Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 98 of 138  Not logged in ELOG logo
ID Date Author Category Type Module Target/Number Subjectdown
  1833   Thursday, November 29, 2018, 06:38 David WangSouth Hot-CellStandard OperationTM4 Leak check TM4 UCx 26 at SHC.

Chad and I did a leak check on TM4 HS line with UCx 26# installed . Base LR 0.0X E-9 atm.cc/sec. Base pressure 0.0XE-4 torr.  No response on leak detector during leak check.

  1799   Wednesday, October 03, 2018, 14:16 David WangSouth Hot-CellStandard OperationTM4Ta #57Leak check TM4 Lp Ta# 57 at SHC.

Tried to leak check TM4 Ta57# at TCS. LD failed to pump down properly at fine range. It always tripped at 4 torr. I cheeked all vacuum lines seals and adapters on top of module to LD. Everything is good. Chad said the VCRs at SHC can not be tightened any more. Discussed with Anders, we decide to move module TCS and helium pressure test there.  The same difficult happened last time on TM4 UCx24# at SHC when leak check. But,it is solved by pressurize the line at SHC last time.  

The HS line was pressurized with 70 psi helium on Oct 04th at TCS.. LD 0,00X E-9atm.cc/sec no change in 2 minutes. No leak.

  310   Monday, April 22, 2013, 09:33 David WangConditioning StationRepairTM3 Leak check TM3 at conditioning station

TM3 leak check at conditioning station without target: TM3 all air to vacuum seals have been leak checked . They are all good. Water lines TAR(+-), TUBE(+-), GAS, MSP , COIL2(+-), EE, HS(1,2) , GE,and WINDOW have been helium pressurized to 70 psi for 2 minutes each . No response had been found on leak detector. They are leak tight.. Leak detector BR 0.0xE-9atm.cc/sec, BP 0.0xE-4 torr. TM3 and CS vacuum: PNG15.2xE-6 torr, IG1 8.8xE-7 torr,IG2 2.8xE-6torr, IG1S 1.3xE-6 torr.      

  591   Tuesday, February 04, 2014, 08:04 David WangSouth Hot-CellRepairTM2 Leak check TM2 tube heater (+) water line.

Chad and I leak checked TM2 tube heater(+) water line yesterday afternoon. The water line was difficult to pump down on base leak rate, but LD  base pressure was fine . The base pressure on leak detector was pumped to 0.0XE-4 torr quickly. The base leak rate only could be pumped  to  4.5 xE-8 atm.cc/sec after 1 hour waiting time. All vacuum connections to leak detector  in the target hall were leak checked and they were good. Chad checked helium flow in SHC. He sprayed helium twice on tube heater(+) water block soldering joints. I did not see any response on leak detector in TH.The base Leak rate and base pressure did not move up during the test.  See attachment pictures.

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  593   Wednesday, February 05, 2014, 14:05 David WangSouth Hot-CellRepairTM2 Leak check TM2 tube heater (+) water line from inside service cap in TH.

Bevan and I did a leak check on TM2 tube heater+ from inside service cap in TH. The leak detector base leak rate 0.0xE-9 atm.cc/sec, base  pressure 0.0xE-4totrr. One of side panel on service cap was opened. Bevan sprayed the helium to the "D" line inside the blue insulator.The helium flow was checked , and he sprayed twice. No response has been found on leak detector.  See attachment pictures

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  597   Thursday, February 13, 2014, 09:24 David WangSouth Hot-CellRepairTM2 Leak check TM2 tube heater (+) water line with rubber insert blocked WB in SHC

Chad and I  did the Leak checked TM2 tube heater (+) water line  with rubber insert plugged water block on " D"  in SHC. The Leak detector was very easy to pump down to the bottom leak rate and pressure. Chad checked the helium flow in SHC, and sprayed 10 second helium on  the block. There is no response had been found during the test. The test was repeated again and no leak has been found. See attachment pictures.

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  467   Thursday, September 26, 2013, 09:46 maicodallavalleConditioning StationRepairTM3 Leak check / Pressure Test

TM3 has had all of the water lines pressurized with Helium and the Helium Leak detector was connected to the turbo pumps. There were no leaks detected.

  469   Thursday, September 26, 2013, 14:37 Bevan MossConditioning StationStandard OperationTM3NiO#2Leak check / Pressure Test

maicodallavalle wrote:

TM3 has had all of the water lines pressurized with Helium and the Helium Leak detector was connected to the turbo pumps. There were no leaks detected.

 While pressurizing the lines it was found some of the lines had water in them. It is unknown where this water came from. Perhaps David connected the conditioning station last time it was in? Lines that were free of water were A, B, C, and window The leak detector pumped down to 4.0 x 10^-3 Torr and the leak rate was 1.4 x 10^-9 atm-cc/sec, there was no response during the leak test and the leak rate continued to decrease during the test.

  726   Thursday, August 07, 2014, 13:58 David WangSouth Hot-CellStandard OperationTM4UCx #10Leak check on TM4 HS water line with new UCX target.

Isaac and I leak checked TM4 HS line with new UCX target. The leak detector base LR 0.0xE-9 atm.cc/sec, base pressure0.0xE-4torr. Isaac sprayed helium  on both VCR connections(5 seconds each) and flushed helium around the target for 6 seconds. No response on leak detector.

  872   Wednesday, March 25, 2015, 14:25 David WangSouth Hot-CellStandard OperationTM4Ta#45Leak check on TM4 HS water line with new Ta#45 target. at SHC

Chad and I leak checked TM4 HS water line with new Ta#45 target installed at SHC. Leak detector base leak rate 0.0Xe-9 atm.cc/sec, base pressure 0.0Xe-4 torr. Chad sprayed helium twice on each of HS 2 VCR joints.No leak has been found. The joints are leak tight. The helium pressure test  will be done at CS later.

  755   Wednesday, September 24, 2014, 15:03 David WangSouth Hot-CellStandard OperationTM4Ta#44Leak check on TM4 HS water line with new Ta#44 target. at SHC

This morning Chad and I leak checked TM4 HS line with new Ta#44 target installed. I calibrated LD before the check. Before check, the LD base LR 0.0xE-9 atm.cc/sec, base LP 0.0xE-4 torr. Chad sprayed helium on both VCR fittings and did a flush around the target. There is no any response had been found on LD,. The line is good on leak tight. with spray method.  No helium pressure test on the HS line at CS since TM4 was moved back to ITE directly.

  632   Wednesday, March 26, 2014, 06:57 David WangSouth Hot-CellStandard OperationTM4Ta#42Leak check on TM4 HS water line with new Ta #42 target.

Chad and I leak checked TM4 HS line with Ta#42 target on the module. The leak detector base LR 0.0xE-9 atm.cc/sec, base pressure0.0xE-4 torr. Chad applied helium to the joints, and flushed the helium around the target. No leak has been found.I will do helium pressure test on this circuit at CS later.

  927   Tuesday, June 02, 2015, 14:32 David WangSouth Hot-CellStandard OperationTM4SiC #31Leak check on TM4 HS water line with new SiC #31 target. at SHC

Chad and I leak checked TM4 HS water line with SiC #31 target installed. leak rate:0.0xE-9atm.cc/sec.  No leak.  The line will be helium pressurized at CS later.

2015-06-03, helium pressure test the line at CS. 70psi 3 minutes. leak rate 0.0xE-9 atm.cc/sec. No leak.   See attachments

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  1016   Monday, July 27, 2015, 15:34 David WangITEStandard OperationTM4 Leak check on TM4 HS water line with new UCX target. at SHC

Chad and I leak checked the HS line at SHC after UCX target installation. On first round helium spray, one of VCR fitting has a leak to E-6 atm.cc/sec range. Chad tightened the fitting, and solved the problem. We leak checked both VCR fittings twice. No leak. The line will be helium pressured at CS tomorrow.

  1075   Tuesday, September 22, 2015, 13:15 David WangSouth Hot-CellStandard Operation Ta#46Leak check on TM4 HS water line with new Ta#46 target. at SHC

Chad and I leak checked the HS line at SHC. No leak. Leak rate 0.0xE-9atm.cc/sec.

  692   Thursday, June 26, 2014, 10:57 David WangSouth Hot-CellStandard OperationTM3 Leak check on TM3 HS water line with new target. installed.

Chad and I leak checked the TM3 HS water line with new target installed.  No leak has been found during the check. Leak detector base LR 0.0xE-9 atm.cc/sec, base pressure 0.0xE-4 torr. The line will be helium pressurized at CS later.

  600   Thursday, February 13, 2014, 14:23 David WangSouth Hot-CellRepairTM2 Leak check on TM2 tube heater (+) water line with blank off(elastic seal) installed on WB.

Chad and I did the leak check on TM2 tube heater (+) water line  with blank off( + elastic o ring seal) installed on "D"  water block in SHC. We got the same no leak result as we got with rubber insert this morning.

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  608   Tuesday, February 25, 2014, 06:53 David WangSouth Hot-CellRepairTM2 Leak check on TM2 tube heater (+) water line with blank off(C-seal) installed on WB.

Chad and I did the leak check   on TM2 tube heater (+) water line  with blank off and C-seal  installed on  WB at South Hot Cell.The line was easy to pump down to 0.0xE-9atm.cc/sec and 0.0XE-4 torr on leak detector. Chad flushed lot helium around the water block (10 sec spray). No response had been found on leak detector.

  1051   Wednesday, August 26, 2015, 14:28 David WangConditioning StationStandard OperationTM2ZrCLeak check on TM2 HS and windowwater line with new ZrC target at SHC

Chad and I leak checked TM2 HS and window circuit VCR joints with ZrC target and containment box installed at SHC. No leak has been found. They will   be helium pressurized  at CS later.

  1068   Tuesday, September 15, 2015, 08:24 David WangSouth Hot-CellRepairTM1UCx 13Leak check on TM1 window circuit soldering stems in service cap.

I did a leak check on TM1 window circuit  2 soldering  stems in service cap.The round side panel was opened for the job. I sprayed helium on the stems for 10 seconds. The leak detector got a tiny response(from 0.0xE-9 atm.cc/sec to 2.0xE-9 atm.cc/sec). The test  repeated again. The second time, LD climbed  to 1.2xE-9atm.cc/sec. It looks like there is a very tiny leak on the stems soldering spots. But , this is not the same leak we found from SHC helium spray which LD climbed to 1.4xE-8atm.cc/sec with only one click helium spray by Chad.

 Because of the high air flow at SHC when the round panel is removed, The result is not conclusive. The same test is done at silo without  airflow. We found a big leak on this soldering stems . See later e-log.

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