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New entries since:Wed Dec 31 16:00:00 1969
Entry  Monday, May 27, 2013, 16:07, Bevan Moss, Conditioning Station, Standard Operation, TM4, Ta #40, HV conditioning 

 The HV conditioning reached a maximum of 44kV today before a spark took out the canbus card. I will attach the data once I have had a chance to format it. 

Entry  Monday, May 27, 2013, 16:01, Bevan Moss, Conditioning Station, Repair, , , CanBUS card 

 During HV conditioning of TM4 with Ta#40 there was a spark at ~43 kV that caused the Bias card to "fry". Dave Morris has been contacted and has said he will replace it tomorrow.

Entry  Monday, May 27, 2013, 15:59, Bevan Moss, Conditioning Station, Repair, , , Compressor fault 

 Once again the 7.5 compressors are tripping due to faults. I believe it is due to over pressure as a result of the chiller fans not coming on. I have contacted ESC.

Entry  Monday, May 27, 2013, 11:55, chad fisher, South Hot-Cell, Standard Operation, , , Special Tooling for RFQ target 

The special tool made for the RFQ target autopsy has been inserted into the hot cell.

 

4-40 button head screws have been successfully lossened.

Entry  Monday, May 27, 2013, 10:37, Bevan Moss, Conditioning Station, Maintenance, TM4, , Cooling Systems topped off 

Rob walker has flushed and refilled the primary side of the system (note the water still looks nasty). This morning the primary side of system needed to be bled as there were air pockets. Also TK2 had reached its low point and needed to be topped up.

Entry  Monday, May 27, 2013, 10:35, Bevan Moss, Conditioning Station, Standard Operation, TM4, Ta #40, Pumps Started HV testing to follow 

The pumps have been turned on at ~9:30 this morning. Current values are 6.61 Mohm TCS:DIC1 @19.4 C. HV testing will start momentarily.

Entry  Thursday, May 23, 2013, 14:12, Bevan Moss, Conditioning Station, Maintenance, , , Primary Circuit Drained and Flushed 

 Rob Walker has drained the primary side of the conditioning station. It will be flushed, filled  and chemically treated. It was desired to chemically treat the primary side before before but it took so long that sediment was found (things started to grow).

Entry  Thursday, May 23, 2013, 14:08, Bevan Moss, Conditioning Station, Standard Operation, TM4, Ta #40, Turbo Pumps on 

 The turbo pumps have been turned on and are running

Entry  Thursday, May 23, 2013, 14:07, Bevan Moss, Conditioning Station, Repair, , , Chiller Unit Repaired 

 ESC came today and "repaired" the chiller. There was something wrong with the VFD controller. The were able to get it to start and run correctly again but were not able to recreate the problem. At this point it appears that it has magically disappeared. 

Entry  Thursday, May 23, 2013, 11:14, David Wang, South Hot-Cell, Standard Operation, TM4, TA#40 , TM4 TA# 40 HS leak check at SHC 

TM4 Ta#40 HS leak check is done at SHC . No leak has been found so far. There will be  a helium pressure test on it at CS.

Entry  Thursday, May 23, 2013, 09:51, Travis Cave, Conditioning Station, Standard Operation, TM4, Ta#40, module move 

TM#4 with Ta#40 has been moved from the south hot cell to the conditioning station.

Entry  Wednesday, May 22, 2013, 14:11, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#40, Ta#40 installed 

Ta#40 has been installed.

Leak checking and high voltage tomorrow before the move.

Entry  Wednesday, May 22, 2013, 10:41, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#28 (RFQ Target), module move 

TM#4 with SiC#28 has been moved from the south west silo to the south hot cell.

Entry  Tuesday, May 21, 2013, 11:52, Bevan Moss, Conditioning Station, Standard Operation, TM3, No Source Tray, May 16th Long HV conditioning 16052013_TM3_long_HV_conditioning.xlsx

On May 16th 2013 the module was HV conditioned all day. As a result the maximum stable voltage has been increased to about 47kV (~4kV more than last test). A maximum voltage of 49kV was achieved but the module was very unstable. Attached is the data from the testing. Note that occasionally the sparking caused the PS to reset, it was turned back on and the voltage increased back to what it was (or lower) quickly.

Entry  Tuesday, May 21, 2013, 11:38, Travis Cave, ITE, Standard Operation, TM4, SiC#28 (RFQ Target), module move 

TM#3 with SiC#28 (RFQ Target) has been moved from the east target station to the south west silo.

Entry  Friday, May 17, 2013, 12:02, Travis Cave, Conditioning Station, Standard Operation, TM3, , module move 

TM#3 with no target or source trays has been moved from the conditioning station to the NE silo.

Entry  Friday, May 17, 2013, 10:04, chad fisher, South Hot-Cell, Repair, , , Manipulator Repair 

Manipulator has been sucessfully repaired. Recieved 0.19 mSv. Took Approx. 10-20 minutes

Entry  Wednesday, May 15, 2013, 18:12, Bevan Moss, Conditioning Station, Standard Operation, TM3, No source tray, HV test repeat 15052013_TM3_HV_test_repeat.xlsx

 After discussion with Friedhelm it was decided to continue trying to condition the module today before moving it tomorrow. The voltage was quickly raised until 40 kV where it was left for ~30 minutes. Sparking was minimal. It was then slowly raised to 44.3 kV it held this voltage for ~8 minutes when the current started to climb (remained below 200uA as set as a limit in previous tesing). There was also sparking at this point. This continued for ~2.5 minutes until once again the water resistivity sensor tripped again. It appears that there is a~ 44kV limit on TM3. Attached is the data. I will present all of the data to the group tomorrow showing the results of multiple testing.

 

 

Entry  Wednesday, May 15, 2013, 17:32, Bevan Moss, Conditioning Station, Standard Operation, TM3, , TM3 in place but not connected 15052013_TM3_in_place_but_not_connected.xlsx

 To confirm that the sparking was coming from the module rather than the conditioning station TM3 was grounded and the conditioning station biased. Attached are the results. Highlights include that there was no sparking and the station was able to achieve 60kV (limited by controls from going higher). The current from the raw file has been corrected by the required factor of 5.

Entry  Wednesday, May 15, 2013, 16:51, Bevan Moss, Conditioning Station, Standard Operation, TM3, No Source Tray, Repeat of HV Test 150502013_TM3_No_Source_Tray.xlsx

 The HV test completed on Monday was repeated today over a much longer time period. By taking longer there was slightly less sparking but once again a maximum voltage of ~44kV was achieved. The  resistivity of the water was much higher during this run so the leakage current was less but still in the >100 uA range. The spark that occurred during the ramp up to the maximum voltage caused the "water resistivity" limit to trip. This was a feed back through the control not the actual water changing as it recovered instantaneously. 

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