Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 65 of 135  Not logged in ELOG logo
Entry  Thursday, March 23, 2017, 11:22, Grant Minor, Crane, Maintenance, , , Target Hall crane 20 ton hoist noise / smell - inspection by Gordon Crane & Hoist Target_Hall_crane_main_hoist_problem_-_A_Mjos_-_22_Mar_2017.pdfUpdate_-_Target_Hall_20T_Hoist_Inspection_-_G_Minor_-_23_Mar_2017.pdfRe__Update__Target_Hall_20T_Hoist_Inspection_-_David_Wang_-_23_mar_2017.pdf

Strange noise and a burning brake type smell was observed yesterday by David and Anders when running the main 20 ton hoist locally.  A service call was arranged today with Gordon Crane.  No major issues were found.  A more detailed summary is in the attached e-mail correspondence.  Gordon Crane will issue a formal report, but they recommend replacing both sets of brake disks and brake calipers. - Grant

Entry  Thursday, March 23, 2017, 09:30, Travis Cave, South Hot-Cell, Standard Operation, TM2, test target, Electrical Check TM2_Ta_Dummytgt_Preandpost.PDF

Electrical check of the Ta test target on TM#2

Entry  Wednesday, March 22, 2017, 14:05, Travis Cave, South Hot-Cell, Standard Operation, TM2, test target, module moved 

TM#2 has been moved from the east target station to the south hot cell.

Entry  Tuesday, March 21, 2017, 11:59, David Wang, Conditioning Station, Repair, TM4, , Rust inpsection on TM4 service cap inside surface and shielding plug surface.  11x

Yasmine and I did a rust inpsection on TM4 service cap inide surface and shielding plug surface. No rust has been found. Also, all steel bolts on this surface look fine. The inside of silo held this module are rust free as well.  See attachments

Entry  Tuesday, March 21, 2017, 10:06, Travis Cave, Conditioning Station, Standard Operation, TM4, no target, module moved 

TM#4 has been moved from the SW Silo to the conditioning station.

Entry  Tuesday, March 21, 2017, 10:05, Travis Cave, Spent Target Vault, Standard Operation, , , Spent target assay. Vault_Storage_March_20_2017.pdf

All target in the ISAC spent target vault have been either assayed or had their fields measured or both.

Entry  Thursday, March 16, 2017, 12:24, chad fisher, South Hot-Cell, Maintenance, , , West 'Z' motion cable replacement 

The west 'Z' motion cable on the east manipulator has successfully been replaced. The job took slightly less than an hour (including inspection of the scissor table hoses) and I received 0.075mSv. Scissor table hoses appear to be fine and also didn't "shed" or flake at all when checked by hand.

Entry  Thursday, March 16, 2017, 10:32, David Wang, Spent Target Vault, Repair, TM4, , TM4 and its silo rust photos 13x

I watched rust on TM4 and its silo. Most of rust are on est side of module and silo. See attachments

Entry  Wednesday, March 15, 2017, 07:45, chad fisher, South Hot-Cell, Maintenance, , , South Hot Cell Fields 

I have moved the suspected "hot" items in the hot cell and placed them under some lead bricks. I have re-measured the fields and it has been reducded to 90 uSv\h at the manipulator repair area and 110 uSv/h at the previous 1.82 mSv\h area.

Entry  Tuesday, March 14, 2017, 11:46, chad fisher, South Hot-Cell, Maintenance, , , 'Z' motion cable dry run 

Did a dry run with the latest procedure with Dan Mcdonald. Elapsed time was approximately 30 min.

Entry  Tuesday, March 14, 2017, 07:34, chad fisher, South Hot-Cell, Maintenance, , , Hot Cell Fields 

I have re-measured the fields in the hot cell. Fields at shield door Al cover are 101 uSv\h, in cell at the east manipulator are 245 uSv\h, and the largest field is 1.84 mSv\h...this appears to be the high current fasteners removed from the last target.

Entry  Friday, March 10, 2017, 09:19, chad fisher, South Hot-Cell, Standard Operation, , , South Hot Cell Field Measurements 

The fields in the hot cell have been measured by means of a pole monitor through the tool port. Field was measured to be 25 uSv/h.

Entry  Wednesday, March 08, 2017, 14:09, David Wang, ITE, Maintenance, TM2, , ITE IG1S increasing. ITE_IGIS_surge.pngITE_IG1S_and_PNG4.pngITE_IG1S_back_to_normal_overnight.pngITE_IG1S_behavior_from_Feb_08th_to_Mar_10th.png

By retrieving data further, It has been found no directly relationship between IG1S surging and dump plug water opening. Vacuum surging is 10minutes ahead dump water supply to circuit. SEE attachment 1. Also, The ITE IG1S start to behavior unusual in middle of Feburary. See attachment 2. Today,  ITE IG1S is still slowly climbing up. I decide to leak check ITE vacuum vessel. Before  leak check, for more information and trouble shooting. I closed water supply to ITE to see if vacuum has response on it. I will return water supply to ITE  tomorrow morning.

Water supply to ITE is returned this afternoon at 2: 10 PM.  Everything works fine so far

I leak checked ITE secondary vessel vacuum. A leak have been found in March 09th noon which is located between entrance module and TM2 top tank flange o-ring seal( on tank flange). It could not be confirm on which side of the o-ring the leak is from.

During last night, ITE IG1S reading went back to normal low E-7 range and stays in this range now. So I leak checked same area again this morning. The leak disappeared now. The o-ring works sometime , but not all the time. The plan for this issue: Change ITE target module side o-ring when TM2 is move out., and watch on the ITE IG1s when TM4 is moved back to ITE and pumped down.

Entry  Tuesday, March 07, 2017, 14:41, David Wang, ITE, Maintenance, , , ITE dump plug water circuit is closed for ITE IG1S small surge. 

It is closed @ 2:35PM by closing supply side valve first , the return side valve of ITE dump plug .

Opened ITE dump plug circuit valves @4:28PM. ITE IG1S still at 1XE-6. No change before and after of circuit closing and reopeneing.

Entry  Tuesday, March 07, 2017, 09:25, David Wang, ITW, Repair, , , ITW HALCW 2" return line ball valve seals replacement. 

Leaking seals on ITW HALCW 2" return line ball valve have been replaced. 8 liter waters are drained out for this job. Water are drained into a thick plastic bag.  The bag is tie strapped , labeled, and put into a yellow garbage bin in MAA. Water sample is given to RPG. After analyzing, RPG will give instruction on how to deal with it. Since we just refilled NALCW to system before this job, the active level on sample is very low. We may dump them into active sump.  After seals change, The system is refilled . I started pump and set everything back to normal configuration. NO leak has been found on new seals. The HALCW system is operating good so far.

Entry  Monday, March 06, 2017, 08:01, David Wang, Cooling, Repair, , , HALCW resin tank replacement. 11x

HALCW resin tank has been replaced. The old tank is stored in middle-west silo now. The field on old resin tank bottom is about 3.5 msv/ hr(on contact). By shielding it into silo and putting two lead blankets on the top cover of the silo,The general field 1 feet above this silo is 25usv/hr. And, The field around the silo area are less affected. This old tank will stay there as long as possible.  For the new resin tank during preparation, It was found that on return line side, the 1.25" pipe thread plug with return line tube  was very difficult to be installed onto the female thread adapter which is welded onto to tank body. It was jammed in half way of threading onto tank at manufacturer. This plug was removed out first and inspected. The first and second male threads were galled.  Maico repaired the thread on a lathe. The female thread on the tank was tapped. A tight spot was found during the tap. After that, the return line plug could be installed onto the tank properly.  The new tank was installed into the vessel and connected back to HALCW system. Water are refilled into new tank. During refill air were trapped into the system. This caused  pump restarting problem. By Several times of starting up the pump, stopping the pump and venting,  Most air were breathed out of  system. Finally,The system was restarted by supply water to ITW( without module) only. ITE and resin can circuits were brought back to system after that without problem.

 Before removing the old tank, We drained water out of old tank to decay tank. Since the resin tank is largely filled with  resin, and water are soaked into resin, we only can drain out less than 10 liters water out of tank. Also, The drain caused some part of return line on pumps have to been drained. This is the main reason air was trapped in system during the new resin tank water refilling. For the future replacement, we should not drain water in old tank. It does not worth to do it. 

Attach TH HALCW resin tank replacement procedure here.

2022-02-17 reload replacement procedure and draining schematic.

Entry  Thursday, March 02, 2017, 15:02, Isaac Earle, North Hot-Cell, Development, , , NHC roughing filter installed IMG_8014.JPGIMG_8018.JPGIMG_8019.JPG

 The roughing filter assembly (RFM0001D) has been installed at the ventilation exhaust hole on the NHC partition wall.  The filter used is Model # 332-528-002 supplied by BGE Service & Supply Ltd (see PO # TR123998).  Installation and removal of the filter using the manipulators will be tested after they have been installed.

 

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Entry  Tuesday, February 28, 2017, 17:51, Isaac Earle, North Hot-Cell, Development, , , NHC flanged ducting connection sealed IMG_8012.JPG

 The North Hot Cell ducting (IRH1617) has been sealed with a bead of Sikaflex 1a polyurethane construction sealant where the flanged connection bolts to the NHC/TCS partition wall.  When this sealant shows signs of aging it may be cut away and re-applied without unbolting the flange.

 

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Entry  Monday, February 27, 2017, 14:23, chad fisher, South Hot-Cell, Repair, , , Manip. 'Z' motion cable run through 

Aaron and I successfully completed a run through on the procedure to replace the 'Z' motion cable. I will be writing up the procedure for review and we will be performing more run through-s for practice before the actual job.

Entry  Friday, February 24, 2017, 15:12, Isaac Earle, North Hot-Cell, Development, , , NHC interior walls/floor/ceiling re-finished, sealed, and painted 8x

The North Hot Cell interior walls, floor, and ceiling were re-finished, sealed, and painted by Omni Coating from Feb 6 - 17 under PO #3036471.  This job required 2-3 people for 4-6 hours per day over the 2 week period.  First the existing surfaces were ground and/or sanded to remove existing coatings and protrusions/sharp edges.  This was followed by a coat of primer to highlight uneven surfaces and improve adhesion of following fillers and coatings.  Metal shims between the cell walls and roof were cut away where they protruded into the cell.  Loose steel cylinders between SHC and NHC spaces were fixed in place using epoxy filler. Epoxy or polyurethane fillers were used to fill all gaps, cracks, holes, etc, as detailed below.  Foam backer rod and polyurethane filler were used to seal all large wall-to-wall and ceiling-to-wall gaps.  An approximate 2cm radius rounded corner was formed at all wall-to-wall and floor-to-wall corners using polyurethane sealant.  The interior of the tool-port, personnel access hatch, as well as the north roof hatch were also re-finished with the same procedure.  After all sealing and finishing work the surfaces were coated with "Mill White"  Macropoxy 646 Fast Cure Epoxy Paint as per manufacturer instructions.  Note:  this paint is recommended by the manufacturer for nuclear applications and has been tested for decontaminability:  99% water wash; 95% overall as per ASTM D4256/ANSI N 5.12 as well as for radiation tolerance:  Passed ASTM D4082 / ANSI 5.12 with a 525 micron thick coating.

 

The following products were used as described (data sheets attached):

Sanitile 120 Universal Acrylic Primer - 50-75 micron dry film thickness coat applied over all existing ceiling, walls, and floor surfaces after preparation by sanding

Sika Duochem 8107 Epoxy Paste - Used for filling voids and cracks in concrete surfaces

Sikaflex 291 Polyurethane Elastomeric Adhesive and Sealant - used for caulking joints and cracks in the concrete walls and aluminum panel wall and for creating radiused corners in wall-to-wall and wall-to-floor corners

Macropoxy 646 Fast Cure Epoxy Paint - 4 coats applied on all surfaces using rollers or brushes to create a total thickness of 525 microns as per data sheet

 

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