ID |
Date |
Author |
Target Material |
Target Oven W.O# |
Source |
Status |
Subject |
611
|
Wednesday, March 01, 2023, 21:49 |
Darwin Ortiz Rosales | Ta | 44692-3 | HP-SIS | Done | TaC coating sintering | Wednesday, March 01, 2023, 21:46
Ta HP-SIS was coated with TaC and wrapped with Ta heat-shields (3 layers + 1 inner layer around fins)
Desired temperature = 1850 C , TBHT will be set fixed at 230A (max).
Evap 2 will be pumped down over previous night
OMEGA slope= 0.990
Good vacuum = 5.00 e-4 Torr
Bad vacuum = 5.00 e-2 Torr
IGP1= 5.7 e-07 Torr
Start autoramp @1A/min to 500 A on TGHT and 230A TBHT.
Thursday, March 02, 2023, 10:10
ramping to 600A on TGHT @ 2A/30s, TBHT at 230A, 3.2V
Thursday, March 02, 2023, 11:22
At 11 am reached 1800s C and 1851C @1120 am.
TGHT = 690 A, 10.5V
TBHT = 230 A, 3.3V
Cool down to start at 3 pm
|
613
|
Monday, March 06, 2023, 21:34 |
Darwin Ortiz Rosales | SiC | 44692-3 | HP-SIS | Done | 230306SiC conditioning | Monday, March 06, 2023, 21:29
Total number of foils:382 ( including 5 analysis discs on the right side of the container)
Total length packed 17 cm (excluding 5 analysis discs that will be removed)
container has 4 Ta heat shields (one inner only around fins)
No endcaps inserted to facilitate out-gassing
Ta coated spring at both ends
ramp to 500A @ 1A/min TGHT and to 230A on TBHT
max approx 700A on TGHT and 230A on TBHT (Omega slope set = 0.990)
Then temperature = 1800C
TBHT will be set fixed at 230 A (max). TBHT heated manually and automatically to max.
Good vac at 5.00 e -4 Torr
Bad vac at 5.00 e-2 Torr
IGP1= 3e-06 Torr at start of initial ramp.
Tuesday, March 07, 2023, 07:23
IGP1= 1.2e-05 Torr
OMEGA = 1288 C
Tuesday, March 07, 2023, 10:01
Will ramp to 715 A and keep there for 4 hours. OMEGA readings not reliable beyond this point due to coating on EVAP2 window.
Tuesday, March 07, 2023, 11:10
TGHT = 715A, 11.0V
TBHT = 230A, 3.2V
OMEGA = 1750 C (but not reliable)
Maintaining for 4 hours then will ramp down @ -2A/min TGHT and -1A/min TBHT
Wednesday, March 08, 2023, 07:27
Final IGP1= 1.3e-07 Torr (before shutting down pumps) |
615
|
Sunday, March 12, 2023, 08:06 |
Darwin Ortiz Rosales | Ta | 44692-2 | HP-SIS | Done | TaC coating sintering | Sunday, March 12, 2023, 08:04
Ta HP-SIS was coated with TaC and wrapped with Ta heat-shields (3 layers + 1 inner layer around fins)
Desired temperature = 1850 C , TBHT will be set fixed at 230A (max).
Evap 2 will be pumped down over previous night
OMEGA slope= 0.990
Good vacuum = 5.00 e-4 Torr
Bad vacuum = 5.00 e-2 Torr
IGP1=1.9 e-07 Torr
Start autoramp @2A/min to120 A on TGHT and TBHT.
OMEGA target temp = 1850 C
Sunday, March 12, 2023, 13:08
start autoramp to 500A on TGHT @ 4A/min (2A/30s)
from 320A, 4.5 V on TGHT
IGP1= 6.8e-07 Torr
Sunday, March 12, 2023, 19:09
Starting ramp down @ -2A/min TGHT, and -1A/min TBHT
@687A, 10.7 V TGHT OMEGA = 1850 C
final pressure IGP1= 2.4e-06 Torr
|
616
|
Monday, March 13, 2023, 22:31 |
Darwin Ortiz Rosales | SiC | 44692-2 | HP-SIS | Done | SiC-230313 | Monday, March 13, 2023, 22:28
Total number of foils:380 ( including 5 analysis discs on the front side of the container)
Total length packed 17 cm (excluding 5 analysis discs that will be removed)
container has 4 Ta heat shields (one inner only around fins)
No endcaps inserted to facilitate out-gassing
Ta coated spring at both ends
ramp to 500A @ 1A/min TGHT and to 230A on TBHT
max approx 700A on TGHT and 230A on TBHT (Omega slope set = 0.990)
Then temperature = 1800 C. Will ramp to 1820 C
TBHT will be set fixed at 230 A (max). TBHT heated manually and automatically to max.
Good vac at 5.00 e -4 Torr
Bad vac at 5.00 e-2 Torr
IGP1= 2.8e-06 Torr at start of initial ramp.
Tuesday, March 14, 2023, 07:26
Increased autoramp to 2A/min to 700 A on TGHT while keeping TBHT to 230A, 3.3V
Tuesday, March 14, 2023, 09:53
At 743A, 11.8V TGHT
OMEGA = 1780 C. (not entirely reliable, will leave at this current for 4 hours)
Tuesday, March 14, 2023, 14:00
Starting rampdown at -2A/min on TGHT and -1A/min TBHT
Final IGP1= 5.5e-06 Torr
OMEGA= 1750C
TBHT= 230A, 3.3V
|
645
|
Tuesday, September 12, 2023, 09:54 |
Darwin Ortiz Rosales | TaC | 41369-2 | HP-SIS | Done | TaC coating sintering | Tuesday, September 12, 2023, 09:51
The coated container was wrapped in 3 Ta foil heatshield and left in evap2 over night to attain vacuum.
Target temperature on OMEGA= 1850-1900 C
OMEGA slope:= 0.990
Target time at max temperature = 4 hours
Final Current TBHT= 230 A
Final TGHT current= ~700A (adjustable)
Heating autoramp starged at 1A/min on TGHT and TBHT to 120A
Then at 2 A/min to =400 A TGHT and 230A TBHT
Good vacuum = 5.0 e-04 Torr
Bad vacuum = 5.0E-02 Torr
Initial IGP1= 2.7e-06 Torr
Tuesday, September 12, 2023, 7:00
Started autoramp @1A/min to 120A on both TGHT and TBHT
Tuesday, September 12, 2023, 09:53
Heating ramp set to 230A for both TGHT and TBHT. Rate at 2A/min for both heaters.
Tuesday, September 12, 2023, 11:21
Continued ramp on TGHT at 2A/min to 335A and now setting to 3A/min (1.5A/30s)
Tuesday, September 12, 2023, 11:47
|
TGHT |
|
Temperature ( C ) |
Voltage (V) |
Current (A) |
1205 |
5.5 |
392.0 |
Continue ramping @3A/min on TGHT
Tuesday, September 12, 2023, 13:33
Reached 1840 C at TGHT =677A and 10.5V
Will keep for 4 hours |
651
|
Thursday, December 14, 2023, 09:58 |
Darwin Ortiz Rosales | SiC | 41369-2 | HP-SIS | Done | 231208SiC conditioning | Thursday, December 14, 2023, 09:53
Target left pumping down in Evap2 overnight.
Initial weight including protective jig = 1474.3 g
Total number of target foils:388
10 analysis discs: 5x 220727-2 labelled as A and 5x 231123-2 labelled as B on the right side (front) of container. Order of discs ABABABABAB.
Total length packed 15.5 cm
container has 3 Ta heat shields including the inner made of three pieces as to cover the center block.
No endcaps inserted to facilitate out-gassing
Ta coated spring at both ends
ramp to 500A @ 1A/min TGHT and to 230A on TBHT
max approx 700A on TGHT and 230A on TBHT (Omega slope set = 0.990)
Then temperature = 1800C
TBHT will be set fixed at 230 A (max). TBHT heated manually and automatically to max.
Good vac at 5.00 e -4 Torr
Bad vac at 5.00 e-2 Torr
IGP1= 9.3e-07 Torr at start of initial ramp.
Thursday, December 14, 2023, 09:56
Started initial ramp up 1A/min on both heaters
Thursday, December 14, 2023, 11:03
Pressure dropping. Will increase ramp speed to 2A/min on both heaters (1A/30s)
Thursday, December 14, 2023, 11:17
pressure dropping. Increase ramp to 4A/min (2A/30s)
Will stop and ramping for temperature measurements
Thursday, December 14, 2023, 13:28
Increased ramp to 5A/min (2.5A/30s)
Will heat to 703A on TGHT and leave for 4 hours |
Attachment 1: Screenshot_2023-12-14_133432.png
|
|
659
|
Friday, April 26, 2024, 06:19 |
Darwin Ortiz Rosales | TaC | 45447-29 | HP-SIS | Done | TaC coating sintering |
Monday, April 29, 2024, 19:50
Started coating with coating stand.
The coated container was wrapped in 3 Ta foil heatshields.
Vacuum IGP1 initial =9.1 e-07 Torr
Target temperature on OMEGA= 1850-1900 C
OMEGA slope:= 0.990
Target time at max temperature = 4 hours
Final Current TBHT= 230 A
Final TGHT current= ~700A (adjustable)
Heating autoramp starged at 2A/min(1A/30s) on TGHT 100A
Then at 2A/min to =700 A TGHT and 230A TBHT
Good vacuum = 5.0 e-04 Torr
Bad vacuum = 5.0E-02 Torr
Monday, April 29, 2024, 20:25
Reached 1810 @700A
Will leave until 1230am |
660
|
Wednesday, May 01, 2024, 11:54 |
Darwin Ortiz Rosales | TaC | 25447-27 | HP-SIS | Done | TaC coating sintering | Wednesday, May 01, 2024, 11:53
The coated container was wrapped in 4 Ta foil heatshields.
Vacuum IGP1 initial =8.1 e-06 Torr
Target temperature on OMEGA= 1850-1900 C
OMEGA slope:= 0.990
Target time at max temperature = 4 hours
Final Current TBHT= 230 A
Final TGHT current= ~500A (adjustable)
Heating autoramp starged at 3A/min(1A/30s) on TGHT 100A
Then at 2A/min to =400 A TGHT and 230A TBHT
Good vacuum = 5.0 e-04 Torr
Bad vacuum = 5.0E-02 Torr
Wednesday, May 01, 2024, 22:19
1830C reached at 670A. 10.0V TGHT
Start cooling after 4 hours. |
559
|
Monday, October 25, 2021, 11:53 |
Darwin Ortiz Rosales | TaC | 42218-4 | HP-IG-LIS | Done | TaC coating/sintering | Monday, October 25, 2021, 11:52
Ta IGLIS tube was coated with TaC and wrapped with Ta heat-shields (3 layers)
Desired temperature = 1900 C (expected TGHT ~430 A), TBHT will be set fixed at 230A (max).
Evap 2 will be pumped down over previous night
Good vacuum = 3.00 e-3 Torr
Bad vacuum = 5.00 e-2 Torr
Initial total weight = 439.0 g
Final weight after sintering = 438.8 g
Tuesday, October 26, 2021, 07:18
IGP1= 9.2 e-07 Torr
Will ramp to 50A at 1A/min on both TGHT and TBHT.
Tuesday, October 26, 2021, 08:37
IGP1= 3.0 e-05 Torr
TGHT= 50.2 A, 0.6 V
TBHT = 49.4 A, 0.5 V
Will allow pressure to drop further then start further ramp up
Tuesday, October 26, 2021, 14:36
TGHT = 100 A, 1.3 V
TBHT = 99 A, 1.0 V
IGP1 = 3.e-5 Torr
ramp up TGHT to 400 A and TBHT to 230 A at 1.5 A/ min
Tuesday, October 26, 2021, 18:46
Will keep at 430A on TGHT and 230A on TBHT for 4 hours.
OMEGA reading = 1653 C is suspicious based on previous coating.
Tuesday, October 26, 2021, 23:05
TGHT = 430.5 A, 6.9 V
TBHT = 232.09A, 2.8 V
IGP1= 8.8e-06 Torr
Start cooling THGT at -2A/min and TBHT at -1A/min |
368
|
Thursday, May 11, 2017, 11:25 |
Laura Lambert | Empty | 41369-10 | HP-FEBIAD-CTL | Done | RUSH! Sintering TaC coated container for SiC#36 | Thursday, May 11, 2017, 11:21
Turns out SiC HP-FEBIAD that has finished conditioning is loaded in the wrong container and it should be a SiC HP-FEBIAD cold transfer line...so rush on new target.
Container coated with TaC using new method: Ends taped off, with liquid poured in and swirled around entire container, then poured back out - 'flushing technique'
Container is wrapped with 1x heatshield around each side of cooling fins, not incl center block.
Loaded into EVAP2 and currently pumping down.
Thursday, May 11, 2017, 13:40
IGP1 = 1.85e-6 Torr.
HS water valves opened.
No leaks detected.
Tapped up manually to 35A.
Vacuum stable.
IGP1 = 3.2e-6 Torr
IGP2 = 4.2e-6 Torr
Initiated auto ramp at 0.2A/min and 0.1A/min for the TGHT and TBHT respectively.
Final setpoints for TGHT = 450A and TBHT = 230A, with final desired temp of 1900C
OMEGA slope = 0.98
Friday, May 12, 2017, 07:57
IGP1 = 4.3e-7 Torr.
IGP2 = 4.4e-7 Torr
TGHT = 233A, 2.8V
TBHT = 130A, 1.6V
Increasing ramping rate to 2.0A/min and 1.0A/min for the TGHT and TBHT respectively.
Friday, May 12, 2017, 08:54
Comparing direct readouts with epics:
IGP1: direct = 1.9e-6 Torr; epics = 1.3e-6 Torr
IGP2: direct = 1.55e-6 Torr; epics = 1.4e-6 Torr
TGHT: direct = 320A, 4.38V; epics = 321A, 4.19V
TBHT: direct = 181A, 2.40V; epics = 178A, 2.34V
Friday, May 12, 2017, 10:28
IGP1 = 1.07e-6 Torr
IGP2 = 1.15e-6 Torr
TGHT = 450A, 6.37V
TBHT = 230A, 3.21V
OMEGA = 1197C
Increasing max setpoint of TGHT = 700A
Friday, May 12, 2017, 13:06
IGP1 = 2.4e-6 Torr
IGP2 = 2.5e-6 Torr
TGHT = 696A, 11.21V
TBHT = 233A, 3.26V
OMEGA = 1758C
Increasing max setpoint of TGHT = 800A
Friday, May 12, 2017, 13:32
TGHT maxed out at 715A but continued ramping.
This was noticed when current set of TGHT = 750A but readout = 715A
This is due to max voltage limit = 12.0V and readout =11.58V
Increasing TGHT max setpoint to 14.0V and restarting auto ramp from 714A
Friday, May 12, 2017, 14:45
Container has reached max setpoint of ~1900C
TGHT setpoint = 775A
TGHT = 769A, 12.54V
TBHT = 233A, 3.28V
IGP1 = 2.94e-6 Torr
IGP2 = 2.99e-6 Torr
OMEGA = 1912C
Will remain at max setpoint over weekend.
See attached photos of temperature measurements using MIKRON while TGHT current set point = 770A.
Photos are not super accurate but good as a rough idea.
Ex. for left side the point in the camera is actually pointed slightly closer to the end of the container but in the photo it looks more centered.
Saturday, May 13, 2017, 10:52 by Anders
Ramping down heaters. Temp 1912 C. Vacuum IGP1 = 5.4e-7 Torr
Monday, May 15, 2017, 13:10
Vented in air and taken out this a.m.
Target container looks good.
Fully sintered coating.
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Attachment 1: LS_during_TaC_sintering.jpg
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Attachment 2: RS_during_TaC_sintering.jpg
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371
|
Tuesday, May 16, 2017, 11:57 |
Laura Lambert | SiC | 41369-10 | HP-FEBIAD-CTL | Done | Sintering SiC#36 | Tuesday, May 16, 2017, 10:56
Target container contains 460 discs of SiC
Target packed length = 17cm.
Mass of SiC(green) = 55.5152g
Consists of 4 packs of 5 and 440 singles.
Container is wrapped with 1x heatshield around each side of cooling fins; no end caps are inserted yet - coated spring inserted both sides to hold discs in place.
Sintering temp = 1800C
Chamber is currently being pumped down.
Tuesday, May 16, 2017, 15:27
HS water valves turned on, no leaks detected.
Tapped up manually to 30A
Waited ~30min , vacuum stable.
IGP1 = 8.25e-6 Torr
Initiating auto-ramp at 0.2A/min and 0.1A/min for the TGHT and TBHT respectively.
TGHT max = 400A. TBHT max at 230A.
Slope on OMEGA = 1.09 [see elog i.d. # 370 for reasoning behind OMEGA slope choice]
Friday, May 19, 2017, 10:13
TGHT = 250A, 3.11V DR = 248A, 3.3V
TBHT = 137A, 1.68V DR = 140A, 1.73V
OMEGA = 1100C
IGP1= 6.9e-6 Torr DR = 1e-5mbar
IGP2 = 5.9e-6 Torr DR = 6.45e-6 Torr
Vacuum stable.
Increasing ramping rate to 1.0A/min and 0.5A/min for the TGHT and TBHT respectively.
Friday, May 19, 2017, 10:33
Change in plan and switching ramping rate to 0.5A/min and 0.2A/min for the TBHT and TGHT respectively.
Friday, May 19, 2017, 14:49
TGHT = 400A, 5.46
TBHT = 200A, 2.66
IGP1 = 2.7e-5 Torr
IGP2 = 2.2e-5 Torr
OMEGA = 1200C
Increasing max setpoint for TGHT to 550A
Decreasing ramping rate to 0.2A/min and 0.1A/min for over the weekend.
Tuesday, May 23, 2017, 09:23
TGHT = 550A, 8.37
TBHT = 230A, 3.14
IGP1 = 1.6e-7 Torr
IGP2 = 1.6e-7 Torr
OMEGA = 1570C
Increasing max setpoint for TGHT to 600A at rate to 0.5A/min
Tuesday, May 23, 2017, 11:45
TGHT = 600A, 9.36
IGP1 = 3.5e-7 Torr
IGP2 = 3.8e-7 Torr
OMEGA = 1675C
Increasing max setpoint for TGHT to 625A at rate to 0.5A/min
Tuesday, May 23, 2017, 13:03
TGHT = 625A, 9.80V
IGP1 = 5.2e-7 Torr
IGP2 = 5.7e-7 Torr
OMEGA = 1715C
OMEGA no longer valid around 640A as temperature drops instantly after tapping up.
Could be due to target movement at high temperature.
No obvious window coating.
Tapped up manually to 660A, 10.49V.
Will remain at max setpoint overnight.
Wednesday, May 24, 2017, 11:13
TGHT = 660A, 10.74V
TGHT power supply = 662A, 11.00V
TBHT = 230A, 3.16V
TBHT power supply = 232A, 3.25V
IGP1 = 4.2e-7 Torr
IGP1 direct readout = 5.9e-7 mbar
IGP2 = 4.6e-8 Torr
IGP2 direct readout = 5e-7 Torr
Evap2 reached max setpoint yesterday afternoon.
Window has thiny coating - see attached photo.
OMEGA = 1800
MIKRON = ~1800
Initiating auto cool at 2.0A/min and 1.0A/min for the TGHT and TBHT respectively.
Wednesday, May 24, 2017, 11:36
Change of plan.
TGHT = 620A, TBHT = 210A
Ramping back-up to max setpoints and will remain at those points until vacuum starts to decrease more.
Friday, May 26, 2017, 15:24
IGP1 = 2.1e-7 Torr
IGP2 = 2.2e-7 Torr
TGHT = 660A, 10.72V
TBHT = 230A, 3.21V
All windows coated.
Remained at max setpoints for ~3.5days.
Conditioning process complete.
Initiating auto-cool at 2A/min and 1A/min for the TGHT and TBHT respectively.
Tuesday, May 30, 2017, 14:41
Target vented in air and removed from evap2
Looks good!
Endcaps inserted and expanded.
See photos attached.
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Attachment 1: window_at_max_setpoint_after_1_day.jpg
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Attachment 2: 20170530_094047_Richtone(HDR).jpg
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Attachment 3: 20170530_094118_Richtone(HDR).jpg
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Attachment 4: 20170530_094137_Richtone(HDR).jpg
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410
|
Wednesday, May 23, 2018, 15:21 |
Laura Lambert | Empty | | HP-FEBIAD-CTL | Done | Sintering TaC coating container for UCx#23 | Wednesday, May 16, 2018, 09:56
Container coated with TaC using 'flushing technique' and let dry over weekend.
Cleaned ionizer tube with acetone, no coating inside ionizer tube.
Wrapped with 3 x Ta heat shields, not incl center block
OMEGA slope = 0.98
*NOTE: realized after pumping down, filament on IGP2 is burnt out and needs replacing, will order a new one and use IGP1 for this process
Thursday, May 17, 2018, 13:15
HS water valves remained open since the last time evap2 was used, no leak check done.
Tapped up manually to 50A.
Waited ~1hr
Vacuum stable.
IGP1 = 1e-6 Torr
Initiating auto ramp for TGHT @ 0.2A/min to a max setpoint of 350A
Initiating auto ramp for TBHT @ 0.1A/min to a max setpoint of 230A
Once max setpoints achieved, will tap up manually to final desired temperature of 1900C
Friday, May 18, 2018, 13:00
Tapped up manually.
TGHT = 495A, 8.84V
TBHT = 230A, 3.26V
MIKRON = 2000C
Filament = 1910C
OMEGA = 1910C
Will remain at max setpoints over weekend.
Tuesday, May 22, 2018, 10:04
Remained at max setpoints over long wknd.
TGHT = 495A, 8.85V
TBHT = 230A, 3.26V
IGP1 = 2.47e-7 Torr
Initiating auto-cool at 2.0A/min and 1.0A/min for the TGHT and TBHT respectively.
Wednesday, May 23, 2018, 10:08
Vented in air this morning.
Container looks good!
Transferred into glove box.
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37
|
Sunday, July 22, 2012, 20:51 |
John Wong | NiO | 38481-7 | HP-FEBIAD | Done | Sintering NiO#1 | Sunday, July 22, 2012, 20:30
The NiO target materials were loaded into the container today.
Total discs = 500, (10 discs/pack)
length (after loaded) = 9.0cm
Target container is wrapped with Ta-heat shields, and will be removed after the sintering process.
One regular end cap is inserted (with Ni-foil inserted as a divider). The caps, however, are very loose (tried 2 caps and still loose). Hopefully the thermo diffusion bonding will seal the cap...
The other end is inserted with a D-cap for out-gassing proposes, and will be replaced with the regular end-cap after the process.
(see attachment#1)
Sunday, July 22, 2012, 20:48
The camber has been pumped down and currently IG1=1.3e-6 Torr.
The HS cooling water was turned on and no leaks were detected.
TGHT and TBHT were stepped up to 50A.
Auto-ramping is initiated at 0.2A/min for TGHT max = 250A, TBHT max = 230A.
Thursday, July 26, 2012, 23:31
TGHT and TBHT have reached to 250A (local @ 242A/2.88V) and 230A, respectively, and have stayed for ~4hrs (see attachment#2)
Currently, IGP1 = 4.9e-7 Torr, IGP2 = 3.5e-7 Torr, CG1B = 13mTorr.
Initiating auto-cool down at 2A/min.
Monday, July 30, 2012, 15:11
The chamber was vented and the target was removed.
There was significant condensation oily fluid coated Cu-heatshield lid and around the ionizer opening.
Overall, the target looks very good. The NiO target material was nicely sintered. No shrinkage or loose particles were observed (see attachment #3).
The endcap, however, was not properly fitted and it just fell off, (see attachment #4).
Both ends of the target are currently opened; the expension tool for the endcap is in order and hopefully this will solve the problem.
The target is being stored in the fumehood
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Attachment 1: NiO#1_sinteringevap2.png
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Attachment 2: NIO#1_TGHT_TBHT_250_220.png
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Attachment 3: Sintered_NiO.GIF
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Attachment 4: Endcap.GIF
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43
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Tuesday, August 14, 2012, 15:57 |
John Wong | SiC | 38295-8 | HP-FEBIAD | Done | Testing endcaps inserted /w the new expansion tool | Tuesday, August 14, 2012, 15:44
This SiC target was prepared in May 2011 with the Evaporator#1. The target will not used for online.
Two endcaps were inserted with the new expansion tool. The target will be heated up to the normal operating condition (TGHT =580A, TBHT = 230A).
The chamber is currently being pumped down.
Tuesday, August 14, 2012, 16:21
Earlier, the Cu-heat shield was removed from the evaporator to replace the insulators, so all the seals were placed with new ones. However,
there seems to be some leaks after the HS cooling water is turned on. (see attachment#1).
The TP off, and the chamber is vented for investigation.
Tuesday, August 14, 2012, 17:25
All the 3 seals for the Cu-heat shield were replaced. The chamber has been pumped down and the HS water valve is open. No leaks are detected.
Tuesday, August 14, 2012, 17:29
Initiated auto-ramping at 2A/min for both TGHT and TBHT.
Parameter constraints: good vac @ 2.0e-5 Torr, bad vac @ 3.0e-5 Torr.
Currently, IG1 @ 6.5e-6 Torr.
Wednesday, August 15, 2012, 09:52
TGHT and TBHT have reached to 520A and 230A, respectively, and have stayed at the currents for about 10 hours. (see attachment #2)
IG is currently at 7.7e-7 Torr.
Initiating auto-cool down at 2A/min.
Thursday, August 16, 2012, 11:23
Chamber is vented.
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Attachment 1: vacuum_leaks.PNG
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Attachment 2: TGHT_TBHT.png
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60
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Wednesday, March 06, 2013, 10:41 |
Anders Mjos | Empty | 38481-4 | HP-FEBIAD | Done | CTL thermal test | Wednesday, March 06, 2013
The Cool Transfer Line (CTL) test target is installed for thermal tests. Drawing number is ITD0431 REV A.
Thermocouple channels are as follows:
T1: Cu block on CTL
T2: Heat Shield above CTL
T3: Heat Shield cooling water Supply
T4: Heat Shield cooling water Return
Cooling water is in Evap2 supplied to the cooling line that goes directly to the area on the Heat Shield above the CTL.
Test results attached.
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Attachment 1: CTL_1st_Assebmly_Thermal_Test_Evap2.pdf
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Attachment 2: 2013-03-08_Evap2_First_Thermal_Test.pdf
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61
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Wednesday, March 06, 2013, 17:53 |
John Wong | Empty | 38481-4 | HP-FEBIAD | Done | CTL thermal test |
Anders Mjos wrote: |
Wednesday, March 06, 2013
The Cool Transfer Line (CTL) test target is installed for thermal tests. Drawing number is ITD0431 REV A.
Thermocouple channels are as follows:
T1: Cu block on CTL
T2: Heat Shield above CTL
T3: Heat Shield cooling water Supply
T4: Heat Shield cooling water Return
Cooling water is in Evap2 supplied to the cooling line that goes directly to the area on the Heat Shield above the CTL.
|
Wednesday, March 06, 2013, 17:23
The target has been pumping down to 5.3 e-7 Torr. On the RGA mass scan, mainly H2O (mass 18 + constituents) was detected at ~2.7pA (see attachment #1).
The target will be heated up: TGHT = 850A (rate @ 1A/min); TBHT = 300A (rate @ 1A/min).
Thursday, March 07, 2013, 11:51
TGHT and TBHT reached to 850A (local, 845A\13.80V) and 300A, respectively. The out gassing of CO (mass 28) reached to ~5pA at the max currents. (see attachment #2)
TBHT will be ramped down to 0A to compare the temperatures.
Thursday, March 07, 2013, 15:55
TBHT at 0A. See attachment#3 for the temperatures and RGA data before further ramping down the TGHT.
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Attachment 1: rampingup_1.PNG
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Attachment 2: rampingup_2.PNG
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Attachment 3: autorampingdown_23.PNG
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Monday, March 11, 2013, 12:23 |
Anders Mjos | Empty | 38481-4 | HP-FEBIAD | Done | CTL thermal test 2 |
Anders Mjos wrote: |
Wednesday, March 06, 2013
The Cool Transfer Line (CTL) test target is installed for thermal tests. Drawing number is ITD0431 REV A.
Thermocouple channels are as follows:
T1: Cu block on CTL
T2: Heat Shield above CTL
T3: Heat Shield cooling water Supply
T4: Heat Shield cooling water Return
Cooling water is in Evap2 supplied to the cooling line that goes directly to the area on the Heat Shield above the CTL.
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Monday, March 11, 2013
The CTL test target was installed again for a second thermal test. CTL block fastened to HS with 1 in lbs. A small piece of Ta-foil of 0.001" thickness was used between the CTL Cu-block and the Ta transfer line to reduce the heat transfer..
Thermocouples were re-attached to CTL and Heat Shield (see above for channels #s).
See attached graph (PDF) for details. |
Attachment 1: 2013-03-11_Evap2_Second_Thermal_Test.pdf
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Monday, March 11, 2013, 15:59 |
John Wong | Empty | 38481-4 | HP-FEBIAD | Done | CTL thermal test 2 |
Anders Mjos wrote: |
Anders Mjos wrote: |
Wednesday, March 06, 2013
The Cool Transfer Line (CTL) test target is installed for thermal tests. Drawing number is ITD0431 REV A.
Thermocouple channels are as follows:
T1: Cu block on CTL
T2: Heat Shield above CTL
T3: Heat Shield cooling water Supply
T4: Heat Shield cooling water Return
Cooling water is in Evap2 supplied to the cooling line that goes directly to the area on the Heat Shield above the CTL.
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Monday, March 11, 2013
The CTL test target was installed again for a second thermal test. CTL block fastened to HS with 1 in lbs. A small piece of Ta-foil of 0.001" thickness was used between the CTL Cu-block and the Ta transfer line to reduce the heat transfer..
Thermocouples were re-attached to CTL and Heat Shield (see above for channels #s).
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Monday, March 11, 2013, 15:55
Chamber was pumped down to 2 e-7 Torr. HS water valve opened and no leaks were detected.
TGHT and TBHT are ramping up to 850A and 300A at 2A/min, respectively.
RGA is running...
Tuesday, March 12, 2013, 10:44
TGHT/TBHT reached to max currents.
See attachment #1 for temperature and RGA measurements.
Cooling down in process... 5A/min.
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Attachment 1: autorampingup_110.PNG
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Wednesday, March 13, 2013, 16:08 |
Anders Mjos | Empty | 38481-4 | HP-FEBIAD | Done | Thermal test | Wednesday, March 13, 2013
Thermocouple channels (see attached PDF for photos)
T1 - Left target leg at tube
T2 - Between cooling fins close to tube, left side
T3 - Supply water HS
T4 - Return water HS
Friday, March 22, 2013
Test not conducted. Target removed. |
Attachment 1: HP-FEBIAD-A_TC_at_fins.pdf
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Thursday, March 14, 2013, 12:27 |
Anders Mjos | Empty | 38481-4 | HP-FEBIAD | Done | CTL thermal test 3 (w/o CTL block) | Thursday, March 12, 2013
The CTL was removed and target heated to 580A / 300A
T1: Left target leg close to tube
T2: Heat Shield above CTL
T3: Heat Shield cooling water Supply
T4: Heat Shield cooling water Return
Thursday, March 13, 2013
The target was cooled down
Results attached as PDF and Excel |
Attachment 1: 2013-03-13_-_FEBIAD-HP-A_TargetLeg_and_HeatShield_TC.pdf
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Attachment 2: 2013-03-13_-_FEBIAD-HP-A_TargetLeg_and_HeatShield_TC.xlsx
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