Hello all,
TM2's first performance in the Conditioning Station with the new source tray was not great, with sparking and HV degradation beginning to occur at 30kV:
https://elog.triumf.ca/TIS/RH-ISAC/1039
This is perplexing, because the module without the source tray performed well at the TCS:
https://elog.triumf.ca/TIS/RH-ISAC/829
AND the new source tray performed well at the test stand (i.e. not inside the module):
https://elog.triumf.ca/TIS/Test-Stand/447
Upon inspection back at the Hot Cell last week after the failure, David Wang was observant enough to notice that one of the steerer coax wires (ground plane) was essentially touching one of the FEBIAD gas lines (HV plane) in the new source tray installation (photo attached). Closer inspection by a group consisting of Anders, Alex, and myself revealed some apparent tracking and damage to the wire sheath.
https://elog.triumf.ca/TIS/RH-ISAC/1045
We believed at this point that the bad HV performance of TM2 was due to this problem. The wires were originally arranged loose as it was believed it would be easier to install them in the Hot Cell this way. However, it turned out to be a bad decision, as the wires at ground ended up becoming stray and touching the HV surface.
To correct the problem, the old wires were removed, and a new steere wire bundle was made using a PEEK material sheath. This new sheath bundle was installed over the last day or so. The penning gauge wire was kept separate from the steerer wire bundle. You can see the new wire bundle and penning gauge wire in the attached photo, now with a healthy clearance to the FEBIAD gas lines.
Chad has been instructed to re-install the Einzel lens wire, install the new ZrC target, and replace the containment box in preparation for transport back to the TCS for another HV test. If anybody would like to see the source tray today before ~3pm, I have asked Chad to wait for my final OK to put the containment box back on the module.
I apologize for this problem. We are hopeful the solution we have installed will improve the HV performance. Much work over the last 2+ years was put into building and installing this source tray by many contributors inside and outside of Remote Handling, and we want this module to succeed more than anybody!
Thanks and best regards,
Grant |
TGHT, TBHT, ANODE and COIL power tested (some amps/volts)
Monday, August 17, 2015, 10:43: BIAS/EL/EE to 15/7.5/1.5 kV
Monday, August 17, 2015, 10:45 : COIL 20A, ANODE 200V
Keiko fixed the auto-ramping program and access rights to it.
Monday, August 17, 2015, 13:06: Auto-ramping at 2/1 A/min. Good/bad vacuum at 6E-6 and 8E-6 T
Monday, August 17, 2015, 13:24 : ANODE current limit set incorrectly. Corrected and 200V (9 mA)
Monday, August 17, 2015, 15:28: COIL to 50 A
Monday, August 17, 2015, 15:43: Reduced ANODE to 100 V
Monday, August 17, 2015, 16:56 : Increased EL to 8.3 kV to increase FC current.
Monday, August 17, 2015, 17:04 : FC0 current at 1.5E-8 A
Beam ionized and accelerated on the new TM2 source tray
Monday, August 17, 2015, 17:12 : TGHT / TBHT at 500 / 250 A. Will leave over night to outgas. ISAC ops are monitoring the source.
Tuesday, August 18, 2015, 08:07: Everything stable overnight. Continue ramping heaters.
Tuesday, August 18, 2015, 08:48: TBHT voltage limited by EPICS (hardcoded) at 273 A.
TGHT/TBHT at 600 / 273 A
Tuesday, August 18, 2015, 09:52: Adjusted COIL current down to 0 and back up. Response seen on FC0.
Tuesday, August 18, 2015, 22:29 : Starting cool down.
Wednesday, August 19, 2015, 08:26: Source and HV off. EE configured to conditioning mode. RGA off.
Wednesday, August 19, 2015, 08:42: BIAS/EL at 15 / 7.5 kV. PNG1 at 3.5E-6 T, IG1 at 3.9E-7 T
Wednesday, August 19, 2015, 08:53: BIAS/EL 20 / 10 kV. 2 sparks.
Wednesday, August 19, 2015, 09:54: BIAS/EL 30 / 15 kV. Some sparking around 28 kV required BIAS voltage to be reduced momentarily.
Wednesday, August 19, 2015, 10:04: Sparking at 30 kV. Reduced BIAS to 13 kV to get spar rate to less than 10/min
Wednesday, August 19, 2015, 10:19 : BIAS current limiting. Switch off BIAS and EL
Wednesday, August 19, 2015, 12:04: Water off for purging and leak test.
Wednesday, August 19, 2015, 12:52: Vacuum response observed while David was working on purging the water lines. This turned out to be when the valve to the leak detector was opened. |