ID |
Date |
Author |
Category |
Type |
Module |
Target/Number |
Subject |
2121
|
Monday, July 06, 2020, 12:20 |
David Wang | ITW | Standard Operation | TM2 | C#1 | Five shielding blocks to ITW |
Five shielding blocks are transferred to ITW |
2205
|
Thursday, March 25, 2021, 10:38 |
David Wang | Spent Target Vault | Standard Operation | | C#1 | Remove pail 237 spent target C#1 from storage vault to mini storage. |
Pail 237 only has 200u sv/hr field at 0.5 meter. On contact measurement: 0.9 to 1.6 m sv/hr.and less than 80 count contamination outside the pail. It is moved to mini storage. We will transfer this pail to cyclotron vault and store it there later. |
2116
|
Friday, July 03, 2020, 07:03 |
David Wang | South Hot-Cell | Standard Operation | TM4 | BEFORE TARGET INSTALLATION | ELECTRICAL CHECK BEFORE TARGET INSTALLATION. |
PQ SHORT TO RU. A TO PQ 1.8 M OHM AT 500 V. THE REST ARE OL |
653
|
Wednesday, April 30, 2014, 12:03 |
Travis Cave | Spent Target Vault | Standard Operation | | 2A3 window | Window now in vault |
The 2A3 window now has a lid, and lift yolk on it and it has been installed in the spent target vault in spot 2A. The lid is a normal unmodified and has no sealant on it. |
1462
|
Friday, March 24, 2017, 11:19 |
Keith C Ng | Spent Target Vault | Standard Operation | | 2A3 window | Window now in vault |
Travis Cave wrote: |
The 2A3 window now has a lid, and lift yolk on it and it has been installed in the spent target vault in spot 2A. The lid is a normal unmodified and has no sealant on it.
|
The pail containing window was transferred from the Storage Vault to the Cyclotron Vault Tunnel Storage 2017 Mar 24. It was placed in a brick bunker along the north wall and marked with item #1434. RPG storage form is attached.
Highest field measured at 0.5 m was 3000 uSv/h with an estimate of 4000 uSv/h on contact with the pail. Pail exterior was not contaminated. See attached storage form for details.
|
1463
|
Friday, March 24, 2017, 13:21 |
Travis Cave | Spent Target Vault | Standard Operation | | 2A window | 2A window has been removed from the vault. |
2A window has been removed from the vault and moved over the cyclotron vault tunnels. Attached is the updated storage vault list. |
94
|
Tuesday, April 24, 2012, 10:38 |
David Wang | Conditioning Station | Standard Operation | TM1 | LP SIS Nb6 | TM1 heat shield circuit leak check with Nb5 |
The pumping down on TM1 and conditioning station is fine over the weed end. The PNG 1(containment box) is 2.4xe-6 Torr, the IG1 (top service cap) is 9.0 xE-7 Torr, and the IG4 is 1.9xE-6Torr (diagnostic box). At this pressure, I connected the leak detector to the system and applied 80psi helium to the heat shield circuit. The leak rate and base pressure on leak detector are 0.0xE-9 Atm.cc/sec and 0.0xE-4Torr. There is no any response on leak detector during 4mins helium applying time. So the heat shield and Nb5 target water circuit is completely leak tight. |
295
|
Friday, April 12, 2013, 10:27 |
David Wang | ITW | Standard Operation | TM1 | | I reconnected TM1 to ITW. |
TM1 has been reconnected in ITW. Water interlock check for TM1 is done. |
4
|
Thursday, June 30, 2011, 16:04 |
Pierre Bricault | Conditioning Station | Repair | TM1 | | TM1 status |
Friday June 24 2011
The target module has been moved to the Conditioning Station (CS)
Pumping overnight
Saturday June 25 2011
Pressure Service Cap (SC) 3E-6 T
Pressure Containment Box (CB) 6.6E-6 T
High voltage test to 40 kV, unfortunately, the pressure is not great so we stop at 40 kV
Pressure at the end of the day: 1650H was, P SC 2.6E-6T
P CB 6.6E-6 T
Sunday June 26 2011
Pressure P SC 1.6E-6T
P CB 6.6E-6 T
It seems we have a leak. The pressure does not drop in the CB over one day.
Today June 27 2011
Pressure P SC 1.2E-6T
P CB 6.6E-6 T
We leak check the target module and found two leaks, one on the ground electrode and one on the mounting plate cooling circuit.
This is a new one. We had test this line three times before and it was ok.
Action for tomorrow.
After CS vent,
Move TM1 to SHC
Survey
Connect LD to Mounting plate cooling circuit
Open Side panel and leak check.
Meeting at 0830H |
11
|
Thursday, July 21, 2011, 17:39 |
Bevan Moss | Conditioning Station | Repair | TM1 | | TM1 Ground Electrode, Thermocouple line, Stem, panel, repairs |
Over the period of July 20-21st TM1 had several repairs completed and tested. The easiest of the repairs was the installation of a gasket and a blank off. The next repair was to replace the 2 oring on the side panels that were removed for inspection and repair. The instrument panel oring was replaced again and the previous one measured. Both were found to have the correct diameter of 0.131 inches for the seal groove. When attempting to cut the thermocouple line back to an acceptable distance it detached from the stainless tube running down the high voltage chase. It was discovered that it was only being held in place with heat shrink and that the bend consisted of a hand made copper tube that was flared slightly, a truly poor electrical and mechanical connection. Also discovered was the thermocouple wire was left in the tube, this too was removed. The stainless steel tube was then secured to the tube heater (C) lines with a PEEK tie wrap. The port where the thermocouple line was then blanked off. The extraction electrode and mounting plate feed through stem repair went as practiced and no unexpected events occurred. One thing of note is that because the lines are twisted and some of the tube was removed the quick connects are no longer facing the same direction they were before. During these repairs the Ion gauge screen contacted a filament and caused a fault, this was repaired by edi who rotated the gauge. Roughing was started at ~10 am on July 21st and the turbo pumps turned on at 10:45. At 13:20 all of the lines and external seals were tested and no leaks were found. The module was at a pressure of 2.9 x 10^-5 Torr (IMG) and 1.4 x 10^-5 Torr (ION). The leak test cart was at a pressure of ~2.7 x 10^-2 Torr and a leak rate of 1.1 x 10^-2 atm cc/sec for the external leak test and the repaired lines. A small response was found in the Tube heater (D) where the leak increased to 2.1 x 10^-8 atm cc/sec. The leak test cart would then no longer drop below 1.9 x 10^-8 atm cc/sec and there was no response measured for lines C, B, and A. Over all very positive results! After 6 hours of pumping down the pressures were 2.0 X 10^-5 Torr (IMG) and 9.7 x 10^-6 Torr (Ion).
|
12
|
Friday, July 22, 2011, 10:30 |
Bevan Moss | Conditioning Station | Repair | TM1 | | TM1 Ground Electrode, Thermocouple line, Stem, panel, repairs |
Bevan Moss wrote: |
Over the period of July 20-21st TM1 had several repairs completed and tested. The easiest of the repairs was the installation of a gasket and a blank off. The next repair was to replace the 2 oring on the side panels that were removed for inspection and repair. The instrument panel oring was replaced again and the previous one measured. Both were found to have the correct diameter of 0.131 inches for the seal groove. When attempting to cut the thermocouple line back to an acceptable distance it detached from the stainless tube running down the high voltage chase. It was discovered that it was only being held in place with heat shrink and that the bend consisted of a hand made copper tube that was flared slightly, a truly poor electrical and mechanical connection. Also discovered was the thermocouple wire was left in the tube, this too was removed. The stainless steel tube was then secured to the tube heater (C) lines with a PEEK tie wrap. The port where the thermocouple line was then blanked off. The extraction electrode and mounting plate feed through stem repair went as practiced and no unexpected events occurred. One thing of note is that because the lines are twisted and some of the tube was removed the quick connects are no longer facing the same direction they were before. During these repairs the Ion gauge screen contacted a filament and caused a fault, this was repaired by edi who rotated the gauge. Roughing was started at ~10 am on July 21st and the turbo pumps turned on at 10:45. At 13:20 all of the lines and external seals were tested and no leaks were found. The module was at a pressure of 2.9 x 10^-5 Torr (IMG) and 1.4 x 10^-5 Torr (ION). The leak test cart was at a pressure of ~2.7 x 10^-2 Torr and a leak rate of 1.1 x 10^-2 atm cc/sec for the external leak test and the repaired lines. A small response was found in the Tube heater (D) where the leak increased to 2.1 x 10^-8 atm cc/sec. The leak test cart would then no longer drop below 1.9 x 10^-8 atm cc/sec and there was no response measured for lines C, B, and A. Over all very positive results! After 6 hours of pumping down the pressures were 2.0 X 10^-5 Torr (IMG) and 9.7 x 10^-6 Torr (Ion).
|
I again checked the TM this morning (July 22) at 10:00 am (24 hours of pumping), There is no external leaks carts pressure was 0.0x10^-4 Torr and leak rate was 0.0X10^-9 atm cc/sec. The IMG gauge was reading 6.8 x 10^-6 Torr and ION gauge was reading 3.1 x 10^-6 Torr. The lowest we have yet to record on the IMG gauge was 6.6 x10^-6 Torr and that was when the ION gauge was reading 1.2 x 10^-6 Torr and there were several leaks. This is a very good sign. I will continue to check the vacuum throughout the day.
One more thing of note is that the copper feed thru stems have a design flaw, the holes for the locating pins are too large. As such a custom step pin had to be made. It work functionally the same but is not as intended. |
14
|
Wednesday, July 27, 2011, 14:34 |
Travis Cave | South Hot-Cell | Standard Operation | TM1 | | Module move |
TM#1 has been moved from the Conditioning Station to the South Hot Cell for the installation of Ta#37. |
39
|
Tuesday, October 25, 2011, 16:57 |
Bevan Moss | Conditioning Station | Standard Operation | TM4 | | Turbo Pump 1 issues |
Roughing on TM1 started at ~15:00 today by ~16:30 the module had reached a pressure of ~200 mTorr and the turbo pumps were turned on. TP1 failed to achieve normal operation and we running at approximately 4KRPM and 50W with 6.1 A of current draw. TP2 was able to achieve normal operation. The controller for TP1 was then powered off and back on but that failed to resolve the issue. The controllers for TP1 & 2 were then switched at which point TP1 again failed normal operation and TP2 achieved it, thus eliminating the controller as the issue. The turbo pumps have been turned off and the roughing pump left on for overnight in case Vacuum group wishes to do any additional diagnosis. |
41
|
Friday, October 28, 2011, 09:30 |
chad fisher | South Hot-Cell | Repair | TM4 | | Tube Heater + Leak Check C.B. |
Base Pressure: 0.0x10-4
Stable Leak Rate: 0.0x10-9
Leak check of tube heater circuit, containment box side was performed.
Initail check at tube heater block on source tray yeilded a response 60 sec after the 2 second spray of helium. The response was very small and recovered immediately.
This area was checked twice more but the reponse could not be recreated.
Joint at the waterblocks was tested with an intial 2 sec spray. No response after 60 sec.
Waterblock joint was tested again with a 4 second spray. No response after 60 sec.
|
43
|
Friday, October 28, 2011, 14:29 |
Bevan Moss | Conditioning Station | Standard Operation | TM4 | | Leak Check on October 27/10/2011 |
A leak check was performed on the module on October 27/10/2011 by David Wang and was reported to Bevan Moss but it never made it into the Elog system. This entry is to summarize the results of that testing. All circuits were pressurized to 80 psi with helium and every line except the tube heater (+) showed no or small responses as experienced before. The tube heater line had a slightly larger response under the conditions summarized below:
Varian 959
Base Pressure 7.0 x 10^-3 Torr
Base Leak Rate 7.5 x 10^-9 atm cc/sec
Gauges
IG1 2.0 x 10^-6 Torr
PNG5 9.6 x 10^-6 Torr
PNG4 (C.S.) 2.4 x 10^-5 Torr
Convectron (Back line) 20mTorr
The leak rate quickly climbed to 3.0 x 10^-8 atm cc/sec then constantly climbed to 1.4 x 10^-7 atm cc/sec for 2 minutes. David repeated this test again at the end of the leak test and found the same results. In the past we have called this a leak and attempted to find its location and repair it. David believes that this isn’t a real leak as we have been able to achieve very good vacuum on TM4 all year and that we do not normally touch the feed through stem on this circuit. This result makes me nervous as the total differential is roughly the same as that we found on the UCx#2 run(which was at a higher vacuum).
The result of this test caused the module to move back to the hot cell for further more localized leak checking.
|
44
|
Friday, October 28, 2011, 14:42 |
Bevan Moss | South Hot-Cell | Maintenance | TM4 | | Leak check on service cap feed through |
After Chad and Davids leak check results from the containment box it was decided to perform a leak check on the feed through stem in the service cap. This is a known point of failure on TM1 and the same design flaw is likely in TM4. Once the service cap was open a visual inspection was performed and some oxidization of the copper line on the tube heater (+) circuit was observed (see attached pictures). The leak check was performed with the cart at a base pressure of 0.0 x 10^-4 Torr and base leak rate of 0.0 10 x 10^-9 atm cc/sec. A total of 4 joints were checked and no response was found. The service cap was then flooded with helium and once again no response was found. It was decided to give the module a clean bill of health, make note of the baseline test from the conditioning station, and continue to monitor the circuit. |
46
|
Tuesday, November 01, 2011, 11:50 |
David Wang | Conditioning Station | Standard Operation | TM4 | | TM4 leak test on conditioning station |
I did a leak check again on TM4 today. This time, the leak detector pump to the bottom on both base pressure(0.0xE-4 torr) and base leak rate(0.0xE-9 atm.cc/sec). All high vacuum gauges on TM4 and conditioning station at -6torr range.IG1 is 3.3-6torr,PNG5(top of service cap)is 6.5-6 torr, and the PNG4(bottom of the vessel )is 8.7-6torr. For air to vacuum leak checking, I checked the panel we moved last week on service cap by spraying helium around the panel. There is no any response on leak detector. The panel is leak tight. Also I sprayed helium around the tube heater (+) water cap and blue nylon stand. They are also leak tight. Then, I put 80 psi pressure air to the “D” circuit first. With 80 psi pressure air for 5 minutes, the leak detector has no any response on it. Also all high vacuum gauges stayed at same level .Then I checked it with 80 psi pressure helium for 3 minutes. The leak detector has a response on leak rate with pressure helium same as last time. It climbed from the 0.0xE-9 atm. cc/sec quickly to high -8 range then slow down. The leak rate finally climbed to 2.0 X E-7 atm.cc/sec this time. There is no base pressure change on leak detector. All high vacuum gauge readings no change during the test time. There is a small helium leak at 80 psi pressure test on “D” circuit. But we can not locate it at this stage. Also I don’t want to disturb this circuit any more before the febiad run since this time I saw a little bit increase on leak rate comparing to last time when I checked it. If we really like to find this small helium leak, I would suggest we do it after the febiad run. Thank you. |
49
|
Thursday, November 10, 2011, 14:33 |
Travis Cave | Spent Target Vault | Standard Operation | | | Spent Target Assay |
For the week of November 7th 2011, four of a possible ten targets that are in storage were assayed. Targets are as follows:
Target General average field @ 1 metre from edge of pail
SiC#24 1.99 mSv/hr
Nb#4 3.89 mSv/hr
Ta#25 4.57 mSv/hr
Ta#37 0.47 mSv/hr
These four are all viable spent targets to be shipped. We still need another couple of days of "UNINTERRUPTED" time to assay the remaining six targets, for us to have enough to make a ship of five to Chalk River. |
51
|
Tuesday, November 15, 2011, 13:08 |
Travis Cave | Conditioning Station | Standard Operation | TM1 | | Move ot TM#1 |
TM#1 has been moved from the south hot cell to the conditioning station. Move went well. |
60
|
Monday, November 21, 2011, 13:49 |
David Wang | Conditioning Station | Standard Operation | TM1 | | TM1 full leak check in conditioning station |
TM1 full leak check in conditioning station has been fulfilled this morning.Both air to vacuum leak check and waterlines helium 80psi pressure test are fine.The result:
Air to vacuum helium spray:base leak rate on leak detector 1.6x E-9 atm .cc/sec.base pressure0.0xE-4 torr. sprayed helium around all flanges, turbo pumps,panels,bellow,insulation stands, gauges. No Response on leak detector. Air to vacuum seals on TM1 is leak tight.
Helium pressure test on all water lines.with 80 psi helium 3minutes test:
PNG1 :2.4XE-7torr .PNG4 :2.6x E-6torr . IG1 :5.1xE-7torr.
A :target oven(+) BL:2.0xE-9 atm.cc/sec .First minute no response,then climbed to1.9xE-8 atm.cc/sec. Stabled at 1.9xE-8 atm.cc/sec to 3 minutes.
B:target oven(-) BL:5.5x E-9 atm.cc/sec.First 80 seconds no response, then climbed to 1.8xE-8atm.cc/sec. Stabled at 1.8xE-8atm.cc/sec to 3 minutes.
C:tube heater(-) BL:8.0xE-9 atm.cc/sec .First minute no response ,then climbed to 2.7xE-8 atm.cc/sec. Stabled at 2.7x E-8 atm.cc /sec to 3 minutes.
D: tube heater(+) BL: 1.0xE-8 atm.cc/sec. First minute no response , then climbed to 1.8xE-8 atm.cc/sec. Stabled at 1.8x E-8 atm.cc/sec to 3minutes.
G:EE BL:1.0xE-8 atm.cc/sec .First 1.5 minutes no response , then climbed to 1.7x E-8 atm.cc/sec. Stabled at 1.7x E-8atm.cc/sec to 3minutes.
F:heat shield BL:1.2x E-8 atm.cc/sec. First 1.5 minutes no response , then climbed to 1.9 xE-8 atm.cc/sec. Stabled at 1.9 xE-8 atm.cc/sec to 4 minutes. Total test time 4 minutes.
I: mounting plate BL:1.2 x E-8 atm.cc/sec. NO RESPONSE on leak detector in 3minutes.
M: window BL:1.2x E-8 atm.cc/sec First 1.5 minutes no response,then climbed to 2.0xE-8 atm.cc/sec . Stabled at 2.0xE-8 atm.cc/sec to 3minutes.
The base pressure on leak detector stayed at 0.0x E-9 torr through all the test, and no pressure response on high vacuum gauges. |