ID |
Date |
Author |
Category |
Type |
Module |
Target/Number |
Subject |
1718
|
Tuesday, May 22, 2018, 10:02 |
Anders Mjos | Conditioning Station | Repair | | | Water leak from TK1 over the weekend |
Link to e-log,
Link to efault
Tank level down from 76 to 55 in on TK1
Valve replaced by Curtis today |
Attachment 1: 2018-05-22_TCS_TK1_water_leak.png
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Attachment 2: Broken_Valve.jpg
|
|
Attachment 3: 2018-05-22_TCS_TK1_water_leak_archiver.png
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820
|
Monday, December 15, 2014, 09:41 |
Anders Mjos | Conditioning Station | Maintenance | TM2 | | Water leak found at the isolation transforer |
Anders Mjos wrote: |
The level dropped below 15 in over the weekend. MP2 stopped, but MP3 condtinued pumping.
|
e-fault submitted and Niel Wong has been contacted.
Niel Wong came and had a look at the system. We decided to close the circuit as the water is no longer used with the new power supplies. The circuit will be monitored, but not repaired unless it is needed again. |
1888
|
Friday, March 08, 2019, 14:10 |
chad fisher | South Hot-Cell | Repair | TM2 | | Water block polishing |
After trials with 2000 grid wet paper I have moved up to "red" scotch brite. This seems to have worked the best so far although it took two minutes to remove the ring that the other materials could not remove (see picture).
I have moved to next circuit. Currently at 3 minutes and 30 seconds with scotch brite but significant ring remains. |
Attachment 1: B_after_SB_(2).jpg
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|
1875
|
Monday, February 25, 2019, 09:44 |
chad fisher | South Hot-Cell | Repair | TM2 | | Water block jig |
module side water block jig has been removed in preparation for electrical checks. |
1889
|
Monday, March 11, 2019, 14:34 |
chad fisher | South Hot-Cell | Repair | TM2 | | Water Block Polishing status |
Stage 1 polishing (water scale and at least 99% of visual indium removed) has been achieved on all 2 seal water blocks that will be used (Ground electrode has not been polished). Process required 3-4 3minute cycles of the tool using scotch brite pads with the tool running at approximately 75 psi. |
1890
|
Tuesday, March 12, 2019, 09:13 |
chad fisher | South Hot-Cell | Repair | TM2 | | Water Block Polishing status |
Stage 1 polish has been achieved on all single seal water blocks using the single pad tool run at 75 psi, 2 3 minute cycles per block using red scotch brite. |
Attachment 1: Blocks_Stage_1_Polish.jpg
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|
1891
|
Thursday, March 14, 2019, 10:25 |
chad fisher | South Hot-Cell | Repair | TM2 | | Water Block Polishing status |
Phase 2 (intermediate) and Phase 3 (Final) polishing is complete on all water blocks on TM2 (minus ground electrode circuit which has only had a cursory cleaning). Phase 2 with 2000 grit wet sand paper and isopropynol for 1 minute with tool at 75 psi, Phase 3 with Veltex polishing cloth for 1 minute with tool at 75 psi. |
Attachment 1: Blocks_final_polished.jpg
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|
335
|
Thursday, May 09, 2013, 14:23 |
chad fisher | South Hot-Cell | Repair | TM3 | | Water Block Jig Removal |
The source tray side of the water block jig has been removed in preparation for moving the module to the conditioning station for electrical tests. |
Attachment 1: IMG_1059[1].JPG
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|
323
|
Friday, April 26, 2013, 11:20 |
chad fisher | South Hot-Cell | Repair | TM3 | | Water Block Jig (back half) |
The back half of the water block jig (services tray side) has been sucessfully located onto the module.
About 50% of the waterblocks have centered themselfs it their respective cups and the rest look good for concentricity but will require some gentle wiggling to get them to seat. |
379
|
Thursday, June 13, 2013, 09:21 |
chad fisher | South Hot-Cell | Development | | | Warm Cell Mock-up |
the warm cell mock-up has been inserted into the warm cell and final preparation for the remote test are being made. |
Attachment 1: 20130613_084421[1].jpg
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Attachment 2: 20130613_084426[1].jpg
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2420
|
Wednesday, March 01, 2023, 09:34 |
David Wang | Cooling | Maintenance | | | Visual inspection of HALCW for possible small water leak or drip. |
I visually inspected HALCW system including water station section, both target pits, and de-ionizer system. No small leak and drip was found . The inspection in both target pits will be repeated after flow sensors are replaced. |
2271
|
Friday, November 19, 2021, 12:48 |
Adam Newsome | South Hot-Cell | Development | | | Vertical motion limit switch installation |
A rotary limit switch was installed, attached to the shaft adjacent to the drive motor for the vertical drive system. This limit switch is not yet wired to the control system and operational - this will be done at a future date and the e-log will be updated.
Relevant electrical drawings: IRH2083 to IRH2085
Edit (2022-03-02): see e-log https://elog.triumf.ca/TIS/RH-ISAC/2309 |
Attachment 1: PXL_20211119_172142852.jpg
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292
|
Monday, April 08, 2013, 16:16 |
Bevan Moss | Conditioning Station | Standard Operation | TM1 | Ta #39 | Venting with Argon |
TM1 started venting at 4:15 pm with Argon. I will leave the valve open over night. |
1435
|
Tuesday, February 07, 2017, 15:57 |
Isaac Earle | North Hot-Cell | Development | | | Ventilation Ducting Gasket Installed |
Lead gasket IRH1633 was installed today according to assembly drawing IRH1618 Rev B. |
269
|
Monday, March 18, 2013, 15:28 |
Bevan Moss | Conditioning Station | Standard Operation | TM4 | CS Test Target #1 | Vented With Argon |
The conditioning station has been vented with argon. Time taken is not known but it is less than 3 hours. See attached picture for convectron gauge readings. CG1A is in air. |
Attachment 1: Vented_with_Argon.JPG
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1950
|
Monday, July 15, 2019, 13:29 |
David Wang | Conditioning Station | Development | TM4 | | Vacuum surge when TM4 B line iwas supplied with water. |
Yesterday, TM4 B line was supplied with water at TCS for testing. TCS: IG1 and IG2 had big response on it. See attachment. The water was disconnected right away, and line was purged. Vacuum recovered after overnight pump. |
Attachment 1: vacuum_surge_on_B_line_with_water.png
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1149
|
Friday, December 18, 2015, 11:42 |
Anders Mjos | Conditioning Station | Repair | | | Vacuum gauges not reading correctly |
It was found that the conversion from voltage to vacuum (Torr) in EPICS is not correct for the XGS-600 controllers in use at the TCS. EPICS did not correspond to local values displayed on the controller. An e-fault has been submitted. |
1150
|
Monday, December 21, 2015, 13:27 |
Anders Mjos | Conditioning Station | Repair | | | Vacuum gauges not reading correctly |
Anders Mjos wrote: |
It was found that the conversion from voltage to vacuum (Torr) in EPICS is not correct for the XGS-600 controllers in use at the TCS. EPICS did not correspond to local values displayed on the controller. An e-fault has been submitted.
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EPICS conversion updated and corrected by Mike Rowe. |
1067
|
Friday, September 11, 2015, 14:31 |
Anders Mjos | Conditioning Station | Maintenance | TM2 | ZrC#7 | Vacuum gauge and EPICS read back calibration |
The corelation betwenn the local value on the gauge controllers and the read back valiues in EPICS was compared. Data can be found in a previous e-log |
481
|
Monday, September 30, 2013, 16:02 |
Bevan Moss | Conditioning Station | Standard Operation | TM3 | NiO#2 | Vacuum |
The roughing pump for TCS was started at ~3:00 and the turbo's turned on at ~4:00. This is the minimum time for the module to pump down. |