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  RH-ISAC, Page 84 of 140  Not logged in ELOG logo
ID Datedown Author Category Type Module Target/Number Subject
  1138   Thursday, November 26, 2015, 06:25 David WangConditioning StationStandard OperationTM4UC#14TM4 vacuum has been connected in TCS.

TM4 vacuum has been connected in TCS. All vacuum pumps were started yesterday. The pumping down of TM4 and TCS are good so far.

  1137   Wednesday, November 25, 2015, 15:37 Anders MjosConditioning StationStandard OperationTM4UC#14Conditioning

 Wednesday, November 25, 2015, 15:36: RGA on


Thursday, November 26, 2015, 09:55: PS energized. EE connected to power supply.

Thursday, November 26, 2015, 11:41: Applied some current and voltage to all power supplies. All looks good.

Some sparking around 5 kV. Turned out to be a bad cable connection. Fixed with David W.

Thursday, November 26, 2015, 15:04: BIAS/EL/EE 20 / 15 1.5 kV

Thursday, November 26, 2015, 15:43: Handed TCS over to ISAC operations


 Target heated over the weekend. EE went into current limiting (down to ~100 V) a while after the target was at temperature.


Monday, November 30, 2015

Target conditioned by ISAC operators to 30 kV without any problems.

EE current limit increased to about 26 mA in an attempt to recover. Cooling down target to investigate.

  1136   Wednesday, November 25, 2015, 14:16 chad fisherSouth Hot-CellRepair  Cell Decon

Cell (table) was systematically cleaned with a swiffer and resulting piles of contaminated waste placed in pail with spent Ta target.

  1135   Wednesday, November 25, 2015, 14:13 chad fisherSouth Hot-CellStandard OperationTM4UC#14UCx#14

UCx#14 installed onto TM4. High current fasteners torqued to 130 in lbs.

  1134   Wednesday, November 25, 2015, 11:55 Travis CaveConditioning StationStandard OperationTM4UC#14Module moved and electrical check.

TM#4 with UC#14 was moved from the south hot cell to the conditioning station.  Here are the results of the electrical check of the module with the UC#14 target while at the hot cell.

  1133   Wednesday, November 25, 2015, 11:52 Travis CaveSouth Hot-CellStandard OperationTM4Ta#46Module moved

Yesterday TM#4 with Ta#46 was moved from the east station to the south hot cell.

  1132   Tuesday, November 24, 2015, 14:03 chad fisherSouth Hot-CellStandard OperationTM4 Ta#46

Ta#46 has been removed from TM4.

  1131   Tuesday, November 24, 2015, 14:02 chad fisherSouth Hot-CellRepair  Left Manip repair

electronics package on left manip died completely yesterday (it has been going for a while).

Disconnected entire package and replaced with package from "spare" manipulator.

everything is back up and working.

  1130   Tuesday, November 24, 2015, 14:00 chad fisherSouth Hot-CellRepair  Compressible waste sorting.

Residual fields from the remaining compressible waste were still too high (as far as I'm concerned) so I have unpacked all compressible waste looking for a "hot" item that has snuck into these items.

I have a hand full of small bolts (possible target components), a hand full of target material/dust (including an entire target disc), and some cloths that had clearly been used to wipe the table (they are black with target dust).

These items will be disposed of with the next spent target.

  1129   Tuesday, November 24, 2015, 13:54 chad fisherSouth Hot-CellRepair  Cell Decon

Decon/removal of large solid waste was performed on Wednesday November 18th."Hot" activated items included containment box cover from TM2, Febiad coil line remnants from TM4 (the hottest ends were previously cut off and disposed of), some target conductor bolts, steerer plugs from TM2, target material remn.

Drum containing these solid items is 2.5mSv/hr at 1/2m.

Drum is stored in the north hot cell temp.

Compressible waste will require another drum.

Swipes were taken of the window... 170k counts per minute of cont.

  1128   Monday, November 16, 2015, 13:59 Travis CaveConditioning StationMaintenanceTM3no targetModule moved

TM#3 has been moved back to the NW silo.

  1127   Monday, November 16, 2015, 10:37 David WangConditioning StationRepairTM3 TM3 has been disconnected at TCS.

I stopped the TM3 and TCS vacuum pumps and water system. The TM3 is disconnected and vented. It will be moved to silo this afternoon.

  1126   Monday, November 16, 2015, 10:33 Anders MjosConditioning StationStandard Operation FEBIAD Test TargetHV conditioning by ISAC operators

ISAC operators attempted HV conditioning over the weekend.

https://web.accel.triumf.ca/isac_elog/Elog_show_result.pl?inid=218447&style=entry

 

  1125   Monday, November 16, 2015, 10:09 Anders MjosConditioning StationStandard OperationTM3FEBIAD Test TargetElectrical check after HV conditioning

 Problem found between ANODE (F) and chassis 90 kOhm. See attachment for details.

  1124   Monday, November 16, 2015, 08:04 David WangConditioning StationStandard Operation  Target Hall schedule from Sep 08th 2015 to Dec 25th 2015

Update TH schedule according to changes. See attachment 1,2 .

update TH schedule weekly. See attachments 3,4

  1123   Thursday, November 12, 2015, 13:25 Anders MjosConditioning StationStandard OperationTM3FEBIAD Test TargetElectrical check and leak check

Target to Anode and target to Common showed ~ 500 kOhm values. No leaks above 3E-9 atm-cc/s seen. See attached.  

  1122   Thursday, November 12, 2015, 10:18 Anders MjosConditioning StationMaintenanceTM3 Air to vacuum leak on service cap

Anders Mjos wrote:

Conducted a more thorough leak check this morning with Edi. He found a leak on the base of the  blue F/T insulator for the multi-pin connector (see attachment). I discovered that all the bolts could rotate freely in the threads as they were too small. The bolts were replaced. The leak rate was reduced but still significant. The o-ring will likely need to be replaced.

Tuesday, November 10, 2015, 17:00: Could not find new o-ring. Cleaned groove and o-ring and applied o-ring grease. Re-attached F/T.

Tuesday

Steerer wire had disconnected again. See DocuShare for photos.


Thursday, November 12, 2015

Leak checked the fixed F/T and the panel for steeerers. No leaks found.

  1121   Tuesday, November 10, 2015, 16:53 Anders MjosConditioning StationDevelopmentTM3FEBIAD test targetTesting TM3

Tuesday, November 10, 2015, 16:53: Roughing

Tuesday, November 10, 2015, 18:24: TP1S started

Tuesday, November 10, 2015, 18:30: TP1 and TP2 started

Tuesday, November 10, 2015, 18:41: All 3 turbos at speed.


Thursday, November 12, 2015, 08:30: Purged backing pump using purging function. Vacuum in backing line recovered to previous value. 


Module connected for HV testing. No target heating possible. All F/Ts tied together to HV common. EZL connected.

Friday, November 13, 2015, 11:20: Started water package

Friday, November 13, 2015, 11:52: 1kV on BIAS and 1 kV on EL

Friday, November 13, 2015, 12:54: BIAS/EL 10 / 5 kV

Friday, November 13, 2015, 12:59: BIAS/EL 15 / 7.5 kV

Friday, November 13, 2015, 13:04: BIAS/EL 20 / 10 kV

Friday, November 13, 2015, 13:08 : BIAS/EL 22 / 11 kV. Some sparks.

Friday, November 13, 2015, 13:17: Sparking at 22.5 kV. Had to return to 20 kV to recover. Back at 22.5

Friday, November 13, 2015, 13:21 : BIAS/EL 24 / 12 kV. 

 Friday, November 13, 2015, 13:27: Heavy spakring around 24.5 kV. Had to return to 20 kV to recover.

Friday, November 13, 2015, 13:31: Attempted to increase voltage again. Sparking started around 23 kV. Had to lower to 20 kV.

Friday, November 13, 2015, 13:36: 9 sparks for the last 5 min.

Friday, November 13, 2015, 13:45: Spark rate reduced, but multiple sparks encountered again at 20.5 kV. Reduced back to 20 kV

Friday, November 13, 2015, 13:50: Increased sparking at 20 kV. Had to lower to 18 kV

Friday, November 13, 2015, 14:07: Back at 20 kV

Friday, November 13, 2015, 14:13: BIAS and EL off


Monday, November 16, 2015, 08:18: Fault on chiller. Reset chiller unit on the roof.

  1120   Tuesday, November 10, 2015, 10:23 Anders MjosConditioning StationMaintenanceTM3 Air to vacuum leak on service cap

Conducted a more thorough leak check this morning with Edi. He found a leak on the base of the  blue F/T insulator for the multi-pin connector (see attachment). I discovered that all the bolts could rotate freely in the threads as they were too small. The bolts were replaced. The leak rate was reduced but still significant. The o-ring will likely need to be replaced.

Tuesday, November 10, 2015, 17:00: Could not find new o-ring. Cleaned groove and o-ring and applied o-ring grease. Re-attached F/T.

  1119   Monday, November 09, 2015, 16:47 Anders MjosConditioning StationMaintenanceTM3FEBIAD Test TargetLeak check of Service Cap

Service cap leak checked this afternoon. Found multiple leaks of 10E-8 to 10E-7 range. Connected to the backing line with IG1 at ~4E-6 T, CG1A around 40 mT. Got responses around large round flange on top, rectangular side panels, water f/t on GND and water f/t on HV. Will resume leak checking tomorrow to attempt to pinpoint sources of leak more accurately.

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