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  RH-ISAC, Page 114 of 140  Not logged in ELOG logo
ID Datedown Author Category Type Module Target/Number Subject
  536   Wednesday, November 06, 2013, 10:41 David WangSouth Hot-CellRepairTM2 Installed 2 turbopumps on TM2

Bevan and I installed 2 turbo pumps on TM2. The o- ring flanges on TM2 had been cleaned before the installation.

  535   Tuesday, November 05, 2013, 10:37 chad fisherSouth Hot-CellRepairTM2 Thermocouple wire removal

The old thermocouple wire has been sucessfully removed from the module.

Thanks Bevan, Travis and David.

  534   Monday, November 04, 2013, 10:46 chad fisherSouth Hot-CellRepairTM2 TM2 Exploration

TM2 is now in the hot cell with the containment box off for inspection and eventual blank off off the water blocks.

Upon initail inspection the status (fron a hot cell point of view) is:

-Water block jig is equipped/on

-There is a thermocouple line that will need to be removed

-TM2 requires a new front containment box cover - already manufactured and waiting for installation

 

  533   Friday, November 01, 2013, 09:08 Travis CaveSouth Hot-CellStandard OperationTM2no targetmodule move

TM#2 has been moved from the north west silo to the south hot cell. The module has a field of about 3.1mSv/hr when it was lowered into the hot cell.

  532   Thursday, October 31, 2013, 11:38 Anders MjosITEStandard OperationTM3NiO#2Padlle wheel frequency measurements

with TM4 in ITW as measured today in the electrical room by David and Anders.

  531   Thursday, October 31, 2013, 10:36 David WangITWStandard OperationTM4 I moved 5 shielding blocks from ITE to ITW.

I moved 5 shielding blocks from ITW to ITE. The ITW  is configured to take proton beam.

  530   Friday, October 25, 2013, 14:09 Travis CaveSouth Hot-CellStandard OperationTM4Ta#41Target conductance

Anders Mjos wrote:

The conductance check on the electrical check was found to be outside of accepted values for the TBHT at 7.0 mOhm. A successful attempt to reduce the conductance was made by re-tightening the bolts on the TGHT legs in the SHC. Grant operated the manipulator and torqued the bolts to about 1/8 of a turn with the air ratchet. The conductance across the TGHT (A-B) could be improved from 7.0 mOhm to 6.2 mOhm by re-tightening the bolts. The value is still somewhat higher than usual, but was deemed to be acceptable. Measurements attached.

 The full electrical check was done on October 25th 2013. The results are in the attached PDF. The higher value of the conductance was dealt with see Anders Mjos elog entry for those details.

  529   Friday, October 25, 2013, 13:39 Anders MjosITEStandard OperationTM3NiO#2Padlle wheel frequency measurements

with TM4 in ITW as measured today in the electrical room by David and Anders.

 

  528   Friday, October 25, 2013, 10:26 Travis CaveITWStandard OperationTM4Ta#41module move

TM#4 with Ta#41 has been moved from the south hot cell to the west target station.

  527   Friday, October 25, 2013, 06:58 David WangSouth Hot-CellStandard OperationTM4 Leak check on TM4 target heat shield

Maico and I leak checked HS circuit after Chad installed the target. The circuit was a little bit difficult o pump down because of residue water moister inside. But once the moisture was pumped out, the pumping down was smooth and fast. The base leak rate 0.0xE-9 atm.cc/sec, base pressure 0.0xE-4 torr. Maico checked helium flow before the leak test. Then,He sprayed helium to all 3 VCR fiitings on target with 2 seconds on each one, He also flushed 10 seconds helium around the target. There were no any response during all these test time on leak detector.He checked the helium flow again after the test  and confirmed the helium flow.  The HS circuit is leak tight.

  526   Thursday, October 24, 2013, 15:54 Grant MinorSouth Hot-CellStandard OperationTM4Ta#41Target conductance

Anders Mjos wrote:

The conductance check on the electrical check was found to be outside of accepted values for the TBHT at 7.0 mOhm. A successful attempt to reduce the conductance was made by re-tightening the bolts on the TGHT legs in the SHC. Grant operated the manipulator and torqued the bolts to about 1/8 of a turn with the air ratchet. The conductance across the TGHT (A-B) could be improved from 7.0 mOhm to 6.2 mOhm by re-tightening the bolts. The value is still somewhat higher than usual, but was deemed to be acceptable. Measurements attached.

1. TGHT leg bolts were loosened, and resistance was measured very high, as expected.

2. TGHT leg bolts were then tightened, loosened, and tightened again, and the resistance improvement was then measured (from 7.0 mOhm to 6.2 mOhm).

3. Another attempt was then made to loosen and tighten to see if there would be further improvement.  The right bolt was loosened, but the left bolt was found to be quite stiff and was left as-is (not fully loosened) for fear of breaking the supporting insulator.  Both bolts were then re-tightened, and resistance was checked to be about the same as achieved during the previous loosening / tightening attempt (step 2 above).

To tighten the bolts in all cases: the air ratchet was used first to turn the bolts "air tight" (air pedal only, no manual force) and then with the air pedal held down, manual torque was applied to turn no more than 1/8th of a turn.

  525   Thursday, October 24, 2013, 15:43 Anders MjosSouth Hot-CellStandard OperationTM4Ta#41Target conductance

The conductance check on the electrical check was found to be outside of accepted values for the TBHT at 7.0 mOhm. A successful attempt to reduce the conductance was made by re-tightening the bolts on the TGHT legs in the SHC. Grant operated the manipulator and torqued the bolts to about 1/8 of a turn with the air ratchet. The conductance across the TGHT (A-B) could be improved from 7.0 mOhm to 6.2 mOhm by re-tightening the bolts. The value is still somewhat higher than usual, but was deemed to be acceptable. Measurements attached.

  524   Thursday, October 24, 2013, 11:32 Travis CaveSouth Hot-CellStandard OperationTM4no targetmodule move

TM#4 with no target has been moved from the conditioning station to the south hot cell.

  523   Thursday, October 24, 2013, 11:31 Travis CaveSpent Target VaultStandard Operation UC#7Spent target move

UC #7 has been moved from the south hot cell to the spent target vault, it was placed in pail #110 and put in slot 8B of the vault, it was 22.6mSv/hr upon removal from the hot cell. See attached PDF for vault details.

  522   Wednesday, October 23, 2013, 12:07 Travis CaveSouth Hot-CellStandard OperationTM1no targetmodule move

TM#1 with no target has been moved back to the south west silo from the south hot cell.

  521   Wednesday, October 23, 2013, 09:28 Travis CaveSouth Hot-CellStandard OperationTM1UC#7module move

TM#1 with UC #7 has been moved from the south west silo to the south hot cell.

  520   Tuesday, October 22, 2013, 17:07 Bevan MossConditioning StationStandard Operation  services shut down

 The turbo pump, roughing pump, have been turned off and the valves for venting opened. The cooling package has also been turned off.

  519   Tuesday, October 22, 2013, 17:04 Bevan MossConditioning StationStandard OperationTM4 HV testing

 This afternoon TM4 with the coil removed was tested with HV. The EINZEL LENS was first tested independently while the bias canbus was being repaired. The current on the EL looked stable at 25kV for 5 minutes. At 27.5kV the current becomes unstable and occasionally sparks. This voltage was held for 30 minutes but the current did not appear to be becoming more stable. Further extended testing would be required to determine if this can be conditioned out. At this point I would suggest the EL has a HV limit near 25kV.

The BIAS and EL were then brought up to 35kV and 17.5kV respectively. This voltage was held for 35 minutes with the BAIS only sparking twice. The module can most likely hold a higher voltage but for the next 2 runs does not require more than 35kV. Further testing was not completed due to time constraints. It is recommended during the shut down that TM4 is tested to its limits. The data from the testing has been attached.

  518   Tuesday, October 22, 2013, 16:52 Bevan MossConditioning StationRepair  Canbus base card for BIAS

 The base card in the canbus BIAS module was determined to be faulty. Dave Morris removed a card VECC to repair the conditioning station. 

  517   Tuesday, October 22, 2013, 14:23 Anders MjosITEStandard OperationTM3NiO#2Padlle wheel frequency measurements

as measured today in the electrical room by David and Anders

ELOG V2.9.2-2455