Wednesday, December 13, 2023, 11:42, Adam Newsome, South Hot-Cell, Standard Operation, TM3, , TM3 Move - TCS TO SHC
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TM3 has been moved from the target conditioning station to the south hot cell. |
Friday, December 15, 2023, 11:07, Adam Newsome, Conditioning Station, Standard Operation, TM3, , TM3 Move - SHC to TCS
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TM3 was moved from the SHC to the TCS (no target installed). |
Tuesday, January 02, 2024, 16:01, Carla Babcock, Conditioning Station, Development, TM3, , TM3 service tray HV testing and conditioning 
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Tuesday, January 02, 2024, 15:58 :
Started HV ramp up on TM3 service tray about 3pm today. Had to bypass TCS:BIAS interlocks to make it work - there are some flow restrictions on the water lines that are causing the flow interlock to periodically trigger. The water flow it not very important for this test as long as the water is moving. Turned out that it was also conveninent to have all the interlocks bypassed because sparks tripped off the IG1 gauge and this did not cause the HV bias supply to turn off. Should use same setup next time.
Some sparking around 35-44kV, tripped off turbos/IG1/IG1S 3 times and so decided to ramp down.
Tried again while standing outside TH door to hear if sparking is outside the vacuum. Went to 48kV very slowy with multiple trips of the turbos, mostly TP2. Lots of sparks but easy to ramp back up to previous high point, so likely just a painful conditioning process. Current draw 167uA at 48kV. No sparks audible outside door, and vacuum response looks too large to be electrical noise.
Continued on Wednesday January 03 - went up to 53kV in the same way as before, lots of TP2 trips making its current a bit unstable... data was dumped as TM3_servicetray_conditioning_jan32023. Tried limiting the current on the power supply to very near the drain current to see if that reduces the number of trips. Didn't notice a significant effect.
Thursday, January 04, 2024, 09:57 :
Restarting conditioning, starting at 180uA at 53kV. Got up to around 60kV with many trips of the turbos, and one restart of the IG1 controller needed. Added a grounding hook to the vacuum controller rack to see if that helps reduce the trips. (doesnt appear to have).
Friday, January 05, 2024, 09:51 :
Continuing conditioning. Starting by sitting at 50kV for 10mins. No sparks observed during this time.
Even though we got to 60kV last time, onset of conditioning started at 58.6kV with a trip at 58.9kV... got up to 70kV.
Got to 72kV on Monday January 08 2024.
On Monday Jan. 15, tried to improve the grounding on the vacuum services rack to reduce sparking through the turbo controllers. Added two welding cables from the vacuum rack ground busbar to the copper grounding strip on the ground. If the spark is travelling from the faraday cage to the rack through conduit or grounding cables, maybe this will help. If it is coming through the turbo cable then it likely won't. Tried to add grounding straps on the turbo controller chassis (there is a brass screw which I think is for this purpose) but couldn't get either of the screws out with any resonable force. They undo a bit then get stuck...
Wednesday, January 17, 2024, 20:39:
David vented TM3 with N, then opened the service cap to install new insulators. We pumped back down and Alexander and I ramped back up today - instabilities started around 55kV and we were back to slow conditioning in the high 50s. Got up to a set point of 65kV. Ray did some work on the TCS bias supply and now neither the set point or readback is correct. The PSU was reading 51.5kV at set point 50kV and 60kV at set point 58kV. Will continue later...
Wednesday, January 31, 2024, 16:23
Ramped up again, some slight instabiities around 56kV but could still go up pretty quick until about 65kV. Since Ray's testing of the TCS:BIAS supply both the readback and the set point are off from the powersupply display. Ran out of time and ramped down at set point 70.5.
Set point |
Readback |
PSU reading |
63 |
64 |
65.5 |
66.5 |
67.5? |
68 |
69.5 |
70.6 |
71.5 |
70.5 |
71.7 |
73 |
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Tuesday, February 06, 2024, 14:47
Testing again after venting the module with air. First tiny spark at 48, then some vacuum reactions starting at 49 but still no issues. Bit more reactive around 53.
Set point |
Read back |
PSU reading |
53 |
53883 |
55 |
57 |
57924 |
59 |
60 |
61 |
62 |
64 |
65 |
66.5 |
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stopped at 69.4
Wednesday, February 07, 2024, 15:28 :
Ramped easily to 60kV set point and let it sit there. Didn't spark at all then after 100mins, sparked TP2 off. Otherwise first sparking happened at set point 67.
Found at limit at around 72.5 on the PSU front output, set point 70.6. think it comes from EPICS. Will have to test the power supply.... stopped there.
Thursday, February 08, 2024, 15:03 :
Long term testing. ramped back up, first spark at set point 65.
Let it sit for 2hrs 20mins. Something like 6 sparks during this time. Current also dropped significantly from 0.32A to 0.27A.

EDIT 2024-11-25, Alexander Shkuratoff:
All the StripTool data related to the above tests are on the server as the following below. Those without "Alexander" in the name were dumped by Carla.
And the StripTool settings:
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Thursday, January 11, 2024, 13:54, David Wang, Conditioning Station, Development, TM3, , TM3 servic cap air to vacumm seals leak check.
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After Tm3 service tray and service cap installation, TM3 service cap air to vacuum seals leak check has been done at TCS. TCS:IG1 and IG1S are at low E-7 torr range. leak detector base 0.0XE-9 atm.cc/sec, base pressure0.0X E-4 torr. I sprayed helium to all new air to vacuum seals on service cap. No leak on seals. The leak check has been repeated 2 times with same result. |
Wednesday, March 13, 2024, 11:12, Keith C Ng, Assembly/Bench Test, Repair, TM3, , optics tray for tm3
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Alignment notes attached for the optics tray for the refurbished tm3 with the new service and source tray.
*Note: Drive screw bracket sheared off during alignment check with source tray. The drive bracket was replaced. The optics tray was re checked. The front element was .015 to left and centered u/d. The rear element remained the same. The center element could not be checked to do the assembly. |
Friday, March 15, 2024, 10:04, Adam Newsome, South Hot-Cell, Standard Operation, TM3, , TM3 Move - SHC to NE Silo
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TM3 was moved from SHC to NE silo. Cable tray was recently installed. |
Wednesday, March 27, 2024, 09:49, David Wang, South Hot-Cell, Standard Operation, TM3, , Tm3 has been moved to SHC from silo.
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Tm3 has been moved to SHC from silo. the move is smooth. |
Thursday, March 28, 2024, 09:26, David Wang, South Hot-Cell, Standard Operation, TM3, , Tm3 has been moved from SHC to silo.
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Tm3 has been moved from SHC to silo. The move is smooth. |
Thursday, April 11, 2024, 06:07, David Wang, South Hot-Cell, Standard Operation, TM3, , Tm3 was moved from silo to SHC yesterday.
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Tm3 was moved from silo to SHC yesterday. the move is smooth. |
Thursday, April 11, 2024, 06:27, David Wang, South Hot-Cell, Development, TM3, , TM3 new source tray was transferred into SHC on this Tuesday.
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TM3 new source tray was transferred into SHC on this Tuesday. one hook arm of transfer jig is very close to optic tray tube when engaging the jig on transfer frame. tube side hook arm should go east side a little bit further to avoid the tube. Also the HS tube top lines to transfer frame beam bottom distance needs to be watched closely when hooking on the frame.Help from HC window is necessary. By watching on this details, Source tray are successfully moved into SHC with crane controlled locally in TH.Transfer frame was retrieved back to TH. It was cleaned, bagged and stored in TH. |
Friday, April 19, 2024, 10:44, David Wang, South Hot-Cell, Development, TM3, , TM3 water lines helium spray leak check at SHC.
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TM3 water lines helium spray leak check at SHC is done. No leak has been found on all lines. seeattachment |
Tuesday, April 23, 2024, 17:34, Carla Babcock, South Hot-Cell, Repair, TM3, , TM3 wire pulling
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Wires were pulled in TM3 and service cap was closed up again:
Einzel lens wire (30kV kapton), routed in the pumping duct and attached with #10 ring tongue to EZL feedthrough in service cap
4 steerer wires, routed in th pumping duct and attached with push on connectors to the 4 SHV feedthroughs on the module side panel. Coax grounding sheath is cut back by about 3cm.
Multipin cable bundle #1, routed through the left cable tube in the service tray then along the heat shield water lines (with PEEK zip ties) to feedthrough A.
Multipin cable bundle #2, routed through the right cable tube in the service tray then along the heat shield water lines (with PEEK zip ties) to feedthrough B. This bundle contains the EE wire as well, which was branched out after exiting the service tray and routed along the gas lines to the EE feedthough. It was attached with a smaller (size?) ring tongue to the EE feedthrough. Do not use this wire again, very fragile. Use the Accuglass 30kV wire instead.
The multipin wires touch the back of the water blocks in the source tray (same as in MT2/4, so far no issues with that) and they also touch the COIL lines in the service cap.
The EZL and steerer wires are routed along the floor of the service cap.
Due to the difficulty of the installation, there is no metal braid over the multipin bundles in the service cap.
Photos here : https://triumfoffice365-my.sharepoint.com/:f:/g/personal/cbabcock_triumf_ca/EslWNUST-UJKh1s8jjxWG6EBpLQEnWxgV4v-NvR4ZJjlOQ?e=Mw5vvI |
Wednesday, April 24, 2024, 10:15, David Wang, Conditioning Station, Standard Operation, TM3, , TM3 has been moved from SHC to TCS.
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TM3 has been moved from SHC to TCS. The move is smooth. |
Friday, April 26, 2024, 08:56, David Wang, Conditioning Station, Development, TM3, , TM3 module top helium spray leak test.
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TM3 module top helium spray leak test was done yesterday. No leak on TM3 module top @ LD base leak rate 0.0 x E-9 atm.cc/sec. |
Friday, April 26, 2024, 08:59, David Wang, Conditioning Station, Development, TM3, , TM3 helium pressure test and electrical check with new source tray at TCS.
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TM3 helium pressure test and electrical check with new source tray at TCS were done yesterday. The results are excellent. See attachment |
Saturday, April 27, 2024, 09:35, Carla Babcock; Alexander Shkuratoff, Conditioning Station, Development, TM3, , TM3 source and service tray testing
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Saturday, April 27, 2024, 09:35 :
Started ramping up HV, EE and EL together. First small spark at 20.5kV on bias, no reaction in other devices.
Note both BIAS and EL are off in their readbacks. See table below
BIAS set pt |
BIAS readback |
BIAS actual |
EL set pt |
EL readback |
EL actual |
24 |
24.4 |
24.5 |
14 |
13.42 |
14 |
30 |
30.52 |
31 |
16 |
15.34 |
16 |
35 |
35.6 |
36 |
19 |
18.2 |
19 |
40 |
40.65 |
41.5 |
20 |
19.16 |
20 |
45 |
45.8 |
46.5 |
22 |
21 |
22 |
50 |
50.8 |
51.5 |
25 |
23.9 |
25 |
55 |
55.9 |
57 |
27 |
25.84 |
27 |
60 |
60.95 |
62.5 |
30 |
28.7 |
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62 |
63 |
64.5 |
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66 |
67.1 |
68.5 |
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67 |
68 |
69.5 |
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69 |
70.1 |
71.5 |
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70 |
71.1 |
?? |
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70.5 |
71.7 |
73 |
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Saturday, April 27, 2024, 10:23 :
Spark on HV only at 25.5, couple sparks from here to 33, then at 33 starts real conditioning.
EL is reacting to some of the sparks, not sure if this is just electrical noise or not.
Saturday, April 27, 2024, 18:14 :
lots of trips above 60kV on the set pt. tripping off turbos and gauges. IG2 needed the controller reset.
RESULT: Got to 64.5 (actual) 62 (set point) with quite a bit of sparking over 60kV. Will go the rest of the way to 73 in the next days. Data dumped as isac/data/TM3_HVtests_Apr272024.dat
Sunday, April 28, 2024, 11:23 :
Ramped back up to 60kV reasonably easily, couple sparks and turbo trips.
Went up to 64kV (set point) with a lot of difficulty. Data dumped as isac/data/TM3_HVtests_Apr282024.dat
Monday, April 29, 2024, 14:58 :
Ramped up to set pt 62 easily, went down to 500V then 100V steps after that.
Went to set pt of 67 and left it there for ~40mins. Not perfectly stable but not too bad.
Tuesday, April 30, 2024, 17:12 :
After rebooting the TCS PLC to fix all the non-responsive devices, everything is working fine again.
Ramped easily to 60kV in 1kV steps.
Still got to 67 without too much trouble. Behaving pretty well...
At 70.2 (set pt, 71.3 readback) the water and vacuum gauge both tripped off and cannot be restarted. I am not sure what the real power supply reading is here but in the past it has been 70.5 set pt = 73 real value, which is as high as the power supply goes.
Stopping here since I'm not sure the water is circulating... the off pump says it is and the on pump says its not... left it at 70.2 for 40mins, still sparking going on (20:28 to 21:10)
Data dumped as isac/data/TM3_HVtests_Apr302024.dat
Sunday, May 05, 2024, 10:50 :
Containment box and target installed.
HV conditioning starting at 47kV.
Spark at 58kV knocked out IG1. Continuing with IG2 and IG1S.
Went up to set point of 63, readback 64. Will continue on Monday.
Data dumped: isac/data/TM3_HVtests_May52024.dat
Monday, May 06, 2024, 09:37 :
Ramping system back up.
First sparks at 50kv while raising the EL voltage (not sure if they are related).
AS: Voltage quickly up to 63 kV from 49 kV. Very smooth, no sparks or instabilities. Ramped at around 250 V steps every 10-20 seconds. First signs of instability at ~62.75 kV and definitely at 63 kV. I guess this is where it was conditioned to last. Let sit at 63 kV for a while while doing something else. It sparked once and turned off a turbo after half an hour. Starting ramping again.
AS: Spark at 65.75 kV killed IG1. Carla manually reset at 69 kV. Still working. A spark at 70.25 kV took out IG1 again.
AS: Maximum voltage reached at about 16:45. Setpoint 70.5 kV, readback 71.7 kV, PS itself ~73 kV. Carla reset IG1.
AS: 18:30, spent about 1.5 hours cumulatively at this maximum voltage. During this time it sparked about 15 times. Not long enough to tell if the spark frequency is decreasing. In the middle of this, Carla did something accidentally and caused the voltage to drop a bunch, so I manually set it to 0 V. She then reset TP1S, which was not staying on. Also, the EE and EL stayed at their respective voltages during this downtime (2 kV and 28.7 kV). I ramped the main BIAS voltage back up to the maximum voltage within 5 minutes and it was smooth all the way but sparked again at the maximum voltage. It seems conditioned up to or near the max voltage. Ramped down and turned off BIAS, EL, and EE.
AS: Dumped data to isac/data/TM3_HVtests_May62024_Alexander.dat
Tuesday, May 07, 2024, 10:02 :
Tested the EE - ramped up easily to 7kV, but then had issues maintaining the voltage. No vacuum response. Ramped down since we never use it that high anyway, though cable should be good for 10kV. More investigations later.
EDIT 2024-11-25, Alexander Shkuratoff:
Summary of StripTool data taken during this round of tests:
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Wednesday, May 01, 2024, 14:51, David Wang, South Hot-Cell, Standard Operation, TM3, , Tm3 has been moved form TCS to SHC.
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Travis and I moved TM3 from TCS to SHC this afternoon. The move is smooth. |
Thursday, May 02, 2024, 14:54, David Wang, Conditioning Station, Standard Operation, TM3, UCx#44, TM3 has been moved from SHC to TCS.
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TM3 has been moved from SHC to TCS by David and Frank. The move is smooth. |
Thursday, May 02, 2024, 14:58, David Wang, South Hot-Cell, Standard Operation, TM3, UCx#44, TM3 with UCx#44 electrical check and leak check.
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TM3 with UCx#44 electrical check and leak check are good. see attachment.
HS line 70 psi helium pressure test at TCS: no leak at 0.0xe-9 torr. |
Thursday, May 02, 2024, 15:23, David Wang, South Hot-Cell, Development, TM3, , Leak check on TM3 new containment box window line VCR fittings.
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After new containment box installation on TM3, Chad and I did a helium spray leak check on two VCR fittings on front side water lines. they are leak free.
Helium pressurize window water line to 70 psi for 3minutes. No response on leak detector which is 0.0xe-9 atm.cc/sec. |
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