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Entry  Monday, September 30, 2013, 16:04, Bevan Moss, Conditioning Station, Repair, TM3, NiO#2, Ion gauge filament replacement  
 The filament on IG1 for TM3 was replaced by myself and Edi. The old filament did not appear to be damaged but the controller claimed it was. The
current gauge on TM3 is a single filament, ideally it would be upgraded to a double.
Entry  Tuesday, October 01, 2013, 11:00, Travis Cave, Conditioning Station, Standard Operation, TM3, NiO#2, Electrical check TM#3_elec_chk_NiO#2_CS2.PDF
TM#3 with NiO#2 electrical check at conditioning station under vacuum, see pdf for details.
Entry  Wednesday, October 02, 2013, 09:40, Bevan Moss, Conditioning Station, Standard Operation, TM3, NiO#2, HP conditioning 01102013_TM3_NiO2_TGHT_and_TBHT_ramp_up_eod.txt02102013_TM3_NiO#2_HP_testing_overnight_run.JPG02102013_TM3_NiO#2_HP_testing_overnight_run_archiver.JPG
Yesterday the TBHT was ramped to 250 amp and the TGHT was ramped to 440 amps. Attached is the data from that run the strip tool that had this screen
shot crashed but it can be recreated with the data. The TBHT ps was not reading back accurate results as such there are large steps in current or voltage
or some instability for no apparent reason. In addition to this the ramping program is still not working so the ramping was a very manual process. The
Entry  Friday, October 04, 2013, 19:05, Grant Minor, Conditioning Station, Standard Operation, TM3, NiO#2, HP Conditioning - e-mail notes from Oct 2nd to Oct 4th 
I have compiled the e-mail comments from people involved in High-Power Conditioning of TM3 w/ the new Rev 3 source tray and NiO#2 since Bevan Moss' last
log on October 2nd below:
On October 2nd at 6:35pm Friedhelm Ames wrote:
Entry  Friday, October 04, 2013, 19:39, Grant Minor, Conditioning Station, Standard Operation, TM3, NiO#2, TCS vacuum improvement w/ heaters off - 2:20 pm to 7:17pm 
Here is the change in the TCS vacuum after heaters were turned off earlier today:
2:20 pm readings
TCS:IG1 (service cap) 9.3 x 10^-7 Torr
Entry  Saturday, October 05, 2013, 14:45, Friedhelm Ames, Conditioning Station, Standard Operation, TM3, NiO#2, vacuum readings 
IG1 8.0 e-7 T
IG1S 2.5 e-6 T
IG2 4.3 e-6 T
Entry  Sunday, October 06, 2013, 00:17, Friedhelm Ames, Conditioning Station, Standard Operation, TM3, NiO#2, high voltage conditioning 
high voltage conditioning was carried out over the day up to 24 kV. i will leave it at 20 kV over night. Current is at 22 micro Amps, heaters off.
vacuum: IG1 7.7e-7
IG2 4.07 e-6
Entry  Sunday, October 06, 2013, 15:39, Friedhelm Ames, Conditioning Station, Standard Operation, TM3, NiO#2, HEATERS STARTED 
The high voltage was sparking several times during the night. It may be correlated with the cycling of the cooling water temperature and conductance.
vacuum levels at 11:00
IG1 7.5e-7 T
Entry  Sunday, October 06, 2013, 17:08, Friedhelm Ames, Conditioning Station, Development, TM3, NiO#2, trip of all power supplies 
All power supplies tripped on high conductivity of the cooling water < 5 MOhm, It is not clear if this was caused by a spark or vice versa. According
to the strip tool for this signal the resistance of the water went up. There might be a fault in this signal. I do not have permission to force this signal
so I keep the heaters off. We should revisit the interlock conditions, this signal should not be included in the interlocks for the heaters. Both target
Entry  Sunday, October 06, 2013, 20:28, Friedhelm Ames, Conditioning Station, Standard Operation, TM3, NiO#2, turbo pumps stopped 
vacuum readings before stopping
IG1: 7.4e-7 T
IG2 3.8 e-6 T
Entry  Friday, October 18, 2013, 14:37, Bevan Moss, Conditioning Station, Standard Operation, TM4, , Roughing Started 
 The roughing pump has been started.
Entry  Friday, October 18, 2013, 15:55, Bevan Moss, Conditioning Station, Standard Operation, TM4, , Turbo Pumps are on 
 The Turbo pumps are now running on TCS
Entry  Monday, October 21, 2013, 10:52, Bevan Moss, Conditioning Station, Standard Operation, TM4, , Cooling On and Electrical Connections Made 
 The electrical connection have been made and cooling package was started at ~10:50am today
Entry  Monday, October 21, 2013, 12:29, Bevan Moss, Conditioning Station, Repair, TM4, , BIAS Canbus 
 There is something wrong with the BIAS canbus controller. It says that it is not alive and has timed out. I have tried unplugging it and plugging
it back in but that has not resolved the problem as it normally does. I have contacted Dave Morris and am waiting to hear from him. I cannot HV test without
this controller.
Entry  Tuesday, October 22, 2013, 16:52, Bevan Moss, Conditioning Station, Repair, , , Canbus base card for BIAS  
 The base card in the canbus BIAS module was determined to be faulty. Dave Morris removed a card VECC to repair the conditioning station. 
Entry  Tuesday, October 22, 2013, 17:04, Bevan Moss, Conditioning Station, Standard Operation, TM4, , HV testing 22102013_TM4_Coil_removed_EL_testing_(1).txt
 This afternoon TM4 with the coil removed was tested with HV. The EINZEL LENS was first tested independently while the bias canbus was being repaired.
The current on the EL looked stable at 25kV for 5 minutes. At 27.5kV the current becomes unstable and occasionally sparks. This voltage was held for 30
minutes but the current did not appear to be becoming more stable. Further extended testing would be required to determine if this can be conditioned out.
Entry  Tuesday, October 22, 2013, 17:07, Bevan Moss, Conditioning Station, Standard Operation, , , services shut down 
 The turbo pump, roughing pump, have been turned off and the valves for venting opened. The cooling package has also been turned off.
Entry  Tuesday, November 12, 2013, 12:43, Bevan Moss, Conditioning Station, Standard Operation, TM2, , TM2 moved from SHC to TCS 
 TM2 was moved by myself and David from the SHC to the TCS. Move went well. Curiously the fields on the module were measured higher than the previous
measurement (now ~5.8mSv/hour) .
Entry  Tuesday, November 12, 2013, 14:31, Bevan Moss, Conditioning Station, Standard Operation, TM2, , Turbo pumps started 
 The turbo pumps have been started on TM2 and the conditioning station.
Entry  Tuesday, November 12, 2013, 14:33, Bevan Moss, Conditioning Station, Repair, , , Cooling manifold returned 
 The cooling manifold for the conditioning station high power water cooled lines has been returned. The cooling package can once again be operated
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