Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 69 of 140  Not logged in ELOG logo
ID Date Authordown Category Type Module Target/Number Subject
  209   Thursday, November 08, 2012, 08:42 David WangConditioning StationStandard OperationTM1TiC #3TM1 TiC #3 target heat shield helium pressure check is done.

TM1 TiC #3 target  heat shield  helium pressure check  is done at conditioning station. Applied 80 psi helium to HS circuit for 5 minutes . There is no response had been found on leak detector. The leak detector base LR 0.0x E-9 atm.cc/sec, and BP 0.0xE-4 torr. CS and TM1 vacuum are at low E-6 torr range. The HS circuit is leak tight.

  214   Wednesday, November 14, 2012, 10:57 David WangITWStandard OperationTM1 TM1connected in ITW

I connected TM1 in ITW yesterday. Everything is good so far. Travis was with me when i did the job.

  215   Wednesday, November 14, 2012, 11:04 David WangITERepairTM4 Change ITE dump water circiut flow wheel

I changed ITE dump water circuit flow wheel due to its poor performance. The new flow wheel works fine. The signal on electrical board is strong and constant. One shielding block on ITE was moved out for the job, and it has been moved back after the job.The ITE is ready to take proton beam. Travis was with me when i did the job.

  220   Tuesday, December 04, 2012, 13:33 David WangITEStandard OperationTM4UCX#5Disconnected TM4 in ITE.

I disconnected TM4 in ITE. All water lines had been purged.Travis was with me .

  225   Wednesday, January 02, 2013, 12:11 David WangITWStandard OperationTM1 I moved 5 shielding blocks from ITW to block storage area

I moved 5 shielding blocks from ITW  to block storage area for preparing the TM1 disconnection. Air sampled and swiped blocks and ITW and everything is fine.Fiona was with me all the time during the moving.

  226   Thursday, January 03, 2013, 10:05 David WangITWStandard OperationTM1 Disconnected TM1 in ITW.

TM1 has been disconnected in ITW. All  water lines had been purged. Travis was with me during the job.

  229   Thursday, January 10, 2013, 10:40 David WangITWMaintenance  Replaced all high active water system magnetic pedal wheels in ITW and ITE.

I replaced all high active water system magnetic pedal wheels in ITW and ITE. This is a preventive maintenance job we planned for this winter shut down.

  231   Tuesday, January 15, 2013, 10:49 David WangITWStandard OperationTM1no targetTM1 vacuum system connection in ITW

I connected TM 1 vacuum system in ITW. The TM1 and ITW will be pumped out for shut down routine leak check.

  237   Friday, January 18, 2013, 11:17 David WangSouth Hot-CellStandard OperationTM4dummy targetTM4 heat shield circuit leak check with dummy target on.

Chad and i did a leak check on TM4 heat shield circuit with installed dummy target at SHC today. The leak detector is pumped to 0.0xE-9atm.cc/sec.Chad sprayed helium twice on each  VCR joints .There is no any response had been found on the leak detector during each 45 seconds waiting time. The TM4 heat shield circuit with dummy  target is leak tight so far.  

  240   Thursday, January 24, 2013, 13:30 David WangITWStandard OperationTM1 ITW-TM1 2013 winter shut down leak check.

2013 winter shut down ITW-TM1 primary vacuum vessel, secondary vacuum vessel, and water lines leak check: connected leak detector to TP2(primary and water lines) and TP4S (secondary). base leak rate 0.0xE-9atm.cc/sec,base pressure 0.0XE-4torr. Sprayed helium to all primary vacuum seal and there is no response on leak detector. Helium pressurized all water lines(except HS) at 70psi ,3mins.Tube heat(+) no response, tube heater(-)1.6xe-9atm.cc/sec, target oven(-)5.8xe-9atm.cc/sec, target oven (+) 6.9xe-9atm.cc/sec, EE 5.7xe-9atm.cc/sec, MSP no response, window 7.5 xe-9atm.cc/sec.All water lines are water leak free.  Two leaks had been found on secondary vacuum vessel. One is on exit 1 to tank o-ring (east side, E-N corner). The leak detector got   responses from 1.4 to1.7 xe-7 atm.cc/sec scale . The test  hadbeen repeated 4-5 times and   confirmed the location   . The second one is a small leak which  is on exit 2 to tank o-ring(east side, close to E-N corner). The leak detector got  responses from 1.4 to 1.8xe-8atm.cc/sec scale. The test had been repeated 3 times and confirmed the location. As the present plan. we will replace the exit1 to tank o-ring during this year shut down time.

  244   Thursday, February 14, 2013, 09:31 David WangITWRepair  ITH MP1 is replaced.

Edi and I replaced the broken ITH MP1 in target hall with a new pump. The old pump was leak on oil. There were no oil had been left in the old pump by checking the sight glass.Thats the reason of  the pump  failure.The tray which the old pump sat on was full of leaking oil ( highly contaminated ). The old pump was bagged in 3 thick plastic bags ,and the tray was cleaned before the new pump was installed. The working area had been cleaned up and surveyed couple of times after the job. Everything is good. The new pump had been tested after the installation. It works fine.

  245   Thursday, February 21, 2013, 14:05 David WangITWRepairTM1 Disconnected EXIT1 in ITW.

Disconnected EXIT1 in ITW. All cables , wires and air lines are label marked.

  250   Tuesday, February 26, 2013, 13:53 David WangConditioning StationRepairTM4 Replaced TM4 TP1

Bevan and I replaced TM4 TP1 today at conditioning station .The pump will be started this week when I do ITE and TM4 leak check .

  251   Friday, March 01, 2013, 11:35 David WangITEMaintenanceTM4 Leak check on ITE and TM4.
 The leak check on TM4 and ITE is done. All primary vacuum vessel , secondary vacuum vessel  on TM4 and ITE are leak tight. There is no any response had been found on leak detector(leak detector base LR 0.0xE-9 arm.cc/sec). All water lines had been pressurized to 70 psi helium for 3 minutes. They are all perfect leak tight( I cant find even a tiny response on leak detector) except GE water cooling line. On the GE water line, the leak detector got a instantaneous response once I applied the helium to the circuit.The leak rate climbed directly from 0.0xe-9 atm.cc/sec to 1.5 xe-5 atmcc/sec even if I stopped the helium pressurizing immediately. Once I purged the helium out of the line, the leak rate return to 0.0XE-9 atm.cc/sec quickly. I repeated the test on GE water line again and got exactly same result as the before. I would say the leak on the ITE GE water circuit isn't a small leak. The same test could be fulfilled once the TM4 is in CS later. 
  254   Wednesday, March 06, 2013, 14:12 David WangITWRepair  ITW EXIT1 tank to module o-ring replacement
 ITW EXIT1 o-ring replacement is fininshed today. The ITW EXIT 1 is back to ITW. The old o-ring lost most its elastic property and changed to stiff sqaure shape inside the slot.The flange surface around the o-ring slot was dirty. I cleaned the o-ring surface completely before putting the new o-ring . Everything should be fine now. There will be a leak check late on this new installed o-ring.
  262   Thursday, March 14, 2013, 07:09 David WangSouth Hot-CellStandard OperationTM4 TM4 electrical test at SHC after windown and containment box back.

TM4 electrical test at SHC after windown and containment box back is done. Everything is fine.

  263   Thursday, March 14, 2013, 07:18 David WangSouth Hot-CellStandard OperationTM4 TM4 window cooling line leak check

It took a long time(more than 1 hour)   to pump down the TM4 window  cooling line during leak check time. The base leak rate could only be pumped to 5.8xE-9 atm.cc/sec.Base pressure is 0.0xE-4 torr which is bottom reading. Chad and i did the leak check at this base leak rate .No leak had been found. The window cooling line is leak tight at this stage. A pressure helium test will be fulfilled in conditioning station on this cooling line later.

  272   Wednesday, March 20, 2013, 08:19 David WangConditioning StationRepairTM4 Leak check new installed TM4 TP1 at conditioning station.

I leak checked new installed TM4 TP1 at conditioning station. The CS vacuum gauges reading were at 1.0-1.5xE-6 torr . Leak detector base leak rate 0.0xe-9atm.cc/sec, base pressure 0.0xe-4torr. I sprayed helium around the pump  inlet flange and KF 25 pump outlet flange to pump joint. There is no response on leak detector. The new installed TP1 is leak tight.

  280   Wednesday, March 27, 2013, 11:49 David WangITEStandard OperationTM4Sic LIS-RFQ Connected TM4 in ITE

TM4 has been reconnected to ITE after the module moving. The roughing is started . The water will be supplied to ITE after  testing  the water  pumps . The water interlock check will be done on next week also.

  281   Wednesday, March 27, 2013, 12:08 David WangSouth Hot-CellStandard OperationTM4Sic LIS-RFQTM4 heat shield circuit leak check with SiC LIS-RFQ target

Chad and I did the TM4 heat shield leak check yesterday at SHC. The leak detector was pumped to 4.6 xE-9atm.cc/sec, and 0.0xE-4 torr after 1.5 hours pumping. Chad sprayed helium twice on both VCR fittings. There is no response had been found during each 45 seconds waiting time. Since the module moved to ITE directly,we didnt have helium pressure test this time. I  would say thee heat shield circuit is leak tight. so far.

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