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ID |
Date |
Author |
Category |
Type |
Module |
Target/Number |
Subject |
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335
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Thursday, May 09, 2013, 14:23 |
chad fisher | South Hot-Cell | Repair | TM3 | | Water Block Jig Removal |
The source tray side of the water block jig has been removed in preparation for moving the module to the conditioning station for electrical tests. |
Attachment 1: IMG_1059[1].JPG
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334
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Thursday, May 09, 2013, 10:13 |
chad fisher | South Hot-Cell | Development | | | Mock-up Progress |
The source tray for the mock-up has been setup for waterline bending and soldering/brazing.
Thanks to Travis for finding the photos for the TM3 rebuild that took place in the anteroom in 09' and Maico and Dan for the support in ironing the issues with the source tray side soldering issues.
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Attachment 1: IMG_1056[1].JPG
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Attachment 2: IMG_1057[1].JPG
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Attachment 3: IMG_1058[1].JPG
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333
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Wednesday, May 08, 2013, 13:48 |
chad fisher | South Hot-Cell | Repair | TM3 | | IMG wiring check |
Checks of the wiring for the IMG are complete and have passed. |
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332
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Wednesday, May 08, 2013, 10:12 |
chad fisher | South Hot-Cell | Repair | TM3 | | TM3 9 pin wiring removal |
The 9 pin wiring has successfully been removed from TM3. |
Attachment 1: IMG_1055[1].JPG
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331
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Tuesday, May 07, 2013, 12:07 |
David Wang | ITW | Standard Operation | TM1 | | I moved 5 shielding blocks from ITE to ITW. |
Water interlock check on ITW is done. All water signals are strong on EL panel. ITW is configured to take proton beam. |
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330
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Monday, May 06, 2013, 15:45 |
Bevan Moss | Conditioning Station | Repair | TM3 | | 55 pin connector removed |
Travis and I removed the 55 pin connector from the service cap today. The feed through was left in place as a new design for the replacement has yet to be designed. It was not possible to test if the cables could be pulled easily as I believe there is still 1 cable tie in the containment box. The wires were cut flush with the top of the copper tube in case Chad cannot remove them via the hot cell. Other items removed include several cable ties and a clamp used to hold a cable tie. The side panels on the service cap we difficult to remove so copper never sieze was added when they were re-installed. I have attached some pictures from before and after a complete record can be found in the TM3 docushare folder. |
Attachment 1: 20130506_55_pin_conector_removal_IMG_3530.JPG
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Attachment 2: 20130506_55_pin_conector_removal_IMG_3525.JPG
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Attachment 3: 20130506_55_pin_conector_removal_IMG_3532.JPG
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Attachment 4: 20130506_55_pin_conector_removal_IMG_3535.JPG
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329
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Friday, May 03, 2013, 09:53 |
chad fisher | South Hot-Cell | Repair | TM3 | | 9 pin connector wiring |
With the aid of nic new manipulator snap fingers made by Maico the peek cable ties restraining the 9 pin connector wiring to the gas lines have been cut. |
Attachment 1: IMG_1047[1].JPG
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Attachment 2: IMG_1048[1].JPG
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Attachment 3: IMG_1050[1].JPG
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328
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Thursday, May 02, 2013, 10:09 |
chad fisher | South Hot-Cell | Repair | TM3 | | Service tray water block leak check |
David and I preformed a helium leak check on the service tray waterblocks and verify that no damage had been done during jig installation. All 14 circuits were checked and verified to be ok except circuit E and circuit I which were unstable when helium was applied. The resonse time on E and I would suggest that it is an issue with the bungs that were used and not the braze joint however. |
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327
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Tuesday, April 30, 2013, 07:51 |
chad fisher | South Hot-Cell | Repair | TM3 | | Coil line flow check |
David and I checked circuits p and q (the water cooled coil ciruit) for flow this morning as, with the source tray still in the module, there was both a leak and a leak tight blockage. Both p and q allowed air flow through them confirming that the blockage was in the surce tray side of the system.
The heat shield circuit was also tested for flow and it passed. |
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326
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Tuesday, April 30, 2013, 07:47 |
chad fisher | South Hot-Cell | Repair | TM3 | | TM3 Source Tray Removal |
The source tray has sucessfully been removed from TM3.
I will put a report in the TM3 rev 3 docushare directory as there were some items of note during this procedure. |
Attachment 1: IMG_1043[1].JPG
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325
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Monday, April 29, 2013, 15:58 |
Bevan Moss | South Hot-Cell | Repair | TM3 | | Source Tray Removal |
Chad removed the source tray from TM3 today, see attached picture (video was also taken). There was some interference between the window cooling lines and the frame work as well as the clamps for the ground electrode and the water block alignment jig. There was also interference between the optics alignment post (specifically the mushroom top) and the water block alignment jig. Investigation into these inferences needs to be completed as they could cause trouble for the insertion of the new source tray and alignment of the copper lines. During removal it was easy to bend copper tubes out of the way but this clearly would not work during installation. |
Attachment 1: 20130429_TM3_SOURCE_TRAY_REMOVAL_IMG_0620.JPG
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324
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Friday, April 26, 2013, 14:31 |
chad fisher | South Hot-Cell | Repair | TM3 | | TM3 refurb E.O.D. |
Service tray side of the waterblock jig is installed and all locking tabs enagaed save the heat shield circuit. Locking tab for heat shield circuit with be worked on Monday morning and installation of the source tray side of the waterblock jig should commence on monday as well. |
Attachment 1: IMG_1039.JPG
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323
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Friday, April 26, 2013, 11:20 |
chad fisher | South Hot-Cell | Repair | TM3 | | Water Block Jig (back half) |
The back half of the water block jig (services tray side) has been sucessfully located onto the module.
About 50% of the waterblocks have centered themselfs it their respective cups and the rest look good for concentricity but will require some gentle wiggling to get them to seat. |
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322
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Wednesday, April 24, 2013, 14:09 |
chad fisher | South Hot-Cell | Repair | TM3 | | TM3 Refurbishment E.O.D. |
Optics tray has been removed from module.
Waterblock jig installation has commenced. Of note, jig installation on TM3 has proven more dificult than the previous installation on TM2. Many of the waterblock assemblies are skewed (not perpendicular to plane that they should be...perpendicular to).
As I am away tomorrow, jig installation willl continue on Friday. With the source tray hopefully being removed on Monday. |
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321
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Wednesday, April 24, 2013, 11:48 |
chad fisher | South Hot-Cell | Repair | TM3 | | TM3 Source Tray Removal |
Work on TM3 source tray removal started at 10:40 am today.
The containment box has been removed, and disconnection of the optics tray is 90 complete.
Pictures can be found in the April Refurb Work Folder in the tm3 rev3 refurb pictures folder. |
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320
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Wednesday, April 24, 2013, 10:36 |
maicodallavalle | Spent Target Vault | Maintenance | | | F-308 |
The F-308's have been serviced and are ready to be filled. All inspection records are stored in docushare.
https://documents.triumf.ca/docushare/dsweb/View/Collection-1085 |
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319
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Wednesday, April 24, 2013, 10:14 |
Travis Cave | South Hot-Cell | Standard Operation | TM3 | no target | module move |
TM#3 has been moved from the conditioning station to the south hot cell, move went well. |
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318
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Wednesday, April 24, 2013, 09:00 |
Bevan Moss | Conditioning Station | Development | | | New user testing |
Controls has created a new user group that can operate the conditioning station but cannot use any of the bypasses or forces. The cooling package will be used to test this new profile. The main loop bypass has been opened to allow this testing to happen without the risk of over pressure. |
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317
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Tuesday, April 23, 2013, 16:11 |
Bevan Moss | Conditioning Station | Maintenance | TM3 | N/A | Chiller Fault 2 |
During Testing it was noticed that Fault 2 was indicated and one of the compressors would not run. Fault 2 does not indicate what the issue was and during inspection nothing could be detected. It had something to do with TCS:CHILCP3 and possibly CP2. CP1 could still be operated and was controlled manually to keep the temperature in the correct range. This was not required but it does affect the conductivity. The main power switch on the chiller unit was turned on and off and the fault was cleared. As far as I know this indicated either a freeze protect, flow, or refrigerant pressure fault. I will ask for TCS:TS6 and TCS:DIF2 to be added to the archiver so this can be further investigated in the future. |
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316
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Tuesday, April 23, 2013, 15:59 |
Bevan Moss | Conditioning Station | Standard Operation | TM3 | N/A | Systems off |
Both the Cooling Package and Vacuum have been turned off in preparation for the module move tomorrow |