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New entries since:Wed Dec 31 16:00:00 1969
ID Date Authordown Category Type Module Target/Number Subject Text Attachments
  341   Monday, May 13, 2013, 14:59 Bevan MossConditioning StationStandard OperationTM3N/AEL testing

    

       
            
 TM3_EL_39.9kV_23042013.txt 
  342   Monday, May 13, 2013, 15:10 Bevan MossConditioning StationStandard OperationTM3N/AHV Test All common

    

       
            
 TM3_40kV_22042013.xlsx 
  344   Wednesday, May 15, 2013, 10:17 Bevan MossConditioning StationStandard OperationTM3No Source TrayPreliminary Results from HV testing Testing on TM3 without a source tray
was completed on 13/05.2013. All items were
tied to common and the water blocks were
 module_hv_test_0KV.rgaMODULE_hv_test_42kv.rgaTM3_13052013_no_source_tray.xlsx 
  345   Wednesday, May 15, 2013, 10:20 Bevan MossConditioning StationRepair  Roof top chiller failedI have been getting a fault on the roof
top chiller for the 2 tandem 7.5  ton chillers.
I have checked and we have water flow and
  
  346   Wednesday, May 15, 2013, 10:25 Bevan MossConditioning StationRepair  ONICON flow meter Scott Adair from Riada sales came
to site to complete diagnostics on the ONICON
flow meter. He could not determine the problem
  
  347   Wednesday, May 15, 2013, 16:21 Bevan MossConditioning StationRepair  BIAS Current readings off by a factor of 5 A special thanks to Kazuya, Jane
and Ray who jumped on this issue right  away!
The limit of the BIAS PS was set as 20000uA
  
  348   Wednesday, May 15, 2013, 16:51 Bevan MossConditioning StationStandard OperationTM3No Source TrayRepeat of HV Test The HV test completed on Monday was
repeated today over a much longer time period.
By taking longer there was slightly less
 150502013_TM3_No_Source_Tray.xlsx 
  349   Wednesday, May 15, 2013, 17:32 Bevan MossConditioning StationStandard OperationTM3 TM3 in place but not connected To confirm that the sparking was
coming from the module rather than the conditioning
station TM3 was grounded and the conditioning
 15052013_TM3_in_place_but_not_connected.xlsx 
  350   Wednesday, May 15, 2013, 18:12 Bevan MossConditioning StationStandard OperationTM3No source trayHV test repeat After discussion with Friedhelm it
was decided to continue trying to condition
the module today before moving it tomorrow.
 15052013_TM3_HV_test_repeat.xlsx 
  354   Tuesday, May 21, 2013, 11:52 Bevan MossConditioning StationStandard OperationTM3No Source TrayMay 16th Long HV conditioningOn May 16th 2013 the module was HV conditioned
all day. As a result the maximum stable voltage
has been increased to about 47kV (~4kV more
 16052013_TM3_long_HV_conditioning.xlsx 
  359   Thursday, May 23, 2013, 14:07 Bevan MossConditioning StationRepair  Chiller Unit Repaired ESC came today and "repaired"
the chiller. There was something wrong with
the VFD controller. The were able to get
  
  360   Thursday, May 23, 2013, 14:08 Bevan MossConditioning StationStandard OperationTM4Ta #40Turbo Pumps on The turbo pumps have been turned
on and are running
  
  361   Thursday, May 23, 2013, 14:12 Bevan MossConditioning StationMaintenance  Primary Circuit Drained and Flushed Rob Walker has drained the primary
side of the conditioning station. It will
be flushed, filled  and chemically treated.
  
  362   Monday, May 27, 2013, 10:35 Bevan MossConditioning StationStandard OperationTM4Ta #40Pumps Started HV testing to followThe pumps have been turned on at ~9:30
this morning. Current values are 6.61 Mohm
TCS:DIC1 @19.4 C. HV testing will start momentarily.
  
  363   Monday, May 27, 2013, 10:37 Bevan MossConditioning StationMaintenanceTM4 Cooling Systems topped offRob walker has flushed and refilled the
primary side of the system (note the water
still looks nasty). This morning the primary
  
  365   Monday, May 27, 2013, 15:59 Bevan MossConditioning StationRepair  Compressor fault Once again the 7.5 compressors are
tripping due to faults. I believe it is due
to over pressure as a result of the chiller
  
  366   Monday, May 27, 2013, 16:01 Bevan MossConditioning StationRepair  CanBUS card During HV conditioning of TM4 with
Ta#40 there was a spark at ~43 kV that caused
the Bias card to "fry". Dave Morris
  
  367   Monday, May 27, 2013, 16:07 Bevan MossConditioning StationStandard OperationTM4Ta #40HV conditioning The HV conditioning reached a maximum
of 44kV today before a spark took out the
canbus card. I will attach the data once
  
  368   Monday, May 27, 2013, 16:36 Bevan MossConditioning StationStandard OperationTM4Ta#40Argon Venting Started Argon venting has started. It will
be left to vent over night. 
  
  375   Tuesday, June 04, 2013, 15:34 Bevan MossConditioning StationRepair  Relay replacedESC was called out again to inspect the
chiller as it was showing the same problem
as before. This time when started one fan
  
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