Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 96 of 138  Not logged in ELOG logo
Entry  Wednesday, October 09, 2024, 14:04, Frank Song, ITE, Standard Operation, TM2, Ta#68, Module Connection TM2_with_new_target_Ta#68_connection_in_ITE.pdf

 TM2 with new target Ta#68 installed is connected in ITE. Pls see form attached.

Entry  Tuesday, December 03, 2024, 10:10, Frank Song, ITE, Standard Operation, TM2, Ta#68, module disconnection TM2_with_spent_target_TA#68_disconnection_in_ITE_2024-12-03.pdf

TM2 with spent target TA#68 was disconnected  in ITE and is being moved to SHC. All water lines are purged for module storage.

Entry  Wednesday, December 04, 2024, 08:05, Frank Song, ITE, Standard Operation, TM3, UCx#47, Module Connection TM3_with_new_target_UCx#47_connection_in_ITE_2024-12-03.pdf

TM3 with new target UCx#47 was connected in ITE right after be moved from TCS. 

Entry  Tuesday, January 07, 2025, 12:05, David Wang, ITE, Standard Operation, TM3, UCx #47, ITE primary and secondary vacuum vessel leak check for 2025 shut down 

ITE primary and secondary vacuum vessel leak check for 2025 shut down have been done. No leak.  The TM3 waterlines helium pressure test will be done at TCS when module is there.

TM3 water lines helium pressure test  are done. 70 psi helium 3 minutes to each line( except HS which has no target on it ) . leak detector base leak rate :0.0Xe-9 atm.cc/sec. No leak on all tested water lines.Helium were purged out after test. and 60 psi nitrogen were filled in lines for storage. 

Entry  Monday, January 13, 2025, 10:36, Frank Song, ITE, Standard Operation, TM3, UCx#47, module disconnection TM3_with_spent_target_UCx#47_disconnection_in_ITE_2025-01-13.pdf

 TM3 with spent target UCx#47 was disconnected in ITE and will be moved to SHC.

Entry  Wednesday, July 17, 2024, 15:06, Adam Newsome, Facilities, Standard Operation, , , Safety Walkaround Complete - SHC/NHC Area 

A safety walkaround for July 2024 was completed for the B2 level by A. Newsome. No deficiencies to report.

Results can be found in the master spreadsheet

Entry  Thursday, October 10, 2024, 12:20, Adam Newsome, Facilities, Standard Operation, , , Safety Walkaround complete - ISAC Hot Cells, Target Hall 

A safety walkaround was completed for the ISAC Hot Cells and Target Hall Areas.

The resulting spreadsheet can be found on DocuShare as Document-242733.

Main deficiencies identified:

  • Hot Cells:
    • Phone not working at North hot cell operator station
  • Target Hall:
    • Uncertain if NHC and SHC ventilation pressure gauges have recently been inspected

Action has been taken on all deficiencies.

Entry  Friday, October 11, 2024, 15:59, Aaron Tam, Facilities, Repair, , , ISAC B2 North Hot Cell Phone Fixed 

 Resolution comment / Commentaire de résolution:

     Fixed issue by changing patch cord that was connected to the switch from patch panel.

Emile V

Entry  Wednesday, December 04, 2024, 09:00, David Wang, Facilities, Standard Operation, TM2, , all water lines on TM2 have been purged. 

all water lines on TM2 have been purged. Refilled them(except HS ) with 60psi nitrogen for module silo storage before next year using. 

Entry  Friday, January 03, 2025, 09:59, Adam Newsome, Facilities, Standard Operation, , , Safety Walkaround complete - ISAC Hot Cells, Target Hall 

A safety walkaround was completed for the ISAC Hot Cells and Target Hall Areas.

The resulting spreadsheet can be found on DocuShare as Document-242733.

Main deficiencies identified:

  • Hot Cells:
    • NHC right manipulator gripper stuck (known, repair planned)
  • Target Hall:
    • 50% of overhead light bulbs burnt out (David Wang contacted Electrical Services to rectify)
    • One RH camera for target pit not working (Travis Cave notified)

Action has been taken on all deficiencies.

Entry  Thursday, January 09, 2025, 11:08, David Wang, Facilities, Maintenance, , , ITH:MP1 is deteriorating by watching on ITH:CG1 and CG2 readings 

ITH:MP1 is deteriorating by watching on ITH:CG1 and CG2 readings and investigation in pit. A fault 17644 has been issued. this pump will be replaced in March when general fielding in vacuum pit is reasonable for the job.

Entry  Friday, July 13, 2012, 16:33, Bevan Moss, Crane, Repair, , , Crane has stopped working 

In the AM today David and I used the crane to raise the ground plate sheet metal into place. This afternoon when I attempted to return the crane to its usual place I discovered that the crane no longer worked. Upon further inspection it appears that the PLC has lost power. I will follow up on this Monday morning. The crane is not supporting any load at this point.

    Reply  Monday, July 16, 2012, 11:55, Bevan Moss, Crane, Repair, , , Crane has stopped working 

Bevan Moss wrote:

In the AM today David and I used the crane to raise the ground plate sheet metal into place. This afternoon when I attempted to return the crane to its usual place I discovered that the crane no longer worked. Upon further inspection it appears that the PLC has lost power. I will follow up on this Monday morning. The crane is not supporting any load at this point.

 Turns out I am just not very observant. David had turned the main break to the crane off as a result when he turned it back on this morning the crane magically started working again.

Entry  Tuesday, October 08, 2013, 18:12, Grant Minor, Crane, Repair, TM4, , Target Hall Crane Stuck in East-West Direction - Update THall_Crane_Bridge_Wheel_at_South_Rail_Splice_8Oct2013.JPGNORELCO_inv13045_joMS-064_31March2013.pdf

Grant Minor wrote this e-mail today:

***

Hello all,

During our planned operation of transporting TM4 from a storage silo to the Hot Cell, we had a problem with the East-West bridge drive on the Target Hall crane.  The crane bridge is currently stuck in position over the silo area.  We were unable to complete the transport operation.  TM4 has been placed back down into the silo and the crane hook block has been disconnected from the module lifting yoke.

We have been on the phone with Norelco this afternoon and have determined the likely cause of the problem.  There is a splice joint in the crane rails at this position, where a small gap exists between the rail sections.  If the crane bridge is stopped during operation such that the wheel comes to rests in this gap, the crane motors have insufficient torque for the wheel to overcome the gap and ride back onto the rail.  The Norelco tech Mike Smith remembers encountering this problem several years ago (before my time) but cannot remember how it was overcome.  The fix likely involved moving the wheel out of the gap with pry bars.

Target Hall Survey Needed at or before 7:00 am, Wednesday Oct 9th (Lynne, Fiona, Danka, Max or Dano?)

Mike Smith and possibly a few others from Norelco will come tomorrow morning at 7:00am, and require access to the Target Hall.  Since we have opened the Hot Cell in preparation for the module move, we will need a survey as early as possible to allow Mike and his crew to enter the hall without a suit and respirator.

Most of the Remote Handling group will be off-site for a Division meeting, but Travis and Maico will stay for the day to accompany the Norelco guys and help with the problem assessment.

Travis: Please take Mike to the control room when he arrives, one of the cameras is currently zoomed in on the wheel and problem rail section.

Maico: Scaffolding may be required to get access to the crane rail.  Unfortunately we don't have an operational crane to transport a man-lift into the hall ;)  Please see what you can do to get this ready in case we need it.  Max's leak check might have to go on hold until we get this resolved.  Please take responsibility for ensuring correct Fall Protection procedures are followed.  This means that nobody should be walking up on the crane rail unless they are tied in with harnesses, or there is scaffolding directly under them.

I can be reached on my cell phone at 778-319-4612.  The Division meeting is on UBC campus so I can return to TRIUMF fairly quickly if needed.

Thank you all for your assistance,

Grant

***

A photo of the THall camera view of the bridge wheel at the rail splice is attached, as well as Mike Smith's crane inspection report from March 2013.

    Reply  Wednesday, October 09, 2013, 19:33, Grant Minor, Crane, Repair, TM4, , Target Hall Crane not operational - likely controls / PLC hardware failure (not stuck wheel) 

Grant Minor wrote:

Grant Minor wrote this e-mail today:

***

Hello all,

During our planned operation of transporting TM4 from a storage silo to the Hot Cell, we had a problem with the East-West bridge drive on the Target Hall crane.  The crane bridge is currently stuck in position over the silo area.  We were unable to complete the transport operation.  TM4 has been placed back down into the silo and the crane hook block has been disconnected from the module lifting yoke.

We have been on the phone with Norelco this afternoon and have determined the likely cause of the problem.  There is a splice joint in the crane rails at this position, where a small gap exists between the rail sections.  If the crane bridge is stopped during operation such that the wheel comes to rests in this gap, the crane motors have insufficient torque for the wheel to overcome the gap and ride back onto the rail.  The Norelco tech Mike Smith remembers encountering this problem several years ago (before my time) but cannot remember how it was overcome.  The fix likely involved moving the wheel out of the gap with pry bars.

Target Hall Survey Needed at or before 7:00 am, Wednesday Oct 9th (Lynne, Fiona, Danka, Max or Dano?)

Mike Smith and possibly a few others from Norelco will come tomorrow morning at 7:00am, and require access to the Target Hall.  Since we have opened the Hot Cell in preparation for the module move, we will need a survey as early as possible to allow Mike and his crew to enter the hall without a suit and respirator.

Most of the Remote Handling group will be off-site for a Division meeting, but Travis and Maico will stay for the day to accompany the Norelco guys and help with the problem assessment.

Travis: Please take Mike to the control room when he arrives, one of the cameras is currently zoomed in on the wheel and problem rail section.

Maico: Scaffolding may be required to get access to the crane rail.  Unfortunately we don't have an operational crane to transport a man-lift into the hall ;)  Please see what you can do to get this ready in case we need it.  Max's leak check might have to go on hold until we get this resolved.  Please take responsibility for ensuring correct Fall Protection procedures are followed.  This means that nobody should be walking up on the crane rail unless they are tied in with harnesses, or there is scaffolding directly under them.

I can be reached on my cell phone at 778-319-4612.  The Division meeting is on UBC campus so I can return to TRIUMF fairly quickly if needed.

Thank you all for your assistance,

Grant

***

A photo of the THall camera view of the bridge wheel at the rail splice is attached, as well as Mike Smith's crane inspection report from March 2013.

E-mail from today:

Hello Dave, Jane, Franco, Michael, Don (controls + Franco), Remy,

We have lost the East-West bridge drive control functionality of the ISAC Target Hall crane, and unfortunately this very much prevents us from operating the ISAC facility.

The problem was originally thought to be a stuck bridge wheel but this was not actually the case.

Mike Smith from Norelco was on-site for most of today working with Michael Rowe in an attempt to diagnose the problem.

Mike believes the problem to be one of the following three items:
- input PLC board on the crane bridge
- output PLC board in the interface panel in B1 level Room 5 (ISAC remote crane control room)
- communication between the two boards (festooning hardware)

We are in a pretty dire situation without the ISAC target hall crane, and we lack the expertise within the Remote Handling group in PLC hardware to diagnose this on our own.  I need to ask for somebody's help from the controls group in diagnosing and repairing this problem.

I have notes from my telephone conversation with Mike Smith which I can discuss with a controls representative in the morning.  There is a pretty muddled history of the design and implementation of these controls but essentially Norelco outsourced the PLCs and festooning to a third party contractor, Seattle Crane in the US, which no longer exists anymore.  Neither Kone, Seattle Crane, or Norelco made appropriate as-built drawings of the wiring of the PLCs.  Mike Smith at Norelco had a stack of hand-written notes about the as-built configuration he made at the time of installation in the late 1990's but these notes have not been located yet.

The PLCs appear to be Allan Bradley but the modules are from approximately 1997 and we're not sure if spare units are available.

Mike Smith says the easiest thing to do at this point is install replacement PLC modules on the crane bridge and in the control room that have confirmed functionality.  If control is not restored then the problem is likely in the festooning.

Control of the crane bridge was temporarily attained by bypassing the controls (speed control / end limits, etc.) and sending drive signal directly to the drive motor controller in order to return the bridge to its home position at the access ladder.  This mode of operation is not safe as the crane has no speed reduction / limits to prevent driving the bridge into the walls at max speed.

Jane / Remy / Franco: please let me know who I should correspond with on the controls side and I will talk with them tomorrow morning.

Thanks,

Grant

Entry  Tuesday, October 15, 2013, 16:44, Grant Minor, Crane, Repair, , , Target Hall Crane - operational with temporary thermal sensor bypass ISAC_THall_Crane_elec_E5_1slash1_15Oct2013.pdf

E-mail correspondence on the Target Hall crane fault diagnosis between October 11th and 15th:

On 15/10/2013 3:34 PM, Grant Minor wrote:

Hello all,

Mike Smith from Norelco arrived this morning and spent some time with Travis from RH and Mike Rowe from Controls group examining the crane controls and electrical schematics.  A common understanding of the wiring and control signal scheme for the thermal sensor circuits was reached.  A scanned copy of Norelco / Seattle Crane drawing E5 - 1/1 with markups by Dave Morris (Oct 11th) and Mike Smith (Oct 15th) is attached.

The group then worked on top of the crane bridge to systematically isolate the thermistor circuits in each drive motor.  The thermistor readings were all normal / as-expected (about 180 Ohms for 3 in series), i.e. there was no indication of failure in any of the motor thermistors.  Fall arrest equipment was used to access the motors where required.

Next, the shunt circuit in each temperature sensor module was measured (terminals T1 and T2 on each module, on drawing E5 - 1/1).  The shunt in the operational module was measured at 500 kOhms.  The shunt in the suspected faulty module was measured at 79 kOhms.

It was concluded that there is most likely a fault in the module with the low shunt resistance.  The suspect module was left wired in bypass (shorted from terminals 14 to 11).  Mike Smith advised at that point that it would be safe to operate the crane in this mode temporarily until a replacement module can be installed.  I discussed this with him and Don Dale, and we agreed the risk is low, as we have not ever experienced a motor overheat scenario in the operating lifetime of the crane.

Mike Smith called me around 1pm to advise that he has located a replacement unit from their supplier in the US and I asked him to order 2 units on expedited overnight.  Mike expects the components to arrive Friday this week or Monday next week latest, factoring in delays at customs and local delivery times.  The units will be sent to Norelco first, then to TRIUMF locally.

Remote Handling is now continuing with Target Hall operations, using the crane as normal with the thermal module bypassed until the replacement module arrives.

Thanks to Dave Morris / Mike Lowe for their assistance in diagnosing this fault.

Here is a short summary of the Fault:

Cause of fault
- Most likely a failed thermal sensor module for one of the two pairs of bridge drive motors

Diagnosis
- Crane company (Norelco) consulted, with on-site inspections by tech Mike Smith on October 9th and October 15th
- Controls group / Mike Smith measured resistances in motor thermistors and sensors to systematically isolate fault to thermal sensor

Remedy actions taken

- Thermal sensor bypassed to temporarily restore crane function
- Risk of operating without sensor determined to be low through discussions with Norelco / Don Dale / Grant Minor
- Replacement thermal sensor + 1 spare (~ $300 ea + shipping) ordered from parts supplier through Norelco - expected delivery Monday October 21st

How could this fault have been prevented?
- Cause of failure within thermal sensor module unknown at this time
- Annual crane inspection performed by Norelco in March 2013 did not indicate any problems with this sensor (crane drive system functioned as normal)
- Suggested for future: routine inspection of sensor module shunt resistance to determine if there are any long-term signs of slow degradation

What can be done to prevent the fault in the future?
- The ISAC crane controls were designed in the late 1990's by Norelco sub-contractor Seattle Crane (now defunct)
- The crane is supposed to have two pairs of independent motors with separate thermal sensors, each capable of driving the crane if the other fails due to thermal trip
- My understanding is that the controls logic design should have been designed so that failure of one pair of motors does not prevent crane operation... it does not seem to be the case with the current design
- The design of the control logic related to these sensors could be re-evaluated and modified so that a trip from one thermal module does not prevent operation of the bridge if the other module is OK
- This is a project that will require some time and some controls and engineering resources
- In the interim, if the same failure occurs again, it may be possible to jumper the thermal sensor from the crane control room and continue operating normally - I will confirm with controls group / Norelco
- However, this is not advisable as it would be difficult in some cases to determine if the trip was due to a faulty thermal module, or an actual motor overheat scenario
- I will discuss further actions with Don Dale

Thanks and best regards,

Grant


On 11/10/2013 4:29 PM, Grant Minor wrote:

Hello all,

I spoke with the Norelco tech Mike Smith this afternoon regarding the failed thermal sensor component / circuit.  He will call Kone on holiday Monday (their office is not closed for Canadian Thanksgiving) and determine if they have a replacement module.

I explained (to the best of my understanding) the diagnosis performed by Dave Morris / controls group and the test that was done to isolate the thermal sensor unit.  Unfortunately, Mike Smith's drawings from Seattle crane contain notes and revisions that don't match the drawing that Dave Morris provided me (Seattle Crane dwg E5 - 1/1 revision 1 02-10-99), and he was unable to confirm in his opinion whether the bypass performed by Dave Morris has correctly isolated the problem components.  In addition, he believes that the bypass he performed on Wednesday isolated portions of circuitry that are inconsistent with this thermal sensor circuit.

Mike Smith will return Tuesday morning to review the bypass and schematics.  He recommended not operating the crane until he has a chance to confirm this thermal sensor issue.

From the drawings I have in hand and from discussions with Dave Morris, the failed component might be the thermistor sets inside the motor housing which are in series with the suspect module, or the module itself.  My understanding is that the crane is designed with two pairs of motors for the bridge drive, and each pair is protected by one of these thermal modules (thus there are two modules total).  Both modules would be the same age and both might be susceptible to the same failure mode.

As it is unclear to me the exact nature of the drive system failure, and I have a recommendation from Norelco to hold on operation of the crane, I must unfortunately state that the crane should not be used and we will have to wait until Tuesday to gather more information.

I am not so concerned about temporary loss of the thermal protection circuitry, as we have not had an overheating scenario in those motors in the lifetime of the crane (to my knowledge).  I am more concerned about getting 100% confirmation that we have addressed the problem.  If we attempt to use the crane and experience another failure during a lift that prevents us from placing the load down safely with the crane stuck in position over a target station, then we would be in much deeper trouble.

My apologies for this situation.

Best regards and have a good weekend,

Grant


On 11/10/2013 1:28 PM, Grant Minor wrote:
Thanks Dave,

I've contacted Norelco, Mike Smith and I are planning a path forward for further diagnosis and repair.

The crane MUST NOT be used to carry a load until it is identified whether the module or the sensors have failed, the reason for the failure, and the functionality of the thermal sensors has been restored.

Without the thermal sensor circuit we lose protection from motor overheat, an event which could have much more serious failure implications to the crane.

Cheers,

Grant

On 11/10/2013 1:04 PM, David Morris wrote:
The fault has been identified in the Target Hall Crane as a failed motor temperature module, or motor temperature sensor, on the East-West motion. The status contact in the module was bypassed allowing crane motion. There was no fault with the controls.

Dave

Entry  Tuesday, November 26, 2013, 14:10, Travis Cave, Crane, Maintenance, , , Thermal relay replaced 

The bad thermal motor protection relay for the crane has been replaced with a new unit. Crane was tested in pendant(local) operation and all drives worked.

Entry  Friday, February 06, 2015, 08:06, David Wang, Crane, Repair, , , TH crane lost movement controls since last Friday. 

Last Friday, During the crane per use check, I found the main power supply to to crane was shut off. I was told   Don and Travis shut off the main power before Triumf power outage. Travis restored crane main power and I  could turn on the main relay on radio pedant  in TH.  But, I didnt have all crane main bridge movement controls on TH raido pedant except rotation. I still have all movement controls on small trolley from the radio pedant. When I operated radio pedant, Travis could hear the relay works in crane control room, but in TH no crane movements. It looks like a crane control problem so Dave Morris was contacted. Dave found one of battery on PLC board is dead and need to be replaced.He did order the battery right way. On this Wednesday, Dave noticed us we could temporarily run the crane. I went to T.H  for checking. At the beginning, I found I cant not turn on the crane main relay from radio pedant in TH. Don was in crane control room. He switched the crane control from TH radio  mode to control room pedant( big yellow control box laid on the ground, the mode switch is located on the up left corner of first main panel)  and he turned on the main relay by doing this and got all movement controls from the big yellow pedant. After switching the mode back to TH radio mode I also got all the controls from TH radio pedant. Everything worked fine on crane so we moved the man lift into TH on Wednesday afternoon and arranged the TH crane inspection on Thursday. On Thursday morning, Gordon Crane guys came in TH and started their inspection. At the beginning, everything works fine. But after they did some operation and checks on crane, the crane main relay could not be switched on again (from TH  raid box). The crane inspection job are suspended. RH group tried to active the main relay by switching the mode back to yellow pedant in crane control room just like we did on Wedsday, but it did not work this time. David Morris was contacted to check from his side if anything wrong. He checked and told us the program is working and everything  is good from his side. A crane expert is needed to trouble shoot this problem. Neil Wong is going to bring Gordon crane guys and start to trouble shoot the problem this morning.

Entry  Friday, February 06, 2015, 12:27, David Wang, Crane, Repair, , , TH crane troubleshoot  

Gordon crane technician started TH crane trouble shooting this morning. The problem is found that there is no 115VAC power supply to energize  a main coil which is used to switch on 450V AC power supply to crane. He did a test and found  the crane could be operated  by big yellow pedant in control room when he manually gave the coil 115VAC power supply to energize it.. At that moment, the crane is set to big yellow pedant operating mode. But, he can not figure out why there is no 115VAC power to this coil.The wiring  tracking back is not an easy job for him. The troubleshooting is  stopped now. The job will be resumed on next week with more skilled technician involving in from Gordon crane.

Entry  Thursday, February 12, 2015, 09:11, David Wang, Crane, Repair, TM4, , TH crane troubleshoot and annual inspection. 

Gordon crane technicians continued their troubleshooting on this Tuesday. They found the crane up-limit protection switch which is installed on the same bracket with the the crane down view camera is broken. The spring inside the limit switch  which is used for pushing the action plunge out in the switch lost its function. This up limit switch is the last protection for the crane so it is set as when it is in action the crane main contact coil  which controls crane  power supply will be in open position. The broken switch is replaced by a new one( same type) on this Wednesday. The crane annual inspection has been  finished after the switch replacement. The crane works fine now.

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