 good vac, 8.0e-5 bad vac.


 Wednesday, September 15, 2021, 11:57

IGP1=2.24e-5 Torr

TGHT= 102.016 A, 1.275 V

Autoramp changed to 1A/min to 450 A


Wednesday, September 15, 2021, 12:53

IGP1 = 3.3e-5 torr

TGHT= 150 A,  V

Autoramp changed to 2A/30s to 450 A

 1e-1 good vac, 5e-1 bad vac


Wednesday, September 15, 2021, 12:59

 


Friday, September 17, 2021, 07:54

IGP1 = 3.81e-6 Torr

TGHT = 449.6 A, 4.31 V

Autoramp set to -2A/min to 0 A 

  279   Wednesday, April 13, 2022, 10:55 Luca EgoritiUC2 P2N-SISDoneP2N carbothermal reduction P2Ncartridge-220323

Wednesday, April 13, 2022, 10:50

P2NC-220323

Preparing the P2N-UCx for online operation on June 2022

Two cartridges were filled with annular UO2/C foils last week.

48 cartridges total

Today, Darwin and I are placing one of the two cartridges in the EVAP1. The cartridge is P2NC-220323.

 


Thursday, April 14, 2022, 09:34

Carbothermal reduction heating process started with a ramp rate of 3 A/min

Pressure 1.8E-6T

 


Thursday, April 14, 2022, 10:31

Paused autoramp because pressure increasing too rapidly. Will continue ramp up once pressure stabilizes.

 


Thursday, April 14, 2022, 11:20

autoramp restarted @3A/min

IGP1=2.7E-4 Torr

 


Thursday, April 14, 2022, 13:24

After first major outgass finished and pressure trending down, increased autoramp to 5A/min to 600A


Thursday, April 14, 2022, 13:27

IGP1 = 3.3E-4A

TGHT = 600A, 2.5V

decrease ramp rate to 3A/min to 650A


Thursday, April 14, 2022, 13:45

Set autoramp to 670A


Thursday, April 14, 2022, 13:52

paused autoramp at 668A because pressure increase too steep. 

Changed ramp rate to 0.5A/min and restarted ramp up to 700A


Thursday, April 14, 2022, 15:20

Continued increase in current towards 700A while pressure decrease indicated completeness of reduction.

Started rampdown to 650A.

Pressure was 1.7E-4 Torr on IGP1


Friday, April 15, 2022, 06:28  

The current was reduced to 500A @ 3:50 PM yestesterday.

Currently, TGHT = 500A, 2.0V

started aurtoramp down @ -2A/min

IGP1= 2.4E-6 Torr

 


Monday, May 02, 2022, 12:32

Cartridge reloaded onto EVAP 1. Will heat back up to check carbothermal reduction. 


Tuesday, May 03, 2022, 08:40

IGP1= 1.32e-6 Torr

Good vacuum 1e-1 Torr

Bad vacuum 5e-1 Torr

Autoramp set to 1A/10s to 500A

Autoramped up to 750A @ 1A/10s.  Only slight pressure increases observed areound 150A and 650A to 700 A.  Parameter curves will be evaluated.


Tuesday, May 03, 2022, 11:11

Started rampdown at -1A/10s. 

IGP1 was 3.0e-5 Torr and trending down when rampdown started

 

 

  280   Wednesday, May 04, 2022, 09:47 Luca EgoritiUC2 P2N-SISDoneP2N carbothermal reduction P2NC220408

 Wednesday, May 04, 2022, 09:42

Yesterday, a second graphite cartridge was installed in EVAP1, it consists of the old, 3-body cartridge design, and was sanded on the outside to be able to fit a P2N container. 

 

 


First I tried ramping manually, but the heating tripped because pressure was too high.

Then the parameters were set as previously, but it tripped again

IGP1= 2e-5 Torr

Good vacuum 8e-2 Torr

Bad vacuum 5e-1 Torr

Autoramp set to 1A/10s to 500A

Autoramped up to 700A @ 1A/10s. 

 

Wednesday, May 04, 2022, 11:40

Another ramping trial, with different heating rate:

IGP1= 3e-5 Torr

Good vacuum 8e-2 Torr

Bad vacuum 5e-1 Torr

Autoramp set to 1A/20s to 700A

Autoramped up to 700A @ 1A/20s.  

 

Wednesday, May 04, 2022, 15:50

IGP1= 3e-2 Torr

Good vacuum 8e-2 Torr

Bad vacuum 5e-1 Torr

Autoramp set to 1A/20s to 730A

Autoramped up to 720A @ 1A/20s.  

Pressure dropping while current is increasing at autoramp rate.

 

Wednesday, May 04, 2022, 16:10

From 730A, once the pressure went down to ~1E-3T, the current was suddenly raised to 750A and 770A to see if significant pressure increase was noticed, but small bumps reaching 1.5E-3T were not considered a sign of further reduction.

The rampdown started from a pressure ~1E-3T, from 770A to zero with rate 2A/10s 

 

 

 

  285   Wednesday, October 19, 2022, 12:28 Darwin Ortiz RosalesUC240253-5LP TUBEDoneC-220510 further conditioning

Wednesday, October 19, 2022, 10:27

Cartridge-220510Cx was installed in the EVAP1 and pumped down yesterday.

Material will be further conditioned at 450A for 4 hours.

The material will be conditioned inside a container tube with both ends open at the ends.  Two springs are inserted at the ends of the graphite cartridge to contain the material as graphite caps not inserted.

IGP1 = 7.8e-07 Torr

 

Good vacuum = 5e-4 Torr

Bad vacuum = 5e-2 Torr

 

Will autoramp @2A/30s (4A/min) to 40 A and then to 120A.  Fast ramp rate because material had previously been conditioned


 

Wednesday, October 19, 2022, 12:23

TGHT 450A, 5.2 V

Will leave for 4 hours and then begin ramp-down.


Wednesday, October 19, 2022, 16:21

IGP1= 3.1e-06Torr

450A, 5.2V

Start rampdown @- 2A/min


Thursday, October 20, 2022, 09:23

IGP1= 4.6e-7 Torr

 

  96   Friday, July 04, 2014, 10:23 John WongThO240282-2TARGET BOATDoneTest: Sintering ThO2 with Nb backing foils

Friday, July 04, 2014, 10:13

Target boat contains 4 set of samples.  Each sample consists of 5pack ThO2/Nb.  (see photos).

The container is wrapped with 3 layers of heat shield. 

TGHT will be ramped up to 520A at 0.1A/min.

Chamber has been pumped over night, pressure at 4.20e-6 Torr.

The purpose of this test:

1.  Will the Ta- target boat survive at that current?

2.  How will ThO2 sintered?  Shrinkage? Grain-growth? mass loss? density? SEM will be done later.

3.  How will the pressure behave at the max operating temperature (or current)?


  Friday, July 04, 2014, 12:29

Stepped up TGHT to 40A,  Vac went to max at 3.5e-5 Torr and is coming down.

Auto-ramping initiated. 


 Tuesday, August 19, 2014, 10:20

Sample was successfully sinterred to 520A. 

SEM on raw, treated powder, and sintered samples were perform.  Pressure vs current plot can also be found. (see attachments)

More information can be found here:

https://www.dropbox.com/sh/fj78m7tyy7mj99p/AABfm-fQMeoaWhf6HjT8Vzn1a


 

 

Attachment 1: 2014-07-03_12.29.29.jpg
2014-07-03_12.29.29.jpg
Attachment 2: ThO_raw_green_sintered_30um.png
ThO_raw_green_sintered_30um.png
Attachment 3: pressure_current_plot.PNG
pressure_current_plot.PNG
  97   Wednesday, July 09, 2014, 13:57 Laura LambertThO240282-2TARGET BOATDoneTest: Sintering ThO2 with Nb backing foils

John Wong wrote:

Friday, July 04, 2014, 10:13

Target boat contains 4 set of samples.  Each sample consists of 5pack ThO2/Nb.  (see photos).

The container is wrapped with 3 layers of heat shield. 

TGHT will be ramped up to 520A at 0.1A/min.

Chamber has been pumped over night, pressure at 4.20e-6 Torr.

The purpose of this test:

1.  Will the Ta- target boat survive at that current?

2.  How will ThO2 sintered?  Shrinkage? Grain-growth? mass loss? density? SEM will be done later.

3.  How will the pressure behave at the max operating temperature (or current)?


  Friday, July 04, 2014, 12:29

Stepped up TGHT to 40A,  Vac went to max at 3.5e-5 Torr and is coming down.

Auto-ramping initiated. 


 

Wednesday, July 09, 2014, 13:55

TGHT reached 520A tuesday morning. [see attached archive screenshot]

Initiated auto-cool at 1.0A/min tuesday afternoon.

Vented in air and took samples out of EVAP1 wednesday morning. [see attached sample photo]


 

Attachment 1: test_batch_full_sintering.JPG
test_batch_full_sintering.JPG
Attachment 2: jul9_2014_(2).jpg
jul9_2014_(2).jpg
  98   Thursday, August 14, 2014, 17:56 John WongThO2 LP-SISDoneSintering ThO2#1

 Thursday, August 14, 2014, 17:54

Target container consists of 240 discs of ThO2/Nb discs.  The container is not required to be wrapped with Ta-heat shields.  

One end cap is inserted on the left end (wrt to the ionizer pointing into the page).  

The chamber is currently being pumped down.  

TGHT will be heated up to 520A, ramping rate at 0.1A/min.


 Friday, August 15, 2014, 15:55

A sampling filter has been installed by RPG; this will be used to analyze any volatile particle releases out from the target. 

An alpha monitor is being install on the exhaust line; air sample will be collected for further analyzse.  

Vacuum has come down to 7.2 e-6 Torr.  

Target heat will be ramped up on Monday since it is coming late to the day.  

Chamber will continue to pump down.  

Next week, RPG will start taking the first air sample before the target is heated up.  More discussion on that later...


 Monday, August 18, 2014, 11:18

Chamber has been pumped down over the weekend. 

Pressure @ 2.67e-6 Torr. 

Note:  RPG decides not to take any gas sample since the filter installed in between the backing and turbo pumps is sufficient for the analysis.

TGHT stepped up to 30A.


 Monday, August 18, 2014, 14:17

TGHT stepped up further to 40A; Pressure stabalized >100min at 4e-6 Torr, bp @ 44mTorr.

Initiated auto-ramping.


 Thursday, August 21, 2014, 17:20

TGHT continues to ramp up and pressure is coming down - Currently @ 7.7-6 Torr.

Increased TGHT ramping rate to 0.5A/min. 

The sintering process will be complete by Friday (Aug 8, 21), and the chamber will be cooled down over the weekend.

By Monday, the chamber can be vented in air, and the target can be removed from the chamber.  Then RPG can remove the filter in the backing pump for the analysis.


 Friday, August 22, 2014, 08:57

TGHT has reached to 520A for just over 10 hrs.  Vac at 8.6e-6 Torr, BP @ 40mTorr.

Cooling initiated at 2A/min


 Friday, August 22, 2014, 16:52

Target was cooled to room temp and was removed from the chamber.

5 discs were removed from the target because it was shrunk up; the rest of the discs were fine.  

2 extra Nb foils and end cap were inserted. 

Target is stored in the Hotlab - awaiting to be assembled.


 

 

 

 

 

  34   Wednesday, September 07, 2011, 13:41 John WongTaC38634-6LP-SISDoneTaC#1: Sintering and Organics burn-off

Wednesday, September 07, 2011, 15:31

125 discs of TaC/C

Total discs mass = 125

Total length = 4.5mm

Total Mass = 30.41g

No Ta-heat shield. 

Left opening with D-TaC-sintered cap, and Right opening with regular TaC-sintered cap (orientation with the ionizer tube pointing out of the page).

Target is currently in the evaporator and being pumped down. 


Thursday, September 08, 2011, 09:13

Evaporator has been pumped down over night, IG1 currently at 1.74 e-6 Torr.   

Will begin TGHT, max @ 580A.

TGHT @ 50A, vac stable @ 1.7e-6 Torr.


Thursday, September 08, 2011, 10:18 

THGT @ 90A, pressure is increasing, currently at 4.7e-5 Torr and going up. 


 Thursday, September 08, 2011, 10:25

Auto-heating has begun. Set rate at 2A/min to max current 580A.

Incrementing if vac < 5.0 e-5 Torr, backing off if vac > 6.0 e-5 Torr. 


Friday, September 09, 2011, 07:58

TGHT auto cool down started @ 02:00, and at 0A.  IG currently @ 1.3e-6 Torr.  Venting chamber in progress.  Target will be removed from the evaporator afterward.

Target looks good :)  No signs of damage on the end cap or the target oven overall. 

See attachment 1 for the striptool. 

See attachment 2 and 3 for the target and endcaps after the sintering process.

 

Attachment 1: TaC#1.jpg
TaC#1.jpg
Attachment 2: endcaps_after_sintering.png
endcaps_after_sintering.png
Attachment 3: TaC_aftersintering.jpg
TaC_aftersintering.jpg
  276   Friday, September 24, 2021, 15:40 Luca EgoritiTa LP-SISIn progressFull target release test 1

 Friday, September 24, 2021, 15:38

Full target loaded with ~500 non-active foils plus 4 active foils.  

Initial pressure when heating: 6.6E-5 T 

Manually went to:

TGHT=125 A 

TBHT=50 A

with increments of 5 A each. Pressure has little spikes but mostly unchanged (going down, actually).

 

Friday, September 24, 2021, 15:42

Manually went to

TGHT=180 A 

TBHT=80 A

Pressure going up steadily, max pressure <2E-4

 

Friday, September 24, 2021, 16:48

From TGHT=180 A, TBHT=80 A we are aiming at going to TGHT=580 A and TBHT=230 A in increments of 50 A each and leave it there for a total of 5 minutes after nominal parameters are reached. Initial pressure 1.3E-5 T.

 

Friday, September 24, 2021, 17:01

Fast rampup done, we were up there in 30 seconds.

TGHT VOL = 6.6 V

TBHT VOL = 3 V

Max pressure 2E-3 T. Both TGHT and TBHT were shut off abruptly on purpose. 

 

 

 

 

 

  277   Friday, November 05, 2021, 13:38 Luca EgoritiTa LP-SISIn progressFull target release test 2

 Friday, November 05, 2021, 13:23

Full target loaded with ~500 non-active foils plus 4 active foils.  

Initial pressure when heating: 1.6E-5 T 

Manually went to:

TGHT=125 A 

TBHT=50 A

with increments of 5 A each. Pressure has little spikes but mostly unchanged (going down, actually).

Stayed at those values for 2 min 


Friday, November 05, 2021, 13:37 

Manually went to

TGHT=180 A 

TBHT=80 A

maximum pressure 6.6e-5 Torr


Friday, November 05, 2021, 13:43

IGP1 =  2.45e-5 Torr

We are aiming at going to TGHT=580 A and TBHT=230 A in increments of 50 A each and leave it there for a total of 5 minutes after nominal parameters are reached 

 


Friday, November 05, 2021, 13:55

IGP1 =  1.7e-5 Torr

Heating done, we stayed at 530A for a bit long (~15 sec) during the heating so the total heat time at 580A was interrupted at 4 mins 50 seconds instead of 5 mins. All good, max pressure during the heating was 0.013 T.

Attachment 1: Ta-ReleaseTest-2_low-current.JPG
Ta-ReleaseTest-2_low-current.JPG
  278   Wednesday, November 24, 2021, 10:38 Luca EgoritiTa  In progressIPF release tests

Wednesday, November 24, 2021, 10:38

A first, short "FullTa1" target was loaded into the evap1. It consists of a short container (10 cm) with lateral thickness of ~0.2mm. The ends of the target connect with the TGHT terminals through two copper adapters.

After pumpdown down to ~4E-5 T, the TGHT was ramped gradually to 200 A in the next ~5 mins, leaving the target at 200 A for about 10 mins. Then, the current was increased fastly to 450 A in about 30 seconds, and was left at 450 A for a minute. 

Note: the one minute at 450 A started when the TGHT voltage drop across stabilized, considered a sign of temperature homogeneity across the target container

 

Wednesday, November 24, 2021, 14:34

The second short container "FullTa2" target has been loaded and heated, following the same procedure as above. In this case, the initial pumpdown went to a lower pressure (1.5E-5 T instead of ~4E-5 T) resulting in lower pressure throughout the whole procedure

  

  20   Wednesday, May 11, 2011, 16:23 John WongSiC38481-8HP-FEBIADProblems Organics burnoff & Sintering

Wed May 11 16:20:21 2011:  The HP-FEBIAD (w.o#38481-8) was filled with SiC (8.5mm, 555 discs).  The target is wrapped with 3 Ta-heat shields and is in the evaporator, which is being pumped down. 

Thu May 12 10:52:48 2011:  The evaporator ion gauge, IEVAPIG1 filament burnt out.  The gauge comes in two filaments, so it is now running on the second one.  The chamber has been pumped down overnight, currently it's @ 2.29e-6 torr. 

Thu May 12 11:15:59 2011:  TGHT was stepped up to 80A, vac @ 2.47e-6 Torr.  Begin auto heating at 1A/min to 820A and will increase the rate to 2A/min if the vacuum is stable. 

Thu May 12 12:27:35 2011:   TGHT went up to 101A, and the vacuum started to reach close to the trip limit (8.7e-6 Torr).  TGHT was auto ramped down but the vacuum kept rising and tripped off the heater @ 94A.  TGHT was turned back on after 30mins, vac @ 8.7e-6 Torr.  TGHT was tapped up slowly to 95A.  The ramping rate has also decreased to 0.5A/min.  (See attachment#1: high_vacuum)

Thu May 12 12:58:51 2011:  Lowered TGHT to 90A.  Vac stayed at 7.8e-5 Torr.

Fri May 13 15:47:42 2011:  TGHT @ 128A, incrementing rate @ 1A/min, Vac @ 5.4e-5 Torr after 30 hrs. (See Attachment#2:  current_pressure_30hrs)

Fri May 13 16:22:54 2011:  THGT and vacuum over the past 12 hrs.  (See Attachment#3: current_pressure_past12hrs)

Mon May 16 11:03:54 2011:  THGT reached to 820A and held for over 12 hrs.   (See Attachment#4_Sintering process). 


Tue May 17 16:26:34 2011

Problem Occurred: 

  • The end caps of the target got vaporized after the sintering process.  (See Attachment#5:  end_caps_vaporized)
  • The caps were not coated with TaC and a D-shaped graphite foil were used. 

Solutions: 

  • The caps were removed - No damage to the target oven.  (See Attachment#6/#7: left_end/ right_end )
  • New caps  were used and coated with TaC.   Two circled-graphite foils were used on the both ends and then sealed with the TaC coated caps. (See Attachment 8: TaC_coated_endcaps)
  • Re-heating the target to 820A.

 


Tue May 17 16:35:13 2011:  Target is wrapped with 3 Ta-heat shields.  The target is in the evaporator which is being pumped down.  

Tue May 17 19:34:55 2011:  TGHT stepped up to 80A, Vac holding at 5.2e-6 Torr.  Auto heating began after 25 mins later.  Rate set at 2A/min to max 820A. 

 Tue May 17 22:02:36 2011:  TGHT @ 382A, Vac @ 1.23 e-5 Torr.  Increased ramping rate @ 3A/min.  Cooling down process will begin at 04:00 of May18, 2011;  ISAC Ops will help to start the auto cooling process.

Wed May 18 11:39:47 2011:  The cooling down process ended; TGHT reached to zero.  The camber will be vented. 


 

Attachment 1: high_vacuum.jpg
high_vacuum.jpg
Attachment 2: current_pressure_30hrs.jpg
current_pressure_30hrs.jpg
Attachment 3: current_pressure_past12hrs.jpg
current_pressure_past12hrs.jpg
Attachment 4: Sintering_process.jpg
Sintering_process.jpg
Attachment 5: end_caps_vaporized.jpg
end_caps_vaporized.jpg
Attachment 6: Left_end.jpg
Left_end.jpg
Attachment 7: right_end.jpg
right_end.jpg
Attachment 8: TaC_coated_endcaps.jpg
TaC_coated_endcaps.jpg
Attachment 9: SiC_EDX.jpg
SiC_EDX.jpg
  22   Wednesday, May 18, 2011, 13:13 John WongSiC38295-8HP-FEBIADProblemsOrganics burnoff & Sintering

Wed May 18 13:12:24 2011:  Target is wrapped with 3 Ta-heat shields and is installed in the evaporator which is being pumped down.

Wed May 18 23:11:42 2011:  TGHT was raised to 40A and held for about 6 hours; Vac gradually came down to 2.1e-6 Torr.  TGHT increased to 90A and pressure is going up, currently vac @ 2.9 e-5 Torr.  Auto heating will begin soon at 0.5A/min --> 820A.  

Thu May 19 10:23:34 2011:  TGHT at 92A/0.32V, vac @ 4.47 e-5 torr.  (See Attachment#1: heating_past_12hrs)

Tue May 24 10:22:59 2011:  TGHT reached to max currrent 820A and held for over the long weekend.  The cooling process began at 15:00 yesterday.  Evaporator is vented.  P/S off.

 


Mon May 30 17:03:01 2011

The end caps of the target after the sintering process were found damage; the caps were vaporized just like the previous SiC target w.o#38481-8.  (See attachments#2: SiC000-003).  After some investigation, it looks like some reaction had occurred when the target heater was ramped up beyond 550A.  (See Attachment#3: SiC_striptool).

The yellow solid will be analyzed using EDX/SEM.  More details will be posted later....


Wednesday, September 14, 2011, 10:16 

SEM/EDX were done.  See attachment #9 for the EDX results. 

The formation of the yellow solid is the condensation of silicon.  As seen on the EDX results, the solid is mainly Si, C and some trace of Al (could be from the loading rod).  

The new D-end cap has be used to allow a better out-gassing.  

 

 

 

Attachment 1: heating_past_12hrs.jpg
heating_past_12hrs.jpg
Attachment 2: SiC_000.png
SiC_000.png
Attachment 3: SiC_001.png
SiC_001.png
Attachment 4: SiC_002.png
SiC_002.png
Attachment 5: SiC_striptool.png
SiC_striptool.png
Attachment 6: SiC_EDX.jpg
SiC_EDX.jpg
  38   Tuesday, September 13, 2011, 16:53 John WongSiC38295-9HP-FEBIADDoneReady

Tuesday, September 13, 2011, 16:51

Target is wrapped with 3-Ta heat shields. 

Loaded with 555 SiC discs (total mass 64.24g)

18cm in length.

D-end cap on one end, and a regular end end on the other.

Chamber is currently being pump down


 Wednesday, September 14, 2011, 09:58

Evaporator has been pumped down over night, currently IG @ 1.71e-6 Torr. BP @ 23mT.

The target will be heated up to 550A and will wait to see any reaction happen before increasing TGHT (Max 820A).

TGHT stepped up to 90A, local @ 87A.  Pressure slowly rising, IG @ 2.7e-6 Torr. BP @ 23mT. 

Start auto-heating @ 0.5A/min to max TGHT @ 500A.  


 Friday, September 16, 2011, 00:27:

TGHT @ 250A and pressure has already started to come down, currently at 2.8e-5 Torr.  

Increased TGHT rate from 0.5A/min to 2A/min, and pressure started to rise.  Stopped auto-ramping after pressure increased to 4.4e-5 Torr.  (see attachment#1: TGHT_270A-300A.jpg).

Decreased TGHT rate back to 0.5A/min and changed pressure limit to 3.0e-5 Torr.  


Friday, September 16, 2011, 01:49 :

TGHT @ 347A, and pressure seems to come down slowly. 

Change TGHT auto heating to 550A and pressure limit at 2.5e-5 Torr.  Vac currently at 2.4e-5 Torr.  Ramping rate at 0.5A/min. 


Friday, September 16, 2011, 10:58  

TGHT reached 580A and no spike in the vacuum.  Ramping up TGHT to 590A, keeping pressure limit @ 1.35e-5 Torr,

Currently IG @ 1.33 e-5 Torr.  Current TGHT @ 585.5A, local @  579A.

(see attachment 3: TGHT_580A)


Friday, September 16, 2011, 11:35:

TGHT reached to 590A, not much of out-gassing.  Pressure increased from 1.30e-5 Torr to 1.40e-5 Torr.  

Continue ramping up TGHT, set to 700A, pressure limiting @ 1.5e-5 Torr.


Friday, September 16, 2011, 15:29:

TGHT reached to 700A, local @ 692A; pressure was stable at 1.38e-5 Torr throughout the whole time.  

Continues ramping up TGHT to 820A (max) at 0.5A/min; pressure limiting @ 1.5e-5 Torr. 


Friday, September 16, 2011, 22:05 

TGHT reached to 820A (local 810A) and held for ~3hrs.  IG @ 5.4e-6Torr and coming down, BP @ 20mT. 

See attachment#4:  TGHT_820A.

TGHT cooling down begins... 


 Monday, September 19, 2011, 10:08

TGHT was cooled down over the weekend. 

See attachment#4: archiver_TGHT_0-820A. 

Currently, IG @ 6.9e-7 Torr, BP @ 27mT.

Evaporator will be vented. 


Tuesday, September 20, 2011, 08:51 

Target turned out well.  

D-cap was removed and replaced with a regular TaC-coated sintered endcap with a graphite foil.  

See attachments for details.

Target is now ready for assembly and test for test-stand. 

 


 

Attachment 1: TGHT_270A-300A.jpg
TGHT_270A-300A.jpg
Attachment 2: TGHT_347A.jpg
TGHT_347A.jpg
Attachment 3: TGHT_580A.JPG
TGHT_580A.JPG
Attachment 4: TGHT_820A.jpg
TGHT_820A.jpg
Attachment 5: archiver_TGHT_0-820A.JPG
archiver_TGHT_0-820A.JPG
Attachment 6: D-cap_outgassing.jpg
D-cap_outgassing.jpg
Attachment 7: D-endcap_aftersintering.jpg
D-endcap_aftersintering.jpg
Attachment 8: Sintered_SiC_&_newcap.jpg
Sintered_SiC_&_newcap.jpg
Attachment 9: SiC_TGHT0-820A.jpg
SiC_TGHT0-820A.jpg
  47   Tuesday, May 08, 2012, 07:42 John WongSiC38817-3HP-SISDoneSintering SiC

Tuesday, May 08, 2012, 07:32

Target oven is filled with 240 discs of SiC/C, and wrapped with 3 Ta-foils.

Tot mass= 31.95g (SiC + C foil + Org)

Tot length packed @ 8.2cm

Target was installed in the chamber yesterday and has been pumped down to low 10e-6 torr.

Increased TGHT to 70A and vacuum is starting to rise, currently at 2.6e-6 Torr.

Max target current = 820A or until there is no further reaction. 


 Tuesday, May 08, 2012, 08:55

Pressue is slowly coming down after heating for a while at 70A. 

Initiated auto heating at 0.5A/min. Parameter set for increasing current if <4.0e-5 torr, and backing off if >5.0e-5 torr.


Wednesday, May 09, 2012, 10:31

 There seems to be a pipe leakage in the ISAC-I B2 level, and the cooling water for the evaporator #1 is connected to the pipe.  

The TGHT was tapped down from 115A, and the p/s was turned off.  The water valve is now shut, and Curtis B. is looking into it.  


Wednesday, May 09, 2012, 13:44

As per Curtis, the drainage pipe was leaky, and it has been fixed. The evaporator is now turned back on.  TGHT was tabbed up to 115A, and has remained at that current for an hour.  The pressure is slowly raising, current at 4.6e-6 Torr.


Wednesday, May 09, 2012, 14:24

Initiated TGHT...


Saturday, May 12, 2012, 23:38 

TGHT is ramping up very slowly (currently at 270A) due to pressure restriction.  It has already taken over 4 days.  (see attachment 1: TGHT 0_270A)

Changed the parameter to <5.0e05 Torr for stepping up in current and >6.0e-5 Torr for backing off current.


 Sunday, May 13, 2012, 20:44

Pressure has started to come down to 3e-6 Torr.  Increased heating rate from 0.5A/min to 1.0A/min.


 Monday, May 14, 2012, 01:09

TGHT has reached to 820A and been holding at that current for about 3hr.  The pressure is coming down steadily, currently at 1.6e-5 Torr.

Asked ISAC OPS (Ed P.) to initial the auto-cool down at 03:00h, at 2A/min.

The target should be ready by 10:00h.


 Monday, May 14, 2012, 10:56

TGHT is now at 0A (see attachment 2).  The chamber is now being vented.  The target will be inspected.


Thursday, May 17, 2012, 12:51 

The target looks good and was tested in the teststand, see https://elog.triumf.ca/TIS/Test-Stand/97

It will be used as SiC#27.  


 

Attachment 1: TGHT_0_270A.png
TGHT_0_270A.png
Attachment 2: SiC#27_0-820A.JPG
SiC#27_0-820A.JPG
  4   Monday, March 28, 2011, 12:29 John WongEmpty38481-8HP-FEBIADDoneFins diffusion bonding

March 28, 2011

12:28:  Target oven is wrapped with 3 Ta-heat shields.  Pumping down evaporator

March 29,

12:14  Evaporator has been pumped down over night.  Vac @ 1.74e-6 Torr. 

12:24  TGHT @ 20A, Vac @ 1.66e-6 Torr.

12:29  TGHT @ 40A, Vac @ 1.56e-6 Torr.

12:30  Auto heating begins,  Paramenter Setup:  TGHT: 2A/min -->  max 820A.  Incrementing if Vac < 4.5e-5 Torr; backing off if vac > 6.5e-5 Torr.

18:37  TGHT @ 772A/7.395V  (see attachment#1 for the striptool).  Auto heating will stop when the TGHT gets to 820A, and the current will stay there over night. 

March 30

11:31 TGHT has been at 820A/7.8V for the past 17 hours.  (See attachment#2 for the striptool details.)

11:34 Auto-cooling beings

19:40 Auto-cooling has finished. TGHT is at zero and p/s has turned off.  Cooling water has stopped running.  Evaporator will be vented tomorrow.

March 31, 2011

11:13:  Venting evaporator.  All pumps are off and TGHT p/s has turned off. 

Thu Mar 31 11:57:20 2011 After removing the target from the evaporator,  some white coating (could be Tantalum oxide?) was found on the copper plate of the evaporator.  The white coating was found to have more on the left end side of the target and some just below the transfer tube.  The white coating was wiped off but it showed black residual on the wipers.  The target over looks fine.  Marik was informed, and we think this white coating could be  the organic substance burnt off from the target or the Tantalum oxide from the re-used Ta heat shields. 

 

Attachment 1: grab.Kxr912.png
grab.Kxr912.png
Attachment 2: grab.L10194.png
grab.L10194.png
  7   Tuesday, April 05, 2011, 10:37 John WongEmpty38481-6HP-FEBIADDoneFins diffusion bonding

Tue Apr 5 10:36:53 2011:  Target oven is wrapped with 3 Ta-heat shields.  The evaporator is in the process of pumping down. 

Tue Apr 5 14:54:00 2011:  Evap has been pumped down for over 4 hours.  Vac is currently at 5.5e-6 Torr. (See Attachment#1)

Tue Apr 5 15:16:31 2011: TGHT is turned on.  Set  @ 20A/0.102V; panel reads 18A.  Vac @ 4.62e-6 Torr. 

Tue Apr 5 15:18:16 2011: TGHT set @ 40A/0.216V; panel reads 37A.  Vac @ 4.63e-6 Torr. 

Tue Apr 5 15:19:03 2011: Start Auto-heating.  Parameter setup:  TGHT rate @ 2A/min --> 820A max.  Incrementing if vac <4.5e-5 Torr, and backing off if vac >6.5e-5 Torr.

 Wed Apr 6 09:18:22 2011: TGHT was left at the auto- heating mode over night and  had been at 850A for about 12hrs; Vac @ 4.36e-6 Torr.  (see Attachment#2) 

Wed Apr 6 09:20:53 2011: Auto-cooling down has just started. 

Wed Apr 6 15:33:51 2011:  Auto-cooling completed.  (see Attachment #3 for the overall process)

Wed Apr 6 15:37:10 2011: TGHT p/s off, Venting evaporator. 

 

Attachment 1: pumping_down.jpg
pumping_down.jpg
Attachment 2: heatingup.jpg
heatingup.jpg
Attachment 3: cooling_down.jpg
cooling_down.jpg
  8   Wednesday, April 06, 2011, 17:07 John WongEmpty37978-1HP-FEBIADDoneFins diffusion bonding

Wed Apr 6 17:06:56 2011: Target oven is wrapped with 3 Ta-heat shields.  Pumping down evaporator in progress.

Thu Apr 7 09:32:36 2011: Evaporator has been pumped down for over 16 hrs, vac @ 1.74e-6 Torr (see attachment#1).   Target heater is turned on and about to ramp up.

 Thu Apr 7 09:37:11 2011: TGHT @ 20A/0.071V, panel reads 18A.

Thu Apr 7 09:38:16 2011: TGHT @ 40A/0.147V, panel reads 37A.

Thu Apr 7 09:40:53 2011:  Auto-heating begins.  (See attachment#2 for Parameter Setup)

Fri Apr 8 10:08:07 2011:  Auto-cooling process began last night at 8:30pm.  Instructions were given to the on shift ISAC-Ops to being the auto cooling.  The process was finished this morning at around 3am.  (See attachment#3 for the cooling down process).  The evaporator p/s is off and ready to be vented.

 

 

Attachment 1: pumping_down.jpg
pumping_down.jpg
Attachment 2: Autoheating_parameter_setup.jpg
Autoheating_parameter_setup.jpg
Attachment 3: cooling_down.jpg
cooling_down.jpg
  9   Friday, April 08, 2011, 14:55 John WongEmpty38295-8HP-FEBIADDoneFins diffusion bonding

Fri Apr 8 14:51:37 2011:  Target is wrapped with 3 Ta-heat shields.  The evaporator has been pumped down for over 4 hrs, currently vac @ 2.8e-6 Torr.  (See attachment #1, note: the drops in the IG1 reading were due to Controls group helping to fix the alarm handler notifications for the pagers.)

 Fri Apr 8 14:56:21 2011:  TGHT @ 20A/0.079V, panel reads 18V.   Vac @ 2.73e-6 Torr.

Fri Apr 8 14:57:42 2011: TGHT @ 40A/0.165V, panel reads 18A.  Vac @ 2.73e-6 Torr. 

Fri Apr 8 14:59:51 2011: Auto heating begins.  (See Attachment#2 for the parameter setup).  The target heater will read to 820A at 21:30.  ISAC Ops will help to cool down the target at around 05:00 on Saturday; instructions will be given.

Mon Apr 11 09:37:40 2011:  Target was cooling on last Saturday April 9 by the help from ISAC Ops.  (See Attachment#3 for the cooling down process).

Mon Apr 11 09:42:09 2011 :  Evaporator is vented.

 

 

 

Attachment 1: pumping_down.jpg
pumping_down.jpg
Attachment 2: Autoheating_parameter_setup.jpg
Autoheating_parameter_setup.jpg
Attachment 3: cooling_down.jpg
cooling_down.jpg
  10   Monday, April 11, 2011, 10:22 John WongEmpty38295-9HP-FEBIADDoneFins diffusion bonding

Mon Apr 11 10:21:56 2011: Target is wrapped with 3 Ta-heat shields.  Evaporator is pumping down. 

Mon Apr 11 14:34:32 2011:  Evaporator has been pumped down for over 4 hours.  Vac @ 2.83e-6 Torr.  (see attachment#1 for pumping down process).

Mon Apr 11 14:38:05 2011:  Auto heating beings.  (see attchement#2 for the parameter setup)

Mon Apr 11 17:06:51 2011:  Auto heating is in process,  TGHT @ 324A/2.031V.  The target heater should reach at the max 820A at around 21:30 and will remain at that current for at least 3 to 4 hours.  ISAC Ops will help start the auto-cooling tomorrow at 03:00.

 Tue Apr 12 09:43:46 2011:  Auto cooling down process ended. TGHT stayed at 820A for about 5.5 hrs.  (see attchment# for cooling down process).

Tue Apr 12 09:59:43 2011: Pumps and p/s off, evaporator vented.

Attachment 1: pumping_down.jpg
pumping_down.jpg
Attachment 2: Autoheating_parameter_setup.jpg
Autoheating_parameter_setup.jpg
Attachment 3: grab.A29589.png
grab.A29589.png
  11   Tuesday, April 12, 2011, 10:30 John WongEmpty38481-5HP-FEBIADDoneFins diffusion bonding

Tue Apr 12 10:29:38 2011:  Target wrapped with 3 Ta-heat shields.  Evaporator is currently being pumped down.

Tue Apr 12 15:03:55 2011:  Evaporator has been pumped down for over 4 hrs.  Set TGHT @ 20A/ 0.066V, Vac @ 2.46e-6 Torr. (See Attachment#1 pumping down process).

Tue Apr 12 15:05:11 2011: TGHT @ 40A/0.142V, VAc @ 2.46e-6 Torr. 

Tue Apr 12 15:14:16 2011  Auto heating process begins (See attachment #2 for the parameter setup).  TGHT will reach to 820A max at around 21:45 and the current will stay there for at least 4 hours.  Instructions have given to ISAC Ops to being the auto-cooling down process tomorrow at 03:00 

Wed Apr 13 10:00:13 2011:  TGHT reached to 820A max and stayed for about 5 hrs before the cooling process begun (see Attachment#2: Cooling down process). 

Wed Apr 13 10:04:19 2011: p/s is now off and evaporator is now vented. 

 

 

 

 

 

Attachment 1: grab.s31535.png
grab.s31535.png
Attachment 2: grab.c31573.png
grab.c31573.png
Attachment 3: cooling_down.jpg
cooling_down.jpg
  12   Wednesday, April 13, 2011, 10:37 John WongEmpty38481-7HP-FEBIADDoneDiffusion bonding of Ta Fins for FEBIAD-HP

Wed Apr 13 10:37:25 2011:  Target is wrapped with 3 Ta-heat shields.  Evaporator is currently being pumped down.

Wed Apr 13 15:28:02 2011:  Evaporator has been pumped down for over 5 hrs.  Vac @ 2.38e-6 Torr.  (See attachment1: Pumping process)

Wed Apr 13 15:29:21 2011: Set TGHT @ 20A/0.074V, Vac 2.98e-6 Torr.

Wed Apr 13 15:30:00 2011: Set TGHT @ 40A/0.158V, Vac @ 2.30e-6 Torr. 

Wed Apr 13 15:37:42 2011:  Auto heating begins.  TGHT will increase to 820A by 2A/min.  Cooling down will take after the current has stayed at 820A for at least 4 to 5 hrs.   ISAC Ops will help to start the cooling process on April 14 at 03:00.  (See attachment#2: Parameter Setup).

Thu Apr 14 09:49:31 2011:  TGHT reached to 820A and stayed there for about 5.5 hrs.  ISAC Ops helped to start the cooling process (see attachment3: Cooling process).  The target is ready to come out from the evaporator.   P/S is off and evaporator is vented.

Mon Apr 18 12:18:55 2011:  A problem with the bolt and washer occurred during the fin diffusion bonding.  (See attachment #1 and Message ID#15 for more details) .  This target needs to be repaired.

 

 

 

Attachment 1: pumping_down.jpg
pumping_down.jpg
Attachment 2: Autoheating_parameter_setup.jpg
Autoheating_parameter_setup.jpg
Attachment 3: cooling_down.jpg
cooling_down.jpg
Attachment 4: washer_on_target_leg.jpg
washer_on_target_leg.jpg
  13   Thursday, April 14, 2011, 09:53 John WongEmpty37810-1HP-FEBIADDoneFins Diffusion bonding

Thu Apr 14 09:52:59 2011: Target is wrapped with 3-Ta heat shield and ready to go into the evaporator. 

Thu Apr 14 11:57:29 2011: The process is on hold until the problem with the screw and the washer of the evaporator is resolved.  See ID#15 for more details.

Fri Apr 15 11:22:27 2011:  The shorter fully threaded bolts and un-threaded washer are being used. 

Fri Apr 15 11:23:30 2011:  Target is in the evaporator and ready for the fin diffusion bonding.  The evaporator is currently being pumped down.

Fri Apr 15 15:57:40 2011: TGHT @ 20A, Vac @ 4.53e-6 Torr.  ISAC Ops will help to start the auto heating process at 18:00hr tonight  and  begin the auto cooling on April 16 @ 18:00 hr. 

 Mon Apr 18 10:53:39 2011:  Target was heated @ 820A over the weekend and pumped down on Saturday April 16 in the evening.  P/S is off and evaporator is vented.  (see Attachment#1 for the striptool)

Mon Apr 18 12:16:22 2011:  Target fin diffusion bonding is nicely done, and the evaporator shows no sign of any coating.  It looks like the problem from the bolts and washers is resolved.  

Attachment 1: cooling_down.jpg
cooling_down.jpg
  15   Thursday, April 14, 2011, 17:03 John WongEmpty38481-7HP-FEBIADProblems resolvedEvap. bolt/washer problems & solutions

 Thu Apr 14 14:03:17 2011:  What did we see after the fin diffusion bonding of Ta fins for FEBIAD-HP (w.o#38481-7) ? :

1.  A problem occurred during the FEBIAD HP Ta fin diffusion bonding and was discovered after the evaporator chamber was opened.  The washer was "wielded" on to the left leg of the target (see attachment #1: washer on target leg). 

2. A look inside the evaporator chamber shows that more coating is found on the evaporator lid and the copper base plate (See attachment#2: Inside evap chamber). This coating was previously found when a HP FEBIAD target underwent for the fin diffusion bonding (See Message ID#4: Diffusion bonding of Ta Fins for FEBIAD-HP (w.o#38481-8)).  The evaporator chamber is cleaned with a wiper sheet and EtOH each time before a target is put in;  however the coating is not easily removed and there are always some residual remain. 

3.  The bolt and the washer are deformed.  The top part of the bolt is expended and can no longer fit into the threaded washer  (See attachment#3: Deformed bolt_washer). 

4.  The TIS group was called in to investigate the problem.  It was believed that the problem might have started from the bolts and the washers.  The un-threaded shank bolts and the threaded washers are made for remote handling purposes, so they do not fall apart everywhere in the hotcell.  However, if these bolts and the washers are used for the evaporator, which are bolted on and tighten against the gravity onto the conductors, this may create a gap if the threaded washer is tilted slightly.  (See attachment#4: Gap).  As a result, this causes an uneven pressure contact of the bolt/washer and the target leg.  

Solutions:

Use fully threaded bolts (same material as before - a mild steel) and remove the threads from the washers (See attachment#5: No Gap).

--> To be tested...

 Fri Apr 15 11:59:31 2011: 

The new bolts/washer were cleaned only with simple green and ultrasonic for 5 min.  The bolts and washer should not be cleaned for too long; some remaining grease actually helps prevent them from getting rusty.  The evaporator is wiped with EtOH and  the target is inside.  The bolts and washers are tighten and they are not showing at space like before (See attachment#6: new bolt_washer) .  The evaporator is being pumped down and the target heater will be raised to 820A; we will have to wait until the fin diffusion bonding is complete and the evaporator chamber is vented. 

 Mon Apr 18 12:30:35 2011: 

After a fin diffusion bonding of a HP FEBIAD target, there is no sign of coating in the evaporator.  The bolts/washer and the target look normal. 

--> The problem is solved.

Attachment 1: washer_on_target_leg.jpg
washer_on_target_leg.jpg
Attachment 2: inside_evap_chamber.jpg
inside_evap_chamber.jpg
Attachment 3: deformed_both_washer.jpg
deformed_both_washer.jpg
Attachment 4: gap.jpg
gap.jpg
Attachment 5: no_gap.jpg
no_gap.jpg
Attachment 6: new_bolt_washer.jpg
new_bolt_washer.jpg
  16   Monday, April 18, 2011, 18:14 John WongEmpty38295-8HP-FEBIADProblemsSintering target oven coated with TaC

Mon Apr 18 18:10:53 2011: 

FEBIAD-HP target (w.o 38295-8) is coated with TaC (previously prepared on Feb 15, 2011).  This target will be used for the SiC run in Oct, 2011.  The target is wrapped with 3 Ta-heat shields and is in the evaporator.  Pumping down of the evaporator is in process, currently vac @ 3.66e-5 Torr.   

Tue Apr 19 11:00:36 2011: Evaporator has been pumped down over night (~17hrs).  Vac is currently at 1.84e-6 Torr (See Attachment#1: pumping down curve).

Tue Apr 19 11:09:49 2011: TGHT @ 30A/0.086V, Vac @ 1.82e-6 Torr.

Tue Apr 19 11:13:05 2011: TGHT @ 60A/0.184V, Vac @ 1.75e-6 Torr.

Tue Apr 19 11:14:06 2011: Auto-heating will begin @ 0.5A/min until vacuum is stable then the auto ramping rate will increase. (See Attachment#2: parameter setup).

Tue Apr 19 14:27:08 2011:  TGHT is currently at 148A/0.65V, vac @ 1.92e-5 Torr.  The pressure spiked up to 7.7e-5 Torr (trip @ 8e-5 Torr) at ~124A.  The current was lowered down to 120A to allow the pressure to come down (See Attachment#3: Vac_curve).   Auto-heating rate has changed to 1A/min. 

Wed Apr 20 10:08:52 2011:  TGHT reached to 700A and stayed for about 5 hours.  ISAC Ops helped to start the auto cooling down process.  (See Attachment#3: Overall Process). 

Tue Apr 26 11:12:36 2011

Result:  The dried coating isn't looking the same like the rest of the target.  Typically, the finished coating looks gray.  But a layer (or line) of light brown coating can been seen from one end of the target to the other end. 

--> This target was heated up to 700A.  Will try to re-heat this again to 820A. 

 

Re-heating the Target

Tue Apr 26 12:44:30 2011:  Target is wrapped with 3 Ta-heat shield and is in the evaporator which is currently being pumped down. 

Tue Apr 26 17:39:40 2011:  TGHT was tapped up to 70A before began with auto-heating @ 2A/min to 820A max.  Currently TGHT at 204A/1.0V, Vac @ 3.97e-6 Torr.  ISAC Ops will help to start auto cooling at 04:00 on April 27.

Wed Apr 27 12:26:41 2011: Auto cooling completed.  P/S off and evaporator is vented, (See Attachment#5: Overall Process_2).  Target oven looks good; finished surface looks gray, as expected. 

 

Attachment 1: pumping_down.jpg
pumping_down.jpg
Attachment 2: Autoheating_parameter_setup.jpg
Autoheating_parameter_setup.jpg
Attachment 3: vac_curve.jpg
vac_curve.jpg
Attachment 4: overall_process.jpg
overall_process.jpg
Attachment 5: overall_process_2.jpg
overall_process_2.jpg
  17   Wednesday, April 20, 2011, 16:42 John WongEmpty38481-8HP-FEBIADDoneSintering target oven coated with TaC

Wed Apr 20 16:39:46 2011:  Target oven was coated with TaC early today.  The target was allowed to dry and then wrapped with 3 Ta heat-shields.  The target is in the evaporator and it is being pumped down.  Vac is currently at 9.48e-6 Torr. 

Wed Apr 20 17:51:12 2011 : TGHT @ 60A/0.225V, Vac @ 5.98e-6 Torr. 

Wed Apr 20 18:20:04 2011: Auto-heating begins @ 0.5A/min to max of 820A.

Thu Apr 21 10:12:34 2011: TGHT was auto ramping up slowly over night to 546A this morning.  The ramping rate has changed to 2A/min since the vacuuum is stable at ~3.9e-6 Torr.

 Tue Apr 26 11:10:03 2011:  TGHT reached to 820A max on April 21 and stayed at that current for a few hours.  ISAC Ops helped to ramped down the heater afterward.  (See attachment#1: Overall Process).

Result:  Good!  TaC is coated evenly on the target. 

 

 

 

Attachment 1: overall_process.jpg
overall_process.jpg
  18   Monday, May 09, 2011, 16:10 John WongEmpty38817-1HP-SISDoneDiffusion bonding of Ta Fins

Mon May 9 16:09:35 2011:  Target is wrapped with 3 Ta heatshields and the evaporator is begin pumped down.

Mon May 9 17:59:57 2011:  Vac is @ 1.33e-5 Torr.  TGHT was stepped up to 60A before starting the auto heating process (See Attachment#1: TGHT_ramping_up).   Note: Although the vacuum is at low e-5 torr, this should be fine to start the TGHT because it takes a while to heat up the high power target.

Tue May 10 11:10:44 2011:  TGHT reached to 820A and stayed for 4 hrs before ISAC Ops helped to begin the cooling process.  (See Attachment#2: Overall process).

Attachment 1: TGHT_ramping_up.gif
TGHT_ramping_up.gif
Attachment 2: overall_process.jpg
overall_process.jpg
  19   Tuesday, May 10, 2011, 14:58 John WongEmpty38817-2HP-SISDoneDiffusion bonding of Ta Fins for HP-SIS (w.o#38817-2)

Tue May 10 14:56:05 2011:  Target is wrapped with 3 heat-shields.  The evaporator is pumping down, vac @ 4.72e-6 Torr.  TGHT was raised to 60A/0.239V.  Auto heating will being now; THGT will be ramped up to 820A @ 2A/min. (See Attachment#1: Staring_process)

Wed May 11 10:16:03 2011: Auto cooling was started by ISAC Ops' help.  TGHT has ramped down to zero.  The p/s will be turned off and the evaporator will be vented soon. (See Attachment#2: Overall Process).

 

Attachment 1: starting_process.jpg
starting_process.jpg
Attachment 2: overall_process.gif
overall_process.gif
  25   Monday, July 18, 2011, 15:55 John WongEmpty38634-3LP-SISDoneSintering TaC coating for UCx#2

 Monday, July 18, 2011, 15:53:  Target oven was coated with TaC and let dry over the weekend.  The target is now installed in the evaporator and currently being pumped down.  No Ta-heat shields are required for LP target ovens. 

Wednesday, July 20, 2011, 11:42:  Evaporator had to be vented to remove the target because Ta-heat shields were actually required for UCx target at 2uA p+.  Target heater was never turned on.   After removing the target oven, it was rolled around Ta wire; this prevent the Ta foil to stick on the oven.  Then 3 Ta-heat shields were wrapped around it, plus 2 shields on the back block.  The evaporator has been pumped down over night, currently vac @ 1.30e-6 Torr. 

Wednesday, July 20, 2011, 12:35: TGHT stepped up to 110A, pressure began to increase exponentially.   Brought THGT down to 100A. Will being auto cooling soon.

Wednesday, July 20, 2011, 12:48:  Auto heating beings.  2A/min, max current @ 520A.

Wednesday, July 20, 2011, 17:49:  TGHT reached to 520A.  Increased heater to 570A according to last year UCx procedures.

Wednesday, July 20, 2011, 19:46:  TGHT held at 570A for about 2 hours.  Cooling down has begun.  Set rate at 0.5A/min for slow cool down.  

Thursday, July 21, 2011, 12:20 :  TGHT cooling rate increased to 2A/min at about 10:25 am.  At 10:55am, TGHT p/s tripped off, and the water valve was closed.  Not sure what was the reason.  Rest p/s and water valve, and turned back the p/s and continue to cool down from 74A.  (see attachment#1: striptool)

Thursday, July 21, 2011, 14:45 :  TGHT off, chamber about to be vented into atmosphere.  

Attachment 1: striptool.jpg
striptool.jpg
  27   Wednesday, August 03, 2011, 17:16 John WongEmpty38634-8LP-SISDoneSintering TaC coating

Wednesday, August 03, 2011, 20:27 :  Target was wrapped with 3 new Ta-heat shields and 2 around the back block.  The tar from the previous UCx conditioning remained in the chamber was removed and cleaned.  Chamber is currently being pumped down, vac currently @ 8.3 e-6 Torr. 

Wednesday, August 03, 2011, 21:01:  Begin to step up TGHT, currently vac @ 7.5e-6 Torr.

Wednesday, August 03, 2011, 21:30 : TGHT stepped to 110A, vac raising exponentially. 

Wednesday, August 03, 2011, 21:34:  Brought down TGHT to 100A, and began auto heating.  Set rate @ 2A/min, max current to 520A. 

Thursday, August 04, 2011, 00:33:  THGT is ramping up nicely and the vacuum is coming down.  It should reach to 520at 01:30.  I asked ISAC Ops to cool down the target heater at 04:00.

Thursday, August 04, 2011, 10:26 :  TGHT has reached to 0A.  Chamber will be vented.  See attachment1 for striptool.

 

Attachment 1: striptool.JPG
striptool.JPG
  29   Monday, August 29, 2011, 11:21 John WongEmpty38634-6LP-SISDoneSintering TaC coating oven for TaC#1

 Monday, August 29, 2011, 13:16: Target oven was coated with TaC and let dry over night.  The target oven is in the evaporator and currently being pumped down.  

Monday, August 29, 2011, 15:12: Currently vac @ 8.41e-6 torr. 

Monday, August 29, 2011, 15:32: Stepped current up to 77A, started to see increase in pressure. 

Monday, August 29, 2011, 15:39:  Stepped current up to 110A.  Vac @ 1.32e-5 Torr.

Monday, August 29, 2011, 15:53: Vac went up to 3.8e-5 Torr @ 110A after 8 mins.  Brought TGHT back down to 100A, and began auto heating @ 2.0A/min to max current of 520A.

Tuesday, August 30, 2011, 08:39:  TGHT reached to 520A and was cool down by ISAC Ops at around 00:30.  See attachment#1 for striptool.  Evaporator will be vented. 

 

 

Attachment 1: TaC_target_oven.JPG
TaC_target_oven.JPG
  30   Tuesday, August 30, 2011, 09:31 Anders MjosEmptyTarget BoatLP-SISDoneSintering of End Caps

Tuesday, August 30, 2011, 09:29: Target Boat wrapped with 3 Ta heat shields. 6 D-End Caps and 6 End Caps coated with TaC. Pumping down - vac at 3.6e-5 torr.

Tuesday, August 30, 2011, 10:35: Stepped heater up to 100 A. Vacuum tripped heater. Stepped back up to 80 A then 70 A. Vac at 4.5e-5 torr.

Tuesday, August 30, 2011, 14:30: Manually increased heater to 580 A. Vac is 2.5e-5 torr. Local reading is 561 A for 570 A and 570 A for 580 A set points.

Tuesday, August 30, 2011, 15:57: Manually decreased heater in 12 min to 0 A from 460 A  vac starting at 6.3e-6 torr.

  31   Tuesday, August 30, 2011, 16:30 John WongEmptyTarget BoatLP-SISDoneSintering of End Caps

Anders Mjos wrote:

Tuesday, August 30, 2011, 09:29: Target Boat wrapped with 3 Ta heat shields. 6 D-End Caps and 6 End Caps coated with TaC. Pumping down - vac at 3.6e-5 torr.

Tuesday, August 30, 2011, 10:35: Stepped heater up to 100 A. Vacuum tripped heater. Stepped back up to 80 A then 70 A. Vac at 4.5e-5 torr.

Tuesday, August 30, 2011, 14:30: Manually increased heater to 580 A. Vac is 2.5e-5 torr. Local reading is 561 A for 570 A and 570 A for 580 A set points.

Tuesday, August 30, 2011, 15:57: Manually decreased heater in 12 min to 0 A from 460 A  vac starting at 6.3e-6 torr.

 Vented evaporator. 

  32   Tuesday, September 06, 2011, 17:05 John WongEmpty38634-6LP-SISDoneSintering TaC coating oven for TaC#1

John Wong wrote:

 Monday, August 29, 2011, 13:16: Target oven was coated with TaC and let dry over night.  The target oven is in the evaporator and currently being pumped down.  

Monday, August 29, 2011, 15:12: Currently vac @ 8.41e-6 torr. 

Monday, August 29, 2011, 15:32: Stepped current up to 77A, started to see increase in pressure. 

Monday, August 29, 2011, 15:39:  Stepped current up to 110A.  Vac @ 1.32e-5 Torr.

Monday, August 29, 2011, 15:53: Vac went up to 3.8e-5 Torr @ 110A after 8 mins.  Brought TGHT back down to 100A, and began auto heating @ 2.0A/min to max current of 520A.

Tuesday, August 30, 2011, 08:39:  TGHT reached to 520A and was cool down by ISAC Ops at around 00:30.  See attachment#1 for striptool.  Evaporator will be vented. 

 

 

 Tuesday, September 06, 2011, 17:04:  Re-conditioning sintered-TaC-coated target oven filled with sintered D-endcap.  No heat-shields.  Evaporator is currently pumping down:  CG2 = 51mT, IG1 = 2.65e-5 Torr.

TGHT auto-heating started by ISAC Ops as per JW at 18:45 yesterday when vacuum level at 6.6 e-6 Torr.  Then auto-cooling began at 05:30 this morning. BP @ 50mT - time to change backing pump oil. (see attachement1: overall striptool)

Wednesday, September 07, 2011, 11:16: Vented evaporator.  BP oil will be changed by Edi. 

 

Attachment 1: striptool.JPG
striptool.JPG
  33   Wednesday, September 07, 2011, 13:33 John WongEmpty  MaintenanceChanged Evaporator#1 Backing Pump oil

Wednesday, September 07, 2011, 11:18:  

IEVAP:CG2 @ 52mT before oil change. 

Edi D.V changed the oil for the backing pump.  WP#2011-09-07-2. CG2 currently @ 21mT.

 

  35   Wednesday, September 07, 2011, 15:40 Anders MjosEmpty  MaintenanceRe-sealing of Glove Box

2011-09-01:

  • Glove box was leaking (air/argon) between base and box. Light was shining through.
  • Removed old neoprene seal at base.
  • Resealed glove box between base and box with DAP Butylflex. No light shining through after repair.
  • Replaced rubber disks at 4 feed-throughs.
  • Maico Dalla Valle replaced the inner ring on the glove ports. See dwg ITA2954 and ECO-2418.
  • After the repair, the glove box has a significantly reduced leak, estimated to a few liters per minute at an air pressure of  0.5" H2O.

Evaporator drawings can be found on ITA2900D

Work Permit: 2011-09-01-2 

  36   Friday, September 09, 2011, 10:05 John WongEmpty HP-FEBIADDoneSintering TaC coating

Friday, September 09, 2011, 10:05

Target oven coated with TaC, and wrapped with 3-Ta heat shields.  Chamber is currently being pumped down. 

TGHT @ 140A, IG 9.2 e-6 Torr, BP 20mT. 

Started auto heating, rate @ 2A/min, to max current of 820A. 


Friday, September 09, 2011, 12:25

Evaporator tripped off at 163A. 

Stepped TGHT back to 160A.  Vacuum holding at 4.3e-5 Torr.


Monday, September 12, 2011, 09:55

Evaporator was cooled down over the weekend. 

Chamber will be vented shortly.

See attachment#1: striptool

 


 

Attachment 1: striptool.JPG
striptool.JPG
  37   Monday, September 12, 2011, 13:08 John WongEmptyTarget Boat DoneSintering TaC coating on End Caps

Monday, September 12, 2011, 13:07

Target boat is loaded with coated TaC end caps for sintering.  Target boat is wrapped with 3 Ta-heat shields. 

Max TGHT = 580A


Monday, September 12, 2011, 14:58 

Vac @ 3.72e-6 Torr.  Stepping up TGHT to 90A; pressure starting to increase.


 Monday, September 12, 2011, 15:33

Evaporator tripped twice when TGHT was at 90A and 85A.  Lowered TGHT to 75A.


Tuesday, September 13, 2011, 09:56 

TGHT was on auto-heating and reached to 580A yesterday evening.  The auto cooling began at mid-night after heated for a few hours. 

The chamber will be vented shortly.

See attachment#1: striptool.

 

Attachment 1: striptool.JPG
striptool.JPG
  39   Wednesday, September 21, 2011, 13:23 John WongEmpty38634-10LP-SISDoneSintering TaC coating on target oven for UCx#3

Wednesday, September 21, 2011, 13:23

Target oven was wrapped with 3-Ta heatshields including the back block. 

Target is in the chamber and currently being pumped down.


Wednesday, September 21, 2011, 15:52  

IG @ 5.9e-6 Torr.  

TGHT stepped up to 85A, and pressure slowly rising. 

Started auto heating:  0.5A/min.  TGHT to max 580A.  


Thursday, September 22, 2011, 10:19 

Target was heated up to 580A, and held for 3 hrs. 

Currently IG @ 6.15e-6 Torr.

Auto-cooling started...


Thursday, September 22, 2011, 20:20 

Target oven was removed from the evaporator, and it was successfully sintered with TaC. 


Friday, September 23, 2011, 13:39 :

See attachment1: Archiver_TGHt0-580A.

 

Attachment 1: archiver_TGHT0-580A.JPG
archiver_TGHT0-580A.JPG
  40   Thursday, September 22, 2011, 20:34 John WongEmpty38634-9LP-SISDoneSintering TaC coating for UCx#2 (spare)

 Thursday, September 22, 2011, 20:21

Target oven was wrapped with 3 Ta-heat shields and has been pumping down.

IG currently @ 3.2e-6 Torr, BP @ 25mT. 

TGHT stepped up to 85A, 

Began auto-heating: TGHT to max 580A @ 0.5A/min. 


Monday, September 26, 2011, 10:23 

TGHT reached to 580A on last Friday and was held at that current for 3hrs then followed by the auto-cooling.

Chamber was vented.

Target oven looks great.


 

 

 

 

  46   Thursday, April 05, 2012, 16:47 John WongEmpty38817-3HP-SISDoneCoating target oven /w TaC & sintering

Thursday, April 05, 2012, 16:43

Target oven is coated with TaC.  The oven is wrapped with 3 Ta-heat shields.

The chamber is currently being pumped down.  Vac @ high 10e-5 Torr.  Heater will be turned on once the pressure is gone down to low 10e-6. 

TGHT will be heated up to 820A.

 

**** Sintering is postponed until the situation with the ventilation in the lab06 is cleared. ****


 Friday, May 04, 2012, 16:59

The short-term solution  for improving the ventilation system and for the safety in operating the evaporators has been implement.  The test results was reviewed and approved by the committee.  The labs (06 and 07) are now back in operational. 


Friday, May 04, 2012, 17:03

Pumping down evaporator, currently a 2.4e-5 Torr.

Turned on TGHT, and stepped up to 85A.  Pressure remained at low e-5 Torr. 

Initiated Auto-heating at 0.5A/min to Max current 820A.  Parameter set:  Increasing current if Vac <4.0e-8 Torr, Backing current if Vac >5.0e-8 Torr.


 Monday, May 07, 2012, 10:38

At 820A, the TaC coating only seemed to have partially sinterred.  Raised TGHT up to 900A and heated for >6hrs.  The vacuum continued to increase as the target heater was raised; that indicated the sintering reaction was ongoing.  (See attachment #1: Targetoven_TaCsintered_acrchive.jpg).

The auto-cool down was initiated last night.  TGHT is now at 0A.  The chamber will be vented.


 

Attachment 1: Targetoven_TaCsintered_archive.JPG
Targetoven_TaCsintered_archive.JPG
  80   Friday, October 04, 2013, 15:56 John WongEmpty LP-SISDoneIgnore this entry - Process was done in Evap2

Friday, October 04, 2013, 15:37

A LP target container is coated with TaC.  The container is wrapped with 3 layers to heat shield.  

This container will be used for the graphite tube test.  

Chamber is being pumped down.

 The HS cooling water valves are open and no leaks are detected. 


 

TGHT will be ramped up to 580A at 0.2A/min

TBHT will be ramped up to 230A at 0.2A/min.

The temperature will be monitored and measured. 


 


 

  85   Thursday, January 23, 2014, 16:29 Laura LambertEmpty40282-1TARGET BOATIn progressSintering Ta target boat with TaC coating

Thursday, January 23, 2014, 16:26 

 A new target boat was sprayed with TaC coating and let dry, the coating appeared slightly bubbly once dried [see attached photos].

The target boat was wrapped with 3-layers of Ta-heat shield.

The boat was installed in Evap#1, chamber is currently being pumped down overnight.


 

Attachment 1: IMG_20140123_143448877.jpg
IMG_20140123_143448877.jpg
Attachment 2: IMG_20140123_143507747.jpg
IMG_20140123_143507747.jpg
  86   Friday, January 24, 2014, 14:45 Laura LambertEmpty40282-1TARGET BOATIn progressSintering Ta target boat with TaC coating

Laura Lambert wrote:

Thursday, January 23, 2014, 16:26 

 A new target boat was sprayed with TaC coating and let dry, the coating appeared slightly bubbly once dried [see attached photos].

The target boat was wrapped with 3-layers of Ta-heat shield.

The boat was installed in Evap#1, chamber is currently being pumped down overnight.


 

 Friday, January 24, 2014, 14:42

Chamber was pumped down to 5.9e-6 Torr overnight.

TGHT was stepped up to 35A.

Waited 20min, vacuum consistently stable, auto-ramp initiated at 0.2A/min and max setpoint to 580A.

Good vacuum: 5e-5 Torr. Bad vacuum: 6e-5 Torr.


 

  87   Monday, January 27, 2014, 11:03 Laura LambertEmpty40282-1TARGET BOATDoneSintering Ta target boat with TaC coating

Laura Lambert wrote:

Laura Lambert wrote:

Thursday, January 23, 2014, 16:26 

 A new target boat was sprayed with TaC coating and let dry, the coating appeared slightly bubbly once dried [see attached photos].

The target boat was wrapped with 3-layers of Ta-heat shield.

The boat was installed in Evap#1, chamber is currently being pumped down overnight.


 

 Friday, January 24, 2014, 14:42

Chamber was pumped down to 5.9e-6 Torr overnight.

TGHT was stepped up to 35A.

Waited 20min, vacuum consistently stable, auto-ramp initiated at 0.2A/min and max setpoint to 580A.

Good vacuum: 5e-5 Torr. Bad vacuum: 6e-5 Torr.


 

 Monday, January 27, 2014, 11:01

TGHT reached 580A over the weekend.

TGHT auto-cooldown initiated at 2.0A/min.


 Tuesday, January 28, 2014, 15:51

Chamber cooled down overnight, vented and opened up this morning.

Target boat looks good! [See attached photos]


 

Attachment 1: IMG_20140128_113257662.jpg
IMG_20140128_113257662.jpg
  108   Monday, March 09, 2015, 16:58 Laura LambertEmpty TARGET BOATMaintenanceTesting new software

 Monday, March 09, 2015, 16:55

After upgrading IOC for CXML program, experienced some issues; therefore, switched to same software as EVAP2.

Testing new software.

Chamber currently pumping down.


 Tuesday, March 10, 2015, 10:46

Chamber pumped down.

Initiated auto-ramp - not working, compilation errors...


 Tuesday, March 17, 2015, 11:47

Keiko fixed software update and rebooted IOC.

Everything seems to be working now.


 

  167   Thursday, September 21, 2017, 11:35 Laura LambertEmpty  DoneTesting TBHT [1st run!], RP [new oil] and IG [new gauge]

 Thursday, September 21, 2017, 11:32

Copper plate attached to TBHT to allow current to be applied.

Started pumping down this a.m.

Roughing pump sounds normal.

Currently Ion Gauge times out before turning on, will attempt again later when lower vacuum achieved...


 Monday, September 25, 2017, 13:30

Ion Gauge hadn't been fully hooked up via eipcs yet.

Ramped down last week/ vented/ hooked up ion gauge in epics/ restarted IOC - now updated and good to go.

Started pumping down again this a.m.

Roughing pump sounds normal.

Ion gauge working well!

IGP1 = 2.7e-5 Torr


 Wednesday, September 27, 2017, 09:20

Cooled down, vented in air and opened up yesterday.

TBHT ran well -  readout on power supply and readout on striptool were very close.

Roughing pump ran smoothly - nothing other than usual problems.

Sometimes when roughing pump is 1st turned on it chokes up and sounds TERRIBLE. At this point if you turn it off and leave it for a few seconds then try turning it on again it usually works fine.

Ion gauge ran well - direct readout vs striptool readout are slightly off because the direct readout is in mBar and the striptool in Torr.

One minor thing noticed with the new ion gauge - when water is turned on the vacuum increases very minorly by ~5e-8 Torr.

This wouldn't show up with the old Ion Gauge - maybe the new one is slightly more sensitive?

Otherwise everything ran great 


 

  172   Tuesday, November 07, 2017, 14:38 Laura LambertEmpty LP-FEBIADDoneTBHT test with LP-FEBIAD

 Tuesday, November 07, 2017, 14:34

LP-FEBIAD used several years ago for temperature measurements is used for this test.

3xTa heat shields on container, incl center block - these heat shields have remained on there since the last round of tests in 2014?

Old version of LP container with larger center block.

Will heat TBHT to 290A and report data.

Loaded into evap1 and pumped down this a.m

IGP1 = 7.73e-6 Torr


Wednesday, November 08, 2017, 13:20

Tapped up to 290A manually.

TBHT epics controls = 287.7A, 2.45V

TBHT power supply = 290.4A, 2.46V

IGP1 epics = 2.51e-6 Toor

IGP1 direct readout = 3.18e-6 Torr

TP = 26.1C

Initiating auto-cool at 2.0A/min


 Thursday, November 09, 2017, 11:41

Vented in air.

TBHT test went well. 

See attachment for data collected.


 

Attachment 1: evap1_data.xlsx
  194   Wednesday, February 28, 2018, 15:21 Laura LambertEmpty TARGET BOATDoneTesting TGHT to induce trip

 Wednesday, February 28, 2018, 15:19

Last two rounds of materials in evap1 have tripped off the TGHT in epics within minutes of the target reaching 520A.

Loaded an empty target boat, no heat shields.

Will ramp up with same speed as last two samples to see how TGHT reacts and whether a trip is induced or not.

Currently pumping down now.


 Thursday, March 01, 2018, 13:53

IGP1 = 9.6e-7 Torr

Tapped up to 100A @ 1.0A/s, waited ~6min

IGP1 = 1.77e-6 Torr

Tapped up 40A/min to 140A, waited ~2min

Tapped up 40A/min to 180A, waited ~2min

Tapped up @ a rate of 1.0A/s for 40sec, then wait 20sec. Used this rate consistently up to 520A.

TGHT = 520A, 5.75V


Friday, March 02, 2018, 10:09 

TGHT = 520A, 5.81V this morning.

TGHT still on! 

No trip induced.

IGP1 = 1.7e-6 Torr.

Initiating auto-cool at 2.0A/min


 Thursday, March 05, 2018, 14:07

Container removed, test complete.


 

 

  252   Wednesday, January 22, 2020, 18:10 Marla CervantesEmptyP2N-02  DoneP2N test#1
The assembly consists of two tantalum foils, 0.001" thick, which are radially crimped to form a cylindrical surface. The outside support are two P2N  conditioning legs, and the inside supports are tantalum tapered rings. The solidworks geometry for this test is ITD0811 in PDM. 
 
A first current ramp up to 600 amperes on the bare naked target is attempted to benchmark the current/voltage increase in a bare target, so that we have reference values for future rampings with graphite and target material inside. 

Wednesday, January 22, 2020, 18:07

A P2N container  with no heat shields, and no graphite container was installed in the EVAP1

Chamber is currently being evacuated.


 Thursday, January 23, 2020, 09:45

Pressure IGP1=1.87e-6 Torr

Final desired current TGHT = 600 A

Manually tapped to 40 A

 The voltage looks ok, at 32 A the voltage's behavior change (see picture "voltage at 32 A") but is stable


Thursday, January 23, 2020, 13:20

Autoramp is set to 4/30s to 300 A 

The voltage and vacuum were stable so the autoramp was kept at 4/30s and the final current was set to 600 A

At 600 A the voltage was 2.4 V, the current and voltage remained stable for 1 hour (see figures 600A and 600A-zoomed)


Thursday, January 23, 2020, 15:57

The current was ramp down to 0 A  at -5A/20s 


Thursday, January 23, 2020, 16:36 

After 10 min at 0A, the current was ramp up to 600 A at 4A/30s.

At 600 A the voltage was 2.43 V (TGHT)

The container was left at 600 A overnight.


Friday, January 24, 2020, 10:51

The PN2 stayed at 600 A for 15 hrs

The voltage increased 0.1 V during the first 7hr at 600 A and then it stabilized at 2.5 V (see figure "second ramp voltage")


Friday, January 24, 2020, 10:57

The current was ramp down to 0A at -5A/20s  


 

Attachment 1: p2n_conditioning_-_Naked_target_installed.jpg
p2n_conditioning_-_Naked_target_installed.jpg
Attachment 2: voltage_at_32_A.JPG
voltage_at_32_A.JPG
Attachment 3: 600A.JPG
600A.JPG
Attachment 4: 600A-zoomed.JPG
600A-zoomed.JPG
Attachment 5: First_current_ramp_up.JPG
First_current_ramp_up.JPG
Attachment 6: Second_ramp_voltage.JPG
Second_ramp_voltage.JPG
  253   Wednesday, January 29, 2020, 10:11 Marla CervantesEmptyP2N-02 DoneP2N test#2
The assembly consists of two tantalum foils, 0.001" thick, which are radially crimped to form a cylindrical surface. The outside support are two P2N  conditioning legs, and the inside supports are tantalum tapered rings. The solidworks geometry for this test is ITD0811 in PDM. 
 
 The P2N is attached to EVAP1 with copper legs and copper shims. A current ramp up to 600 A on the target wrapped with heat shields is attempted to benchmark the current/voltage increase in a bare target, so that we have reference values for future rampings with graphite and target material inside. 
The heat shields consist on two layers of Ta sheets on the body of the P2N secured with Ta-wire and two layers of Ta sheets on one side of the P2N.

Tuesday, January 28, 2020, 10:11

A P2N container  with heat shields, and without graphite container was installed in the EVAP1

Chamber is currently being evacuated.


Wednesday, January 29, 2020, 10:12

Pressure IGP1=1.87e-6 Torr

Final desired current TGHT = 600 A

Manually tapped to 40 A.

Voltage increased accordingly in an stable way.


Wednesday, January 29, 2020, 10:33 

Autoramp is set to 3/30s to 300 A 

The voltage and vacuum were stable so the autoramp was kept at 4/30s and the final current was set to 600 A

Accidentally went up to 600 A (1.98 V)!

When updating autoramp to 600 A, did not realize that procedure status was Active.

NOTE: If the procedure status is "active" the heater autoramp, does not "ramp" the current input in "final value", it will go in one step to that current.

The current was manually ramp down to 300 A

TGHT=299.52A, 0.89 V


Wednesday, January 29, 2020, 13:25

After approximately 2 hours conditions IGP1=1.6e-6Torr, TGHT =300 A, 1V.

The current ramp was started again: 4A/30s  to final value of 600 A


 Wednesday, January 29, 2020, 14:07

After 15 min, TGHT=599.424A, and 1.983 V (unstable) (see figure "P2N-test2_final voltage")

The current was ramp down to 0 A  at -5A/20s 


EVAP1 was vented with aair and the container was removed,

the copper shims and legs did not present signs of damage

the body's tantalum sheet had wrinkles inside,

the tantalum foils unfasten a bit, but were adjusted.

Attachment 1: P2N-test2_final_voltage.JPG
P2N-test2_final_voltage.JPG
Attachment 2: P2N-test2.JPG
P2N-test2.JPG
  62   Thursday, October 25, 2012, 15:03 John WongBeOTa-target boat (old) In progressSintering BeO pellets #5 - testing Re foil as the protective under layer

Thursday, October 25, 2012, 14:50

Previous sintering BeO tests, pellets 1 to 4 were done in Evaporator#2.

3 BeO pellets were made.  Each weights about 1.3g (including org mass). 

A piece of Re foil (0.002" thick) is used as the under layer to protect the reaction between Be(g) and the Ta-boat.  (see attachment#1)

Another layer of Ta-foil is used as the heat-shield to wrap around the Ta-boat.

The chamber is currently being pumped down. 

TGHT will be ramped up to 600A (~1360C) at 0.2A/min.

The pressure, voltage and current will be closely monitored. 

If the Ta-boat survives, the TGHT will continue to ramp up to max 800A (~1580C).


 Friday, October 26, 2012, 11:15

Chamber has been pumped down over night. 

IG1 @ 8.93e-6 Torr. 

Auto-ramping parameter:

Good Vac @ 2.0e-5 Torr, Bad Vac @ 3.0e-5 Torr.

rate @ 0.2A/min. 


 Tuesday, October 30, 2012, 10:57

TGHT has reached to 370A. The organic binder has burnt off. 

The pressure came down to  6.6e-6 Torr, but it is slowly going up to 8.6e-6 Torr (something is outgassing... Dissociation of BeO --> Be(g) + O(g) ?).  BP @ 39mTorr.  (see attachment#2).


 Wednesday, October 31, 2012, 12:07

TGHT has reached to 600A/6.338V for just over 6 hours.  IG is slowly coming down fro 1.2e-5 Torr.  BP @ 38mTorr. (see attachment #3)


 Wednesday, October 31, 2012, 16:49

Vacuum is coming down to 8.49e-6Torr.  TGHT has stayed at 600A/6.24V for over 11hrs.  (see attachment #4)

Auto-cooling initiated at 1A/min. 

The chamber will be vented tomorrow and the material will be inspected.


 Thursday, November 01, 2012, 10:57

TGHT has reached to 0A.  Vacuum holding at 1.9e-6Torr.

Turning off P/S and pumps prior to venting chamber.


 

 

Attachment 1: BeO_pellets_on_Re_foil.PNG
BeO_pellets_on_Re_foil.PNG
Attachment 2: TGHT_0-400A.PNG
TGHT_0-400A.PNG
Attachment 3: BeO_pellet#5_TGHT_100-600A.PNG
BeO_pellet#5_TGHT_100-600A.PNG
Attachment 4: BeO_pellet#5_@_600A__11hrs.PNG
BeO_pellet#5_@_600A__11hrs.PNG
  1   Wednesday, March 23, 2011, 18:23 John Wong    Diffusion Bonding of Ta Fins for FEBIAD HP-A (w.o#38481-4)

March 23, 2011

12:30: Target oven is wrapped with 3 Ta-heat shields.  Pumping down evaporator

18:24: IEVAPIG1 is reading at 4.55e-6 Torr.  The p/s will be turned on tomorrow since there is no ISAC Ops on site. 

March 24

11:57: Evaporator has pumped down over night.  Vacuum @ 2.01e-6 Torr.  

14:42: TGHT @ 20A, Vac @ 1.65e-6 Torr.

14:52: TGHT @ 40A, Vac @ 1.66e-6 Torr.

14:52: Auto Heating begins: TGHT to max 820A.  Incrementing if vac < 4.5e-5 Torr, backing off if vac > 6.5e-5 Torr.

 16:04: TGHT @ 181A, vac @ 7.59e-6 Torr.

18:03: TGHT @ 420A, vac @ 4.71e-6 Torr.   (See attachment 2 for TGHT/IG1 for the past 4 hours)

March 25,

11:15:  TGHT has been at 820A for 14hr.  Vac @ 4.27e-6 Torr.  (See attachement 3 for TGHT/IG1 for these past hours)

11:17:  Auto cooling down is in progress...

17:21:  Auto cooling down ended at TGHT ~100A.  The TGHT was tabbed down manually from 100A to zero.  (See attachment #4 for the cooling down progress)

Attachment 1: grab.K18246.png
grab.K18246.png
Attachment 2: grab.g20718.png
grab.g20718.png
Attachment 3: grab.r27097.png
grab.r27097.png
Attachment 4: grab.t30095.png
grab.t30095.png
  2   Friday, March 25, 2011, 17:22 John Wong    Diffusion Bonding of Ta Fins for FEBIAD HP-A (w.o#38481-4)

John Wong wrote:

March 23, 2011

12:30: Pumping down evaporator

18:24: IEVAPIG1 is reading at 4.55e-6 Torr.  The p/s will be turned on tomorrow since there is no ISAC Ops on site. 

March 24

11:57: Evaporator has pumped down over night.  Vacuum @ 2.01e-6 Torr.  

14:42: TGHT @ 20A, Vac @ 1.65e-6 Torr.

14:52: TGHT @ 40A, Vac @ 1.66e-6 Torr.

14:52: Auto Heating begins: TGHT to max 820A.  Incrementing if vac < 4.5e-5 Torr, backing off if vac > 6.5e-5 Torr.

 16:04: TGHT @ 181A, vac @ 7.59e-6 Torr.

18:03: TGHT @ 420A, vac @ 4.71e-6 Torr.   (See attachment 2 for TGHT/IG1 for the past 4 hours)

March 25,

11:15:  TGHT has been at 820A for 14hr.  Vac @ 4.27e-6 Torr.  (See attachement 3 for TGHT/IG1 for these past hours)

11:17:  Auto cooling down is in progress...

17:21:  Auto cooling down ended at TGHT ~100A.  The TGHT was tabbed down manually from 100A to zero.  (See attachment #4 for the cooling down progress)

 All the pumps are off.  The evaporator will be vented next week. 

  3   Monday, March 28, 2011, 11:20    HP-FEBIADDoneDiffusion Bonding of Ta Fins for FEBIAD HP-A (w.o#38481-4)

John Wong wrote:

John Wong wrote:

March 23, 2011

12:30: Pumping down evaporator

18:24: IEVAPIG1 is reading at 4.55e-6 Torr.  The p/s will be turned on tomorrow since there is no ISAC Ops on site. 

March 24

11:57: Evaporator has pumped down over night.  Vacuum @ 2.01e-6 Torr.  

14:42: TGHT @ 20A, Vac @ 1.65e-6 Torr.

14:52: TGHT @ 40A, Vac @ 1.66e-6 Torr.

14:52: Auto Heating begins: TGHT to max 820A.  Incrementing if vac < 4.5e-5 Torr, backing off if vac > 6.5e-5 Torr.

 16:04: TGHT @ 181A, vac @ 7.59e-6 Torr.

18:03: TGHT @ 420A, vac @ 4.71e-6 Torr.   (See attachment 2 for TGHT/IG1 for the past 4 hours)

March 25,

11:15:  TGHT has been at 820A for 14hr.  Vac @ 4.27e-6 Torr.  (See attachement 3 for TGHT/IG1 for these past hours)

11:17:  Auto cooling down is in progress...

17:21:  Auto cooling down ended at TGHT ~100A.  The TGHT was tabbed down manually from 100A to zero.  (See attachment #4 for the cooling down progress)

 All the pumps are off.  The evaporator will be vented next week. 

 Evaporator Vented.

  5   Tuesday, March 29, 2011, 10:20     ProblemsLoss of cooling water

According to Jonathan Aoki, the electricians will be servicing another MCC which will result in loss of cooling water for about 8 hours starting at 16:00 March 30.  We shouldn't be running the evaporator or any condensers at that time.

  6   Tuesday, March 29, 2011, 10:30     DoneLoss of cooling water update

It's the NON-ACTIVE water that will go off.  The evaporator is on sity water, so it will be OK.

  21   Tuesday, May 17, 2011, 16:43 John Wong   MaintenanceEvaporator Ion gauge replaced

The evaporator ion gauge filament burnt out on May 11, 2011.  A target was in the evaporator at that time and was about to being the sintering process.  The gauge had two filaments, so vacuum group helped to switch to the second filament.  The evaporator was vented on May 17, 2011, and a new ion gauge with two filaments was installed.  The gauge was tested and it's working fine. 

 

 

  48   Monday, May 14, 2012, 15:22 John Wong Target boat  Testing the new graphite foil from Ceramaterial

Monday, May 14, 2012, 15:04

Due to the differences in the use of the graphite foils in past SiC targets (C-grv foil from Alpha Aesar) and the newly prepared SiC#27 (C-grv foil from Ceramaterial), the out-gassing period for SiC#27 took over 6 days compared to 3 days for the vacuum to come down (see https://elog.triumf.ca/TIS/Evaporator_1/47). 

A few pieces of the new graphite foil is loaded on the target boat to test the out gassing reaction. 

The Evap #1 chamber has been pumped down to low 10e-5. 

Set to same parameter, see attachment#1

Initiated auto heating...


 Tuesday, May 15, 2012, 14:46

The target heater was ramped up to 820A.  There was so much out gassing as the temperature was increased.  The voltage did not hold at that current and the target heater was tripped off after the midnight.  (see attachment #2)

After the chamber was vented, it was discovered that the target boat's legs were bent due to over heating.  Both end of the targets where they touched the base got vaporized.  The boat was also got squeezed.  (see attachment #3).  

However, the heated graphite foils (~1600C at 820A) looks pretty good.  As per the supplier, CeraMaterials, the graphite was treated to 2000C.  See attachment #4 for the certificate.


 

Attachment 1: parameter.JPG
parameter.JPG
Attachment 2: TGHT_0-820A.GIF
TGHT_0-820A.GIF
Attachment 3: graphite_test_target_boat.pdf
graphite_test_target_boat.pdf
Attachment 4: Graphite_Foil-Certifcate_of_Compliance-Triumf_Order-1-16-12.pdf
Graphite_Foil-Certifcate_of_Compliance-Triumf_Order-1-16-12.pdf
  52   Tuesday, June 12, 2012, 14:43 John Wong   MaintenanceChanging backing pump oil

 Tuesday, June 12, 2012, 14:38

The backing pump oil was changed (ISAC WP#2012-06-12-1). 


  82   Friday, November 01, 2013, 13:08 Anders Mjos   MaintenanceGloves, window and window gasket replaced.

Work covered under work permit 2013-11-01-3 and performed by Anders and Rick with the help of Danno (RPG).

No significant contamination was found during the work. The old window could be disposed as normal waste.

  83   Monday, December 02, 2013, 16:09 Anders Mjos   Problems resolvedTGHT connector repositioned and tightened

The right connector for the TGHT had rotated. It has now been repositioned and both connectors have been tightened to reduce the chance for further rotation.

Attachment 1: Evap1_rotated_TGHT_conductor_2013-12-02.pdf
Evap1_rotated_TGHT_conductor_2013-12-02.pdf Evap1_rotated_TGHT_conductor_2013-12-02.pdf
  84   Monday, December 02, 2013, 16:10 Anders Mjos   DoneCopper bar on TGHT

The conductivity of the TGHT circuit will be measured with a copper bar shunt.

Monday, December 02, 2013, 16:00: Pumping down. 

Tuesday, December 03, 2013, 09:40: Stepped current up to 600A. Impedance of system ~0.7 mOhm. See attached graph for P(I).

Tuesday, December 03, 2013, 12:06: Stopped turbo. Vacuum at 1.3E-5 Torr

Wednesday, December 04, 2013, 09:20: Copper bar removed from vacuum chamber.

Test finished.

Attachment 1: Current_and_Voltage.pdf
Current_and_Voltage.pdf
  89   Tuesday, March 04, 2014, 15:48 John Wong  TARGET BOATIn progressRe-sinterring end caps

Tuesday, March 04, 2014, 15:43

Theses endcaps (4) were previously sinterred in Evap#2 but some surfaces were not fully sinterred. (See Evaporator2 E-log ID119: https://elog.triumf.ca/TIS/Evaporator_2/119)

The endcaps are inserted in a target boat wrapped with 3 heat-shields. 

Chamber is currently being pumped down. 

TGHT will be rampped up to 580A and heat for >4hrs.


 

  90   Wednesday, March 05, 2014, 10:30 Laura Lambert  TARGET BOATIn progressRe-sinterring end caps

John Wong wrote:

Tuesday, March 04, 2014, 15:43

Theses endcaps (4) were previously sinterred in Evap#2 but some surfaces were not fully sinterred. (See Evaporator2 E-log ID119: https://elog.triumf.ca/TIS/Evaporator_2/119)

The endcaps are inserted in a target boat wrapped with 3 heat-shields. 

Chamber is currently being pumped down. 

TGHT will be rampped up to 580A and heat for >4hrs.


 

 Wednesday, March 05, 2014, 10:20

IGP1 = 9.2e-7 Torr.

TGHT was stepped up to 35A and stabilized after half an hour.

Auto-ramp initiated at 2.0A/min, max setpoint = 580A.

Vacuum started to climb too fast, auto-ramp aborted.

Will step up manually...


 Wednesday, March 05, 2014, 12:18

Slowly stepped up to 100A manually.

Vacuum stable.

Initiating auto-ramp at 1.0A/min


 Wednesday, March 05, 2014, 13:17

IGP1 = 9.8e-6 Torr.

Current = 200A

Vacuum stable.

Stepping ramping rate up to 2.0A/min.


 Wednesday, March 05, 2014, 16:12

IGP1 = 4.6e-5 Torr, TGHT = 548A

Stopped auto-ramp to allow vacuum to settle back down.

Waited ~10min

IGP1 = 3.6e-5 Torr

Re-initiating auto-ramp at 2.0/min


 

  91   Wednesday, March 05, 2014, 23:05 John Wong  TARGET BOATDoneRe-sinterring end caps

Laura Lambert wrote:

John Wong wrote:

Tuesday, March 04, 2014, 15:43

Theses endcaps (4) were previously sinterred in Evap#2 but some surfaces were not fully sinterred. (See Evaporator2 E-log ID119: https://elog.triumf.ca/TIS/Evaporator_2/119)

The endcaps are inserted in a target boat wrapped with 3 heat-shields. 

Chamber is currently being pumped down. 

TGHT will be rampped up to 580A and heat for >4hrs.


 

 Wednesday, March 05, 2014, 10:20

IGP1 = 9.2e-7 Torr.

TGHT was stepped up to 35A and stabilized after half an hour.

Auto-ramp initiated at 2.0A/min, max setpoint = 580A.

Vacuum started to climb too fast, auto-ramp aborted.

Will step up manually...


 Wednesday, March 05, 2014, 12:18

Slowly stepped up to 100A manually.

Vacuum stable.

Initiating auto-ramp at 1.0A/min


 Wednesday, March 05, 2014, 13:17

IGP1 = 9.8e-6 Torr.

Current = 200A

Vacuum stable.

Stepping ramping rate up to 2.0A/min.


 Wednesday, March 05, 2014, 16:12

IGP1 = 4.6e-5 Torr, TGHT = 548A

Stopped auto-ramp to allow vacuum to settle back down.

Waited ~10min

IGP1 = 3.6e-5 Torr

Re-initiating auto-ramp at 2.0/min


 

 Wednesday, March 05, 2014, 23:02

End caps have been heated for 6.5 hours at 580A. Vac @ 7.4e-6 Torr. 

Auto-cooilng initiated at 2A/min. 


 Thursday, March 06, 2014, 14:48

The TaC on the endcaps is fully sinterred. (see attachment#1).

 


 

Attachment 1: endcaps_Mar3_2014.PNG
endcaps_Mar3_2014.PNG
  105   Thursday, December 11, 2014, 10:17 Laura Lambert   Maintenancewater supply shut off for lab closure over holidays

 Thursday, December 11, 2014, 10:16

water valve shut off for lab closure over the holidays.


 

  106   Friday, January 23, 2015, 15:02 Laura Lambert   Maintenancewater supply turned back on to EVAP1 and fume hoods

 Friday, January 23, 2015, 15:02

water supply turned back on to EVAP1 and fume hoods


 

  110   Tuesday, April 21, 2015, 11:28 Laura Lambert   MaintenanceIon Gauge replaced March 23rd 2015
  119   Saturday, August 29, 2015, 16:12 Anders Mjos   ProblemsRestarting vacuum after power outage

Saturday, August 29, 2015, 16:10: Roughing

Saturday, August 29, 2015, 16:10: Starting turbo

Saturday, August 29, 2015, 16:12: Turbo running. IG1 at 2.4E-4 T

  131   Monday, May 16, 2016, 15:52 Laura Lambert    Full clean of EVAP1

 Monday, May 16, 2016, 15:51

full clean of inside evap1 this afternoon.


 

  134   Tuesday, August 23, 2016, 17:35 John Wong  TARGET BOAT Sintering TaC coated target boat

Tuesday, August 23, 2016, 17:33

Target boat coated with TaC (sprayed) and wrapped with Ta-heat shield. 

chamber is currently being pumped down. Vac currently at 3.3e-5Torr. 

TGHT to be ramped up to 580A.

Initiate autoramping at 0.1A/min


 Wednesday, August 24, 2016, 10:34

TGHT at 111A/1.07V.  Vac at 7.5e-6 Torr and coming down.

Increase ramping rate to 2A/min.


 Thursday, August 25, 2016, 12:01

TGHT has been stabilized at 580A/6.89V for over 24 hours.  Vac at 7.5e-6 Torr.

Initiated cooling at 2A/min.


 Monday, September 12, 2016, 17:30

Container was properly sintered.


 

  135   Monday, September 12, 2016, 17:41 John Wong  TARGET BOATIn progressRUSH. Sintering end-caps

Monday, September 12, 2016, 17:30

A bunch of end caps (12?) and a long Ta-wire in spring sharp  were coated with TaC coating and wrapped in a small sheet of graphite foil. 

Container is then wrapped with a sheet of Ta heat shield.

These caps and wires will be sintered in Evap 1, so they may be prompted to contamination from the uranium processes. 

I have no choice but to use Evap1 to do this work since we are falling behind with the schedule.  

In the future, please have all the materials (targets, end caps, binder, etc) well prepared. 

I do not know what is the required current to sinter the caps since there is no temp measurement.  So, the best is to go with how the container was sintered, 580A. 


Monday, September 12, 2016, 17:36

Chamber has been pumped down to mid 10-6 Torr. 

Auto ramp to 580A at 2A/min.


 

  136   Tuesday, September 20, 2016, 10:49 Laura Lambert  TARGET BOATDoneRUSH. Sintering end-caps

John Wong wrote:

Monday, September 12, 2016, 17:30

A bunch of end caps (12?) and a long Ta-wire in spring sharp  were coated with TaC coating and wrapped in a small sheet of graphite foil. 

Container is then wrapped with a sheet of Ta heat shield.

These caps and wires will be sintered in Evap 1, so they may be prompted to contamination from the uranium processes. 

I have no choice but to use Evap1 to do this work since we are falling behind with the schedule.  

In the future, please have all the materials (targets, end caps, binder, etc) well prepared. 

I do not know what is the required current to sinter the caps since there is no temp measurement.  So, the best is to go with how the container was sintered, 580A. 


Monday, September 12, 2016, 17:36

Chamber has been pumped down to mid 10-6 Torr. 

Auto ramp to 580A at 2A/min.


 

 Tuesday, September 20, 2016, 10:41

vented in air and removed from evap1

managed to remove carefully using napkins and not touching boat directly with gloves as to avoid contamination.

endcaps and springs look good, fully sintered

one endcap looks like coating has started to peel off, possibly due to too thick of a TaC coating pre-sintering. see photos attached.


 

Attachment 1: Evernote_Camera_Roll_20160919_154129.jpg
Evernote_Camera_Roll_20160919_154129.jpg
Attachment 2: Evernote_Camera_Roll_20160919_154130.jpg
Evernote_Camera_Roll_20160919_154130.jpg
Attachment 3: Evernote_Camera_Roll_20160919_154131.jpg
Evernote_Camera_Roll_20160919_154131.jpg
Attachment 4: Evernote_Camera_Roll_20160919_154132.jpg
Evernote_Camera_Roll_20160919_154132.jpg
  143   Tuesday, December 20, 2016, 15:03 Laura Lambert   MaintenanceRETURN and SUPPLY valves CLOSED for xmas break
  148   Wednesday, May 24, 2017, 09:34 Laura Lambert   MaintenanceVACUUM TRIP OFF SETPOINT CHANGED

 Wednesday, May 24, 2017, 09:31

Last week the vacuum trip off point was changed to 8e-4 Torr when previously it was set to 8e-5 Torr.

Vacuum limits were set to stop at 5e-5 Torr and back-off at 6e-5 Torr

Now vacuum limits will be changed by an order of magnitude in an attempt to speed up the processes in the evaporator.


 

  153   Wednesday, June 07, 2017, 12:48 Aaron Schmidt    Turbo pump cooling

 Wednesday, June 07, 2017, 10:00-12:00: Cooling was split/routed from two bottom lines with tees and run to the turbo pump.

 

  156   Thursday, July 13, 2017, 12:49 Laura Lambert   Problems*hot lab is HOT*

Thursday, July 13, 2017, 12:48

NOTE: hot lab reached 27degrees every day this week and went up to 28C today! 

This is with the small portable fan running.

27C was reached even with both evaporators off.

When at 28C: evap2 = ~1500C and evap1 = 35A


 Thursday, July 20, 2017, 15:58

Hot lab reached 30C today.

Small fan off - unsure if able to run due to contamination spread...

Both evap1 and evap2 were under vacuum but had not initiated ramping up yet.


 

Attachment 1: Capture.JPG
Capture.JPG
  163   Thursday, July 27, 2017, 09:08 Laura Lambert   Problems resolved*hot lab is HOT*

Laura Lambert wrote:

Thursday, July 13, 2017, 12:48

NOTE: hot lab reached 27degrees every day this week and went up to 28C today! 

This is with the small portable fan running.

27C was reached even with both evaporators off.

When at 28C: evap2 = ~1500C and evap1 = 35A


 Thursday, July 20, 2017, 15:58

Hot lab reached 30C today.

Small fan off - unsure if able to run due to contamination spread...

Both evap1 and evap2 were under vacuum but had not initiated ramping up yet.


 

 Thursday, July 27, 2017, 09:06

There was a broken valve motor affecting all ISAC rooms - temporary fix in place.

Ventilation in ISAC hot lab has been increased.

Temperature back to a reasonable level - currently sitting at 22C!


 

  165   Thursday, September 07, 2017, 14:26 Aaron Schmidt   Maintenanceroughing pump oil replaced

 Thursday, September 07, 2017, 11:00 -12:00

The roughing pump was disconnected from Evaporator 1, along with the exhaust/ventilation. No contamination was found on swipes.

The oil was refilled.

The roughing pump was then moved away from the PLC to allow access for Dave Morris. The RP can be reconnected and tested after the PLC work is complete.

Work permit # I2017-09-07-1

 

  166   Wednesday, September 20, 2017, 08:07 Aaron Schmidt   MaintenanceIon gauge & RP status

Wednesday, September 20, 2017, 08:00: 

-A new ion gauge was installed yesterday afternoon and the old one removed. The old IG was found to be contaminated (300 cpm) and as of 20/09/2017, it is double bagged and stashed underneath the evaporator for the time being. 

Completed under work permit: I2017-09-19-9

-The roughing pump was reconnected this morning without issue.

  170   Tuesday, November 07, 2017, 11:57 Laura Lambert   MaintenanceInterlocks limits changed to 100mTorr

 Tuesday, November 07, 2017, 11:55

Interlocks limits updated/ changed to 100mTorr for both TGHT and TBHT by Ray


 

  171   Tuesday, November 07, 2017, 12:04 Laura Lambert   MaintenanceNoise levels checked - ear protection not required.

 Tuesday, November 07, 2017, 11:58

Noise levels were checked with monitor by Terry.

Max readings in lab reached ~83dB but sat between 70-78dB in most areas.

This is under limit for requirement to wear ear protection [85dB].

To reach limit - noise levels would need to increase drastically.

Conclusion: ear protection not required in lab.

Recommended if working in there for long periods of time for personal preference, but not a requirement.


 

  174   Wednesday, November 22, 2017, 14:20 Laura Lambert   MaintenanceNew eye wash for hot lab!

 Wednesday, November 22, 2017, 11:05

Eye wash installed yesterday, simple attachment on sink spout.

Easy to use, simply twist attachment 180 degrees.

Water for tap can be turned on before or after twist.

Adjust pressure/ temperature accordingly.

Auto shut-off for eye-wash at ~38C [100F] - no accidental eye-burning when trying to wash eyes!


 

  212   Tuesday, June 26, 2018, 12:12 Aaron Schmidt   Problems resolvedGloves replaced.

 Tuesday, June 26, 2018, 09:30. Gloves on evap 1 changed out. 

The original right one was otrn. Left was o but worn. Both replaced with new gloves.

  233   Thursday, March 21, 2019, 09:03 Aaron Schmidt   In progressEvap 1 pump down issue

On Tuesday it was noted that evaporator 1 was not pumping down properly. It was vented and the seal & seal face wiped with a cloth. The initial pump down rate was faster, however after 48 hrs, it has still not pumped down to appropriate levels. 

Thursday, March 21, 2019, 08:59: IV1 closed & TP1 off. 

  234   Tuesday, March 26, 2019, 08:58 Aaron Schmidt   MaintenanceRoughing pump oiled.

Oiled as per work permit:  I2019-03-26-2.

Tuesday, March 26, 2019, 08:53: Start RP1

Tuesday, March 26, 2019, 09:03: Holding at 0.303T on CG2. 

Tuesday, March 26, 2019, 09:10: Turned off RP1. Vent chamber slightly. Close VV1. Restarted RP1.

Open RV1.

Tuesday, March 26, 2019, 09:13: Vacuum stalls out at approx 0.300T.

Tuesday, March 26, 2019, 09:16: Shut off RP1. Contact Vacuum group.


 Checked as per work permit: I2019-03-26-5

Tuesday, March 26, 2019, 13:50: Filter checked. OK

Tuesday, March 26, 2019, 14:00: Tees checked. OK.

Tuesday, March 26, 2019, 14:05: Line / bellows. Fail

Tuesday, March 26, 2019, 14:11: New line / bellows. OK 

Tuesday, March 26, 2019, 14:19: TP1 on, IV1 opened. Vacuum @ 3.5e-05T and dropping.

Pumping down evap1. Dispose of the old line. Replacement successful. No contamination was found on the swipes.

Tuesday, March 26, 2019, 14:36: Vacuum @ 1.12e-05T and dropping. 

  235   Wednesday, March 27, 2019, 08:56 Marla Cervantes 43630-6 DoneGraphite insert test 4

 Wednesday, March 27, 2019, 08:50

A graphite insert was set into a tantalum tube in the evaporator 2 for 3 days

The objective of the test was to determine the current and voltage required to reach 2000 C

Current 424.2 A, voltage 7.17 V, P = 3 kW 

details can be find here https://elog.triumf.ca/TIS/Evaporator_2/433

The test will continue for 2 weeks in the EVAP1.


 Good vacuum 5e-4 Torr

Bad vacuum 1.00e-4

Pressure IGP1 = 1.55e-6 Torr

The autoramp was set to 420 A, at 1 A/min,


Monday, April 01, 2019, 07:57

TGHT = 4.68 V, 424.32 A

IGP1 = 9.61e-7 Torr


Autoramop is set to -1 A/min to 0 A

Monday, April 01, 2019, 11:19 

IGP1=5.43e-7 Torr

At TGHT = 223 A and 2.1 V the autoramp was increased to -2 A/min


Monday, April 01, 2019, 11:20

Sudden and unexpected  pressure increment to 1.4e-5 Torr, might be a glitch.


Monday, April 01, 2019, 13:10

IGP1 = 4.34e-7Torr

The autoramp was stopped at TGHT = 17.28 A, 0.0625 V,

and it was lower down to 0 A manually


 Results: The tantalum tube deformed in the contact points with the graphite insert

  236   Friday, April 05, 2019, 10:08 Marla Cervantes 43630-3 DoneTaC coating/sintering for graphite insert test

 Friday, April 05, 2019, 10:04

A tantalum tube was coated with TaC and wrapped with Ta heat-shield (3 layers)

Desired temp = 1900 C (expected TGHT ~445A/7.5V), TBHT will be set fixed at 230A (max).

Yesterday the tube was set in the EVAP1 and pumped down.


Friday, April 05, 2019, 10:07 

IGP1= 1.61e-6 Torr

The current is manually tapped to 40 A.


Friday, April 05, 2019, 13:25

After ~2 hours 

IGP1 = 1.54e-6 Torr

TGHT = 0.61 V, 40.39 A

Autoramp is set to 1 A/min to 400 A

Good vac at 3.00-5 Torr

Bad vac at 5.0e-5 Torr.


Sunday, April 07, 2019, 9:00

The current was increased to 424 A


Monday, April 08, 2019, 16:36

EVAP1 vented with air, sintered tube was removed. 

Attachment 1: EVAP1-TaC_Coating.JPG
EVAP1-TaC_Coating.JPG
  237   Wednesday, April 10, 2019, 13:38 Marla Cervantes 43630-3  DoneGraphite insert test #6

 Wednesday, April 10, 2019, 13:30

Tantalum foil caps were added to a graphite insert (see picture caps)

 The insert was set in a tantalum tube previously coated and wrapped with 3 Ta sheets.

The system was installed in the EVAP1, and it will be heated for a week at 2000 C.

Currently pumping down.


 Thursday, April 11, 2019, 13:26

IGP1 = 9.9e-7 Torr

The current is tapped to 40 A

After 1hr the autoramp is set to 1 A/min to TGHT 500 A


The TGHT current remained at 500 A for week

until at April 18 at ~4:30 pm

a localized power outage tripped the EVAP1.


The EVAP1 was ventd with air and the tantalum tube was removed

The tantalum tube did not break.

Attachment 1: caps.jpg
caps.jpg
Attachment 2: Curren-voltage-plot.JPG
Curren-voltage-plot.JPG
  238   Friday, May 24, 2019, 15:25 Marla Cervantes 43943-1 DoneGraphite insert test - FOILS

 Friday, May 24, 2019, 15:04

A TaC coated tantalum tube, loaded with graphite foils was transferred to EVAP1

https://elog.triumf.ca/TIS/Evaporator_2/445

The tueb will be heated with the same power used in EVAP2,

the power of the EVAP2 and EVAP1 will be matched using the fit from Document-126503

The chamber is currently pumping down


 Monday, May 27, 2019, 08:58

The current will be tapped to 50 A to replicate the procedure of EVAP2 

then the current will be set to 1 A/min to 500 A and increased to match with EVAP2 power.


 

  250   Tuesday, November 05, 2019, 14:50 Aaron Schmidt   MaintenanceFallen Bolt.

 One of the TBHT bolts  fell out of reach and may be sitting on the isolation valve or TP.

Remove TP as per WP:  I2019-11-05-9

Tuesday, November 05, 2019, 14:48: Completed. Found 2 TBHT bolts, a broken insulator, one small vented screw, and a piece of rubber.

Turbo pump mesh clear. Magnetic grabbing tool left in Evap 1 to potentially pickup /  grab materials before they fall down the hole if needed. The tip of the tool is contaminated.

Tuesday, November 05, 2019, 15:03: Evap 1 pumped down. TP1 started, IV1 opened. Ok. 

 

 

  261   Monday, June 01, 2020, 09:29 Aaron Schmidt   ProblemsIEVAP:IGP1 swap out

 Replacement of electronic / controller head from INIFICON - BPG to Agilent - Model: FRG-730 due to EVAP 1 trips.

Monday, June 01, 2020, 09:37: Swap complete. 

  260   Monday, June 01, 2020, 09:29 Aaron Schmidt   ProblemsIEVAP:IGP1 swap out

 Replacement of electronic / controller head from INIFICON - BPG to Agilent - Model: FRG-730 due to EVAP 1 trips.

  264   Tuesday, August 18, 2020, 12:40 Aaron Schmidt    IEVAP:IGP1 swap out

 INIFICON -  BPG - SN: 232

PN: 353-573

Tuesday, August 18, 2020, 10:38: Control head for IGP1 swapped with bagged one.

 

Had been roughing.

Tuesday, August 18, 2020, 12:37: Turbo pump on. 

Tuesday, August 18, 2020, 12:54: Vacuum @ 1.28e-05T & dropping. 

  270   Thursday, April 15, 2021, 15:01 Marla Cervantes    IGP1 patch

Thursday, March 31, 2021, 14:42

 

EVAP1's TGHT has been tripping even when the pressure is below the tripping limits. The temperature of the turbo pump and the TGHT's power supply were monitored discarding the possibility of tripping due to the overheating of these pieces of equipment.

Gelo has been monitoring the IGP1 during carbothermal reductions to pinpoint the tripping issue, below is Gelo description to the issue and the patch he implemented to fix it.

 

"IGP loses its STATON (On status) if the value from the device is not within the valid voltage window (0.7 to 10 V). IEVAP:IGP1 for some reason goes to 0V for a few seconds then goes back up to where it left off.

Prior to the latest software updated, I added a 2 second delay in the code so that any invalid signal <=2s will be ignored.

 

Here is the data that you sent me specifically looking at when it tripped. I also attached the data that you sent me.  << File: 310321-P2N-3-CR (1).txt >>

 

 

Time

 

IEVAP:TGHT:RDVOL [V]

 

IEVAP:TGHT:RDCUR [A]

 

IEVAP:IGP1:RDVAC [T]

03/31/2021 12:00:25

3.07

740.9

0.01866428

03/31/2021 12:00:26

3.07

741.1

0.01838651

03/31/2021 12:00:27

3.07

740.7

0.01838651

03/31/2021 12:00:28

3.07

740.8

0.01797758

03/31/2021 12:00:29

3.08

740.9

0.0178433

03/31/2021 12:00:30

3.08

740.6

0.0178433

03/31/2021 12:00:31

3.08

740.8

0

03/31/2021 12:00:32

3.08

741.1

0

03/31/2021 12:00:33

0.14

42.2

0.01680456

03/31/2021 12:00:34

0

3.3

0.01513015

03/31/2021 12:00:35

0

3.4

0.01071685

03/31/2021 12:00:36

0

3.2

0.00788081

03/31/2021 12:00:37

0

3.2

0.00673278

03/31/2021 12:00:38

0

2.6

0.00445774

 

TGHT Voltage and TGHT current are both read from the same PLC module, which tells me that the PLC module is not likely the issue since we were still reading other signals when IGP was reading 0.

 

For the new update, I adjusted the delay to 5 seconds since the signal drop seemed like it was about 2s and was enough to lose the IGP STATON bit which tripped TGHT.

 

The delay only applies for the STATON status which can also be described as reading OK status in this case. Any other trip will be instantaneous and work as normal. 

 

STATON is “ANDed” with other trips. i.e. IEVAPIGP_LESS10MTORR = IEVAPIGP1_RDVAC < 10mTorr AND IEVAPIGP1_STATON."

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