Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 80 of 140  Not logged in ELOG logo
New entries since:Wed Dec 31 16:00:00 1969
Entry  Friday, October 18, 2013, 15:55, Bevan Moss, Conditioning Station, Standard Operation, TM4, , Turbo Pumps are on 

 The Turbo pumps are now running on TCS

Entry  Monday, October 21, 2013, 10:52, Bevan Moss, Conditioning Station, Standard Operation, TM4, , Cooling On and Electrical Connections Made 

 The electrical connection have been made and cooling package was started at ~10:50am today

Entry  Monday, October 21, 2013, 12:29, Bevan Moss, Conditioning Station, Repair, TM4, , BIAS Canbus 

 There is something wrong with the BIAS canbus controller. It says that it is not alive and has timed out. I have tried unplugging it and plugging it back in but that has not resolved the problem as it normally does. I have contacted Dave Morris and am waiting to hear from him. I cannot HV test without this controller.

Entry  Tuesday, October 22, 2013, 16:52, Bevan Moss, Conditioning Station, Repair, , , Canbus base card for BIAS  

 The base card in the canbus BIAS module was determined to be faulty. Dave Morris removed a card VECC to repair the conditioning station. 

Entry  Tuesday, October 22, 2013, 17:04, Bevan Moss, Conditioning Station, Standard Operation, TM4, , HV testing 22102013_TM4_Coil_removed_EL_testing_(1).txt

 This afternoon TM4 with the coil removed was tested with HV. The EINZEL LENS was first tested independently while the bias canbus was being repaired. The current on the EL looked stable at 25kV for 5 minutes. At 27.5kV the current becomes unstable and occasionally sparks. This voltage was held for 30 minutes but the current did not appear to be becoming more stable. Further extended testing would be required to determine if this can be conditioned out. At this point I would suggest the EL has a HV limit near 25kV.

The BIAS and EL were then brought up to 35kV and 17.5kV respectively. This voltage was held for 35 minutes with the BAIS only sparking twice. The module can most likely hold a higher voltage but for the next 2 runs does not require more than 35kV. Further testing was not completed due to time constraints. It is recommended during the shut down that TM4 is tested to its limits. The data from the testing has been attached.

Entry  Tuesday, October 22, 2013, 17:07, Bevan Moss, Conditioning Station, Standard Operation, , , services shut down 

 The turbo pump, roughing pump, have been turned off and the valves for venting opened. The cooling package has also been turned off.

Entry  Friday, October 25, 2013, 06:58, David Wang, South Hot-Cell, Standard Operation, TM4, , Leak check on TM4 target heat shield 

Maico and I leak checked HS circuit after Chad installed the target. The circuit was a little bit difficult o pump down because of residue water moister inside. But once the moisture was pumped out, the pumping down was smooth and fast. The base leak rate 0.0xE-9 atm.cc/sec, base pressure 0.0xE-4 torr. Maico checked helium flow before the leak test. Then,He sprayed helium to all 3 VCR fiitings on target with 2 seconds on each one, He also flushed 10 seconds helium around the target. There were no any response during all these test time on leak detector.He checked the helium flow again after the test  and confirmed the helium flow.  The HS circuit is leak tight.

Entry  Thursday, October 31, 2013, 10:36, David Wang, ITW, Standard Operation, TM4, , I moved 5 shielding blocks from ITE to ITW. 

I moved 5 shielding blocks from ITW to ITE. The ITW  is configured to take proton beam.

Entry  Monday, November 04, 2013, 10:46, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Exploration TM2_20131104.jpg

TM2 is now in the hot cell with the containment box off for inspection and eventual blank off off the water blocks.

Upon initail inspection the status (fron a hot cell point of view) is:

-Water block jig is equipped/on

-There is a thermocouple line that will need to be removed

-TM2 requires a new front containment box cover - already manufactured and waiting for installation

 

Entry  Tuesday, November 05, 2013, 10:37, chad fisher, South Hot-Cell, Repair, TM2, , Thermocouple wire removal 

The old thermocouple wire has been sucessfully removed from the module.

Thanks Bevan, Travis and David.

Entry  Wednesday, November 06, 2013, 10:41, David Wang, South Hot-Cell, Repair, TM2, , Installed 2 turbopumps on TM2 

Bevan and I installed 2 turbo pumps on TM2. The o- ring flanges on TM2 had been cleaned before the installation.

Entry  Tuesday, November 12, 2013, 09:51, David Wang, ITE, Standard Operation, TM3, , TM3 disconnection 

TM3 has been disconnected this morning and  purged all HV water lines. I found the power plug for all turbo pump fans wasnt connected  during the last run. That maybe the one of the reason on that ITE TP3 failure.

Entry  Tuesday, November 12, 2013, 10:59, Bevan Moss, South Hot-Cell, Standard Operation, TM2, , Electrical Test tm2_elec_test.pdf

 Don Jackson and Myself completed started an electrical test on TM2. All lines passed the with OL to ground. When testing in between the lines individually there were several lines that read other than OL. It was decided to abandon the testing as there were too many "failures". The results are attached. The testing will be repeated in the conditioning station with vacuum. It is not expected that this will change anything as during a quick visual inspection it appears the lines are touching. Of note the water block jig was removed this morning by Chad.

Entry  Tuesday, November 12, 2013, 12:43, Bevan Moss, Conditioning Station, Standard Operation, TM2, , TM2 moved from SHC to TCS 

 TM2 was moved by myself and David from the SHC to the TCS. Move went well. Curiously the fields on the module were measured higher than the previous measurement (now ~5.8mSv/hour) .

Entry  Tuesday, November 12, 2013, 14:31, Bevan Moss, Conditioning Station, Standard Operation, TM2, , Turbo pumps started 

 The turbo pumps have been started on TM2 and the conditioning station.

Entry  Tuesday, November 12, 2013, 14:33, Bevan Moss, Conditioning Station, Repair, , , Cooling manifold returned 

 The cooling manifold for the conditioning station high power water cooled lines has been returned. The cooling package can once again be operated

Entry  Wednesday, November 13, 2013, 10:01, David Wang, Conditioning Station, Repair, TM2, , TM2 leak check at conditioning station TM2_leak_check_at_CS_2013-11-13.pdf

I leak checked TM2 at conditioning station this morning. All air to vacuum seals on the top of the module are good. All water lines are pressured with 60 psi helium for minutes each. One of the tube heater + water line( 2lines for tube heater + for supply and return) has a huge response on 60 psi helium pressurizing. The leak rate went from 6.0xE-9atm.cc/sec to maximum leak rate in 5 seconds and I saw a pressure increasing either. when I pressurize the other side tube heater + line ,the leak detector also had a response,but it is slower than first side .Since the top of the water adaptor isn't sealed , so I think the leak should be in one line only. All other water lines are leak tight since I didnt see any obvious response on leak detector at 5 to 6x E-9 atm.cc/sec which is very low on leak rate. 

Entry  Thursday, November 14, 2013, 08:08, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Blank off and jig removal TM2_20131108.jpgTM2_20131112.jpg

Firday, November 8 all water blocks (excluding I and K) were blanked off and vacuum leak checked. No responses were found. (First Picture)

I and K could not be blanked off without removal of the water block jig. Also, I dropped one of the blank offs onto the table, so one line could not be blanked off until a new clean blank off was inserted into the cell. In addition, there was still reminace of a bolt in block Ias it aslo could not be removed until the water block jig was removed.

Tuesday, November 12 a new blank off was put into the cell. The water block jig was removed, which was very easy, confirming documentation from installation (in 2008?) that it fit very well / the blocks were bent and soldered to the jig very carefully.

Screw was removed from I and both I and K were blanked off and vacuum leak checked. No response. (Second Piccture)

Containment box was re-installed and module ready to move to the conditioning station by noon.

 

 

 

Entry  Friday, November 15, 2013, 16:48, Bevan Moss, Conditioning Station, Standard Operation, TM2, , HV Testing TM2_conditioning_15112013.JPG15112013_TM2_No_source_tray_HV_test.txt

 High voltage testing was started on TM2 with no source tray today. The maximum stable for 1 minute voltage reached was 47.5kV but the module is still conditioning. With every step up in voltage the current goes up a large amount and slowly bleeds down. Large sparks disrupts the connection of the CANBUS to the PS which is irritating but the module can be brought up to the equivalent voltage in less than 30 seconds. Attached is a screen shot of most of the strip tool. I have also attached all of the dumped data. The module will be left under vacuum with the water running over the weekend and HV testing will continue on Monday. 

Entry  Monday, November 18, 2013, 11:54, Bevan Moss, Conditioning Station, Repair, TM2, , Fault on TCS Chill 

 This morning when I went to start HV conditioning CP2 and CP3 both had faults and the temperature of the water was ~27C. I reset the compressors by flipping the system reset switch. This cleared the fault and allowed the compressors to come one. To the best of my knowledge these faults happen as a result of compressor fluid pressure too low or high and temperature too low or high and lack of flow. The system cannot determine which one it was that caused the trip. The system restarted and faulted again. As I was watching this time it can be determined that the fault was the result of an over temperature event. This was the caused by the cooling fans not coming on. Which was traced to the fan VFD controllers which both read OP3 which is an Over voltage during constant speed operation. The operating manual lists these as the possible causes

The input voltage is fluctuating abnormally.

• Power network is greater than 200 kVA

• Power factor capacitor switching

• SCR switching on power network

• The drive controller is regenerating— the load causes the motor to run at a frequency higher than drive controller output frequency.

• Intermittent output phase fault

The proposed solutions are

• Install a line reactor.

• Check the input and output circuits for phase failure and rectify. 

I will continue to monitor over the next few days to see if this continues to happen. If it does I will contact ESC.

ELOG V2.9.2-2455