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  Evaporator_1, Page 11 of 15  Not logged in ELOG logo
ID Date Author Target Material Target Oven W.O# Source Status Subject
  95   Friday, June 13, 2014, 15:21 John WongUC239165-10LP-SISDoneConditioning UCx#10

Friday, June 13, 2014, 15:02

Target container was previously coated and sintered with TaC.  It's wrapped with 3-layers of Ta heat shield, including the center block.

The target consists of 280 discs of UCx with 9cm in length.

A regular TaC coated/sintered endcap is inserted on right, wrt to the ionizer tube pointing down, so the left end is open with no cap to allow out-gassing.

The chamber is being dumping down.

TGHT will be ramped up to 520A - keep heating at that current for ~4 to 5 hours.

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac. The auto-ramping rate is set to 0.1A/min.


 Friday, June 13, 2014, 16:26

Pressure at 1.9e-5 Torr. 

Initiate auto-ramping- stepping up from 0A at 0.1A/min - leaving for the weekend.


 Wednesday, June 25, 2014, 11:45

TGHT has reached 520A and target has been conditioned at that current for 13hrs. 

Auto-cooling initiated at 2A/min.

Once the target is cooled, the chamber will be vented in Ar.


 Friday, July 04, 2014, 10:06

Process is complete.  Target is stored in the Ar-glove box and ready for assembly.


 

  94   Wednesday, May 21, 2014, 11:41 John WongUC2 TARGET BOATIn progressTests: Sintering carbon Mesh coated with UC2

Tuesday, May 20, 2014, 16:01

Target boat contains one pellet of carbon mesh coated with UC2.  The sample was prepared in the Ar-glove box and the container is wrapped with 2 layer of Ta foil (it wasn't easy to do the wrapping).

Chamber is currently being pumped down.

TGHT will be heated up to 600A. 


Wednesday, May 21, 2014, 11:40

Chamber has been pumped down overnight, vac @ 6.7e-6 Torr.


Tuesday, May 27, 2014, 10:51 

TGHT was heated up to 600A and stayed for 12hrs before cooled down (see attachment).

EDX/SEM/XRD will be done soon...

More information about this sample structure can be found here: https://www.dropbox.com/sh/hirm808pgjwzg71/AAB1-kP399IbIa8AGdI-OMGua


 Friday, June 13, 2014, 14:57

Chamber was vented and cleaned for UCx target production. 

Will re-visit this later...


 

Attachment 1: Vac_Cur_plot.PNG
Vac_Cur_plot.PNG
  93   Wednesday, April 30, 2014, 14:58 John WongUC239165-9LP-SISDoneConditioning UCx#9

Wednesday, April 30, 2014, 14:50

The target container was previously coated with TaC and sintered in Evap 2.

The target is loaded with 250 discs of UCx (material from batch#09_06022014)

Total length = 9.3cm

The container is wrapped with 3 layers of Ta-heat shield, including the back block.

A regular TaC coated/sintered endcap is inserted on left, wrt to the ionizer tube pointing out of the page, so the right end is open with no cap to allow out-gassing.

(Did not use a D-cap... This worked for UCx#8. Need to be careful when handling the target!)

The chamber is being dumping down.

TGHT will be ramped up to 520A - keep heating at that current for ~4 to 5 hours.

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac. The auto-ramping rate is set to 0.1A/min.


 Wednesday, April 30, 2014, 16:41

Vacuum at 1.5 e-5 Torr.  Stepped up TGHT to 25A.


 Wednesday, April 30, 2014, 17:42

Pressure 9.2 e-6 Torr.  Initiate auto-heating.


 Friday, May 16, 2014, 16:02

Conditioning complete. (see attachment)

End-caps need to be expended before assembly.


 

Attachment 1: UCx#9_final_conditioning.PNG
UCx#9_final_conditioning.PNG
  92   Monday, March 24, 2014, 17:53 John WongUO2/C TARGET BOATDoneProcessing UC2Flk_02

 Monday, March 24, 2014, 17:50

UO2/C cast was prepared on March 21 and let dry over the weekend.  The cast looks pretty good, and it was rolled up and wrapped in a piece of graphite sheet. 

 

The Ta-target boat was wrapped with 3-layers of heat shield and installed in EVAP1.

Chamber is currently being pumped down.

Target will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Tuesday, March 25, 2014, 15:55

Chamber has been pumped down to 6.8e-6 Torr. BP 47mTorr.

Stepping up TGHT 35A/0.264V.  Vac stabilizing at 6.0e-5 Torr. 


Tuesday, March 25, 2014, 17:43

Auto-ramping initiated.


 Friday, April 11, 2014, 11:49

TGHT reached to max 520A.

Carbonization process is complete (see attachment)

IG at 9.3e-6 Torr.

 Cooling down TGHT at 2A/min

Will vent the chamber with Ar on Monday


 Monday, April 14, 2014, 16:41

UC2 flakes was removed from the chamber and transferred in to the Ar glovebox.

Evap off.


 

Attachment 1: UC2_flakes_batch#09-03242014.PNG
UC2_flakes_batch#09-03242014.PNG
  91   Wednesday, March 05, 2014, 23:05 John Wong  TARGET BOATDoneRe-sinterring end caps

Laura Lambert wrote:

John Wong wrote:

Tuesday, March 04, 2014, 15:43

Theses endcaps (4) were previously sinterred in Evap#2 but some surfaces were not fully sinterred. (See Evaporator2 E-log ID119: https://elog.triumf.ca/TIS/Evaporator_2/119)

The endcaps are inserted in a target boat wrapped with 3 heat-shields. 

Chamber is currently being pumped down. 

TGHT will be rampped up to 580A and heat for >4hrs.


 

 Wednesday, March 05, 2014, 10:20

IGP1 = 9.2e-7 Torr.

TGHT was stepped up to 35A and stabilized after half an hour.

Auto-ramp initiated at 2.0A/min, max setpoint = 580A.

Vacuum started to climb too fast, auto-ramp aborted.

Will step up manually...


 Wednesday, March 05, 2014, 12:18

Slowly stepped up to 100A manually.

Vacuum stable.

Initiating auto-ramp at 1.0A/min


 Wednesday, March 05, 2014, 13:17

IGP1 = 9.8e-6 Torr.

Current = 200A

Vacuum stable.

Stepping ramping rate up to 2.0A/min.


 Wednesday, March 05, 2014, 16:12

IGP1 = 4.6e-5 Torr, TGHT = 548A

Stopped auto-ramp to allow vacuum to settle back down.

Waited ~10min

IGP1 = 3.6e-5 Torr

Re-initiating auto-ramp at 2.0/min


 

 Wednesday, March 05, 2014, 23:02

End caps have been heated for 6.5 hours at 580A. Vac @ 7.4e-6 Torr. 

Auto-cooilng initiated at 2A/min. 


 Thursday, March 06, 2014, 14:48

The TaC on the endcaps is fully sinterred. (see attachment#1).

 


 

Attachment 1: endcaps_Mar3_2014.PNG
endcaps_Mar3_2014.PNG
  90   Wednesday, March 05, 2014, 10:30 Laura Lambert  TARGET BOATIn progressRe-sinterring end caps

John Wong wrote:

Tuesday, March 04, 2014, 15:43

Theses endcaps (4) were previously sinterred in Evap#2 but some surfaces were not fully sinterred. (See Evaporator2 E-log ID119: https://elog.triumf.ca/TIS/Evaporator_2/119)

The endcaps are inserted in a target boat wrapped with 3 heat-shields. 

Chamber is currently being pumped down. 

TGHT will be rampped up to 580A and heat for >4hrs.


 

 Wednesday, March 05, 2014, 10:20

IGP1 = 9.2e-7 Torr.

TGHT was stepped up to 35A and stabilized after half an hour.

Auto-ramp initiated at 2.0A/min, max setpoint = 580A.

Vacuum started to climb too fast, auto-ramp aborted.

Will step up manually...


 Wednesday, March 05, 2014, 12:18

Slowly stepped up to 100A manually.

Vacuum stable.

Initiating auto-ramp at 1.0A/min


 Wednesday, March 05, 2014, 13:17

IGP1 = 9.8e-6 Torr.

Current = 200A

Vacuum stable.

Stepping ramping rate up to 2.0A/min.


 Wednesday, March 05, 2014, 16:12

IGP1 = 4.6e-5 Torr, TGHT = 548A

Stopped auto-ramp to allow vacuum to settle back down.

Waited ~10min

IGP1 = 3.6e-5 Torr

Re-initiating auto-ramp at 2.0/min


 

  89   Tuesday, March 04, 2014, 15:48 John Wong  TARGET BOATIn progressRe-sinterring end caps

Tuesday, March 04, 2014, 15:43

Theses endcaps (4) were previously sinterred in Evap#2 but some surfaces were not fully sinterred. (See Evaporator2 E-log ID119: https://elog.triumf.ca/TIS/Evaporator_2/119)

The endcaps are inserted in a target boat wrapped with 3 heat-shields. 

Chamber is currently being pumped down. 

TGHT will be rampped up to 580A and heat for >4hrs.


 

  88   Wednesday, February 05, 2014, 14:29 Laura LambertUO2/C40282-1TARGET BOATDoneProcessing UC2Flk_01

 Wednesday, February 05, 2014, 14:13

1st attempt:

UO2/C green was prepared on Feb 4, 2014 [tues]. The slurry was cast on a piece of glass coated with WD40.

The cast was let dry until Feb 5, 2014 [wed] - the cast was cracked and too much WD40 was used because there were oil patches [see attached photo: cast1]; however, the cast peeled off the glass very nicely.

2nd attempt:

Due to cracked and oil patches, decided to re-mill and try again.

Scrapped off cast, added the additional compositions:

1g PEG400, 1g Glycerol, 14g 5% PVA, 2mL n-butanol, 2mL methanol, 20mL DI H2O

Re-milled for 3 hours and cast onto glass coated with slightly less WD40.

Before even allowing cast to dry, can see the slurry is far too thick. The slurry would not spread at all.

Will let dry overnight and attempt to scrape off and re-mill with more DI H2O tomorrow.


 Thursday, February 06, 2014, 10:57

Second cast was a lot thicker, but peeled off the glass nicely, will not re-cast. [see attached photo: cast2]

Some material was stuck to the WC jar wall and the balls, same as previously.

Initial UO2 powder used = 50.24g (Inventory R-00855A UO2 + bottle = 695.52g before use)

Graphite powder used = 10.05g

1st attempt = did not measure

2nd attempt dried UO2/C + organic mass = 46.56g (expecting to lose more uranium from re-casting a second time/ sticking to jar + balls)

The green was rolled up and wrapped in a piece of graphite sheet. [see attached photo: target boat]

The Ta-target boat was wrapped with 3-layers of heat shield and installed in EVAP1.

Chamber us currently being pumped down.

Target will be ramped up to 520A at the rate of 0.1A/min.

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr.


 Friday, February 07, 2014, 10:15

Chamber has pumped down overnight. IG1 currently @ 2.4e-6 Torr.

 Stepped up TGHT to 35A/0.187V.


Friday, February 07, 2014, 12:02 

TGHT sat at 35A for 2hrs. Pressure took a while to fully stabilize, currently sitting at 1.9e-5 Torr [see attached photo: pre auto-ramp]

Initiating auto-ramping.


 Monday, February 24, 2014, 13:37

TGHT reached max setpoint of 520A on friday night.

Power = 5.45V

IGP1 = 3.2e-6 Torr.

Carbonization process is complete.

Initiating auto-cooling at 2.0A/min.


 Thursday, October 09, 2014, 13:41

update rename: batch #09 - 02062014 to UC2Flk_01


 

 

 

 

Attachment 1: UO2_cast1.jpg
UO2_cast1.jpg
Attachment 2: UO2_cast2.jpg
UO2_cast2.jpg
Attachment 3: UO2_target_boat.jpg
UO2_target_boat.jpg
Attachment 4: pre_auto-ramp.JPG
pre_auto-ramp.JPG
  87   Monday, January 27, 2014, 11:03 Laura LambertEmpty40282-1TARGET BOATDoneSintering Ta target boat with TaC coating

Laura Lambert wrote:

Laura Lambert wrote:

Thursday, January 23, 2014, 16:26 

 A new target boat was sprayed with TaC coating and let dry, the coating appeared slightly bubbly once dried [see attached photos].

The target boat was wrapped with 3-layers of Ta-heat shield.

The boat was installed in Evap#1, chamber is currently being pumped down overnight.


 

 Friday, January 24, 2014, 14:42

Chamber was pumped down to 5.9e-6 Torr overnight.

TGHT was stepped up to 35A.

Waited 20min, vacuum consistently stable, auto-ramp initiated at 0.2A/min and max setpoint to 580A.

Good vacuum: 5e-5 Torr. Bad vacuum: 6e-5 Torr.


 

 Monday, January 27, 2014, 11:01

TGHT reached 580A over the weekend.

TGHT auto-cooldown initiated at 2.0A/min.


 Tuesday, January 28, 2014, 15:51

Chamber cooled down overnight, vented and opened up this morning.

Target boat looks good! [See attached photos]


 

Attachment 1: IMG_20140128_113257662.jpg
IMG_20140128_113257662.jpg
  86   Friday, January 24, 2014, 14:45 Laura LambertEmpty40282-1TARGET BOATIn progressSintering Ta target boat with TaC coating

Laura Lambert wrote:

Thursday, January 23, 2014, 16:26 

 A new target boat was sprayed with TaC coating and let dry, the coating appeared slightly bubbly once dried [see attached photos].

The target boat was wrapped with 3-layers of Ta-heat shield.

The boat was installed in Evap#1, chamber is currently being pumped down overnight.


 

 Friday, January 24, 2014, 14:42

Chamber was pumped down to 5.9e-6 Torr overnight.

TGHT was stepped up to 35A.

Waited 20min, vacuum consistently stable, auto-ramp initiated at 0.2A/min and max setpoint to 580A.

Good vacuum: 5e-5 Torr. Bad vacuum: 6e-5 Torr.


 

  85   Thursday, January 23, 2014, 16:29 Laura LambertEmpty40282-1TARGET BOATIn progressSintering Ta target boat with TaC coating

Thursday, January 23, 2014, 16:26 

 A new target boat was sprayed with TaC coating and let dry, the coating appeared slightly bubbly once dried [see attached photos].

The target boat was wrapped with 3-layers of Ta-heat shield.

The boat was installed in Evap#1, chamber is currently being pumped down overnight.


 

Attachment 1: IMG_20140123_143448877.jpg
IMG_20140123_143448877.jpg
Attachment 2: IMG_20140123_143507747.jpg
IMG_20140123_143507747.jpg
  84   Monday, December 02, 2013, 16:10 Anders Mjos   DoneCopper bar on TGHT

The conductivity of the TGHT circuit will be measured with a copper bar shunt.

Monday, December 02, 2013, 16:00: Pumping down. 

Tuesday, December 03, 2013, 09:40: Stepped current up to 600A. Impedance of system ~0.7 mOhm. See attached graph for P(I).

Tuesday, December 03, 2013, 12:06: Stopped turbo. Vacuum at 1.3E-5 Torr

Wednesday, December 04, 2013, 09:20: Copper bar removed from vacuum chamber.

Test finished.

Attachment 1: Current_and_Voltage.pdf
Current_and_Voltage.pdf
  83   Monday, December 02, 2013, 16:09 Anders Mjos   Problems resolvedTGHT connector repositioned and tightened

The right connector for the TGHT had rotated. It has now been repositioned and both connectors have been tightened to reduce the chance for further rotation.

Attachment 1: Evap1_rotated_TGHT_conductor_2013-12-02.pdf
Evap1_rotated_TGHT_conductor_2013-12-02.pdf Evap1_rotated_TGHT_conductor_2013-12-02.pdf
  82   Friday, November 01, 2013, 13:08 Anders Mjos   MaintenanceGloves, window and window gasket replaced.

Work covered under work permit 2013-11-01-3 and performed by Anders and Rick with the help of Danno (RPG).

No significant contamination was found during the work. The old window could be disposed as normal waste.

  81   Friday, October 11, 2013, 18:10 John WongUC239814-IVLP-IG-LISDoneUCx#8 - Final Conditioning

 Friday, October 11, 2013, 18:00

 

The target container was previously coated with TaC and sintered in Evap 2.

The target is loaded with ??? discs of UCx (material from batch #???)

Total length = ???

The container is wrapped with 3 layers of Ta-heat shield, including the back block.

A regular TaC coated / sintered endcap is inserted on left, wrt the ionizer tube pointing out of the page. The right end is open with no cap.

The chamber is pumping down.


Instructions for conditioning the UCx target:

1. TGHT will need to heat up to ~ 175A to burn off the organics.

    Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac. The auto-ramping rate is set to 0.1A/min.

2. Once the organics have burnt off, ramp down the TGHT to 0A at 2A/min.

3. Purge the glovebox with argon gas.

4. Vent the chamber with Ar gas. Close the valve when it is completely vented.

5. Remove the target. Be careful the left end (view from the top) is open with the D-cap.

6. Clean the chamber with TCE and remove all the gunge.

7. Install the target back

8. Pump down the chamber to at least low 10e-6 Torr before begin the final carbonization process.

9. Auto-ramp the TGHT current to 175A at 1A/min.

10. Once the TGHT reach to 175A. Auto-ramp TGHT to 520A at 0.1A/min.

11. At 520A, keep heating the target for at least 4-5 hours.

12. Auto ramp TGHT to 0A at 2A/min.

13. Purge the glovebox with argon for at least 5 min.

14. Vent the chamber with argon gas. Close the valve when it is completely vented.

15. Remove the target from the chamber and put in the "orange james bond box" and transport to the Ar-glove box.


Friday, October 11, 2013, 18:03 
 
Chamber has been pumping down, IG1 currently at 1.58e-6 Torr.
 
TGHT stepped up to 25A and auto ramping initiated... 

 Monday, October 21, 2013, 11:29
 
TGHT to max current at 520A and heated for about 2 days (over the weekend).
 
IG came down to 4.6 e-6 Torr.
 
Cooling down initiated at 2A/min.

 

 

  80   Friday, October 04, 2013, 15:56 John WongEmpty LP-SISDoneIgnore this entry - Process was done in Evap2

Friday, October 04, 2013, 15:37

A LP target container is coated with TaC.  The container is wrapped with 3 layers to heat shield.  

This container will be used for the graphite tube test.  

Chamber is being pumped down.

 The HS cooling water valves are open and no leaks are detected. 


 

TGHT will be ramped up to 580A at 0.2A/min

TBHT will be ramped up to 230A at 0.2A/min.

The temperature will be monitored and measured. 


 


 

  79   Friday, September 20, 2013, 13:49 John WongUO2/CTarget Boat #2 DoneProcessing UC2Flk_00

Laura Lambert wrote:

Thursday, September 19, 2013, 15:35

UO2/C green was prepared on Aug 17, 2013. The slurry was cast on a piece of glass coated with WD40.

The cast was let dry until Aug 19, 2013.

Initial UO2 powder used = 49.97g (Inventory R-00835A UO2 + bottle = 745.42 before use)

Graphite powder used = 10.12g

Green cast dried UO2/C + organic mass = 59.62g

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-Ta layers of heat shield and installed in Evap1 on Sept 19, 2013.

Chamber is currently being pumped down. IG1 @ 9.97e-12T.

Target will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr


 

 Friday, September 20, 2013, 13:48

Chamber has been pumped down overnight.  IG at 6.2e-6 Torr, BP @ 32mT.

Stepping up TGHT to 30A.


 Friday, September 20, 2013, 15:12

TGHT auto ramping initiated.  


 Monday, October 07, 2013, 14:09

TGHT has reached to 520A/5.5V.

Vac at 7.7e-6 Torr. 

The carbonization process is complete.

Auto-cooling is initiated at 2A/min, and the chamber will be vented in Ar after the target is cooled.


 Thursday, October 09, 2014, 13:36

*update* RENAME: batch #07 - 09192013 to UC2Flk_00 used for UCx#11


 

  78   Thursday, September 19, 2013, 15:41 Laura LambertUO2/CTarget Boat #2 In progressProcessing UC2 flakes (batch #07 - 09192013)

Thursday, September 19, 2013, 15:35

UO2/C green was prepared on Aug 17, 2013. The slurry was cast on a piece of glass coated with WD40.

The cast was let dry until Aug 19, 2013.

Initial UO2 powder used = 49.97g (Inventory R-00835A UO2 + bottle = 745.42 before use)

Graphite powder used = 10.12g

Green cast dried UO2/C + organic mass = 59.62g

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-Ta layers of heat shield and installed in Evap1 on Sept 19, 2013.

Chamber is currently being pumped down. IG1 @ 9.97e-12T.

Target will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr


 

  77   Tuesday, September 10, 2013, 12:20 Laura LambertUO2/CTarget Boat #2 DoneProcessing UC2 flaskes (batch#06 - 08222013

John Wong wrote:

John Wong wrote:

Thursday, August 22, 2013, 17:31

1st attempt:

UO2/C green was prepared on Aug 14, 2013 (wed).  The slurry was cast on a piece of glass coated with WD40.

The cast was let dry until Aug 26 (Mon) - couldn't peel off from the glass. 

2nd attempt:

So, scrapped off cast, mixed with 30ml H20 in the WC jar, re-milled for 3 hrs, and cast/let dry over night  - SAME SHIT! couldn't peel off!  Don't understand why?!

3rd attempt:

scrapped off, added the additional compositions:

1g PEG400,1g Glycerol, 10g 7% PVA, 2ml n-butanol, 2ml methonal, 20ml DI H2O.

Re-milled for 3 hours, cast and let dry!  Wahlaa... it works! (See attachment#1: pretty uranium pancake!)

However... During this process, some lost of uranium was resulted.  The slurry was more viscous than normal.  Some material was stuck to the WC jar wall and the balls.

Initial UO2 powder used = 50.14g (Inventory R-00835A UO2 + bottle = 795.56 before use)

Graphite powder used = 10g.

1st attempt dried UO2/C + organic  mass = 55.75g

2nd attempt = didn't measure

3rd attempt + additional org mass = 44.5g  (expecting to loss more uranium from the scraping/sticking to jar/balls)

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-Ta layers of heat shield and installed in Evap1 on Aug 22, 2013.

Chamber is currently being pumped down. IG1 @ 2.4e-4 Torr.

Target will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr


 

 

 Friday, August 23, 2013, 15:08

The chamber wasn't pumping down well; there was a problem with the seal on the lid.

Rick M. replaced it. 

The chamber is currently being pumped down;  it seems OK!


 

 Tuesday, September 10, 2013, 12:13

The TGHT reached zero on Monday and the chamber was left under vacuum overnight at 1.3e-6 Torr.

The chamber was accidentally vented in air until ~25mTorr for ~10min, then it was quickly pumped down again for ~10min before it was vented in Ar.

The chamber was vented in Ar and the UC2 flakes were transported into the Ar-glove box.

The process is complete 


 

  76   Friday, August 23, 2013, 16:11 John WongUO2/CTarget Boat #2 Problems resolvedProcessing UC2 flaskes (batch#06 - 08222013

John Wong wrote:

Thursday, August 22, 2013, 17:31

1st attempt:

UO2/C green was prepared on Aug 14, 2013 (wed).  The slurry was cast on a piece of glass coated with WD40.

The cast was let dry until Aug 26 (Mon) - couldn't peel off from the glass. 

2nd attempt:

So, scrapped off cast, mixed with 30ml H20 in the WC jar, re-milled for 3 hrs, and cast/let dry over night  - SAME SHIT! couldn't peel off!  Don't understand why?!

3rd attempt:

scrapped off, added the additional compositions:

1g PEG400,1g Glycerol, 10g 7% PVA, 2ml n-butanol, 2ml methonal, 20ml DI H2O.

Re-milled for 3 hours, cast and let dry!  Wahlaa... it works! (See attachment#1: pretty uranium pancake!)

However... During this process, some lost of uranium was resulted.  The slurry was more viscous than normal.  Some material was stuck to the WC jar wall and the balls.

Initial UO2 powder used = 50.14g (Inventory R-00835A UO2 + bottle = 795.56 before use)

Graphite powder used = 10g.

1st attempt dried UO2/C + organic  mass = 55.75g

2nd attempt = didn't measure

3rd attempt + additional org mass = 44.5g  (expecting to loss more uranium from the scraping/sticking to jar/balls)

The green was rolled up and wrapped in a piece of graphite sheet.

The Ta-target boat was wrapped with 3-Ta layers of heat shield and installed in Evap1 on Aug 22, 2013.

Chamber is currently being pumped down. IG1 @ 2.4e-4 Torr.

Target will be ramped up to 520A at the rate of 0.1A/min

Vacuum limit stop at 5.0e-5 Torr, backing off at 6.0e-5 Torr


 

 

 Friday, August 23, 2013, 15:08

The chamber wasn't pumping down well; there was a problem with the seal on the lid.

Rick M. replaced it. 

The chamber is currently being pumped down;  it seems OK!


 

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