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New entries since:Wed Dec 31 16:00:00 1969
Entry  Friday, October 04, 2013, 16:21, John Wong, Empty, , LP-SIS, Done, Sintering TaC coating on a LP target container to be used for C-grv tube test  LP_C_grv_tempcurve.PNGLP_C_grv_TGHT632_1960C.PNG

Friday, October 04, 2013, 15:37

A LP target container is coated with TaC.  The container is wrapped with 3 layers to heat shield.  

This container will be used for the graphite tube test.  

Chamber is being pumped down.

 The HS cooling water valves are open and no leaks are detected. 


 

TGHT will be ramped up to 580A at 0.2A/min

TBHT will be ramped up to 230A at 0.2A/min.

The temperature will be monitored and measured. 


 Sunday, October 06, 2013, 19:55

 
TGHT and TBHT have reached to 580A/230A, respectively.  And the target has been heated for about 5 hours.  
 
The temperature inside the tube is measure at 1000C; this is much lower than expected as to previously measured at 1700C.
 
The temperature outside the container is at 1400C.

I'm suspecting the thermocouple inside the tube could be shorted.  
 
Cooling down the heaters down to zero at 2A/min for TGHT and 1A/min for TBHT. 
 
Tomorrow, the chamber will be vented and the target will be inspected.  
 
I like to re-adjust the thermocouple again, and re-heat the target back up, hoping to reach 1700C at TGHT = 580A.  

 Monday, October 07, 2013, 15:24
 
The sintering of the TaC coating is complete.
 
The chamber was vented this morning.  Apparently, there was a short in the thermocouple so the temperature measure was recorded much lower.
 
The thermocouples are adjusted, and the chamber is pumped down. 
 
Vac currently at 1.17e-6 Torr. 
 
TGHT and TBHT will be ramped up to 580A/230A at 2A/min. 
 
Continue monitoring the temperature...

 Monday, October 07, 2013, 16:13
 
TGHT and TBHT were ramped up to 90A.  Temperature inside the tube was measure just at 75C and the outside surface was at 207C.
Maybe the thermocouple is F up; will replace with a new one tomorrow.
Cooling down the target down...

Tuesday, October 22, 2013, 16:49

The target was heated up to 580A and the temperature inside the tube was measured to be ~1800C and the outside surface was ~1400C.

The target was cooled down.  Then the graphite tube was inserted.

There are two thermcouples inserted inside the tube on both ends.

Chamber has been pumped down to 4.33 e-7 Torr.  No leaks were detected.

Target will be heated up again to TGHT @ 580A / TBHT @ 230A at 0.2A/min.

The temperatures will be monitored.

T1 = left (floating)

T2 = right (toughing C-grv tube)

(wtf ionizer pointing into the page).


 Thursday, October 24, 2013, 16:35

TGHT/TBHT reached to 580A/230A. 

T1 = 1642C

T2 = Error?? Reading goes on/off intermittently, showing 900 - 1900C


Thursday, October 24, 2013, 16:45 

Ramping up TGHT to 680A to see if T1 can reach 1700C.

IG1 currently at 5.2e-7 Torr.


 Friday, October 25, 2013, 12:30

TGHT was ramped up to 632A (stopped due to voltage limiting). 

T1 was measured at 1960C.  Vac went up as it was heated up.  (see attachment #2)

Target was cooled down at 5A/min, now at 0A.

The chamber will be vented and the target will be inspected.

This run is complete.


 

Entry  Thursday, September 26, 2013, 15:17, John Wong, Empty, 39814-VI-?, LP-IG-LIS, Done, Sintering empty target oven coated with TaC for UCx#8 UCx#8_container_TaC_coat_sintering.PNG

Thursday, September 26, 2013, 13:04

The LP-IG-LIS target container is coated with TaC. 

Container is wrapped with 3 layers of Ta heat shield and about to go through the sintering process.

A thermocouple is inserted to measure the temperature inside the tube (1st attempt ever). 

Click on the link for detailed pictures:

https://www.dropbox.com/sh/6dc5arajg87mws9/6cU5OxjkZg


TGHT will be ramped up to 580A at 0.2A/min

TBHT will be ramped up to 230A at 0.2A/min.

Chamber has been pumped down.  HS cooling H2O valves are opened, and no leaks are detected. 

Currently IGP1 @ 5.9e-6 Torr.


 Thursday, September 26, 2013, 15:44

TGHT stepped up to 30A.  TBHT currently @ 0A. 

Temp @ 35C, Vac @ 1.4e-5 Torr.


 Monday, September 30, 2013, 14:54

The container was heated up to 580A TGHT/ 230A TBHT for a day (see attachment #1 for vac vs cur plot).

The temperature was measure at ~1780C. (see link for details: https://www.dropbox.com/sh/d8d9j2t60qlm3jk/nkMh7dx_R8 )

The target was cooled down and vented. 

Proceed complete.


 

 

Entry  Tuesday, September 17, 2013, 11:21, John Wong, Nb, target boat #3 (brand new!) , , , Nb thermo treatment (Bob's samples)  Nb_sample_setup.PNGNb_800C.PNG

Tuesday, September 17, 2013, 11:14

Target boat contains 5 Nb discs.  3 discs are wraps with 0.001" thin of Nb foil (99.8% pure), and 2 are wraps with 0.001" Ta foil (see attachment#1)

Chamber has been pumped down over night.  Pressure is currently at 9.8e-7 Torr. 

Heating instructions:

Samples will be heated up to 800C.  TGHT will be ramped up accordingly. (Two thermocouples are wielded on the target container.)

Once at the desired temperature; the samples will be heat for 4 hours before cooling down.


 Tuesday, September 17, 2013, 14:37

Target temperature has reached to 800C at around 13:00 (see attachment#2)

TGHT @ 230A/3.07V (local 233A/3.25V). 

IG @ 1.06e-6 Torr. 

The heater will be ramped down at ~17:00 at 2A/min.


 Tuesday, September 17, 2013, 17:36

Target temp: T1 = 805C, T2=797.6C

IG @ 9.4e-7 Torr.

Cooling down initiated. 


 Wednesday, September 18, 2013, 11:34

TGHT at 0A.  Temp at 22C. 

IG @ 5.8e-7 Torr.

Venting chamber.


 

    Reply  Thursday, September 19, 2013, 11:56, Laura Lambert, Nb, target boat #3 (brand new!) , , , Nb thermo treatment (Bob's samples)  Capture.PNG

John Wong wrote:

Tuesday, September 17, 2013, 11:14

Target boat contains 5 Nb discs.  3 discs are wraps with 0.001" thin of Nb foil (99.8% pure), and 2 are wraps with 0.001" Ta foil (see attachment#1)

Chamber has been pumped down over night.  Pressure is currently at 9.8e-7 Torr. 

Heating instructions:

Samples will be heated up to 800C.  TGHT will be ramped up accordingly. (Two thermocouples are wielded on the target container.)

Once at the desired temperature; the samples will be heat for 4 hours before cooling down.


 Tuesday, September 17, 2013, 14:37

Target temperature has reached to 800C at around 13:00 (see attachment#2)

TGHT @ 230A/3.07V (local 233A/3.25V). 

IG @ 1.06e-6 Torr. 

The heater will be ramped down at ~17:00 at 2A/min.


 Tuesday, September 17, 2013, 17:36

Target temp: T1 = 805C, T2=797.6C

IG @ 9.4e-7 Torr.

Cooling down initiated. 


 Wednesday, September 18, 2013, 11:34

TGHT at 0A.  Temp at 22C. 

IG @ 5.8e-7 Torr.

Venting chamber.


 

 Thursday, September 19, 2013, 11:41

Target boat contains batch#2 Nb samples (see attachment #1)

Chamber has been pumped down over night.  

IG @ 5.5e-07 Torr. 

CG1B @ 0.033 T

CG1A @ 0.127 T

There is a leak in the backing line.  BV1 was bypassed in order to turn on the turbo pump. (Will investigate the leaks after the processes are done)  

*See attached picture to view samples


       Reply  Thursday, September 19, 2013, 17:02, John Wong, Nb, target boat #3 (brand new!) , , , Nb thermo treatment (Bob's samples)  

Laura Lambert wrote:

John Wong wrote:

Tuesday, September 17, 2013, 11:14

Target boat contains 5 Nb discs.  3 discs are wraps with 0.001" thin of Nb foil (99.8% pure), and 2 are wraps with 0.001" Ta foil (see attachment#1)

Chamber has been pumped down over night.  Pressure is currently at 9.8e-7 Torr. 

Heating instructions:

Samples will be heated up to 800C.  TGHT will be ramped up accordingly. (Two thermocouples are wielded on the target container.)

Once at the desired temperature; the samples will be heat for 4 hours before cooling down.


 Tuesday, September 17, 2013, 14:37

Target temperature has reached to 800C at around 13:00 (see attachment#2)

TGHT @ 230A/3.07V (local 233A/3.25V). 

IG @ 1.06e-6 Torr. 

The heater will be ramped down at ~17:00 at 2A/min.


 Tuesday, September 17, 2013, 17:36

Target temp: T1 = 805C, T2=797.6C

IG @ 9.4e-7 Torr.

Cooling down initiated. 


 Wednesday, September 18, 2013, 11:34

TGHT at 0A.  Temp at 22C. 

IG @ 5.8e-7 Torr.

Venting chamber.


 

 Thursday, September 19, 2013, 11:41

Target boat contains batch#2 Nb samples (see attachment #1)

Chamber has been pumped down over night.  

IG @ 5.5e-07 Torr. 

CG1B @ 0.033 T

CG1A @ 0.127 T

There is a leak in the backing line.  BV1 was bypassed in order to turn on the turbo pump. (Will investigate the leaks after the processes are done)  

*See attached picture to view samples


Thursday, September 19, 2013, 17:01  

TGHT reached to 800A.  Temp at 795.9C for 4 hours.  Vac at 5.8e-7 Torr.

Cooling down initiated.  ramping rate at 2A/min. 


 

    Reply  Friday, September 20, 2013, 14:59, John Wong, Nb, target boat #3 (brand new!) , , , Nb thermo treatment (Bob's samples)  

John Wong wrote:

Tuesday, September 17, 2013, 11:14

Target boat contains 5 Nb discs.  3 discs are wraps with 0.001" thin of Nb foil (99.8% pure), and 2 are wraps with 0.001" Ta foil (see attachment#1)

Chamber has been pumped down over night.  Pressure is currently at 9.8e-7 Torr. 

Heating instructions:

Samples will be heated up to 800C.  TGHT will be ramped up accordingly. (Two thermocouples are wielded on the target container.)

Once at the desired temperature; the samples will be heat for 4 hours before cooling down.


 Tuesday, September 17, 2013, 14:37

Target temperature has reached to 800C at around 13:00 (see attachment#2)

TGHT @ 230A/3.07V (local 233A/3.25V). 

IG @ 1.06e-6 Torr. 

The heater will be ramped down at ~17:00 at 2A/min.


 Tuesday, September 17, 2013, 17:36

Target temp: T1 = 805C, T2=797.6C

IG @ 9.4e-7 Torr.

Cooling down initiated. 


 Wednesday, September 18, 2013, 11:34

TGHT at 0A.  Temp at 22C. 

IG @ 5.8e-7 Torr.

Venting chamber.


 

 Friday, September 20, 2013, 14:56

Target contains batch#3 sample wrapped with Nb foil. 

Chamber has been pumped down to 1.03e-6 Torr. 

Samples will be heated up to 1200C for 4 hours.  


 Friday, September 20, 2013, 16:54

TGHT at 450A, temp stabilizes at 1238C.

Will cool down at 20:30 tonight.


Friday, September 20, 2013, 20:40  

Samples has been heated for 4 hours at 1235C.  

Cooling down initiated. 


 Monday, September 23, 2013, 14:40

Chamber was vented.

Batch#3 process completed.


 

       Reply  Monday, September 23, 2013, 16:18, John Wong, Nb, target boat #3 (brand new!) , , , Nb thermo treatment (Bob's samples)  

John Wong wrote:

John Wong wrote:

Tuesday, September 17, 2013, 11:14

Target boat contains 5 Nb discs.  3 discs are wraps with 0.001" thin of Nb foil (99.8% pure), and 2 are wraps with 0.001" Ta foil (see attachment#1)

Chamber has been pumped down over night.  Pressure is currently at 9.8e-7 Torr. 

Heating instructions:

Samples will be heated up to 800C.  TGHT will be ramped up accordingly. (Two thermocouples are wielded on the target container.)

Once at the desired temperature; the samples will be heat for 4 hours before cooling down.


 Tuesday, September 17, 2013, 14:37

Target temperature has reached to 800C at around 13:00 (see attachment#2)

TGHT @ 230A/3.07V (local 233A/3.25V). 

IG @ 1.06e-6 Torr. 

The heater will be ramped down at ~17:00 at 2A/min.


 Tuesday, September 17, 2013, 17:36

Target temp: T1 = 805C, T2=797.6C

IG @ 9.4e-7 Torr.

Cooling down initiated. 


 Wednesday, September 18, 2013, 11:34

TGHT at 0A.  Temp at 22C. 

IG @ 5.8e-7 Torr.

Venting chamber.


 

 Friday, September 20, 2013, 14:56

Target contains batch#3 sample wrapped with Nb foil. 

Chamber has been pumped down to 1.03e-6 Torr. 

Samples will be heated up to 1200C for 4 hours.  


 Friday, September 20, 2013, 16:54

TGHT at 450A, temp stabilizes at 1238C.

Will cool down at 20:30 tonight.


Friday, September 20, 2013, 20:40  

Samples has been heated for 4 hours at 1235C.  

Cooling down initiated. 


 Monday, September 23, 2013, 14:40

Chamber was vented.

Batch#3 process completed.


 

 Monday, September 23, 2013, 16:14

Batch#4.  Target container contains 2 Nb stables (a bullet type and a disc).  

Samples are wrapped with "dimpled" Nb foil to prevent diffusion bonding. 

Chamber has been pumped down to 8.3e-7 Torr, CG1B @ 30mT, CG1A @ 118mT. 

Samples will be heated up to 1400C for 4 hours. 


Monday, September 23, 2013, 17:46

TGHT at 620A. Temp at 1400C. Current pressure @ 2.5e-6 Torr. 


Tuesday, September 24, 2013, 16:45

Sample#4 was heated up to 1400C and after about 3hrs, the target container started to break.

See the link below for more details:

https://www.dropbox.com/s/9mhpkz66u6yqldm/Nb_1400C.mp4


 

Entry  Tuesday, August 27, 2013, 17:01, John Wong, , targetboat (TaC coated), , Done, Sintering TaC coated regular caps  Sintering__endcap_.jpg

Tuesday, August 27, 2013, 16:48

Target boat is filled with TaC coated endcaps (brown) and some partial sinterred ones (gray) from before.  (see attachment#1).

The container is wrapped with Ta heat-shield.

Chamber has been pumped down; IG currently @ 7.3e-7 Torr. 

Heat-shield cooling water valves are open; no leaks are detected.

Initiated TGHT auto-ramping at 0.5A/min, set TGHT max at 580A.


 Wednesday, August 28, 2013, 16:09

TGHT has reached to 580A and been heated for over 4 hours.

IG is coming down, currently at 1.9 e-6 Torr.

Initiated auto-cooling.  2A/min. 


 

    Reply  Thursday, August 29, 2013, 11:53, Laura Lambert, , targetboat (TaC coated), , Done, Sintering TaC coated regular caps  

John Wong wrote:

Tuesday, August 27, 2013, 16:48

Target boat is filled with TaC coated endcaps (brown) and some partial sinterred ones (gray) from before.  (see attachment#1).

The container is wrapped with Ta heat-shield.

Chamber has been pumped down; IG currently @ 7.3e-7 Torr. 

Heat-shield cooling water valves are open; no leaks are detected.

Initiated TGHT auto-ramping at 0.5A/min, set TGHT max at 580A.


 Wednesday, August 28, 2013, 16:09

TGHT has reached to 580A and been heated for over 4 hours.

IG is coming down, currently at 1.9 e-6 Torr.

Initiated auto-cooling.  2A/min. 


 

 Thursday, August 29, 2013, 11:50

TGHT at 0 A

IG at 3.5e-7 Torr

Turning off EVAP2 and venting chamber

Process complete


 

Entry  Wednesday, August 21, 2013, 12:30, John Wong, Ta, 38817-10, HP-SIS, Done, Conditioning Ta target  Ta#41_conditioning.PNG

Wednesday, August 21, 2013, 12:28

Container is filled with 400 discs of Ta foils, and wrapped with 3 layers of Ta heat shields.

No caps are inserted during the conditioning. 

Chamber is currently being pumped down. 


 Wednesday, August 21, 2013, 15:54

HS cooling water valves opened, no leaks were detected.

IG @ 2.9e-6 Torr.

Heating setting:

TGHT max = 820A,

TBHT max = 230A

ramping rate 2A/min.


 Thursday, August 22, 2013, 12:45

TGHT/TBHT reached to 820A/230A, respectively. 

So much out-gassing was observed at the max currents.  (see attachment#1).

TGHT/TBHT are ramping down at 4A/min. 

Chamber will be vented in air.

The target will will be inspected.

More info later...


 Thursday, August 22, 2013, 16:44

Target was removed from the evaporator and inspected.

The container and the Ta materials look OK. 

The outgassing could be from the Ta-heat shields; they look burnt and brittle.

Overall, the target is good.


 

Entry  Thursday, August 08, 2013, 15:41, Laura Lambert, NiO, 39530-6, HP-FEBIAD, In progress, Sintering NiO # 2 NiO#2.PNG

Thursday, August 08, 2013, 15:19

NiO target materials loaded into the container yesterday.

Total discs = 530, (5 discs/pack)

length [after loaded] = 9.0cm

Target container is wrapped with Ta-heat shields, and will be removed after sintering process.

No end caps were inserted.

The chamber has been pumped down and currently IG1 = 3.8x10-06 Torr.

The HS cooling water was turned on and no leaks were detected.

TGHT and TBHT have been stepped up to 50A.

Auto-ramping setting:

0.2A/min for TGHT max = 250A, TBHT max = 230A.

Good vacuum = 3.00e-05 Torr

Bad vacuum = 4.00e-05 Torr

**See attachment #1 for pictures of target pre-sintering


 

    Reply  Thursday, August 08, 2013, 17:28, John Wong, NiO, 39530-6, HP-FEBIAD, Done, Sintering NiO # 2 

Laura Lambert wrote:

Thursday, August 08, 2013, 15:19

NiO target materials loaded into the container yesterday.

Total discs = 530, (5 discs/pack)

length [after loaded] = 9.0cm

Target container is wrapped with Ta-heat shields, and will be removed after sintering process.

No end caps were inserted.

The chamber has been pumped down and currently IG1 = 3.8x10-06 Torr.

The HS cooling water was turned on and no leaks were detected.

TGHT and TBHT have been stepped up to 50A.

Auto-ramping setting:

0.2A/min for TGHT max = 250A, TBHT max = 230A.

Good vacuum = 3.00e-05 Torr

Bad vacuum = 4.00e-05 Torr

**See attachment #1 for pictures of target pre-sintering


 

 Thursday, August 08, 2013, 17:26

Pressure is stabilizing at ~2.2e-5 Torr.  TGHT/TBHT at 50A.

Initiated auto-ramping... 


Sunday, August 11, 2013, 21:30  

TGHT/TBHT have reached to 250A/230A.  Target have been heated over the weekend.  

Cooling down initiated; 2A/min.  

The chamber wil be vented in air tomorrow. 


 Monday, August 12, 2013, 18:01

The sinterring process is complete. 

The target is ready to be removed from the evaporator, and the endcaps will be inserted.


 

Entry  Monday, July 22, 2013, 15:03, John Wong, Empty, 38634-7, LP-SIS, Done, Sintering empty target oven coated with TaC for UCx#7 

Monday, July 22, 2013, 15:00

Target container is coated with TaC - this container will be used for UCx#7.

Container is wrapped with 3 layers of Ta, including the back-block.

For the sintering process:

TGHT will be ramped up to 580A at 0.2A/min

TBHT will be ramped up to 230A at 0.2A/min.

Chamber has been pumped down.  HS cooling H2O valves are opened, and no leaks are detected. 

Currently IGP1 @ 7.03e-6 Torr. 


 Monday, July 22, 2013, 15:19

TGHT/TBHT was stepped up to 20A.  Pressure increased to ~1.2e-5 Torr.

Auto-ramping initiated...


 Wednesday, July 24, 2013, 18:40

TGHT and TBHT have reached to 580A/230A, respectively.  Target has been heated for ~4 hours at that max current.

Vacuum currently at 1.65e-6 Torr.

Auto-cooling initiated... (TGHT @ -1A/min, TBHT -0.5A/min)

Target will be vented in air tomorrow.


 

Entry  Monday, June 17, 2013, 16:59, Laura Lambert, SiC, 38481-6, HP-FEBIAD, Done, Sintering of SiC #29 

Monday, June 17, 2013, 16:57

Target is loaded with 510 SiC discs

Container was previously coated with TaC and sintered

SiC is wrapped with tantalum heat shield

Chamber is currently being pumped down


 

    Reply  Tuesday, June 18, 2013, 16:40, John Wong, SiC, 38481-6, HP-FEBIAD, Done, Sintering of SiC #29 

Laura Lambert wrote:

Monday, June 17, 2013, 16:57

Target is loaded with 510 SiC discs

Container was previously coated with TaC and sintered

SiC is wrapped with tantalum heat shield

Chamber is currently being pumped down


 

 Tuesday, June 18, 2013, 16:16

HS water valves opened; no leaks were detected.

IG @ 8.9e-7 Torr.

Note: This target has a regular end cap inserted on one end, and the other with a D-cap. 

TGHT will be heated up to 820A and TBHT to 300A; ramping rate at 1A/min.

Stepped up TGHT/TBHT to 60A.  Vacuum slowly increasing... 


 Tuesday, June 18, 2013, 17:55

Stepped up TGHT/TBTH to 80A.  10 mins later, pressure went beyond the limit and tripped of the p/s.  F!

Allowed vacuum to come down below 8e-5 Torr.  Stepped down TGHT/TBHT to 50A.

Currently IG @ 4.8-5 Torr. 

Initiated auto-ramping:  setting: Good Vac = 3e-5 Torr, Bad Vac = 4.0e-5 Torr. 


 Thursday, June 20, 2013, 06:21

About 10 min ago, Evap tripped off due to high vacuum. 

Vacuum came back down below the trip limit and both TGHT/TBHT p/s were stepped down to 40A and turned back on.

Changed auto ramping rate to 05A/120min.  

The process continues...  (And I'm going back to sleep!) 


 Friday, June 21, 2013, 15:19

Vacuum is close to the trip limit. 

Change the ramping rate to 0.2A/120min. 


 Monday, June 24, 2013, 17:04

Organic burnt out is complete and vacuum has come down to ~9.0e-6 Torr.

Increase ramping rate to 0.2A/60min - The sintering process should take about another 2 days if everything goes smoothly. 


 Wednesday, June 26, 2013, 17:29

TGHT & TBHT have reached to 820A and 300A, respectively, for 4 hours.

Vacuum is at 9e-7 Torr. 

Cooling down is in progress, at a rate of 1.0A/min for TGHT and 0.5A/min for TBHT.

The target will be ready to come out by tomorrow.


 Thursday, June 27, 2013, 11:02

TGHT/TBHT reached to 0A.  Vacuum is leveled at 1.2e-7 Torr. 

Chamber will be vented in air soon.


 

 

Entry  Tuesday, May 28, 2013, 17:50, John Wong, , Target Boat #2 , , Done, Sintering TaC coated end caps 

Tuesday, May 28, 2013, 17:36

The target containers endcaps were coated with TaC solution and let dry. 

Each cap is wrapped with a small piece of graphite foil and inserted in the target boat.

The chamber is currently being pumped down. 

The HS cooling water valve will be opened tomorrow; any leak will be inspected.

When the vacuum is good,  TGHT will be ramped up to 580A. 


 Wednesday, May 29, 2013, 17:06

HS water valve was opened early this morning; no leaks were detected.

TGHT has stepped up to 50A.  IG is currently at 2.0e-6Torr. 

Initiated auto-ramping at 1.0A/min.


 Thursday, May 30, 2013, 11:12

TGHT reached to 580.  The end caps have been heated at that current for more than 7 hrs.

IG is coming down, currently at 8e-7 Torr.

Auto-cooling initiated, ramping down at 2A/min .


 

Entry  Tuesday, May 14, 2013, 17:15, John Wong, Empty, 38481-6, HP-FEBIAD, Done, SinteringTaC coating 

Tuesday, May 14, 2013, 17:04

Target oven is coated with TaC, and wrapped with 3-Ta heat shields.

TGHT and TBHT will be ramped up to 820A and 300A, respectively.

Ramping rate set to 1A/min.

Good Vac at 3.e-5 Torr, Bad Vac @ 4.0e-5 Torr.

Chamber is currently being pumped...


 Wednesday, May 15, 2013, 10:56

Chamber has pumped down to 4.5e-7 Torr. 

HS cooling water valves opened; no leaks were detected.

Stepping up TGHT/TBHT to 80A; monitoring vacuum.


 Wednesday, May 15, 2013, 11:26

Pressure is increasing.  TGHT setpoint @ 80A, readback @ 88.6A/0.603V, local @ 83A/0.80V.


 Wednesday, May 15, 2013, 12:08

TGHT/TBHT stepped up to 140A and tripped off at high limit vacuum.

Restarted p/s and set TBHT/TGHT at 100A

Initiated auto ramping...


 Friday, May 17, 2013, 11:39

TGHT and TBHT reached to 820A and 300A, respectively.  Target has been heating at the max currents for ~12hrs. 

Vacuum is coming down to 4.3e-7 Torr. 

The TaC coating sintering is completed.

Autocooling is initiated.  TGHT ramping rate @ 2A/min, and 1A/min for TBHT.


Wednesday, May 22, 2013, 10:43

Sintering complete.

Chamber will be vented


 

Entry  Tuesday, May 07, 2013, 16:53, Nikita Bernier, BeO, , , Done, Sintering BeO pellets #6 

 Tuesday, May 07, 2013, 16:48

 

5 BeO pellets were made.  Each weights about 1.3 g (including org mass). 

A piece of Re foil (0.002" thick) is used as the under layer to protect the reaction between Be(g) and the Ta-boat.  (see Pictures)

Another layer of Ta-foil is used as the heat-shield to wrap around the Ta-boat.

The chamber was pumped down. 

TGHT will be ramped up to 600 A (~1360°C) at 0.2 A/min. The vacuum limit parameter was set for good vacuum at < 3.0e-5 Torr and bad vacuum at > 4.0e0-5 Torr.

The pressure, voltage and current will be closely monitored. 

If the Ta-boat survives, the TGHT will continue to ramp up to max 800 A (~1580°C).

 

    Reply  Monday, May 13, 2013, 12:53, Nikita Bernier, BeO, , , Done, Sintering BeO pellets #6 600Down.png

Nikita Bernier wrote:

 Tuesday, May 07, 2013, 16:48

 

5 BeO pellets were made.  Each weights about 1.3 g (including org mass). 

A piece of Re foil (0.002" thick) is used as the under layer to protect the reaction between Be(g) and the Ta-boat.  (see Attachments)

Another layer of Ta-foil is used as the heat-shield to wrap around the Ta-boat.

The chamber was pumped down. 

TGHT will be ramped up to 600 A (~1360°C) at 0.2 A/min. The vacuum limit parameter was set for good vacuum at < 3.0e-5 Torr and bad vacuum at > 4.0e0-5 Torr.

The pressure, voltage and current will be closely monitored. 

If the Ta-boat survives, the TGHT will continue to ramp up to max 800 A (~1580°C).

 

 Monday, May 13, 2013, 12:48

 

TGHT has been at 600 A for about 13 hours with stable very low vacuum (10^-7). See Attachment #1.

Temperature measurement has been lost on Saturday. Last measurement was was above 1350°C, at around 480 A.

TGHT was ramped down at 1 A/min.

The chamber will be vented later today. The pellets and the thermocouples will be inspected.


 

 

       Reply  Monday, May 13, 2013, 17:17, Nikita Bernier, BeO, , , Done, Sintering BeO pellets #6 

Nikita Bernier wrote:

Nikita Bernier wrote:

 Tuesday, May 07, 2013, 16:48

 

5 BeO pellets were made.  Each weights about 1.3 g (including org mass). 

A piece of Re foil (0.002" thick) is used as the under layer to protect the reaction between Be(g) and the Ta-boat.  (see Attachments)

Another layer of Ta-foil is used as the heat-shield to wrap around the Ta-boat.

The chamber was pumped down. 

TGHT will be ramped up to 600 A (~1360°C) at 0.2 A/min. The vacuum limit parameter was set for good vacuum at < 3.0e-5 Torr and bad vacuum at > 4.0e0-5 Torr.

The pressure, voltage and current will be closely monitored. 

If the Ta-boat survives, the TGHT will continue to ramp up to max 800 A (~1580°C).

 

 Monday, May 13, 2013, 12:48

 

TGHT has been at 600 A for about 13 hours with stable very low vacuum (10^-7). See Attachment #1.

Temperature measurement has been lost on Saturday. Last measurement was was above 1350°C, at around 480 A.

TGHT was ramped down at 1 A/min.

The chamber will be vented later today. The pellets and the thermocouples will be inspected.


 

 

 Monday, May 13, 2013, 17:21

 

The following table shows the characteristics of the pellets after sintering at 600 A for 13 hours.

Sample,   Mass (g),   Thickness (mm),   Density (g/cm3),    Diameter (mm)

 

1    0.8904 4.875 1.364 13.058

2    0.8991 4.744 1.396 13.148

3    0.8846 4.579 1.482 12.884

4    0.9142 4.981 1.254 13.650

5    0.9022 4.978 1.250 13.586

Avg 0.8981 4.831 1.345 13.265

 

 
All pellets are rugged and slightly greyish. They will be sintered up to 800 A when the thermocouples get replaced.
 
 

 

 

 

 

 

Entry  Tuesday, April 30, 2013, 11:20, Anders Mjos, Empty, 38481-5, HP-FEBIAD, Done, CTL thermal test StripTool_2013-05-02.pngCTL_ITD0431_Evap2.pdf2013-04-30_Evap2_ITD0431_CTL_Thermal_Test.pdf

 CTL block on T/C F/T Ch 1
Supply on Ch 3
HS Return on Ch 4

Tuesday, April 30, 2013, 11:20: Roughing

Tuesday, April 30, 2013, 11:45: Turbo started


Wednesday, May 01, 2013, 08:43: Cooling water opened. Vacuum stable at 5.1E-7 T (IGP1)

Wednesday, May 01, 2013, 08:48: Ramping TGHT and TBHT to 850A and 300A at 1A/60s


Thursday, May 02, 2013, 09:10: TGHT reached voltage limit (12V) at ~780A yesterday at ~10pm. Increased limit to 12.5V and continued auto ramping. CTL block temp ~80C

Thursday, May 02, 2013, 10:08: TGHT voltage limit changed to 13V. TGHT:RDCUR goes to ~810A with TGHT:RDVOL at 12.5V. CTL block temp ~80C

Thursday, May 02, 2013, 11:33: TGHT manually stepped to 850A RDCUR at 846A, RDVOL at 13.1V. CTL block temp ~84C

Thursday, May 02, 2013, 15:13: Ramping down TGHT and TBHT to 580A and 280A at 2A/min and 1A/min


Friday, May 03, 2013, 08:30:  TGHT and TBHT at 580A and 280A. CTL block temp ~60C 

Friday, May 03, 2013, 08:37: Ramping down TGHT and TBHT to 0 at 2/min and 1A/min

Friday, May 03, 2013, 11:04: T/C logger removed


Monday, May 06, 2013, 09:37: Turbo stopped.

Monday, May 06, 2013, 10:26: Venting

Entry  Friday, April 19, 2013, 15:27, Anders Mjos, Empty, 38481-4, HP-FEBIAD, Done, CTL test 

Target installed with 4 T/C

The target assembly is ITD0300 with the CTL Cu cooling block slightly modified.

Ch1 - CTL cooling block T/C feedtrough
Ch2 - Heat shield below left gripper arm - T/C feedthrough
Ch3 - Heat shield below left gripper arm - 9 pin connector
Ch4 - Target left side leg on tube - 9 pin connector

Friday, April 19, 2013, 15:23: Roughing

Friday, April 19, 2013, 15:41: Started turbo


Monday, April 22, 2013, 09:43: Opened water supply. Vacuum stable at 2.8E-7 T (IGP1)

    Reply  Monday, April 22, 2013, 18:49, John Wong, Empty, 38481-4, HP-FEBIAD, Done, CTL test 

Anders Mjos wrote:

Target installed with 4 T/C

The target assembly is ITD0300 with the CTL Cu cooling block slightly modified.

Ch1 - CTL cooling block T/C feedtrough
Ch2 - Heat shield below left gripper arm - T/C feedthrough
Ch3 - Heat shield below left gripper arm - 9 pin connector
Ch4 - Target left side leg on tube - 9 pin connector

Friday, April 19, 2013, 15:23: Roughing

Friday, April 19, 2013, 15:41: Started turbo


Monday, April 22, 2013, 09:43: Opened water supply. Vacuum stable at 2.8E-7 T (IGP1)

Monday, April 22, 2013, 18:48

Ramping TGHT/TBHT to 850A/300A at 1A/min.


 

       Reply  Tuesday, April 23, 2013, 10:11, Anders Mjos, Empty, 38481-4, HP-FEBIAD, Done, CTL test 2013-04-23_Evap2_ITD0300_CTL_Thermal_Test.xlsxCTL_ITD0300_Evap2.pdfDeformed_Ionizer_Tube.jpg

 

John Wong wrote:

 

Anders Mjos wrote:

Target installed with 4 T/C

The target assembly is ITD0300 with the CTL Cu cooling block slightly modified.

Ch1 - CTL cooling block T/C feedtrough
Ch2 - Heat shield below left gripper arm - T/C feedthrough
Ch3 - Heat shield below left gripper arm - 9 pin connector
Ch4 - Target left side leg on tube - 9 pin connector

Friday, April 19, 2013, 15:23: Roughing

Friday, April 19, 2013, 15:41: Started turbo


Monday, April 22, 2013, 09:43: Opened water supply. Vacuum stable at 2.8E-7 T (IGP1)

 

Monday, April 22, 2013, 18:48

Ramping TGHT/TBHT to 850A/300A at 1A/min.


 

 

Tuesd ay, April 23, 2013, 10:07

TBHT / TGHT: 820A / 300A

TGHT:RDCUR: 816.6A
TBHT:RDCRU: 303.5A

Local P/S displays
TGHT: 821A / 11.05V
TBHT: 307A / 4.37V

Tuesday, April 23, 2013, 10:45: Ramping down TBHT to 0A @ 5A/min

Tuesday, April 23, 2013, 12:49: Ramping down TGHT to 0A @ 5A/min

Tuesday, April 23, 2013, 15:52: Swithced off TGHT and TBHT P/S. TGHT P/S showed 30A read back value, while local value was 0A


 Wednesday, April 24, 2013, 09:53: Turbo stopped

Wednesday, April 24, 2013, 12:00: Target removed 


The ionizer tube was found to have deformed as seen in the attached photo.

Entry  Friday, April 19, 2013, 09:39, Rick Maharaj, Empty, , , Done, thermocouple Feedthru 

 A thermocouple feedthru was installed via 9 pin sub-D connector. It runs from the the conflat cross on the top of the evaporator to the upper 9 pin connector of the target mounting plate.

Entry  Thursday, April 11, 2013, 14:20, John Wong, Empty, 39165-6, LP-SIS, Done, Coating target oven /w TaC & sintering for UCx#6 

Monday, April 08, 2013, 17:39

Target container is coated with TaC; the container will be used for the UCx#6 target. 

No Ta-heat shields are used.

For the sintering process:

TGHT will be ramped up to 580A at 0.2A/min

TBHT will be ramped up to 230A at 0.2A/min

Chamber has been pumped down.  HS cooling H2O valve opened; no leaks have detected.


Thursday, April 11, 2013, 14:35 

Target and tube heaters have reached to optimum.

Auto-cooling initiated...


 Friday, April 12, 2013, 11:17

P/S off.  Chamber vented. 

Done!


 

Entry  Thursday, March 14, 2013, 12:27, Anders Mjos, Empty, 38481-4, HP-FEBIAD, Done, CTL thermal test 3 (w/o CTL block) 2013-03-13_-_FEBIAD-HP-A_TargetLeg_and_HeatShield_TC.pdf2013-03-13_-_FEBIAD-HP-A_TargetLeg_and_HeatShield_TC.xlsx

Thursday, March 12, 2013 

The CTL was removed and target heated to 580A / 300A

T1: Left target leg close to tube
T2: Heat Shield above CTL
T3: Heat Shield cooling water Supply
T4: Heat Shield cooling water Return


Thursday, March 13, 2013  

The target was cooled down 


Results attached as PDF and Excel

Entry  Wednesday, March 13, 2013, 16:08, Anders Mjos, Empty, 38481-4, HP-FEBIAD, Done, Thermal test HP-FEBIAD-A_TC_at_fins.pdf

Wednesday, March 13, 2013 

Thermocouple channels (see attached PDF for photos)
T1 - Left target leg at tube
T2 - Between cooling fins close to tube, left side
T3 - Supply water HS
T4 - Return water HS


Friday, March 22, 2013

Test not conducted. Target removed.

Entry  Wednesday, March 06, 2013, 10:41, Anders Mjos, Empty, 38481-4, HP-FEBIAD, Done, CTL thermal test CTL_1st_Assebmly_Thermal_Test_Evap2.pdf2013-03-08_Evap2_First_Thermal_Test.pdf

Wednesday, March 06, 2013

The Cool Transfer Line (CTL) test target is installed for thermal tests. Drawing number is ITD0431 REV A.

Thermocouple channels are as follows:

T1: Cu block on CTL
T2: Heat Shield above CTL
T3: Heat Shield cooling water Supply
T4: Heat Shield cooling water Return

Cooling water is in Evap2 supplied to the cooling line that goes directly to the area on the Heat Shield above the CTL.

Test results attached.
 

    Reply  Wednesday, March 06, 2013, 17:53, John Wong, Empty, 38481-4, HP-FEBIAD, Done, CTL thermal test rampingup_1.PNGrampingup_2.PNGautorampingdown_23.PNG

Anders Mjos wrote:

Wednesday, March 06, 2013

The Cool Transfer Line (CTL) test target is installed for thermal tests. Drawing number is ITD0431 REV A.

Thermocouple channels are as follows:

T1: Cu block on CTL
T2: Heat Shield above CTL
T3: Heat Shield cooling water Supply
T4: Heat Shield cooling water Return

Cooling water is in Evap2 supplied to the cooling line that goes directly to the area on the Heat Shield above the CTL.
 

 Wednesday, March 06, 2013, 17:23

The target has been pumping down to 5.3 e-7 Torr.  On the RGA mass scan, mainly H2O (mass 18 + constituents) was detected at ~2.7pA (see attachment #1).

The target will be heated up: TGHT = 850A (rate @ 1A/min); TBHT = 300A (rate @ 1A/min).


 Thursday, March 07, 2013, 11:51

TGHT and TBHT reached to 850A (local, 845A\13.80V) and 300A, respectively.  The out gassing of CO (mass 28) reached to ~5pA at the max currents.  (see attachment #2) 

 TBHT will be ramped down to 0A to compare the temperatures.  


 Thursday, March 07, 2013, 15:55

TBHT at 0A.  See attachment#3 for the temperatures and RGA data before further ramping down the TGHT.


 

    Reply  Monday, March 11, 2013, 12:23, Anders Mjos, Empty, 38481-4, HP-FEBIAD, Done, CTL thermal test 2 2013-03-11_Evap2_Second_Thermal_Test.pdf

 

Anders Mjos wrote:

Wednesday, March 06, 2013

The Cool Transfer Line (CTL) test target is installed for thermal tests. Drawing number is ITD0431 REV A.

Thermocouple channels are as follows:

T1: Cu block on CTL
T2: Heat Shield above CTL
T3: Heat Shield cooling water Supply
T4: Heat Shield cooling water Return

Cooling water is in Evap2 supplied to the cooling line that goes directly to the area on the Heat Shield above the CTL.
 

 

Monday, March 11, 2013

The CTL test target was installed again for a second thermal test. CTL block fastened to HS with 1 in lbs. A small piece of Ta-foil of 0.001" thickness was used between the CTL Cu-block and the Ta transfer line to reduce the heat transfer..

Thermocouples were re-attached to CTL and Heat Shield (see above for channels #s).

See attached graph (PDF) for details.

       Reply  Monday, March 11, 2013, 15:59, John Wong, Empty, 38481-4, HP-FEBIAD, Done, CTL thermal test 2 autorampingup_110.PNG

Anders Mjos wrote:

Anders Mjos wrote:

Wednesday, March 06, 2013

The Cool Transfer Line (CTL) test target is installed for thermal tests. Drawing number is ITD0431 REV A.

Thermocouple channels are as follows:

T1: Cu block on CTL
T2: Heat Shield above CTL
T3: Heat Shield cooling water Supply
T4: Heat Shield cooling water Return

Cooling water is in Evap2 supplied to the cooling line that goes directly to the area on the Heat Shield above the CTL.
 

Monday, March 11, 2013

The CTL test target was installed again for a second thermal test. CTL block fastened to HS with 1 in lbs. A small piece of Ta-foil of 0.001" thickness was used between the CTL Cu-block and the Ta transfer line to reduce the heat transfer..

Thermocouples were re-attached to CTL and Heat Shield (see above for channels #s).

 Monday, March 11, 2013, 15:55

Chamber was pumped down to 2 e-7 Torr.  HS water valve opened and no leaks were detected.  

TGHT and TBHT are ramping up to 850A and 300A at 2A/min, respectively.  

RGA is running... 


Tuesday, March 12, 2013, 10:44  

TGHT/TBHT reached to max currents. 

See attachment #1 for temperature and RGA measurements. 

Cooling down in process... 5A/min. 


 

Entry  Monday, March 04, 2013, 17:41, John Wong, Empty, LP-SIS RFQ ver 2.0, , , Testing LPSIS RFQ ver 2.0 

 Monday, March 04, 2013, 17:39

This is the 2nd modified target container for RFQ LPSIS.  The container will be heated up to 650A TGHT and 150A on TBHT.  No Ta-heat shield is being used.  

Heating rate at 1A/min for both TGHT & TBHT.  Once the target is at the currents, TBHT will be further ramped up to 300A.  

Temperatures are being measured by two thermocouples (one on RFQ component and the other on the Cu heat-shield).  

Gases are being analyzed using the RGA. 


 

Entry  Friday, February 22, 2013, 15:55, John Wong, SiC, , LP-SIS, Done, Sintering SiC#28-RFQ RFQ_SiC#28_-production_process.mp4

Friday, February 22, 2013, 15:49

The LP-SIS RFQ target container was previously coated with TaC and sintered up to ~1500C (TGHT @ 600A, TBHT @ 300A). 

The container is loaded with 325 discs of SiC, a total of 10.9cm in length. 

For this process,

TGHT will be ramped up to 600A and at the same time TBHT will go up to 300A.  No Ta-heat shield is used. 

The ramping rate is set to 0.2A/min.

The chamber is currently being pumped down. 


 Friday, March 01, 2013, 15:57

The target was further heated up to 650A TGHT and 300A TBHT for 4 hours yesterday; then it was cooled down.  

Some reactions on the target end (where the D-cap inserted) was observed.  

Yellow crystals on the D-cap was formed, just as we have seen before.  

Overall, the target looks good!  

See attachment#2 for the target production. 

More about the gasses analyst from the RGA later...  


 

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