Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 79 of 140  Not logged in ELOG logo
ID Date Author Category Type Module Target/Numberdown Subject
  454   Friday, September 13, 2013, 08:05 David WangSouth Hot-CellRepairTM4 TM4 coil 1 leak check in SHC

Leak checked TM4 coil1 in SHC with Isaac . The leak detector only can pump down to 1.5xE-7 atm.cc/sec. The leak detector got the response once the helium valve is open, not even close to the leak area. The leak detector got a very big response when the helium probe was put close to the coil terminal block on target front side and spray helium for 2 clicks. The leak detector got a small  response when the probe was put close to water block area and spray helium for 2 clicks. The leak is located on the front target side coil line but not from water blocks. The leak is too big to be further pin pointed by this method. See attachment

Attachment 1: TM4_coil_1_leak_check.pdf
TM4_coil_1_leak_check.pdf TM4_coil_1_leak_check.pdf
  455   Tuesday, September 17, 2013, 14:36 Bevan MossSouth Hot-CellStandard OperationTM3 Containment Box has been removed

 The containment box has been removed. Tomorrow the wiring harness will be installed.

  458   Thursday, September 19, 2013, 15:56 Bevan MossSouth Hot-CellRepairTM3 Activities for September 18th and 19th

September 18th

The wiring harness was completed by Maico and Travis today (see pics) and was installed into the target module. During installation the bracket went on with ease. The junction box appeared to be hung up on something but did engage eventually. The plug for the collimator is not quite long enough for the manipulators to install completely. I was only able to get it to just engage by sneaking the manipulator in from the shutter side and then pushing on it with a long rod. The wiring for the collimator is several inches too long but does not interfere with anything. The remote installation of the wiring to the IMG gauge was easy but there at least 1 foot of extra wire and with the thicker gauge it has a mind of its own. I was eventually able to wrap the wire under the table before so it will not interfere with anything. The module side junction box bracket was not clamped to the table I was able to do up one bolt but other one was blocked by the new steerer strain relief. There is no requirement for both to be done up.

 

September 19th

Travis completed and electrical test this morning and it was found that coil 1 touches coil 2 touch each other very slightly. By inserting a piece of cardboard between the closest water block and the lines we no longer in contact and passed the test. Once the cardboard was removed the lines remained separated but if touched slightly they would spring back into place and make contact. There was some debate as to if we should make a custom part to separate the line or if we should attempt to tweak the lines. I decided that it is known that a very small change in the position of the module will cause separation between the lines, that we should attempt to tweak the lines. I braced the lines with one manipulator to prevent loading the ceramic while Maico "tweaked" the line. The line was successfully moved to cause separation. Maico and I then completed a visual inspection of the remaining water blocks and noticed that the ground electrode cooling lines are estimated 1/8" away from one of the module side coil lines. All other places that can easily be inspected appear to have enough clearance.

Travis and Don then completed an electrical check again (https://elog.triumf.ca/TIS/RH-ISAC/457). This module still failed the test but as noted not due to continuity rather lower than infinite resistance from the coil to coil and positive coil to 60kV common. This indicates that there is dirty or failing insulation that is either from the fiber glass wrap or something within the service tray. From inspection from outside the hot cell the best guess as to where this is happening is just before to after the exit of the water lines from the service tray but there is no way to confirm this.

Although the module may be able to run for a period of time with these resistances the insulation may continue to break down and there is the risk that during a module move the lines may shift and touch again. This combined with the known HV issues of TM3 paints a dark picture of the service tray.

Friedhelm and Lia have been advised of these recent results and have decided to continue with the installation of the target and conditioning of the target. Should the module be able to operate and extract beam it will be installed in ITE. Friedhelm also came for a visual inspection of the module and agreed that the issue is on the module side and that the lines are too close to tell exactly where the issue may lie. The possibility of separating the the blocks with further insulation was discussed but there is limited area that this can be completed remotely. In addition to this there is no indication that further insulation/bracing will improve the problem and there is considerable risk that it could make the issue worse.

Installation of the containment box started this afternoon and is completed other than the tightening of the window VCR joints. 

Attachment 1: IMG_1127.JPG
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Attachment 2: IMG_1134.JPG
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Attachment 3: IMG_1137.JPG
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Attachment 4: IMG_1139.JPG
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Attachment 5: IMG_1143.JPG
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  459   Monday, September 23, 2013, 13:55 David WangSouth Hot-CellStandard OperationTM3 window circuit leak check

This morning, Bevan and I leak checked window circuit on TM3 at SHC after containment box was installed. It took about 20minutes to pump down the circuit to  0.0xE-9atm.cc/sec. Bevan sprayed helium on both VCR joints and a final splash. No response had been found on leak detector.

  460   Monday, September 23, 2013, 16:10 Bevan MossSouth Hot-CellRepairTM3 Activities Sept 20 - 23 2013

 September 20th

Today was a trying day. When attempting to make the water line connections for the window the VCR seal fell off several times. Each time this happens the seal becomes stuck at the bottom of the containment box. While trying to replace the seal the nut slipped down the line to the bottom of the containment box. When trying to recover said nut with the pick tool it too fell to the bottom of the containment box. Due to the design of the containment box the only way to recover the pick is to remove the containment box (several other attempts were made with no luck). Before anyone asks no the pick cannot be left in the containment box. When attempting to remove the containment box one of the bolts for the shutter panel stripped. I then found the stud removing tool and have successfully removed the bolt. Isaac is now going to finish removing the containment box and that will be as far as we can get today. 

September 22nd 

- containment box removed
- dropped tool and seals removed from box
- containment box reinstalled
- window water lines done up
- target installed (with difficulties detailed below)

The threads for the middle tube heater connection (circuit D) appear to be damaged and the bolt in that location cannot be fully screwed in.  The bolt was removed and showed damage to the threads.

September 23rd

A leak check of the window line was completed (https://elog.triumf.ca/TIS/RH-ISAC/459) and several electrical checks of the coil with and without the target in place. The values for the electrical checks continued to fail the open circuit criteria, an elog on the testing will be reported tomorrow. Isaac and Maico removed the target so that the helicoil could be repaired. The helicoil was repaired by chasing the threads with a modified tap but it was noted during the repair that the bolt holding the line in place and come loose and was no longer clamping the tube heater and ceramic tight. The target was also checked electrically to confirm that the coil was not shorted to common. It showed a open circuit resistance with a ohmmeter.

It was then attempted to re-install the target but as the target was being lifted a cable for the tong motion schematic broke (A-11682). 

Currently the target is sitting in the hot cell with the manipulator still broken. We are attempting to find parts and instructions as to how to replace the cable.

 

  462   Tuesday, September 24, 2013, 14:46 Bevan MossSouth Hot-CellRepair  Right manipulator repair

 The right manipulator A-9885 Handle Cable Assembly has been repaired by Maico and myself. We repaired the manipulator following some verbal instructions from Chad on the modified repair strategy. This allows the repair to be completed without going into the hot cell. The instructions in the repair manual are very vague and can actually cause problems. For example it is best to pin the manipulator before completing any work. Other than that the work went smoothly with the exception that the counter weight hangs up on the manipulator occasionally and can cause the cable to come off of the pulley. Also it appears that the left manipulator has had the cable installed incorrectly as it rides on the housing of the wrist.

  463   Wednesday, September 25, 2013, 06:59 maicodallavalleSouth Hot-CellStandard OperationTM3 Containment box cover

The containment box cover has had all  the bolts installed and all bolts were checked with a mirror. TM3 has been raised and is ready for the last electrical  test before  it goes to the conditioning station.

  467   Thursday, September 26, 2013, 09:46 maicodallavalleConditioning StationRepairTM3 Leak check / Pressure Test

TM3 has had all of the water lines pressurized with Helium and the Helium Leak detector was connected to the turbo pumps. There were no leaks detected.

  486   Wednesday, October 02, 2013, 13:44 Bevan MossSouth Hot-CellStandard OperationTM4 Right Coil is leaking

 Today Maico and Travis completed and electrical test to determine the right and left coil on TM4. The left coil is the negative side. From there Maico pumped on both lines for a leak test. The leak cart pumped down to its lower limits on the left line and there was no response when sprayed with helium. The right line would not pump below 2.5 x 10^-2 Torr and had a base leak rate of 3.3 x 10^-7 atm*cc/sec (this indicates a massive leak). Without spraying helium the leak cart responded and peaked at 1.9 x 10^-6 atm*cc/sec. Attached is a picture of the module indicating the line.

 

Attachment 1: tm4leak.jpg
tm4leak.jpg
  500   Tuesday, October 08, 2013, 18:12 Grant MinorCraneRepairTM4 Target Hall Crane Stuck in East-West Direction - Update

Grant Minor wrote this e-mail today:

***

Hello all,

During our planned operation of transporting TM4 from a storage silo to the Hot Cell, we had a problem with the East-West bridge drive on the Target Hall crane.  The crane bridge is currently stuck in position over the silo area.  We were unable to complete the transport operation.  TM4 has been placed back down into the silo and the crane hook block has been disconnected from the module lifting yoke.

We have been on the phone with Norelco this afternoon and have determined the likely cause of the problem.  There is a splice joint in the crane rails at this position, where a small gap exists between the rail sections.  If the crane bridge is stopped during operation such that the wheel comes to rests in this gap, the crane motors have insufficient torque for the wheel to overcome the gap and ride back onto the rail.  The Norelco tech Mike Smith remembers encountering this problem several years ago (before my time) but cannot remember how it was overcome.  The fix likely involved moving the wheel out of the gap with pry bars.

Target Hall Survey Needed at or before 7:00 am, Wednesday Oct 9th (Lynne, Fiona, Danka, Max or Dano?)

Mike Smith and possibly a few others from Norelco will come tomorrow morning at 7:00am, and require access to the Target Hall.  Since we have opened the Hot Cell in preparation for the module move, we will need a survey as early as possible to allow Mike and his crew to enter the hall without a suit and respirator.

Most of the Remote Handling group will be off-site for a Division meeting, but Travis and Maico will stay for the day to accompany the Norelco guys and help with the problem assessment.

Travis: Please take Mike to the control room when he arrives, one of the cameras is currently zoomed in on the wheel and problem rail section.

Maico: Scaffolding may be required to get access to the crane rail.  Unfortunately we don't have an operational crane to transport a man-lift into the hall ;)  Please see what you can do to get this ready in case we need it.  Max's leak check might have to go on hold until we get this resolved.  Please take responsibility for ensuring correct Fall Protection procedures are followed.  This means that nobody should be walking up on the crane rail unless they are tied in with harnesses, or there is scaffolding directly under them.

I can be reached on my cell phone at 778-319-4612.  The Division meeting is on UBC campus so I can return to TRIUMF fairly quickly if needed.

Thank you all for your assistance,

Grant

***

A photo of the THall camera view of the bridge wheel at the rail splice is attached, as well as Mike Smith's crane inspection report from March 2013.

Attachment 1: THall_Crane_Bridge_Wheel_at_South_Rail_Splice_8Oct2013.JPG
THall_Crane_Bridge_Wheel_at_South_Rail_Splice_8Oct2013.JPG
Attachment 2: NORELCO_inv13045_joMS-064_31March2013.pdf
NORELCO_inv13045_joMS-064_31March2013.pdf NORELCO_inv13045_joMS-064_31March2013.pdf NORELCO_inv13045_joMS-064_31March2013.pdf NORELCO_inv13045_joMS-064_31March2013.pdf NORELCO_inv13045_joMS-064_31March2013.pdf NORELCO_inv13045_joMS-064_31March2013.pdf
  501   Wednesday, October 09, 2013, 19:33 Grant MinorCraneRepairTM4 Target Hall Crane not operational - likely controls / PLC hardware failure (not stuck wheel)

Grant Minor wrote:

Grant Minor wrote this e-mail today:

***

Hello all,

During our planned operation of transporting TM4 from a storage silo to the Hot Cell, we had a problem with the East-West bridge drive on the Target Hall crane.  The crane bridge is currently stuck in position over the silo area.  We were unable to complete the transport operation.  TM4 has been placed back down into the silo and the crane hook block has been disconnected from the module lifting yoke.

We have been on the phone with Norelco this afternoon and have determined the likely cause of the problem.  There is a splice joint in the crane rails at this position, where a small gap exists between the rail sections.  If the crane bridge is stopped during operation such that the wheel comes to rests in this gap, the crane motors have insufficient torque for the wheel to overcome the gap and ride back onto the rail.  The Norelco tech Mike Smith remembers encountering this problem several years ago (before my time) but cannot remember how it was overcome.  The fix likely involved moving the wheel out of the gap with pry bars.

Target Hall Survey Needed at or before 7:00 am, Wednesday Oct 9th (Lynne, Fiona, Danka, Max or Dano?)

Mike Smith and possibly a few others from Norelco will come tomorrow morning at 7:00am, and require access to the Target Hall.  Since we have opened the Hot Cell in preparation for the module move, we will need a survey as early as possible to allow Mike and his crew to enter the hall without a suit and respirator.

Most of the Remote Handling group will be off-site for a Division meeting, but Travis and Maico will stay for the day to accompany the Norelco guys and help with the problem assessment.

Travis: Please take Mike to the control room when he arrives, one of the cameras is currently zoomed in on the wheel and problem rail section.

Maico: Scaffolding may be required to get access to the crane rail.  Unfortunately we don't have an operational crane to transport a man-lift into the hall ;)  Please see what you can do to get this ready in case we need it.  Max's leak check might have to go on hold until we get this resolved.  Please take responsibility for ensuring correct Fall Protection procedures are followed.  This means that nobody should be walking up on the crane rail unless they are tied in with harnesses, or there is scaffolding directly under them.

I can be reached on my cell phone at 778-319-4612.  The Division meeting is on UBC campus so I can return to TRIUMF fairly quickly if needed.

Thank you all for your assistance,

Grant

***

A photo of the THall camera view of the bridge wheel at the rail splice is attached, as well as Mike Smith's crane inspection report from March 2013.

E-mail from today:

Hello Dave, Jane, Franco, Michael, Don (controls + Franco), Remy,

We have lost the East-West bridge drive control functionality of the ISAC Target Hall crane, and unfortunately this very much prevents us from operating the ISAC facility.

The problem was originally thought to be a stuck bridge wheel but this was not actually the case.

Mike Smith from Norelco was on-site for most of today working with Michael Rowe in an attempt to diagnose the problem.

Mike believes the problem to be one of the following three items:
- input PLC board on the crane bridge
- output PLC board in the interface panel in B1 level Room 5 (ISAC remote crane control room)
- communication between the two boards (festooning hardware)

We are in a pretty dire situation without the ISAC target hall crane, and we lack the expertise within the Remote Handling group in PLC hardware to diagnose this on our own.  I need to ask for somebody's help from the controls group in diagnosing and repairing this problem.

I have notes from my telephone conversation with Mike Smith which I can discuss with a controls representative in the morning.  There is a pretty muddled history of the design and implementation of these controls but essentially Norelco outsourced the PLCs and festooning to a third party contractor, Seattle Crane in the US, which no longer exists anymore.  Neither Kone, Seattle Crane, or Norelco made appropriate as-built drawings of the wiring of the PLCs.  Mike Smith at Norelco had a stack of hand-written notes about the as-built configuration he made at the time of installation in the late 1990's but these notes have not been located yet.

The PLCs appear to be Allan Bradley but the modules are from approximately 1997 and we're not sure if spare units are available.

Mike Smith says the easiest thing to do at this point is install replacement PLC modules on the crane bridge and in the control room that have confirmed functionality.  If control is not restored then the problem is likely in the festooning.

Control of the crane bridge was temporarily attained by bypassing the controls (speed control / end limits, etc.) and sending drive signal directly to the drive motor controller in order to return the bridge to its home position at the access ladder.  This mode of operation is not safe as the crane has no speed reduction / limits to prevent driving the bridge into the walls at max speed.

Jane / Remy / Franco: please let me know who I should correspond with on the controls side and I will talk with them tomorrow morning.

Thanks,

Grant

  502   Tuesday, October 15, 2013, 15:34 Bevan MossITEStandard OperationTM3 Blocks moved from ITW to ITE

 Blocks 1-4 have been moved from ITW to ITE. Block 5 was moved to a storage area as it will be in the way of the harp repair. Danka took air samples and found 200 counts of alpha on the air samples but nothing on the swipes. It is recommended that resporators be worn while blocks are being lifted and lowered. She will check the monitor tomorrow to confirm it is behaving as it should.

  503   Tuesday, October 15, 2013, 16:44 Grant MinorCraneRepair  Target Hall Crane - operational with temporary thermal sensor bypass

E-mail correspondence on the Target Hall crane fault diagnosis between October 11th and 15th:

On 15/10/2013 3:34 PM, Grant Minor wrote:

Hello all,

Mike Smith from Norelco arrived this morning and spent some time with Travis from RH and Mike Rowe from Controls group examining the crane controls and electrical schematics.  A common understanding of the wiring and control signal scheme for the thermal sensor circuits was reached.  A scanned copy of Norelco / Seattle Crane drawing E5 - 1/1 with markups by Dave Morris (Oct 11th) and Mike Smith (Oct 15th) is attached.

The group then worked on top of the crane bridge to systematically isolate the thermistor circuits in each drive motor.  The thermistor readings were all normal / as-expected (about 180 Ohms for 3 in series), i.e. there was no indication of failure in any of the motor thermistors.  Fall arrest equipment was used to access the motors where required.

Next, the shunt circuit in each temperature sensor module was measured (terminals T1 and T2 on each module, on drawing E5 - 1/1).  The shunt in the operational module was measured at 500 kOhms.  The shunt in the suspected faulty module was measured at 79 kOhms.

It was concluded that there is most likely a fault in the module with the low shunt resistance.  The suspect module was left wired in bypass (shorted from terminals 14 to 11).  Mike Smith advised at that point that it would be safe to operate the crane in this mode temporarily until a replacement module can be installed.  I discussed this with him and Don Dale, and we agreed the risk is low, as we have not ever experienced a motor overheat scenario in the operating lifetime of the crane.

Mike Smith called me around 1pm to advise that he has located a replacement unit from their supplier in the US and I asked him to order 2 units on expedited overnight.  Mike expects the components to arrive Friday this week or Monday next week latest, factoring in delays at customs and local delivery times.  The units will be sent to Norelco first, then to TRIUMF locally.

Remote Handling is now continuing with Target Hall operations, using the crane as normal with the thermal module bypassed until the replacement module arrives.

Thanks to Dave Morris / Mike Lowe for their assistance in diagnosing this fault.

Here is a short summary of the Fault:

Cause of fault
- Most likely a failed thermal sensor module for one of the two pairs of bridge drive motors

Diagnosis
- Crane company (Norelco) consulted, with on-site inspections by tech Mike Smith on October 9th and October 15th
- Controls group / Mike Smith measured resistances in motor thermistors and sensors to systematically isolate fault to thermal sensor

Remedy actions taken

- Thermal sensor bypassed to temporarily restore crane function
- Risk of operating without sensor determined to be low through discussions with Norelco / Don Dale / Grant Minor
- Replacement thermal sensor + 1 spare (~ $300 ea + shipping) ordered from parts supplier through Norelco - expected delivery Monday October 21st

How could this fault have been prevented?
- Cause of failure within thermal sensor module unknown at this time
- Annual crane inspection performed by Norelco in March 2013 did not indicate any problems with this sensor (crane drive system functioned as normal)
- Suggested for future: routine inspection of sensor module shunt resistance to determine if there are any long-term signs of slow degradation

What can be done to prevent the fault in the future?
- The ISAC crane controls were designed in the late 1990's by Norelco sub-contractor Seattle Crane (now defunct)
- The crane is supposed to have two pairs of independent motors with separate thermal sensors, each capable of driving the crane if the other fails due to thermal trip
- My understanding is that the controls logic design should have been designed so that failure of one pair of motors does not prevent crane operation... it does not seem to be the case with the current design
- The design of the control logic related to these sensors could be re-evaluated and modified so that a trip from one thermal module does not prevent operation of the bridge if the other module is OK
- This is a project that will require some time and some controls and engineering resources
- In the interim, if the same failure occurs again, it may be possible to jumper the thermal sensor from the crane control room and continue operating normally - I will confirm with controls group / Norelco
- However, this is not advisable as it would be difficult in some cases to determine if the trip was due to a faulty thermal module, or an actual motor overheat scenario
- I will discuss further actions with Don Dale

Thanks and best regards,

Grant


On 11/10/2013 4:29 PM, Grant Minor wrote:

Hello all,

I spoke with the Norelco tech Mike Smith this afternoon regarding the failed thermal sensor component / circuit.  He will call Kone on holiday Monday (their office is not closed for Canadian Thanksgiving) and determine if they have a replacement module.

I explained (to the best of my understanding) the diagnosis performed by Dave Morris / controls group and the test that was done to isolate the thermal sensor unit.  Unfortunately, Mike Smith's drawings from Seattle crane contain notes and revisions that don't match the drawing that Dave Morris provided me (Seattle Crane dwg E5 - 1/1 revision 1 02-10-99), and he was unable to confirm in his opinion whether the bypass performed by Dave Morris has correctly isolated the problem components.  In addition, he believes that the bypass he performed on Wednesday isolated portions of circuitry that are inconsistent with this thermal sensor circuit.

Mike Smith will return Tuesday morning to review the bypass and schematics.  He recommended not operating the crane until he has a chance to confirm this thermal sensor issue.

From the drawings I have in hand and from discussions with Dave Morris, the failed component might be the thermistor sets inside the motor housing which are in series with the suspect module, or the module itself.  My understanding is that the crane is designed with two pairs of motors for the bridge drive, and each pair is protected by one of these thermal modules (thus there are two modules total).  Both modules would be the same age and both might be susceptible to the same failure mode.

As it is unclear to me the exact nature of the drive system failure, and I have a recommendation from Norelco to hold on operation of the crane, I must unfortunately state that the crane should not be used and we will have to wait until Tuesday to gather more information.

I am not so concerned about temporary loss of the thermal protection circuitry, as we have not had an overheating scenario in those motors in the lifetime of the crane (to my knowledge).  I am more concerned about getting 100% confirmation that we have addressed the problem.  If we attempt to use the crane and experience another failure during a lift that prevents us from placing the load down safely with the crane stuck in position over a target station, then we would be in much deeper trouble.

My apologies for this situation.

Best regards and have a good weekend,

Grant


On 11/10/2013 1:28 PM, Grant Minor wrote:
Thanks Dave,

I've contacted Norelco, Mike Smith and I are planning a path forward for further diagnosis and repair.

The crane MUST NOT be used to carry a load until it is identified whether the module or the sensors have failed, the reason for the failure, and the functionality of the thermal sensors has been restored.

Without the thermal sensor circuit we lose protection from motor overheat, an event which could have much more serious failure implications to the crane.

Cheers,

Grant

On 11/10/2013 1:04 PM, David Morris wrote:
The fault has been identified in the Target Hall Crane as a failed motor temperature module, or motor temperature sensor, on the East-West motion. The status contact in the module was bypassed allowing crane motion. There was no fault with the controls.

Dave

Attachment 1: ISAC_THall_Crane_elec_E5_1slash1_15Oct2013.pdf
ISAC_THall_Crane_elec_E5_1slash1_15Oct2013.pdf
  505   Wednesday, October 16, 2013, 18:53 Grant MinorITERepair  ITE Harp 9 Removed & Blanked-Off - blocks NOT YET replaced

The blocks above the pre-separator section of the ISAC beam lines were removed today in the Target Hall by Bevan Moss and Chad Fisher with Lynne LeMessurier present from RPG.

The two blocks in the layer below the top layer above the pre-separator were damaged on removal (see attached photos).  This was due to an attempt to lift them in the incorrect sequence caused by misinterpretation of the labeling / numbering system drawn on the top of the blocks.  The blocks are labelled for the replacement sequence, but not for the removal sequence.  An attempt was made to lift a block that had an overlap with an adjacent block that was not visible, causing damage to two blocks.  A note was added in black marker to the critical block to indicate that it should be removed last (shown in attached photo).  The block replacement sequence will be photographed and a procedure document will be written by Bevan, with a bound copy of the procedure provided in the Target Hall, in order to prevent such an incident from occurring again.  Broken pieces of the blocks were collected and placed in a 5-gallon pail.

The removal of all of the blocks caused the depression in the target station to fluctuate around the trip point (17 inches of water column), which caused the ventilation alarm to trip on and off constantly.  Operations contacted me to ask if this could be remedied.  Bevan closed the damper to ITW, which brought the depression to a low enough value so that the alarm could be defeated properly.  This was around 2pm.

Preliminary co-ordination of the ITE Harp 9 removal job was discussed by Scott Kellogg and Ron Kuramoto around lunch time.  Keith Ng (RH) and Scott searched for the blank-off that was used during the last Harp 9 repair (removed from B/L in March 2013) but they could not locate it.  I was later able to find the blank-off bagged in a grey rubbermaid bin at the bottom of the stairs in the target storage vault pit (under the SHC / NHC ventilation and filters).  The blank-off was found bagged and tagged as surveyed at 100 counts @ 0.5m on March 27, 2013.  I gathered Scott, Ron Kuramoto, and Danka Krsmanovic to co-ordinate the Harp 9 removal and blank-off installation, starting at around 2:30 pm.

For the Target Hall Harp work, Ron Kuramoto and Scott prepared the required tools and plastic coverings / bags.  I acted as crane operator.  Danka was the surveyor present.  Anders Mjos joined the group for photos and moral support.

Scott disconnected services from the Harp device, and prepared it for lift.  I called operations to confirm that the section of B/L had been vented.  Ron and Scott used the RH tools to disconnect the 2 vacuum flange bullet bolts.  Ron directed the crane with signals and I lowered the chain rigging to the Harp, it was connected and removed from the BL with the main hoist.  (I made the mistake of directing the rigging of the harp to the main 20T hoist, when in fact the 3T Aux hoist should have been used, as the main hoist can't reach to the vacuum / storage pit on the west side of the hall.)

Danka performed several swipes and measurements of the Harp after removal.  Alpha contamination was discovered on the bottom of the Harp flange.

Ron and Scott installed the blank-off flange, then I called operations to indicate that pumping should start.

Ron and Scott retrieved the vacuum test flask jig / support structure from the West storage pit and brought it down to the pre-separator pit.  I lowered the Harp into this flask jig, and Scott used the side-wall location bolts from the top of the harp assembly to fasten the flanges of the Harp and the jig.

I had trouble at first activating the Aux hoist but soon realized that it's necessary to press the Aux pendant "ON" button down for several seconds before the power actually turns on to this hoist.

We then removed the main hoist hook and attached the Aux hoist to the Harp / flask.  The assembly was transported to the West storage pit.

Some of the handrails had to be removed to facilitate initial movements of the Harp assembly.  These handrails should be replaced tomorrow morning.

Scott also submitted a Work Order for a back-up blank-off today, job number 40303.

The pre-separator blocks have NOT been replaced yet, we will do this tomorrow morning.

It was a busy day, thanks to all for their efforts and for staying a bit late to get the blank-off installed.

Best regards,

Grant

Attachment 1: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013.JPG
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Attachment 5: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-007.JPG
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Attachment 6: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-009.JPG
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Attachment 7: Closing_Damper_for_ITE_16Oct2013.JPG
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Attachment 8: ITE_Harp_9_Remove_and_Blank_16Oct2013-012.JPG
ITE_Harp_9_Remove_and_Blank_16Oct2013-012.JPG
Attachment 9: ITE_Harp_9_Remove_and_Blank_16Oct2013-021.JPG
ITE_Harp_9_Remove_and_Blank_16Oct2013-021.JPG
Attachment 10: ITE_Harp_9_Remove_and_Blank_16Oct2013-031.JPG
ITE_Harp_9_Remove_and_Blank_16Oct2013-031.JPG
Attachment 11: ITE_Harp_9_Remove_and_Blank_16Oct2013-038.JPG
ITE_Harp_9_Remove_and_Blank_16Oct2013-038.JPG
  506   Thursday, October 17, 2013, 10:24 chad fisherSouth Hot-CellRepairTM4 Coil Line Removal

The containment box was removed from TM4 earlier this morning in preparation for removal of the C2 circuit water lines, their respective water blocks and conductor block.

Attachment 1: TM4_C2_circuit.pdf
TM4_C2_circuit.pdf TM4_C2_circuit.pdf TM4_C2_circuit.pdf
  507   Thursday, October 17, 2013, 17:16 Grant MinorITERepair  Pre-Separator-area (ITE Harp 9) Blocks Replaced

The pre-separator-area blocks were replaced today by Bevan and Travis, with Grant present for photos and observation.

Photos are attached of each block replacement.

Some difficulty was encountered in replacing the "Layer #3" blocks (photo 9 attached).  An interference occurred between the outside of the west "Layer #3" block and an aluminum channel directly beside the rubber pad that supports the block.  The block was initially resting on this channel but slipped off, breaking off some concrete at the edge.   See photo 12 attached and notice crumbled concrete inside this channel around the area where the interference occurred. Photo 14 shows the damaged block edge.

It should be noted that when these two blocks are resting flat, there should be a gap between them (i.e. they should NOT be touching as shown in photo 9).

 

Attachment 1: PreSeparatorHarp9Blocks_17Oct2013.JPG
PreSeparatorHarp9Blocks_17Oct2013.JPG
Attachment 2: PreSeparatorHarp9Blocks_17Oct2013-008.JPG
PreSeparatorHarp9Blocks_17Oct2013-008.JPG
Attachment 3: PreSeparatorHarp9Blocks_17Oct2013-009.JPG
PreSeparatorHarp9Blocks_17Oct2013-009.JPG
Attachment 4: PreSeparatorHarp9Blocks_17Oct2013-012.JPG
PreSeparatorHarp9Blocks_17Oct2013-012.JPG
Attachment 5: PreSeparatorHarp9Blocks_17Oct2013-017.JPG
PreSeparatorHarp9Blocks_17Oct2013-017.JPG
Attachment 6: PreSeparatorHarp9Blocks_17Oct2013-020.JPG
PreSeparatorHarp9Blocks_17Oct2013-020.JPG
Attachment 7: PreSeparatorHarp9Blocks_17Oct2013-021.JPG
PreSeparatorHarp9Blocks_17Oct2013-021.JPG
Attachment 8: PreSeparatorHarp9Blocks_17Oct2013-014.JPG
PreSeparatorHarp9Blocks_17Oct2013-014.JPG
  508   Friday, October 18, 2013, 10:17 Bevan MossITWRepair  Paddle Wheel

 Yesterday I visually inspected the paddle wheel and noticed that it was spinning freely and constant. As the signal was intermittent replaced the coil at the back of the wheel only. This does not require access to the high active water. With the coil replaced the signal looked strong. I asked operations to keep and eye on it and advise if the problem has been resolved. I also discussed with David this morning and he informed me that this is the same procedure he would have followed.

  509   Friday, October 18, 2013, 13:43 chad fisherSouth Hot-CellRepairTM4 C2 Circuit Removal

The C2 circuit (coil 2) water lines and blocks have been revoed from TM4.

Water block jig could not be used as the window water block connection was nowhere near fitting into the jig (IMG_1224 image below) and therefore caused an interference causing the rest of the blocks to not mate with the jig. A different tool that has never been used was implimented and sucessful (IMG_1227 below).

 Sorry about the picture numbering format...new format will be implimented next time.

Attachment 1: IMG_1224[1].JPG
IMG_1224[1].JPG
Attachment 2: IMG_1227[1].JPG
IMG_1227[1].JPG
Attachment 3: IMG_1230[1].JPG
IMG_1230[1].JPG
  510   Friday, October 18, 2013, 14:33 Bevan MossSouth Hot-CellStandard OperationTM4 Module move

 TM4 without a source tray was moved from the SHC to the TCS.  All went well.

  511   Friday, October 18, 2013, 14:37 Bevan MossConditioning StationStandard OperationTM4 Roughing Started

 The roughing pump has been started.

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