Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 131 of 141  Not logged in ELOG logo
ID Date Authordown Category Type Module Target/Number Subject
  1584   Monday, July 17, 2017, 16:28 Anders MjosConditioning StationDevelopmentTM3No targetConditioning TM3

50 kV stable with less than 1 spark/h during the weekend by RIB obs.

Today 57 kV reached, but observed sparking on the resistors of the new HV cable. The cable will be removed to take out the resistors, before reinstalling it.

The target hall was locked out, but has now been reopened. This was to avoid sparking to the HV cover.

Attachment 1: TM3_HV_conditioning_2017-07-17.docx
  1587   Tuesday, July 18, 2017, 16:53 Anders MjosConditioning StationDevelopmentTM3No targetConditioning TM3

Conditioning continues today with resistors removed from the HV cable

Tuesday, July 18, 2017, 16:53: BIAS / EZL 50 / 25 kV - no sparks

 Tuesday, July 18, 2017, 16:56: BIAS / EZL 55 / 27.5 kV - one spark


TM3 remained at 55 kV over night. Turbo pumps tripped twice and was restarted and HV recovered by RIB ops. Last recovery brought EZL to 16 kV (not 27.5 kV)

About 25 sparks over 15 h. No sparks for the last 3 h

Wednesday, July 19, 2017, 08:12: EZL to 27.5 kV

Wednesday, July 19, 2017, 08:38: BIAS to 57 kV

Wednesday, July 19, 2017, 08:46: BIAS to 57.5 kV

Wednesday, July 19, 2017, 09:05: BIAS to 59 kV

Wednesday, July 19, 2017, 09:19: BIAS to 60 kV

Wednesday, July 19, 2017, 09:28: EZL to 30 kV

Wednesday, July 19, 2017, 12:25: Heavy sparking. Lowered BIAS to 30 kV

Wednesday, July 19, 2017, 12:37: Increased BIAS again towards 50 kV, but heavy sparking again between 45 and 50 kV. Lowered back to 30 kV

Wednesday, July 19, 2017, 12:40: BIAS at 46 kV

Wednesday, July 19, 2017, 12:42: BIAS at 47 kV

Wednesday, July 19, 2017, 12:44: BIAS at 48 kV

Wednesday, July 19, 2017, 12:48: BIAS at 50 kV

Wednesday, July 19, 2017, 14:50: BIAS at 55 kV after ~2h without sparking at 50 kV

Wednesday, July 19, 2017, 15:12: Sparking. Lowered to 40 kV

Wednesday, July 19, 2017, 16:39: BIAS at 55 kV


Friday, July 21, 2017

Observed top of module inside target hall during HV sparks using crane cameras. No sparks observed, but some faint sound could be heard. Module still sparks at 60 and 55 kV. Have to lower to 40 kV to stop sparking.

Friday, July 21, 2017, 13:25: BIAS / EZL at 50 / 25 kV for without sparking for the last 90 min

  1594   Thursday, August 03, 2017, 17:08 Anders MjosConditioning StationRepairTM2 Power bump

 Thursday, August 03, 2017, 17:08: Restarting vacuum and water system

  1597   Tuesday, August 15, 2017, 09:27 Anders MjosSouth Hot-CellStandard OperationTM2SiC#36Electrical Check of target in SHC

Travis Cave wrote:

The electrical check of TM#2 with SiC#36 attached. Post beam at the south hot cell. See attached results allow the before beam electrical check results are posted here as well.

by David and Chad after target removed from module:

Anode to target @500V - 65Kohm
Anode to HS - dead short
Target to HS@500V -62Kohm.

  1598   Tuesday, August 15, 2017, 09:30 Anders MjosITWStandard OperationTM2Ta#53TM2 radiation fields

Travis Cave wrote:

TM#2 with Ta#53 has been moved from the conditioning station to the west target station.

 by Travis (measured at ~ 2' from module on service tray side):

at 3' 325 uSv/h

at 2' 640 uSv/h

  1601   Friday, August 25, 2017, 16:33 Anders MjosConditioning StationRepair  Testing HV after cooling line repair

 The BIAS voltage was brought up to 70 kV today and held there for 1h. No sparking observed.

Attachment 1: 2017-08-25_HV_Water_Line_Test.xlsx
  1622   Thursday, September 21, 2017, 16:26 Anders MjosSouth Hot-CellStandard OperationTM2 Inspection of Source Tray

Chad and Anders inspected the Source Tray today using the camera in the hot cell. A dark spot was observed on one of the four insulators separating the Extraction Electrode from the Ground Electrode. This could potentially influence the high leakage current. Some discolored areas were also observed in the Service Tray, but these was present when the module was built. See attachment for details.

Attachment 1: TM2_Source_Tray_EE_Insulator.pdf
TM2_Source_Tray_EE_Insulator.pdf TM2_Source_Tray_EE_Insulator.pdf
  1631   Thursday, September 28, 2017, 15:34 Anders MjosConditioning StationDevelopmentTM2 Changes to MP3 startup

 Due to problems with the regulating valve WPV1, the VFD (Variable Frequency Drive) for the pump has been programmed to do a slow (2 min) ramp up. WPV1 has been bypassed and left fully opened. Work was done by Dave Morris

  1632   Thursday, September 28, 2017, 17:44 Anders MjosConditioning StationStandard OperationTM2Ta#54Conditioning Ta#54

Thursday, September 28, 2017

Cooling water not yet connected to TM.

High leakage current still observed. 200 uA at 22 kV. Did not go past 25 kV. 


Friday, September 29, 2017, 14:05: Started heater ramping to 580 / 200 A at 1 A/min

Friday, September 29, 2017, 14:09: BIAS / EZL / EE at 20 / 10 / 1.5 kV. BIAS current at 90 uA


Monday, October 02, 2017, 10:29: Accidentally set BIAS current limit to 0 A (step size too large) at 28 kV. This also caused the TGHT to got to 0 A. Recovered to 580 A in 10 - 15 s.

Monday, October 02, 2017, 12:07: Ramping down heaters at 2 A / min

Attachment 1: Ta#54.docx
Attachment 2: Ta#54_BIAS_current_vs_voltage.xlsx
  1634   Thursday, October 05, 2017, 11:04 Anders MjosITWMaintenance  Installation of new valve for module move ventilation

David installed the new ball valve and connections for the SAS project module move ventilation. SASP0482. Drawing reference ISK5029B.

  1637   Friday, October 06, 2017, 13:25 Anders MjosConditioning StationRepair  HV Test

 HV was brought up to 70 kV for 1 h without sparks to test the new water installation.

Attachment 1: 2017-10-06_HV_Water_Line_Test.xlsx
  1646   Wednesday, October 18, 2017, 14:54 Anders MjosAssembly/Bench TestStandard Operation  Source tray assembly electrical check

Source tray meggered today by Anders and Keith

GND - MSP OL @ 1000V
MSP - EE OL @ 1000V
EE - GND OL @ 1000V
4x Steerers - GND OL @ 500V

Steerer continuity verified from socket to steerer plates
(looking in the direction of the RIB, labeled top to bottom on sockets)

1 - Top
2 - Left
3 - Right
4 - Bottom

Attachment 1: Steerer_Connections_2017-10-18.pdf
Steerer_Connections_2017-10-18.pdf
  1648   Thursday, October 19, 2017, 14:20 Anders MjosAssembly/Bench TestStandard Operation  Source tray inspection

 Two minor chips in the main 60 kV insulators on the source tray was inspected today by Anders, Tom and Aurelia. The chips are small enough that they should not be a problem. See photos for details.

Attachment 1: Left_Insulator.jpg
Left_Insulator.jpg
Attachment 2: Right_Insulator.jpg
Right_Insulator.jpg
  1649   Thursday, October 19, 2017, 14:20 Anders MjosConditioning StationStandard OperationTM4SiC#37SiC#37 Conditioning

Thursday, October 19, 2017, 14:20: EE configured for conditioning. HV cage locked up

Thursday, October 19, 2017, 16:46: BIAS / EL / EE at 45 / 22.5 / 0 kV

Thursday, October 19, 2017, 17:16: 30 min without sparking. Lowering to 0. Continue conditioning tomorrow.


Friday, October 20, 2017, 08:22: Resuming HV conditioning

Friday, October 20, 2017, 08:44:  BIAS / EL / EE at 45 / 22.5 / 0 kV

Friday, October 20, 2017, 09:48: No sparking. Continue conditionoing

Friday, October 20, 2017, 10:40: BIAS / EL / EE at 50 / 22.5 / 0 kV

Friday, October 20, 2017, 11:30: HV spark (at 52.5 kV) tripped TP2 and TP1s resulting in IG1S and power supplies tripping.

Friday, October 20, 2017, 13:50: Gelo is troubleshooting flickering on/off of ANODE, TGHT and TBHT power supplies.

Friday, October 20, 2017, 13:51: BIAS / EL / EE at 50 / 25 / 0 kV

Friday, October 20, 2017, 14:26: BIAS / EL / EE at 55 / 28 / 0 kV

Friday, October 20, 2017, 14:37: TP2 tripped on spark

Friday, October 20, 2017, 14:51: Gelo has determined there is a communication problem with the PLC on the HV platform. Troubleshooting continues.

Friday, October 20, 2017, 19:02: Troubleshooting did not succeed. Not able to control power supplies. Troubleshooting continue on Monday.


Monday, October 23, 2017, 09:00: After starting the TCS again today communication has been reestablished. Started heater conditioning.

Monday, October 23, 2017, 14:03: Heater ramping previously aborted and ramp down started due to ongoing PLC communication issues. TGHT and TBHT power supplies tripped on timeout around 13:45. Gelo will continue the troubleshooting.

Monday, October 23, 2017, 19:55: Switching off source after operating for 5 hours without any communication glitches detected (fiber optic communication cables swapped between HV platform and BIAS/EZL PLCs)

Attachment 1: SiC#37_BIAS_current_vs_voltage.xlsx
Attachment 2: SiC#37.docx
  1652   Thursday, October 26, 2017, 09:56 Anders MjosITERepairTM4SiC#37Leak on multi pin connector feedthrough

On maintenance day Tuesday, the roughing of the target station could not go below 1.5 Torr. A brief troubleshooting on Tuesday was unsuccessful in determining the cause. Leak checking continued on Wednesday by David and Anders. A leak was finally found on the multi pin connector feedthrough due to the seal between the connector and flange on top of the nylon insulator. Upon re-tightening the connector, the leak could be stopped and the module pumped down to allow starting of turbo pumps.

  1655   Thursday, November 09, 2017, 08:46 Anders MjosConditioning StationRepair  Communication fiber replaced for HV PLC

 After extensive troubleshooting the communication fiber was found to be damaged and has been replaced by Gelo.

  1658   Thursday, November 09, 2017, 10:39 Anders MjosConditioning StationStandard OperationTM2Ta#55Conditioning Ta#55

Thursday, November 09, 2017, 10:40: BIAS / EL to 30 / 15 kV. 400 uA on BIAS

Bias was stable for 1 hour. Handed over to RIB ops for heater conditioning.

  1665   Wednesday, December 06, 2017, 09:33 Anders MjosConditioning StationMaintenance  Running chiller for maintenance tech

 Dakine is on site to do maintenance on the chiller. The tech requested the chiller to operate.

  1666   Wednesday, December 13, 2017, 15:32 Anders MjosAssembly/Bench TestMaintenanceTM2 Source Tray inspection

The Source tray was inspected in the RH shop today by Anders, Friedhelm and Jens. The routing of the lines are satisfactory, however a design proposal to remove the ground electrode line will be made. This design will have to ensure a proper connection from the electrode to ground (using the window cooling lines). All other lines are OK at this point. Some fine adjustments are expected after brazing and soldering to maintain high voltage separation. Photos are available on DocuShare Collection-21401

  1668   Tuesday, December 19, 2017, 10:41 Anders MjosCraneMaintenance  Crane powered down

The target hall crane has been powered down by Don today in preparation for the power shutdown over the Holidays.

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