Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 98 of 140  Not logged in ELOG logo
ID Date Author Categorydown Type Module Target/Number Subject
  147   Monday, July 16, 2012, 11:55 Bevan MossCraneRepair  Crane has stopped working

Bevan Moss wrote:

In the AM today David and I used the crane to raise the ground plate sheet metal into place. This afternoon when I attempted to return the crane to its usual place I discovered that the crane no longer worked. Upon further inspection it appears that the PLC has lost power. I will follow up on this Monday morning. The crane is not supporting any load at this point.

 Turns out I am just not very observant. David had turned the main break to the crane off as a result when he turned it back on this morning the crane magically started working again.

  500   Tuesday, October 08, 2013, 18:12 Grant MinorCraneRepairTM4 Target Hall Crane Stuck in East-West Direction - Update

Grant Minor wrote this e-mail today:

***

Hello all,

During our planned operation of transporting TM4 from a storage silo to the Hot Cell, we had a problem with the East-West bridge drive on the Target Hall crane.  The crane bridge is currently stuck in position over the silo area.  We were unable to complete the transport operation.  TM4 has been placed back down into the silo and the crane hook block has been disconnected from the module lifting yoke.

We have been on the phone with Norelco this afternoon and have determined the likely cause of the problem.  There is a splice joint in the crane rails at this position, where a small gap exists between the rail sections.  If the crane bridge is stopped during operation such that the wheel comes to rests in this gap, the crane motors have insufficient torque for the wheel to overcome the gap and ride back onto the rail.  The Norelco tech Mike Smith remembers encountering this problem several years ago (before my time) but cannot remember how it was overcome.  The fix likely involved moving the wheel out of the gap with pry bars.

Target Hall Survey Needed at or before 7:00 am, Wednesday Oct 9th (Lynne, Fiona, Danka, Max or Dano?)

Mike Smith and possibly a few others from Norelco will come tomorrow morning at 7:00am, and require access to the Target Hall.  Since we have opened the Hot Cell in preparation for the module move, we will need a survey as early as possible to allow Mike and his crew to enter the hall without a suit and respirator.

Most of the Remote Handling group will be off-site for a Division meeting, but Travis and Maico will stay for the day to accompany the Norelco guys and help with the problem assessment.

Travis: Please take Mike to the control room when he arrives, one of the cameras is currently zoomed in on the wheel and problem rail section.

Maico: Scaffolding may be required to get access to the crane rail.  Unfortunately we don't have an operational crane to transport a man-lift into the hall ;)  Please see what you can do to get this ready in case we need it.  Max's leak check might have to go on hold until we get this resolved.  Please take responsibility for ensuring correct Fall Protection procedures are followed.  This means that nobody should be walking up on the crane rail unless they are tied in with harnesses, or there is scaffolding directly under them.

I can be reached on my cell phone at 778-319-4612.  The Division meeting is on UBC campus so I can return to TRIUMF fairly quickly if needed.

Thank you all for your assistance,

Grant

***

A photo of the THall camera view of the bridge wheel at the rail splice is attached, as well as Mike Smith's crane inspection report from March 2013.

  501   Wednesday, October 09, 2013, 19:33 Grant MinorCraneRepairTM4 Target Hall Crane not operational - likely controls / PLC hardware failure (not stuck wheel)

Grant Minor wrote:

Grant Minor wrote this e-mail today:

***

Hello all,

During our planned operation of transporting TM4 from a storage silo to the Hot Cell, we had a problem with the East-West bridge drive on the Target Hall crane.  The crane bridge is currently stuck in position over the silo area.  We were unable to complete the transport operation.  TM4 has been placed back down into the silo and the crane hook block has been disconnected from the module lifting yoke.

We have been on the phone with Norelco this afternoon and have determined the likely cause of the problem.  There is a splice joint in the crane rails at this position, where a small gap exists between the rail sections.  If the crane bridge is stopped during operation such that the wheel comes to rests in this gap, the crane motors have insufficient torque for the wheel to overcome the gap and ride back onto the rail.  The Norelco tech Mike Smith remembers encountering this problem several years ago (before my time) but cannot remember how it was overcome.  The fix likely involved moving the wheel out of the gap with pry bars.

Target Hall Survey Needed at or before 7:00 am, Wednesday Oct 9th (Lynne, Fiona, Danka, Max or Dano?)

Mike Smith and possibly a few others from Norelco will come tomorrow morning at 7:00am, and require access to the Target Hall.  Since we have opened the Hot Cell in preparation for the module move, we will need a survey as early as possible to allow Mike and his crew to enter the hall without a suit and respirator.

Most of the Remote Handling group will be off-site for a Division meeting, but Travis and Maico will stay for the day to accompany the Norelco guys and help with the problem assessment.

Travis: Please take Mike to the control room when he arrives, one of the cameras is currently zoomed in on the wheel and problem rail section.

Maico: Scaffolding may be required to get access to the crane rail.  Unfortunately we don't have an operational crane to transport a man-lift into the hall ;)  Please see what you can do to get this ready in case we need it.  Max's leak check might have to go on hold until we get this resolved.  Please take responsibility for ensuring correct Fall Protection procedures are followed.  This means that nobody should be walking up on the crane rail unless they are tied in with harnesses, or there is scaffolding directly under them.

I can be reached on my cell phone at 778-319-4612.  The Division meeting is on UBC campus so I can return to TRIUMF fairly quickly if needed.

Thank you all for your assistance,

Grant

***

A photo of the THall camera view of the bridge wheel at the rail splice is attached, as well as Mike Smith's crane inspection report from March 2013.

E-mail from today:

Hello Dave, Jane, Franco, Michael, Don (controls + Franco), Remy,

We have lost the East-West bridge drive control functionality of the ISAC Target Hall crane, and unfortunately this very much prevents us from operating the ISAC facility.

The problem was originally thought to be a stuck bridge wheel but this was not actually the case.

Mike Smith from Norelco was on-site for most of today working with Michael Rowe in an attempt to diagnose the problem.

Mike believes the problem to be one of the following three items:
- input PLC board on the crane bridge
- output PLC board in the interface panel in B1 level Room 5 (ISAC remote crane control room)
- communication between the two boards (festooning hardware)

We are in a pretty dire situation without the ISAC target hall crane, and we lack the expertise within the Remote Handling group in PLC hardware to diagnose this on our own.  I need to ask for somebody's help from the controls group in diagnosing and repairing this problem.

I have notes from my telephone conversation with Mike Smith which I can discuss with a controls representative in the morning.  There is a pretty muddled history of the design and implementation of these controls but essentially Norelco outsourced the PLCs and festooning to a third party contractor, Seattle Crane in the US, which no longer exists anymore.  Neither Kone, Seattle Crane, or Norelco made appropriate as-built drawings of the wiring of the PLCs.  Mike Smith at Norelco had a stack of hand-written notes about the as-built configuration he made at the time of installation in the late 1990's but these notes have not been located yet.

The PLCs appear to be Allan Bradley but the modules are from approximately 1997 and we're not sure if spare units are available.

Mike Smith says the easiest thing to do at this point is install replacement PLC modules on the crane bridge and in the control room that have confirmed functionality.  If control is not restored then the problem is likely in the festooning.

Control of the crane bridge was temporarily attained by bypassing the controls (speed control / end limits, etc.) and sending drive signal directly to the drive motor controller in order to return the bridge to its home position at the access ladder.  This mode of operation is not safe as the crane has no speed reduction / limits to prevent driving the bridge into the walls at max speed.

Jane / Remy / Franco: please let me know who I should correspond with on the controls side and I will talk with them tomorrow morning.

Thanks,

Grant

  503   Tuesday, October 15, 2013, 16:44 Grant MinorCraneRepair  Target Hall Crane - operational with temporary thermal sensor bypass

E-mail correspondence on the Target Hall crane fault diagnosis between October 11th and 15th:

On 15/10/2013 3:34 PM, Grant Minor wrote:

Hello all,

Mike Smith from Norelco arrived this morning and spent some time with Travis from RH and Mike Rowe from Controls group examining the crane controls and electrical schematics.  A common understanding of the wiring and control signal scheme for the thermal sensor circuits was reached.  A scanned copy of Norelco / Seattle Crane drawing E5 - 1/1 with markups by Dave Morris (Oct 11th) and Mike Smith (Oct 15th) is attached.

The group then worked on top of the crane bridge to systematically isolate the thermistor circuits in each drive motor.  The thermistor readings were all normal / as-expected (about 180 Ohms for 3 in series), i.e. there was no indication of failure in any of the motor thermistors.  Fall arrest equipment was used to access the motors where required.

Next, the shunt circuit in each temperature sensor module was measured (terminals T1 and T2 on each module, on drawing E5 - 1/1).  The shunt in the operational module was measured at 500 kOhms.  The shunt in the suspected faulty module was measured at 79 kOhms.

It was concluded that there is most likely a fault in the module with the low shunt resistance.  The suspect module was left wired in bypass (shorted from terminals 14 to 11).  Mike Smith advised at that point that it would be safe to operate the crane in this mode temporarily until a replacement module can be installed.  I discussed this with him and Don Dale, and we agreed the risk is low, as we have not ever experienced a motor overheat scenario in the operating lifetime of the crane.

Mike Smith called me around 1pm to advise that he has located a replacement unit from their supplier in the US and I asked him to order 2 units on expedited overnight.  Mike expects the components to arrive Friday this week or Monday next week latest, factoring in delays at customs and local delivery times.  The units will be sent to Norelco first, then to TRIUMF locally.

Remote Handling is now continuing with Target Hall operations, using the crane as normal with the thermal module bypassed until the replacement module arrives.

Thanks to Dave Morris / Mike Lowe for their assistance in diagnosing this fault.

Here is a short summary of the Fault:

Cause of fault
- Most likely a failed thermal sensor module for one of the two pairs of bridge drive motors

Diagnosis
- Crane company (Norelco) consulted, with on-site inspections by tech Mike Smith on October 9th and October 15th
- Controls group / Mike Smith measured resistances in motor thermistors and sensors to systematically isolate fault to thermal sensor

Remedy actions taken

- Thermal sensor bypassed to temporarily restore crane function
- Risk of operating without sensor determined to be low through discussions with Norelco / Don Dale / Grant Minor
- Replacement thermal sensor + 1 spare (~ $300 ea + shipping) ordered from parts supplier through Norelco - expected delivery Monday October 21st

How could this fault have been prevented?
- Cause of failure within thermal sensor module unknown at this time
- Annual crane inspection performed by Norelco in March 2013 did not indicate any problems with this sensor (crane drive system functioned as normal)
- Suggested for future: routine inspection of sensor module shunt resistance to determine if there are any long-term signs of slow degradation

What can be done to prevent the fault in the future?
- The ISAC crane controls were designed in the late 1990's by Norelco sub-contractor Seattle Crane (now defunct)
- The crane is supposed to have two pairs of independent motors with separate thermal sensors, each capable of driving the crane if the other fails due to thermal trip
- My understanding is that the controls logic design should have been designed so that failure of one pair of motors does not prevent crane operation... it does not seem to be the case with the current design
- The design of the control logic related to these sensors could be re-evaluated and modified so that a trip from one thermal module does not prevent operation of the bridge if the other module is OK
- This is a project that will require some time and some controls and engineering resources
- In the interim, if the same failure occurs again, it may be possible to jumper the thermal sensor from the crane control room and continue operating normally - I will confirm with controls group / Norelco
- However, this is not advisable as it would be difficult in some cases to determine if the trip was due to a faulty thermal module, or an actual motor overheat scenario
- I will discuss further actions with Don Dale

Thanks and best regards,

Grant


On 11/10/2013 4:29 PM, Grant Minor wrote:

Hello all,

I spoke with the Norelco tech Mike Smith this afternoon regarding the failed thermal sensor component / circuit.  He will call Kone on holiday Monday (their office is not closed for Canadian Thanksgiving) and determine if they have a replacement module.

I explained (to the best of my understanding) the diagnosis performed by Dave Morris / controls group and the test that was done to isolate the thermal sensor unit.  Unfortunately, Mike Smith's drawings from Seattle crane contain notes and revisions that don't match the drawing that Dave Morris provided me (Seattle Crane dwg E5 - 1/1 revision 1 02-10-99), and he was unable to confirm in his opinion whether the bypass performed by Dave Morris has correctly isolated the problem components.  In addition, he believes that the bypass he performed on Wednesday isolated portions of circuitry that are inconsistent with this thermal sensor circuit.

Mike Smith will return Tuesday morning to review the bypass and schematics.  He recommended not operating the crane until he has a chance to confirm this thermal sensor issue.

From the drawings I have in hand and from discussions with Dave Morris, the failed component might be the thermistor sets inside the motor housing which are in series with the suspect module, or the module itself.  My understanding is that the crane is designed with two pairs of motors for the bridge drive, and each pair is protected by one of these thermal modules (thus there are two modules total).  Both modules would be the same age and both might be susceptible to the same failure mode.

As it is unclear to me the exact nature of the drive system failure, and I have a recommendation from Norelco to hold on operation of the crane, I must unfortunately state that the crane should not be used and we will have to wait until Tuesday to gather more information.

I am not so concerned about temporary loss of the thermal protection circuitry, as we have not had an overheating scenario in those motors in the lifetime of the crane (to my knowledge).  I am more concerned about getting 100% confirmation that we have addressed the problem.  If we attempt to use the crane and experience another failure during a lift that prevents us from placing the load down safely with the crane stuck in position over a target station, then we would be in much deeper trouble.

My apologies for this situation.

Best regards and have a good weekend,

Grant


On 11/10/2013 1:28 PM, Grant Minor wrote:
Thanks Dave,

I've contacted Norelco, Mike Smith and I are planning a path forward for further diagnosis and repair.

The crane MUST NOT be used to carry a load until it is identified whether the module or the sensors have failed, the reason for the failure, and the functionality of the thermal sensors has been restored.

Without the thermal sensor circuit we lose protection from motor overheat, an event which could have much more serious failure implications to the crane.

Cheers,

Grant

On 11/10/2013 1:04 PM, David Morris wrote:
The fault has been identified in the Target Hall Crane as a failed motor temperature module, or motor temperature sensor, on the East-West motion. The status contact in the module was bypassed allowing crane motion. There was no fault with the controls.

Dave

  557   Tuesday, November 26, 2013, 14:10 Travis CaveCraneMaintenance  Thermal relay replaced

The bad thermal motor protection relay for the crane has been replaced with a new unit. Crane was tested in pendant(local) operation and all drives worked.

  840   Friday, February 06, 2015, 08:06 David WangCraneRepair  TH crane lost movement controls since last Friday.

Last Friday, During the crane per use check, I found the main power supply to to crane was shut off. I was told   Don and Travis shut off the main power before Triumf power outage. Travis restored crane main power and I  could turn on the main relay on radio pedant  in TH.  But, I didnt have all crane main bridge movement controls on TH raido pedant except rotation. I still have all movement controls on small trolley from the radio pedant. When I operated radio pedant, Travis could hear the relay works in crane control room, but in TH no crane movements. It looks like a crane control problem so Dave Morris was contacted. Dave found one of battery on PLC board is dead and need to be replaced.He did order the battery right way. On this Wednesday, Dave noticed us we could temporarily run the crane. I went to T.H  for checking. At the beginning, I found I cant not turn on the crane main relay from radio pedant in TH. Don was in crane control room. He switched the crane control from TH radio  mode to control room pedant( big yellow control box laid on the ground, the mode switch is located on the up left corner of first main panel)  and he turned on the main relay by doing this and got all movement controls from the big yellow pedant. After switching the mode back to TH radio mode I also got all the controls from TH radio pedant. Everything worked fine on crane so we moved the man lift into TH on Wednesday afternoon and arranged the TH crane inspection on Thursday. On Thursday morning, Gordon Crane guys came in TH and started their inspection. At the beginning, everything works fine. But after they did some operation and checks on crane, the crane main relay could not be switched on again (from TH  raid box). The crane inspection job are suspended. RH group tried to active the main relay by switching the mode back to yellow pedant in crane control room just like we did on Wedsday, but it did not work this time. David Morris was contacted to check from his side if anything wrong. He checked and told us the program is working and everything  is good from his side. A crane expert is needed to trouble shoot this problem. Neil Wong is going to bring Gordon crane guys and start to trouble shoot the problem this morning.

  841   Friday, February 06, 2015, 12:27 David WangCraneRepair  TH crane troubleshoot

Gordon crane technician started TH crane trouble shooting this morning. The problem is found that there is no 115VAC power supply to energize  a main coil which is used to switch on 450V AC power supply to crane. He did a test and found  the crane could be operated  by big yellow pedant in control room when he manually gave the coil 115VAC power supply to energize it.. At that moment, the crane is set to big yellow pedant operating mode. But, he can not figure out why there is no 115VAC power to this coil.The wiring  tracking back is not an easy job for him. The troubleshooting is  stopped now. The job will be resumed on next week with more skilled technician involving in from Gordon crane.

  843   Thursday, February 12, 2015, 09:11 David WangCraneRepairTM4 TH crane troubleshoot and annual inspection.

Gordon crane technicians continued their troubleshooting on this Tuesday. They found the crane up-limit protection switch which is installed on the same bracket with the the crane down view camera is broken. The spring inside the limit switch  which is used for pushing the action plunge out in the switch lost its function. This up limit switch is the last protection for the crane so it is set as when it is in action the crane main contact coil  which controls crane  power supply will be in open position. The broken switch is replaced by a new one( same type) on this Wednesday. The crane annual inspection has been  finished after the switch replacement. The crane works fine now.

  844   Monday, February 16, 2015, 11:57 David WangCraneRepair  TH crane

Dave.Morris installed a new battery on crane control PLC board and uploaded the program. Travis, Dan and I tested the crane in local, remote, and test mode. The crane works fine. Also, the TH lock up has been tested. Everything is good.

  1459   Thursday, March 23, 2017, 11:22 Grant MinorCraneMaintenance  Target Hall crane 20 ton hoist noise / smell - inspection by Gordon Crane & Hoist

Strange noise and a burning brake type smell was observed yesterday by David and Anders when running the main 20 ton hoist locally.  A service call was arranged today with Gordon Crane.  No major issues were found.  A more detailed summary is in the attached e-mail correspondence.  Gordon Crane will issue a formal report, but they recommend replacing both sets of brake disks and brake calipers. - Grant

  1476   Tuesday, April 04, 2017, 14:39 David WangCraneStandard Operation  Crane check main hoist on jogging with shielding plug lifted.

Today, I checked TH crane main hoist  when shielding plug is installed into ITE pit. I did  some jogging actions on main hoist during the operation. Everything looks fine. No burning smell, no strange noise. An outside crane expert suggest that jogging is the worst working situation for crane. We have to use jogging actions during our crane operation. But, we could try to use less jogging when operate the crane.

  1482   Thursday, April 06, 2017, 15:11 Grant MinorCraneMaintenance  Target Hall Crane 20 ton hoist - Report by Gordon Crane 5-Apr-2017

-------- Forwarded Message --------

Subject:

ISAC Hoist Brake Repair

Date:

Wed, 05 Apr 2017 20:42:49 -0700

From:

Aidan C. Gordon <aidan@gordoncrane.com>

To:

Curtis Ballard <ballard@triumf.ca>, Neil Wong <nwong@triumf.ca>

CC:

Peter Neumann <peter@gordoncrane.com>, Shelley Cherkowski <Shelley@gordoncrane.com>

 

Hi Curtis

 

Further to the emergency service call at the Isac Target Hall on Thursday March 23rd, we advise as follows:

 

It was reported that the hoist was making an unusual noise and that there was a strong brake odour during operation.

The lift was completed using the auxiliary hoist.

 

A man-lift was arranged and Senior Service Technician Tom Kauss attended site the next morning to troubleshoot.

He determined that one of two hoist brakes (walkway side) had a strong odour and on closer examination it appeared that the 

brake lining material was breaking down and particulate lining material was getting caught between the lining and the discs.

These lining fragments were rubbing and burning off during the hoist operation.

The end cover of the brake had an accumulation of brake lining fragments 

The lining was not overly worn, but appears to be becoming friable, perhaps with age or exposure to radiation.

 

The brake was cleaned with compressed air to remove the friable material and thoroughly tested. 

A test load of approximately 10 tons was lifted and the hoist handled the load without issue

The brake fragment issue did not recur while we on site and the hoist was recommissioned for use.

 

To guard against the likely recurrence of this condition on this critical application crane, and as both brakes have seen identical conditions in operation, 

we recommend that both brake assemblies be replaced.

The brake assembly would include the brake coil, friction discs, steel brake discs and the brake springs

TRIUMF does not have a spare brake on hand, therefore one of the removed brakes could be rebuilt and kept on hand. 

 

Two (2) each  XL-60009637 Complete Brake Assemblies   $ 5,706.00  Each

 

One (1) only XL-60009674 Brake Repair Kit $ 2,435.00

            For Rebuild

 

One (1) only XL-52272125 Brake Spring Kit $     59.72 For Rebuild

Installation & Testing of New Brakes estimated at: $ 1,250.00 Lot

We have one brake in stock in our Vancouver Service Depot. A second brake is available Ex-Ontario

FOB Site

Applicable Taxes Extra

Quote Valid for 30 days, subject to prior sale.

 

We are available next week to perform this work on site.

Please let us know if you have any questions or if you would like us to proceed.

 

Best Regards

          Aidan

 

------------------

Aidan C. Gordon

General Manager

aidan@gordoncrane.com

Gordon Crane & Hoist Inc.

Celebrating 34 years of Excellence (1983-2017)


www.gordoncrane.com

Toll Free 1-866-HOIST-IT

              (1-866-464-7848)

Tel:  (604) 324-2441

105-8475 Ontario St

Vancouver BC  V5X 3E8


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  1497   Thursday, April 13, 2017, 14:16 David WangCraneRepair  TH crane: east side main hoist brake assembly is replaced.

Gordon Crane technician Tom Kauss finished the replacement of the east side main hoist brake assembly. A new set up is installed. he adjusted gap too close during first time try. So, the smell appeared when operate the brake. He increased the gap to a proper distance then. It looks like everything works fine now. Still, The brake need to be tested with 10K lBS load on it. We will do the load test on next Thursday when he come here to replace west side brake assembly.  Before that, No module move or other heavy lifting action should be fulfilled on TH crane.

2017-04-20. Tom Kauss finished the replacement of west side main hoist brake assembly. The old set up will be rebuilt, and stored as spare for the future. The load test is done.  10k lbs load was used for testing. Brakes work fine. No strange noise and smell has been found during the test. 

  1503   Tuesday, April 25, 2017, 19:35 Grant MinorCraneRepair  ISAC Target Hall Crane - West Hoist Brake Rattle

Below is a report on the ISAC Target Hall crane brake issue observed yesterday and addressed today:

 

- On April 13th, both the East and West hoist brake assemblies were replaced by Gordon Crane & Hoist, after David observed a burning smell

- The East assembly was replaced with a completely new brake assembly from Kone crane

- The West assembly was replaced with a refurbished assembly, which used the East assembly housing fitted with a rebuild kit by Gordon Crane

 

- Yesterday while preparing TM3 for a lift, David noticed a vibration / rattle sound coming from the West hoist brake

- This issue was only observed when starting the hoist from a complete stop, at the slowest possible upwards hoist speed

- Once the hoist speed increased, the sound went away, even after returning to a slower speed

 

- Tom from Gordon Crane & Hoist came in this morning at 7am and replaced the new West assembly with the original West assembly, which had at that point also been fitted with a rebuild kit at Gordon Crane’s shop

- Tom also inspected the East brake assembly again

- Tom commented that he had issues setting the right gap between the friction plates and the brake rotor – too close and the brake would not release properly, too far and the brake rattle issue would be observed

- He also commented that during this most recent repair of the West brake, he applied never seize to the shaft and spline to ensure that this friction point was not an issue

 

- After Tom finished his repair and inspection of the brakes, David attempted a test lift of an SEG block (10 ton) at the slowest lift speed

- The rattle noise coming from the West brake was still observed

- Travis also tested the slowest speed in Remote Test mode from the control room, with David and Grant present in the Target Hall, the rattle was also still observed

 

- Tom advised that the rattle would not affect the safety of the hoist, and no damage would be done to the brake assemblies by running the hoist normally with the rattle noise

- Tom ensured that he would consult with Aiden and they would likely order a brand new West brake assembly from Kone

- Tom called Aiden Gordon to confirm that it was ok to proceed

- Aiden called me around 1:30pm and left a message that the slow speed rattle sound was benign and that we could proceed with normal operations, but he would definitely address the problem moving forward, and we should standby for his report

 

Photos and video have been uploaded to Docushare.  The hoist noise before the repair and after the repair during the test lifts can be heard in the videos.

 

https://documents.triumf.ca/docushare/dsweb/View/Collection-19812

 

Thanks and regards,

 

Grant

 

--

Grant Minor, M.A.Sc., P.Eng.

TRIUMF Remote Handling Group Leader

Nuclear Engineer

4004 Wesbrook Mall, Vancouver

BC, Canada, V6T2A3

gminor@triumf.ca

(604) 222-7359

http://www.triumf.ca/profiles/4557

  1516   Monday, May 01, 2017, 12:32 David WangCraneRepair  TH crane burning smell

TH crane burning smell showed again this morning. It appeared after 1-1.5 hours of continuously using during the F308 flasks moving in TH.After a certain time of using I think the brake gap is reduced because of  thermal expansion. The main hoist and brakes work fine still. We knew these brakes gap are tight especially on west side. So, It is not surprised that this burning smell appeared again. It does not affect the safe of crane use in my view. But, The life of this brake assembly could be affected.  I would like everyone know this issue. We may need to consult Gordon crane as well. Maybe, The gap should be increased up a little bit.  On this Friday, I will use crane to transfer 30K lbs shielding blocks. It will be a good test on crane main hoist again. 

  1523   Friday, May 05, 2017, 11:06 David WangCraneStandard OperationTM3 TH crane is used for 5 shielding blocks transferring.

  TH crane is used for transferring five shielding blocks(30000lbs) today. All brakes work fine. Mostly, I do not need crane slow up motion for this job so during 1 hour moving, no rattle sound and burning smell has been found.  I think TH crane is good to use as we decided. 

  1534   Friday, May 12, 2017, 07:42 David WangCraneRepair  TH crane burning smell, smoke, and big noise on east side main hoist brake assembly.

This morning, when I prepare for today's crane check, The crane made a very strong noise without any load during the full speed up motion. I stopped the crane right away, and noticed that east side of main hoist motor area was smoking . The crane was moved to east end. And, I climbed up to the top, and found the smoke is coming form brake side, and should be produced by braking. The smell is same as before.Unless other thing is wrong,  I think Gordon crane technician has to adjust the gap to a proper distance on both side of the main hoist. I feel very uncomfortable by operating the crane this way. They have to figure out what is wrong on these new brake assembly installation.

2017-05-12. This morning , Crane technicians increased both side of main hoist brake gaps today. They found on east side brake assembly, The gap is automatically closed after some  jogging motions. Peter think this is caused by torque produced by automatic adjustment springs on brake. This torque rotate  the gap adjustment device and closed the gap.  We operate the crane for a while with 20000lbs load on it after gap adjustment. The rattling sound is still there at slow up motion.  But, The main hoist braking sound is softer and gentle comparing to past month.This sound is more close to the sound before we replaced the brake assembly. So, This adjustment could be right in my view.  They checked  gaps after 0.5 hours operation. Everything is still fixed there . No change. They suggest we keep operating the main hoist, and they will be back on next Monday check again.  I operated the main hoist up and down in different speed motion for 1 hour after they left. Everything works fine. Braking are gentle. No strange sound and smoke during up or down. I will do  more operation on Monday morning before they come. Lets see the result after their checking.  

2017-05-15 This morning, 20minutes of crane main hoist up and down test with lots jogging and braking. The braking sound is softer and gentle. Everything works fine.

2017-05-15.  Gordon crane technician Peter came in during lunch time. Both side main hoist brake gaps have been checked. They are still at the same position as last Friday. The gap is not changed after operation. Peter will be back on next Monday and check everything again.  

  1558   Tuesday, June 13, 2017, 11:10 Grant MinorCraneMaintenance  ISAC THall Crane 100% / 125% Load Test Documentation - 2011

The ISAC Target Hall Crane was load tested and re-certified in January 2011 prior to doing a near-capacity lift for the North Hot Cell roof structure (IRH1112E).

Photos and documentation from Norelco is attached.

- Grant

  1563   Friday, June 23, 2017, 12:08 David WangCraneRepair  TH crane inspection and probem fixing by Gordon crane

Gordon crane technician Peter came in today and checked TH crane. Maico and I were there with him. What he found is that brake gap on both side of main hoist decreased after months of using.  The solution is to lock the automatic self adjustment system so the gap will be fixed there. Each year during annual inspection, they will adjust the gap manually. After he locked both side of device, I tested the crane up and down couple of times. The brakes work fine. 

  1586   Tuesday, July 18, 2017, 15:04 Travis CaveCraneMaintenance  Failure of the ISAC TH Crane Rotate.

 Earlier in the day it was noted that the rotate function of the crane had creased operation. After David has finished the block moves. Don and I checked the Crane's control unit in the ISAC crane control room and found the breaker tripped for the rotation. The breaker was reset and the crane's rotation is now operational. If this occurs in the future only Travis Cave, Don Jackson or a TRIUMF Electrician are allowed in that control box as it is a 480Volt system. Don or I because we know what we are looking for and the Electrician because they are allowed to touch with and deal 480 V systems. 

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