|
ID |
Date |
Author |
Category |
Type |
Module |
Target/Number |
Subject |
|
2010
|
Tuesday, October 22, 2019, 16:26 |
Isaac Earle | Safe Module Parking | Development | | | SMP shield box grounding |
A braided grounding strap was attached to the aluminum gear box support on the SMP shield box structure, and grounded by attaching it to the exterior of an electrical conduit located in the south-west corner of the B2 area at the top of the silo in that corner. The braiding was also connected to the stainless steel support structure for the SMP vacuum pump. |
|
2015
|
Monday, October 28, 2019, 11:50 |
Travis Cave | Spent Target Vault | Standard Operation | | UC#28 | Spent Target Move |
UC#28 has been moved from the south hot cell to spent target storage. The target was placed in pail number 219 and placed in spot 1C of the vault, it was 12.6mSv/hr upon removal from the south hot cell. Also the spent target vault is now full and can not currently accept anymore targets. |
Attachment 1: Target_Index_2019-10-28.pdf
|
|
|
2016
|
Monday, October 28, 2019, 12:00 |
Isaac Earle | Safe Module Parking | Development | | | SMP shielding attenuation measured & compared to theoretical values |
The attenuation of the SMP shielding was measured as part of SMP commissioning (Document-170404, R1, Section 4, Test #8)
The field on the shutter side of TM3 was measured without any shielding as it was removed from a storage silo. At 0.5m from the edge of the module the maximum field was 5.00mSv. After installation into the SMP the maximum field outside the SMP shielding at 0.5m from the edge of the module was found to be 27uSv/hr. The resulting attenuation is 185x
Expected attenuation was calculated by Joe Mildenberger assuming that the majority of the activated components in that module are either copper or aluminum. With 6" of steel shielding (SMP shield vessel plus vacuum vessel), the attenuation factors were found for the following isotopes:
Na-22 (created in Al): 115
Co-60 (created in steel (Fe) or Cu): 70
Mn-54: (created in steel (Fe) or Cu): 200
Based on these figures, the measured result of 185 seems to be reasonable. |
|
2017
|
Tuesday, October 29, 2019, 10:00 |
Adam Newsome | Safe Module Parking | Development | | | SMP Updates to E-stop circuit and feedback signals |
The SMP main control panel and remote control module were updated in order to implement the following items which were deemed desirable during commissioning:
- 24 VDC line added to E-stop circuit:
Previously the E-stop relay cut power to only 120 VAC. This means that the lid rotation motor would stop instantly, but since the lid open/close valve is powered by 24 VDC which comes from a power supply unit, there would be a short delay while the unit powers off in which the valve was still active. This could result in a situation in which, for example, someone is operating the pendant to close the lid and another person recognizes a hazard and presses the E-stop on the main panel, but the lid does not stop closing for approximately 3 seconds while the operator is still holding the "close" button down.
To rectify this issue, the 24 VDC line was routed through a NO contact of the same E-stop relay that controls the entire 120 VAC supply to the system. This was tested on Oct. 25, 2019 - working.
- Status feedback signals to remote control room:
Previously status signals for "Lid raised", "Lid Centred", "CW Limit", and "CCW Limit" were only displayed as light indicators on the main control panel. It was determined during remote operation that it would be helpful to have these signals sent back to the software interface so that an operator does not need to use a camera to look at the light indicators.
Electrical drawings and cable schedule have been updated to reflect these changes. The SMP will be tested again using the commissioning plan checklist to confirm no there were no inadvertent effects on the rest of the same from these changes.
|
|
2019
|
Thursday, October 31, 2019, 08:49 |
Anders Mjos | Conditioning Station | Repair | | | Water leak on non-active cooling water circuit |
Yesterday a leak was discovered in the ISAC-I experimental hall. The leak appears to be at the connection between the evaporator and the return water line. 1 in of water was lost from TCS:TK1. The water is currently valved off to prevent further leakage.
A fault reportt has been submitted to mechanical services - awaiting response.
Friday, November 01, 2019
Leak repaired by Mechanical Services. A brass fitting had cracked and was replaced with a galvanized fitting. |
|
2028
|
Tuesday, November 12, 2019, 10:07 |
Travis Cave | Spent Target Vault | Standard Operation | | Ta#59 | Spent Target Move |
The spent Ta#59 was moved from the south hot cell to the spent target vault. See the attached for details. |
Attachment 1: Target_Index_2019-11-08.pdf
|
|
|
2029
|
Thursday, November 14, 2019, 13:52 |
Travis Cave | Spent Target Vault | Standard Operation | | UC#22,23,24 | Targets repackaged |
The targets UC#22,23,24 have been repackaged into the newer stronger pails, and have been placed back in the mini vault with new numbers. See attached PDF for details. |
Attachment 1: Target_Index_2019-11-14_Mini_Vault.pdf
|
|
|
2036
|
Tuesday, December 03, 2019, 12:45 |
Adam Newsome | Spent Target Vault | Standard Operation | | SiC#38 | SiC#38 in Pail 205 moved to Storage Vault: 4B |
SiC#38 in Pail 205 was moved to section 4B of the storage vault. Dose rate when retrieving from Hot Cell was 22.2 mSv/h. |
Attachment 1: Target_Index_2019-12-03.pdf
|
|
|
2037
|
Thursday, December 12, 2019, 14:39 |
Isaac Earle | Safe Module Parking | Development | | | SMP assembly shifted 1.0" north |
The SMP assembly was shifted approximately 1.0" north today by pushing it, braced against the south wall, using a 100 Ton capacity air lifting bag supplied by Beamlines Group. The move was one of the action items identified at the Gate 4A/4B close-out review. During commissioning of the SMP, TM3 was installed into the vacuum vessel, which required the crane to be all the way at its south limit, so the move is to provide some margin for future use, particularly if TM1 is put in the SMP as the extent of its shielding is slightly larger than the other modules.
One of the air fittings for the lid actuation cylinder on the north side was damaged during the move. It was replaced and correct functionality of lid actuation was then confirmed. |
|
2038
|
Thursday, January 02, 2020, 09:55 |
David Wang | Cooling | Standard Operation | | | I turned on HALC water pump MP2. |
HALCW MP2 is switched onnow. There is a small amount of air trapped in system. The pump works fine. Water level and system resistivity will be monitored for a while.
LALCW P5 and P6 are switched on for cooling HALCW. HALCW MP2 is in operation now. |
|
2039
|
Thursday, January 02, 2020, 10:10 |
David Wang | Crane | Standard Operation | | | TH crane issue. |
Target hall crane does not work properly after TH crane main power is switched off during Christmas time in control room. I switched the main power back this morning. The only movement could be operated is crane rotation. Power is supplied crane. The control on N-S, E-W and up-down movements do not work. We had the same problem last year. After trouble shooting, It was pointed to a PLC battery issue. Control group changed the battery and reloaded the program. I guess the battery is drained out very fast for some reason. So, We face the same problem again this year.
Adam checked control room main power supply. I checked in TH crane again. The problem is still there. We can confirm this is the same issue like last year. |
|
2040
|
Friday, January 03, 2020, 13:15 |
Adam Newsome | Crane | Repair | | | Target Hall Crane PLC Module/Battery Replacement |
The Target Hall Crane bridge and trolley motion was lost after a period of the crane having power disconnected over winter holidays. This is reported in the following e-log: https://elog.triumf.ca/TIS/RH-ISAC/2039. This issue is a duplicate of what happened in 2019 at this time: https://elog.triumf.ca/TIS/RH-ISAC/1845
It was determined from troubleshooting via PLC indicator lights that the memory battery had died during the power-off time, and because of this, the program stored was lost. Note that this is an anomaly - the battery should have lasted much longer than the shutoff duration of ~2 weeks.
The SLC500 module was replaced with a spare, which contained a new battery. The old SLC500 module is still functioning but the battery has been removed (spares will be ordered) - this module is stored in a cabinet drawer in the control room. It will need to be re-programmed if re-installed as the program was lost. The original program titled TargetHallCrane.RSS was downloaded to the module. The crane was tested in local mode and determined to be functioning.
The following links are resources for resolving this issue:
https://isaccontrols.wiki.triumf.ca/index.php/ISAC_Target_Hall_Crane
https://isaccontrols.wiki.triumf.ca/index.php/SHUTDOWN_2015_Tasks#ISAC_Target_Hall_Crane_Controls_DM_-_Completed
|
|
2041
|
Tuesday, January 07, 2020, 08:02 |
David Wang | Cooling | Standard Operation | | | Switch on HALCW MP2 |
HALCW MP2 is switched on this morning after yesterday cooling tower maintenance. LALCW P5 and P6 pumps are started by isac operator as well. The system is good so far. |
|
2042
|
Tuesday, January 07, 2020, 09:37 |
David Wang | ITW | Standard Operation | | | 5 shielding blocks are moved out of ITW top. |
5 shielding blocks are moved out of itw top. |
|
2043
|
Wednesday, January 08, 2020, 10:34 |
David Wang | Assembly/Bench Test | Development | | | Module lifting assembly ITA0490 |
The second module lifting assembly ITA0490 is moved into TH and installed onto TM3 . It will stay with TM3. I adjusted the CofG on the assembly. It is same to the first lifting assembly we are using now. After adjustment, The installation of assembly on TM3 are smooth. |
|
2046
|
Friday, January 10, 2020, 10:26 |
David Wang | ITE | Standard Operation | | | ITE water signal inerlock check. |
ITE water signal interlock check is done. Everything is good. It is a annual check we do in winter shut down time. |
|
2047
|
Monday, January 13, 2020, 14:19 |
Travis Cave | Spent Target Vault | Standard Operation | | Ta#49 and Ta#52 | spent target repackaging and moved to mini vault. |
Targeta Ta#49 and Ta#52 have been repackaged anf moved to the mini vault. Ta#49 was taken out of pail number 146 and placed into pail 229. Ta#52 was taken out of pail number 152 and placed into pail 230. |
|
2052
|
Monday, January 27, 2020, 10:40 |
David Wang | Cooling | Maintenance | | | ITE/ITW supply water presuure on dump circuits. |
With both stations in operation,ITE dump supply gauge reading is 27 psi. ITW is 20 Psi. I adjusted ITW dump pressure to 25 psi by changing the return line side pressure relieve valve.
ITE full operation+ ITW no TM: ITE dump pressure 27psi, ITW dump pressure 27psi.
2019-01-30: Water only supply to 2A beam lines only on both side, No TM2 and TM4 in water loop. ITE dump pressure 27psi, ITW dump pressure 27psi. |
|
2063
|
Thursday, February 06, 2020, 13:31 |
Adam Newsome | Spent Target Vault | Standard Operation | | UC#29 | UC#29 moved to vault location 6A, in pail 225 |
UC#29 in pail 225 was moved to the storage vault, location 6A. Field measured at 22.4 mSv/hr at ~1m. |
|
2069
|
Thursday, February 20, 2020, 09:27 |
David Wang | Spent Target Vault | Standard Operation | | | Inventory of mini storage and vault. |
Repacked nSiC#1 in SHC and moved it to mini storage vault. Transferred UCx26 and UCx28# from vault to mini-storage. See attachment for vault and mini-storage inventory. |
Attachment 1: Mini_Vault_2020-02-20.pdf
|
|
Attachment 2: Vault__2020-02-20.pdf
|
|