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  ID Date Author Category Type Moduledown Target/Number Subject
  835   Monday, January 26, 2015, 09:36 chad fisherSouth Hot-CellRepairTM2 TM2 Tray Alignment

TM2 tray alignment was confirmed with the alignment tray this morning:

Front target 0.000 vertically, 0.000 horizontally.

Back target 0.003 low, 0.000 horizontally

Also, the master target jig was installed and measurements taken:

Front master target - 0.007 high, 0.000 left/right

Rear Master Target - 0.007 high, 0.000 left/right

Rear tray target - 0.003 low

 

Attachment 1: TM2_Tray_20150126_090448.jpg
TM2_Tray_20150126_090448.jpg
  836   Wednesday, January 28, 2015, 10:42 Anders MjosConditioning StationMaintenanceTM2 TCS shut down for site wide power outage
  837   Thursday, January 29, 2015, 11:31 chad fisherSouth Hot-CellRepairTM2 TM2 Tray Build

On Tuesday morning I attempted to complete assembly of the source tray for TM2 however discovered that 3 1/4-20 x 0.25 titanium helicoils had not been installed into the mounting plate as they should have been. Checked and asked around for them but to no avail. I have ordered some, they should have been here yesterday.

Also, I have noticed that the threaded portion of the target pins ITA0328A appear to be too long and as such may be (are indeed) touching the supports. I am going to remove 1/32" or appropriate to remedy this problem (drawing shows 0.035 clearance).

Attachment 1: TM2_Tray_20150126_112232.jpg
TM2_Tray_20150126_112232.jpg
  838   Monday, February 02, 2015, 09:59 chad fisherSouth Hot-CellRepairTM2 TM2 Tray Build

Missing heli coils installed this morning.

Threads had to be chased with tap for 1/4-20 heli coil and missing countersinks hand applied to allow for installation. Care was taken to ensure no "swarf" was spread and operation was super clean. Chased holes blown out with canned air and a vacuum placed on the other side.

Final assembly can and will now continue.

  839   Monday, February 02, 2015, 14:06 chad fisherSouth Hot-CellRepairTM2 TM2 Tray build

Master target jig installed to locate attachment bracket ITA3389 as well as conductor insulator block b (aluminum / for soldering version) and oven conductor blocks (ITD0353 and 03356). 

There were NO ITA6145 fasteners or TGN0076 either. Standard 1/4-20 x 1" fasteners have been used in there place for now. Keith is following up with getting the missing fasteners into the shop.

Oven conductor blocks will have to be lapped before lines are attached as they both have dents on the high current mating surfaces.

 

 

 

Attachment 1: TM2_Tray_20150202_134752.jpg
TM2_Tray_20150202_134752.jpg
Attachment 2: TM2_Tray_20150202_134759.jpg
TM2_Tray_20150202_134759.jpg
  858   Thursday, March 12, 2015, 09:48 Travis CaveSouth Hot-CellStandard OperationTM2No target Module move

TM#2 with no target and no source tray has been moved from the conditioning station to the north east silo.

  879   Tuesday, March 31, 2015, 11:36 chad fisherSouth Hot-CellDevelopmentTM2 TM2 Optics Tray Complete

TM2 optics tray is complete.

Master alignment tray: 0 up/down, 0 left/right

Optics tray: Front 0 up/down, 0 left/right. Middle 0 up/down, 0 left/right. Back 0 up/down, 0 left right.

 

Attachment 1: 20150331_OPTICS_FRONT.jpg
20150331_OPTICS_FRONT.jpg
Attachment 2: 20150331_OPTICS_MIDDLE.jpg
20150331_OPTICS_MIDDLE.jpg
Attachment 3: 20150331_OPTICS_BACK.jpg
20150331_OPTICS_BACK.jpg
  893   Tuesday, April 21, 2015, 13:01 Grant MinorITWDevelopmentTM2 TM2 MK4 Optics Tray - banana plug bore modification (on bench)

The MK4 optics tray prepared for TM2 (as per ITA6082) had an undersized bore for the banana plug, making insertion of the plug extremely difficult / impossible.

Reference stores parts were collected to check the fit:  male plug 3-4/01152 and female jack 1-6/1201.  The size of the female jack was checked with a #21 drill at .159".

The bore on the optics tray was drilled out dry using the #21 drill to the same depth as the original blind hole, by Maico and Dan McDonald.  Chips were carefully collected in a rag, and the hole was blown out with compressed air.

The fit was checked to be snug but possible, using the male plug and the Remote Handling ultem base (ref ITA6023).

Redlines and photos are attached.

 

Attachment 1: ita6092_redlines_gminor_21apr2015.pdf
ita6092_redlines_gminor_21apr2015.pdf
Attachment 2: TM2_Optics_Tray_Bore_Mod_21Apr2015_1.JPG
TM2_Optics_Tray_Bore_Mod_21Apr2015_1.JPG
Attachment 3: TM2_Optics_Tray_Bore_Mod_21Apr2015_2.JPG
TM2_Optics_Tray_Bore_Mod_21Apr2015_2.JPG
Attachment 4: TM2_Optics_Tray_Bore_Mod_21Apr2015_3.JPG
TM2_Optics_Tray_Bore_Mod_21Apr2015_3.JPG
  899   Monday, April 27, 2015, 16:12 Keith C NgSouth Hot-CellDevelopmentTM2 Ceramic Standoffs in TM2 source tray steerer assembly

On drawing ITA6008 for the Encole 0.5" ceramic standoffs there is a note to match pairs of ceramics to within +/-0.001". This step was missed on the current build of TM2 source tray (ceramics were not measured).

Measured the lengths of the rest of the ceramic standoffs in inventory and they range from 0.5035" to 0.4950" in length. The ceramics have been sorted by length and grouped into bags.

 IMG_3106.JPG

  900   Monday, April 27, 2015, 17:09 Grant MinorITEDevelopmentTM2 TM2 - New Source Tray - Water Block Seal Groove Inspection Report

The water blocks soldered to the TM2 cooling lines (see Ref. Assy. ITA6144) were inspected.

See attached inspection reports and drawings.

It was found that only 18% of the seal groove diameters and 55% of the depths were in spec.

The source tray must be tested on the test stand with c-seals to ensure that these blocks will seal properly on the module.

Attachment 1: IMG_1859.JPG
IMG_1859.JPG
Attachment 2: TM2_New_Source_Tray_Water_Block_Inspection_Results_24_April_2015.pdf
TM2_New_Source_Tray_Water_Block_Inspection_Results_24_April_2015.pdf
Attachment 3: TM2_water_block_inspect_24Apr2015.pdf
TM2_water_block_inspect_24Apr2015.pdf TM2_water_block_inspect_24Apr2015.pdf TM2_water_block_inspect_24Apr2015.pdf TM2_water_block_inspect_24Apr2015.pdf
Attachment 4: TM2_New_Source_Tray_Water_Block_Inspection_Results_April_2015.xlsx
  906   Thursday, April 30, 2015, 08:50 Travis CaveSouth Hot-CellStandard OperationTM2No targetModule move

TM#2 with no source tray has been moved from the north east silo to the south hot cell.

  907   Friday, May 01, 2015, 08:27 chad fisherSouth Hot-CellRepairTM2 Containment Box Removal

Containment box has been removed in preparation for wire replacement.

  908   Friday, May 01, 2015, 13:48 David WangSouth Hot-CellStandard OperationTM2 Target Hall Scheduled Activities April 07 - June 26 2015 update

Target Hall Scheduled Activities  April 07 - June 26  2015 update.      2015-05-01. All TH scheduled jobs are finished on time this week.

Attachment 1: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mpp
Attachment 2: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
  910   Tuesday, May 05, 2015, 10:57 chad fisherSouth Hot-CellRepairTM2 TM2 Wiring

Old wiring was removed yesterday, new wiring run thru the vacuum chase. Old IMG gauge removed today, new cable trays installed and wires installed into cable trays.

Attachment 1: TM2_New_Wiring_20150504_13.jpg
TM2_New_Wiring_20150504_13.jpg
Attachment 2: TM2_Wiring_20150505_10.jpg
TM2_Wiring_20150505_10.jpg
  911   Wednesday, May 06, 2015, 14:30 Travis CaveSouth Hot-CellRepairTM2No targetWiring of TM#2

Wires for TM#2 steering elements, and png gauge have been run down to the containment box level. Chad has placed them in the little cable trays. Slack has been pulled back. and termination of the wire will be done on the 7th of May. A modification was done to the signal line of the png gauge wire ultem block, as grounded screw was inserted to allow for strain relief so the end would hopefully quit breaking. See attached pictures for the details.

Attachment 1: Photo_2015-05-06_8_26_10_AM.JPG
Photo_2015-05-06_8_26_10_AM.JPG
Attachment 2: Photo_2015-05-06_8_26_17_AM.JPG
Photo_2015-05-06_8_26_17_AM.JPG
  912   Thursday, May 07, 2015, 11:02 Travis CaveSouth Hot-CellRepairTM2No targetWiring of TM#2

Wires in TM#2 have been terminated at the top of the module.

  914   Monday, May 11, 2015, 11:20 David WangSouth Hot-CellStandard OperationTM2 Target Hall Scheduled Activities April 07 - June 26 2015

The schedule has some changes due to  new TM2 source tray coil cooling line leaking at test stand. Now,It is re-scheduled in such an estimation  that TM2 source tray could be ready at teat stand by this Friday(May-15th). see attachment 1,2.

2015-05-12,  Changed  and updated the TH activity schedule according to Dons new beam schedule which is re-arranged after the coil line leaking issue. See attachments 3,4. No major conflicts has been found on the new schedule.

2015-05 25, Updated the TH activity schedule according to present TM2 job processing. See attachment 5,6.

Attachment 1: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mpp
Attachment 2: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
Attachment 3: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mpp
Attachment 4: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
Attachment 5: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
Attachment 6: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mpp
  915   Wednesday, May 13, 2015, 13:55 chad fisherSouth Hot-CellRepairTM2 Shutter removal

TM2 has been successfully de-shuttered.

All went pretty much according to plan except I had to remove one fastener out of the upper wiring harness (the one that has just been installed) to allow for enough clearance to rotated the shutter guide out of the way...I shutter to think what would have happened otherwise...anyways...

Close inspection of the shutter does show that the "thin" area isn't in very good shape; whether this is a result of removal or just the way it was is hard.Due to the ease of removal I would quess that it may have been a preexisting condition. That being said...I think we may want to consider replacing it.

 

Attachment 1: TM2_20150513_131339.jpg
TM2_20150513_131339.jpg
Attachment 2: TM2_20150513_134232.jpg
TM2_20150513_134232.jpg
  917   Tuesday, May 26, 2015, 11:49 Grant MinorAssembly/Bench TestRepairTM2 TM2 New Source Tray - Braze & Solder Report - 22 May 2015

Hello,

For reference, I have attached a list of all solder joints in the TM2 Source Tray, and the alloys used for the most recent build (as per ITA6144).   I have also provided data sheets for the alloys, and PDF copies of all the drawings calling out the joints.

Certanium 34 C (222 deg C melt point) was used for all low-temperature solder applications, except for the steel inserts in the water blocks.  Previous revisions of the Source Tray drawings called out a higher-temperature McMaster lead-based solder (304 deg C melt point).  The change to Certanium 34 C on the prints was made in Bevan's era, during the transitional update of the source tray drawings between the TM1 and TM3 source tray projects, just before I took over updating the drawing packages.  I believe Bevan made this change on general advice from Guy Stanford, who stated that Certanium 34 C is a much easier solder to work with and makes a more mechanically reliable joint.  However, the change really should have had more review and validation testing before being implemented.

This said, we now have a source tray that uses Certanium 34 C, and rework of every joint would set us back too far in the schedule to meet the deadline, so we will have to run with it as it is.

Of particular concern are the joints on the target oven and coil heating blocks, which are now using a lower temperature solder (222 deg C melt vs 304 deg C melt).  We have experienced a coil block failure on TM4 due to a failed solder joint, although the failure mode is not known for certain.  We also had two recent failures on the test stand of a coil joint soldered with Certanium 34 C, but this was due to an error in the connection of cooling water to the joints (i.e. the joints had no coolant flow and the solder melted... this is expected!).

Anders and I have performed independent thermal analysis on the joints due to the radiative and electric heating from the target, and have concluded that even with a lower temperature solder, there is a lot of margin, so the risk seems to be low.  This work will be published in a separate report to be circulated later.

Thank you and regards,

Grant

Attachment 1: TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf
TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf
Attachment 2: 1005_Bare_DS.pdf
1005_Bare_DS.pdf
Attachment 3: 1005_Bare_MSDS.pdf
1005_Bare_MSDS.pdf 1005_Bare_MSDS.pdf 1005_Bare_MSDS.pdf 1005_Bare_MSDS.pdf
Attachment 4: Certanium_34C_Data_Sheet.pdf
Certanium_34C_Data_Sheet.pdf Certanium_34C_Data_Sheet.pdf
Attachment 5: Certanium_34C_MSDS.pdf
Certanium_34C_MSDS.pdf Certanium_34C_MSDS.pdf Certanium_34C_MSDS.pdf Certanium_34C_MSDS.pdf Certanium_34C_MSDS.pdf Certanium_34C_MSDS.pdf
Attachment 6: mcmaster_carr_solder_7667A23.pdf
mcmaster_carr_solder_7667A23.pdf
  918   Tuesday, May 26, 2015, 14:34 chad fisherSouth Hot-CellRepairTM2 Shutter replacement

The shutter in TM2 was successfully replaced today.

New lock washer and nut were installed onto shutter and nut torqued to 120 ft lbs.

Shutter guide alignment tool was used to insure tapped shutter guide holes were concentric with thru holes in shutter side mounting panel, button head screws replaced and torqued to 110 ft-lbs.

The shutter was manually cycled open and closed by David and everything is to operate well.

Attachment 1: Shutter.jpg
Shutter.jpg
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