Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 90 of 140  Not logged in ELOG logo
Entry  Monday, April 20, 2015, 07:27, David Wang, ITE, Standard Operation, TM4, , Target Hall Scheduled Activities April 07 - June 26 2015 Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mppTarget_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mpp

Weekly target hall schedule update.2015-04-20

weekly target hall schedule update 2015-04-27 attachments 3,4.

Entry  Tuesday, April 21, 2015, 13:01, Grant Minor, ITW, Development, TM2, , TM2 MK4 Optics Tray - banana plug bore modification (on bench) ita6092_redlines_gminor_21apr2015.pdfTM2_Optics_Tray_Bore_Mod_21Apr2015_1.JPGTM2_Optics_Tray_Bore_Mod_21Apr2015_2.JPGTM2_Optics_Tray_Bore_Mod_21Apr2015_3.JPG

The MK4 optics tray prepared for TM2 (as per ITA6082) had an undersized bore for the banana plug, making insertion of the plug extremely difficult / impossible.

Reference stores parts were collected to check the fit:  male plug 3-4/01152 and female jack 1-6/1201.  The size of the female jack was checked with a #21 drill at .159".

The bore on the optics tray was drilled out dry using the #21 drill to the same depth as the original blind hole, by Maico and Dan McDonald.  Chips were carefully collected in a rag, and the hole was blown out with compressed air.

The fit was checked to be snug but possible, using the male plug and the Remote Handling ultem base (ref ITA6023).

Redlines and photos are attached.

 

Entry  Wednesday, April 22, 2015, 11:05, David Wang, Conditioning Station, Standard Operation, TM1, , electrical check on TM1 at CS under vacuum 

I did an electrical check on TM1 at CS. The resistance check:A-B 3.918m ohm, A-C 5.905m ohm,A-D 4.070m ohm,B-C5.462m ohm,B-D3.633m ohm. They are very close to the check we did in SHC. The only unusual thing I found during the check is the ohmmeter reading between A and 60 KV common (6.2K )and the Megga reading between them  at 250 V which is 0. I repeated 4 times and always got the same readings. However, after so many times check, the Megga reading between A and 60KV   suddenly went back to normal(300 M at 250V) at the final check.  And,it stays at 300M now.  All other measurements are same as we did at SHC before.         

Entry  Thursday, April 23, 2015, 12:56, Anders Mjos, Conditioning Station, Maintenance, TM1, , IG1 Good Vacuum limit changed IG1GoodVacuum.png

Changed by Dave Morris. 

New value is 1E-5 T (old value was 7.09E-5 T)

Entry  Monday, April 27, 2015, 16:12, Keith C Ng, South Hot-Cell, Development, TM2, , Ceramic Standoffs in TM2 source tray steerer assembly IMG_3106.JPG

On drawing ITA6008 for the Encole 0.5" ceramic standoffs there is a note to match pairs of ceramics to within +/-0.001". This step was missed on the current build of TM2 source tray (ceramics were not measured).

Measured the lengths of the rest of the ceramic standoffs in inventory and they range from 0.5035" to 0.4950" in length. The ceramics have been sorted by length and grouped into bags.

 IMG_3106.JPG

Entry  Monday, April 27, 2015, 17:09, Grant Minor, ITE, Development, TM2, , TM2 - New Source Tray - Water Block Seal Groove Inspection Report IMG_1859.JPGTM2_New_Source_Tray_Water_Block_Inspection_Results_24_April_2015.pdfTM2_water_block_inspect_24Apr2015.pdfTM2_New_Source_Tray_Water_Block_Inspection_Results_April_2015.xlsx

The water blocks soldered to the TM2 cooling lines (see Ref. Assy. ITA6144) were inspected.

See attached inspection reports and drawings.

It was found that only 18% of the seal groove diameters and 55% of the depths were in spec.

The source tray must be tested on the test stand with c-seals to ensure that these blocks will seal properly on the module.

Entry  Tuesday, April 28, 2015, 11:09, Anders Mjos, ITW, Maintenance, , , Resistance measured of TGHT and TBHT lines to ITW Resistance_from_Electrical_Room_to_Target_Station.xlsx

The new TBHT and TGHT power supplies were brough up to high current; 350 A and 420 A respectively. The TGHT power supply was limited by PLC to 420 A. The resistance calculated for both the TBHT and TGHT copper lines from the electrical services room to the ITW pit was 1.35 mOhm. See attached spreadsheet for details.

Dave Morris has been contacted to correct the current limit for the TGHT supply to 600 A.

Entry  Friday, May 01, 2015, 08:27, chad fisher, South Hot-Cell, Repair, TM2, , Containment Box Removal 

Containment box has been removed in preparation for wire replacement.

Entry  Friday, May 01, 2015, 13:48, David Wang, South Hot-Cell, Standard Operation, TM2, , Target Hall Scheduled Activities April 07 - June 26 2015 update Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mppTarget_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf

Target Hall Scheduled Activities  April 07 - June 26  2015 update.      2015-05-01. All TH scheduled jobs are finished on time this week.

Entry  Monday, May 04, 2015, 13:32, Anders Mjos, Conditioning Station, Maintenance, , , TK2 expansion tank topped up 

Caled cyclotron ops to open P23 and confirmed penthouse valve open.

Filled up TK2 to 21 in water leve.

Entry  Tuesday, May 05, 2015, 10:57, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Wiring TM2_New_Wiring_20150504_13.jpgTM2_Wiring_20150505_10.jpg

Old wiring was removed yesterday, new wiring run thru the vacuum chase. Old IMG gauge removed today, new cable trays installed and wires installed into cable trays.

Entry  Monday, May 11, 2015, 10:45, Anders Mjos, Conditioning Station, Maintenance, , , RGA electronics box installed 2015-05_RGA_GND_connection.pdf

 The communications chip has been replaced. The electronics box has been grounded (see attached pdf).

Entry  Monday, May 11, 2015, 11:20, David Wang, South Hot-Cell, Standard Operation, TM2, , Target Hall Scheduled Activities April 07 - June 26 2015 6x

The schedule has some changes due to  new TM2 source tray coil cooling line leaking at test stand. Now,It is re-scheduled in such an estimation  that TM2 source tray could be ready at teat stand by this Friday(May-15th). see attachment 1,2.

2015-05-12,  Changed  and updated the TH activity schedule according to Dons new beam schedule which is re-arranged after the coil line leaking issue. See attachments 3,4. No major conflicts has been found on the new schedule.

2015-05 25, Updated the TH activity schedule according to present TM2 job processing. See attachment 5,6.

Entry  Wednesday, May 13, 2015, 13:55, chad fisher, South Hot-Cell, Repair, TM2, , Shutter removal TM2_20150513_131339.jpgTM2_20150513_134232.jpg

TM2 has been successfully de-shuttered.

All went pretty much according to plan except I had to remove one fastener out of the upper wiring harness (the one that has just been installed) to allow for enough clearance to rotated the shutter guide out of the way...I shutter to think what would have happened otherwise...anyways...

Close inspection of the shutter does show that the "thin" area isn't in very good shape; whether this is a result of removal or just the way it was is hard.Due to the ease of removal I would quess that it may have been a preexisting condition. That being said...I think we may want to consider replacing it.

 

Entry  Tuesday, May 26, 2015, 11:49, Grant Minor, Assembly/Bench Test, Repair, TM2, , TM2 New Source Tray - Braze & Solder Report - 22 May 2015 6x

Hello,

For reference, I have attached a list of all solder joints in the TM2 Source Tray, and the alloys used for the most recent build (as per ITA6144).   I have also provided data sheets for the alloys, and PDF copies of all the drawings calling out the joints.

Certanium 34 C (222 deg C melt point) was used for all low-temperature solder applications, except for the steel inserts in the water blocks.  Previous revisions of the Source Tray drawings called out a higher-temperature McMaster lead-based solder (304 deg C melt point).  The change to Certanium 34 C on the prints was made in Bevan's era, during the transitional update of the source tray drawings between the TM1 and TM3 source tray projects, just before I took over updating the drawing packages.  I believe Bevan made this change on general advice from Guy Stanford, who stated that Certanium 34 C is a much easier solder to work with and makes a more mechanically reliable joint.  However, the change really should have had more review and validation testing before being implemented.

This said, we now have a source tray that uses Certanium 34 C, and rework of every joint would set us back too far in the schedule to meet the deadline, so we will have to run with it as it is.

Of particular concern are the joints on the target oven and coil heating blocks, which are now using a lower temperature solder (222 deg C melt vs 304 deg C melt).  We have experienced a coil block failure on TM4 due to a failed solder joint, although the failure mode is not known for certain.  We also had two recent failures on the test stand of a coil joint soldered with Certanium 34 C, but this was due to an error in the connection of cooling water to the joints (i.e. the joints had no coolant flow and the solder melted... this is expected!).

Anders and I have performed independent thermal analysis on the joints due to the radiative and electric heating from the target, and have concluded that even with a lower temperature solder, there is a lot of margin, so the risk seems to be low.  This work will be published in a separate report to be circulated later.

Thank you and regards,

Grant

Entry  Tuesday, May 26, 2015, 14:34, chad fisher, South Hot-Cell, Repair, TM2, , Shutter replacement Shutter.jpg

The shutter in TM2 was successfully replaced today.

New lock washer and nut were installed onto shutter and nut torqued to 120 ft lbs.

Shutter guide alignment tool was used to insure tapped shutter guide holes were concentric with thru holes in shutter side mounting panel, button head screws replaced and torqued to 110 ft-lbs.

The shutter was manually cycled open and closed by David and everything is to operate well.

Entry  Wednesday, May 27, 2015, 08:57, Travis Cave, Conditioning Station, Standard Operation, TM2, , Module moved 

TM#2 with no source tray has been moved from the south hot cell to the conditioning station.

Entry  Tuesday, June 02, 2015, 06:51, David Wang, South Hot-Cell, Standard Operation, TM4, , Target Hall Scheduled Activities April 07 - June 26 2015 Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mppTarget_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf

Target Hall schedule weekly update. All jobs are finished on time so far.

Entry  Tuesday, June 02, 2015, 14:38, David Wang, Conditioning Station, Repair, TM4, , replace broken TM4 IG1 002.JPG006.JPG

 TM4 IG1 filament was broken during last run  at ITE.  The broken filament is replaced with a new one today when TM4 is located at CS.

2015-06-03 , Leak checked the new 25 conflat gasket today. No leak. See attachments

Entry  Wednesday, June 03, 2015, 11:22, David Wang, Conditioning Station, Standard Operation, , , Target Hall Scheduled Activities April 07 - July 21 2015 Target_Hall_Scheduled_Activities__Apr_07_to_July_21__2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.mppTarget_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.mpp

I revised the Target Hall schedule to July 21 2015. It is the time new TM2 with ZrC target started at ITW.

2015-06-04, Updated the schedule with   new PDF view. See attachments 3, 4

ELOG V2.9.2-2455