Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 80 of 140  Not logged in ELOG logo
ID Date Author Category Type Module Target/Numberdown Subject
  513   Friday, October 18, 2013, 15:55 Bevan MossConditioning StationStandard OperationTM4 Turbo Pumps are on

 The Turbo pumps are now running on TCS

  514   Monday, October 21, 2013, 10:52 Bevan MossConditioning StationStandard OperationTM4 Cooling On and Electrical Connections Made

 The electrical connection have been made and cooling package was started at ~10:50am today

  515   Monday, October 21, 2013, 12:29 Bevan MossConditioning StationRepairTM4 BIAS Canbus

 There is something wrong with the BIAS canbus controller. It says that it is not alive and has timed out. I have tried unplugging it and plugging it back in but that has not resolved the problem as it normally does. I have contacted Dave Morris and am waiting to hear from him. I cannot HV test without this controller.

  518   Tuesday, October 22, 2013, 16:52 Bevan MossConditioning StationRepair  Canbus base card for BIAS

 The base card in the canbus BIAS module was determined to be faulty. Dave Morris removed a card VECC to repair the conditioning station. 

  519   Tuesday, October 22, 2013, 17:04 Bevan MossConditioning StationStandard OperationTM4 HV testing

 This afternoon TM4 with the coil removed was tested with HV. The EINZEL LENS was first tested independently while the bias canbus was being repaired. The current on the EL looked stable at 25kV for 5 minutes. At 27.5kV the current becomes unstable and occasionally sparks. This voltage was held for 30 minutes but the current did not appear to be becoming more stable. Further extended testing would be required to determine if this can be conditioned out. At this point I would suggest the EL has a HV limit near 25kV.

The BIAS and EL were then brought up to 35kV and 17.5kV respectively. This voltage was held for 35 minutes with the BAIS only sparking twice. The module can most likely hold a higher voltage but for the next 2 runs does not require more than 35kV. Further testing was not completed due to time constraints. It is recommended during the shut down that TM4 is tested to its limits. The data from the testing has been attached.

  520   Tuesday, October 22, 2013, 17:07 Bevan MossConditioning StationStandard Operation  services shut down

 The turbo pump, roughing pump, have been turned off and the valves for venting opened. The cooling package has also been turned off.

  527   Friday, October 25, 2013, 06:58 David WangSouth Hot-CellStandard OperationTM4 Leak check on TM4 target heat shield

Maico and I leak checked HS circuit after Chad installed the target. The circuit was a little bit difficult o pump down because of residue water moister inside. But once the moisture was pumped out, the pumping down was smooth and fast. The base leak rate 0.0xE-9 atm.cc/sec, base pressure 0.0xE-4 torr. Maico checked helium flow before the leak test. Then,He sprayed helium to all 3 VCR fiitings on target with 2 seconds on each one, He also flushed 10 seconds helium around the target. There were no any response during all these test time on leak detector.He checked the helium flow again after the test  and confirmed the helium flow.  The HS circuit is leak tight.

  531   Thursday, October 31, 2013, 10:36 David WangITWStandard OperationTM4 I moved 5 shielding blocks from ITE to ITW.

I moved 5 shielding blocks from ITW to ITE. The ITW  is configured to take proton beam.

  534   Monday, November 04, 2013, 10:46 chad fisherSouth Hot-CellRepairTM2 TM2 Exploration

TM2 is now in the hot cell with the containment box off for inspection and eventual blank off off the water blocks.

Upon initail inspection the status (fron a hot cell point of view) is:

-Water block jig is equipped/on

-There is a thermocouple line that will need to be removed

-TM2 requires a new front containment box cover - already manufactured and waiting for installation

 

  535   Tuesday, November 05, 2013, 10:37 chad fisherSouth Hot-CellRepairTM2 Thermocouple wire removal

The old thermocouple wire has been sucessfully removed from the module.

Thanks Bevan, Travis and David.

  536   Wednesday, November 06, 2013, 10:41 David WangSouth Hot-CellRepairTM2 Installed 2 turbopumps on TM2

Bevan and I installed 2 turbo pumps on TM2. The o- ring flanges on TM2 had been cleaned before the installation.

  537   Tuesday, November 12, 2013, 09:51 David WangITEStandard OperationTM3 TM3 disconnection

TM3 has been disconnected this morning and  purged all HV water lines. I found the power plug for all turbo pump fans wasnt connected  during the last run. That maybe the one of the reason on that ITE TP3 failure.

  538   Tuesday, November 12, 2013, 10:59 Bevan MossSouth Hot-CellStandard OperationTM2 Electrical Test

 Don Jackson and Myself completed started an electrical test on TM2. All lines passed the with OL to ground. When testing in between the lines individually there were several lines that read other than OL. It was decided to abandon the testing as there were too many "failures". The results are attached. The testing will be repeated in the conditioning station with vacuum. It is not expected that this will change anything as during a quick visual inspection it appears the lines are touching. Of note the water block jig was removed this morning by Chad.

  539   Tuesday, November 12, 2013, 12:43 Bevan MossConditioning StationStandard OperationTM2 TM2 moved from SHC to TCS

 TM2 was moved by myself and David from the SHC to the TCS. Move went well. Curiously the fields on the module were measured higher than the previous measurement (now ~5.8mSv/hour) .

  540   Tuesday, November 12, 2013, 14:31 Bevan MossConditioning StationStandard OperationTM2 Turbo pumps started

 The turbo pumps have been started on TM2 and the conditioning station.

  541   Tuesday, November 12, 2013, 14:33 Bevan MossConditioning StationRepair  Cooling manifold returned

 The cooling manifold for the conditioning station high power water cooled lines has been returned. The cooling package can once again be operated

  542   Wednesday, November 13, 2013, 10:01 David WangConditioning StationRepairTM2 TM2 leak check at conditioning station

I leak checked TM2 at conditioning station this morning. All air to vacuum seals on the top of the module are good. All water lines are pressured with 60 psi helium for minutes each. One of the tube heater + water line( 2lines for tube heater + for supply and return) has a huge response on 60 psi helium pressurizing. The leak rate went from 6.0xE-9atm.cc/sec to maximum leak rate in 5 seconds and I saw a pressure increasing either. when I pressurize the other side tube heater + line ,the leak detector also had a response,but it is slower than first side .Since the top of the water adaptor isn't sealed , so I think the leak should be in one line only. All other water lines are leak tight since I didnt see any obvious response on leak detector at 5 to 6x E-9 atm.cc/sec which is very low on leak rate. 

  543   Thursday, November 14, 2013, 08:08 chad fisherSouth Hot-CellRepairTM2 TM2 Blank off and jig removal

Firday, November 8 all water blocks (excluding I and K) were blanked off and vacuum leak checked. No responses were found. (First Picture)

I and K could not be blanked off without removal of the water block jig. Also, I dropped one of the blank offs onto the table, so one line could not be blanked off until a new clean blank off was inserted into the cell. In addition, there was still reminace of a bolt in block Ias it aslo could not be removed until the water block jig was removed.

Tuesday, November 12 a new blank off was put into the cell. The water block jig was removed, which was very easy, confirming documentation from installation (in 2008?) that it fit very well / the blocks were bent and soldered to the jig very carefully.

Screw was removed from I and both I and K were blanked off and vacuum leak checked. No response. (Second Piccture)

Containment box was re-installed and module ready to move to the conditioning station by noon.

 

 

 

  544   Friday, November 15, 2013, 16:48 Bevan MossConditioning StationStandard OperationTM2 HV Testing

 High voltage testing was started on TM2 with no source tray today. The maximum stable for 1 minute voltage reached was 47.5kV but the module is still conditioning. With every step up in voltage the current goes up a large amount and slowly bleeds down. Large sparks disrupts the connection of the CANBUS to the PS which is irritating but the module can be brought up to the equivalent voltage in less than 30 seconds. Attached is a screen shot of most of the strip tool. I have also attached all of the dumped data. The module will be left under vacuum with the water running over the weekend and HV testing will continue on Monday. 

  545   Monday, November 18, 2013, 11:54 Bevan MossConditioning StationRepairTM2 Fault on TCS Chill

 This morning when I went to start HV conditioning CP2 and CP3 both had faults and the temperature of the water was ~27C. I reset the compressors by flipping the system reset switch. This cleared the fault and allowed the compressors to come one. To the best of my knowledge these faults happen as a result of compressor fluid pressure too low or high and temperature too low or high and lack of flow. The system cannot determine which one it was that caused the trip. The system restarted and faulted again. As I was watching this time it can be determined that the fault was the result of an over temperature event. This was the caused by the cooling fans not coming on. Which was traced to the fan VFD controllers which both read OP3 which is an Over voltage during constant speed operation. The operating manual lists these as the possible causes

The input voltage is fluctuating abnormally.

• Power network is greater than 200 kVA

• Power factor capacitor switching

• SCR switching on power network

• The drive controller is regenerating— the load causes the motor to run at a frequency higher than drive controller output frequency.

• Intermittent output phase fault

The proposed solutions are

• Install a line reactor.

• Check the input and output circuits for phase failure and rectify. 

I will continue to monitor over the next few days to see if this continues to happen. If it does I will contact ESC.

ELOG V2.9.2-2455