Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 67 of 138  Not logged in ELOG logo
ID Date Author Category Type Module Target/Number Subject
  1428   Friday, January 27, 2017, 08:44 chad fisherSouth Hot-CellStandard OperationTM2Ta#50UCx #18 - Ta Feibiad Dummy installed. Target Change Waterline interference

On Tuesday, January 24th UCx#18 was removed from TM2 and Ta febiad dummy installed. I encountered the same issue mounting the new target as last time. Was able to determine that the issue is the routing of the waterlines to the right-hand (as viewed from the operator) high current tube heater. The lines interfer the the target mounting plate (bottom right hand corner).

  1427   Tuesday, January 24, 2017, 15:32 David WangITWStandard OperationTM2 TM2 was moved from ITW to SHC this morning.

The move is smooth. Yasmine and Travis did the move.

  1426   Tuesday, January 24, 2017, 15:29 David WangConditioning StationStandard OperationTM2 TM2 has been moved to TCS .

I connected TCS vacuum system to TM2. The station is under roughing now. All turbo pumps will be started soon.

  1425   Tuesday, January 24, 2017, 15:24 David WangConditioning StationStandard OperationTM2 TM2 electrical check and leack check.

I did electrical check before and after Fefiad target installation on TM2. The RU (coil) Is till short to 60KV as before. Other result are good. After Febiad target is installed, Tm2 HS line is leak checked. On leak detector, base leak rate pumping down is much slow  than before.  The base pressure still could be pumped down to 0.0XE-4 torr.  After a long time wait, Chad and I leak checked at 2.2XE-8 atm.cc/sec base leak rate. Chad sprayed lots helium around the fittings and target. No any response has been found on LD. At this leak rate, the target and HS line is leak tight.  The Tm2 has been moved to THC so a heium pressure check will be fulfilled on HS line at TCS to confirm this leak check result.  

TM2 HS line is pressurized with 70 psi helium at TCS. LD base leak rate: 0.0 X E-9 atm.cc/sec. Base pressure 0.0XE-4 torr. 5 minutes test time. The leak rate slowly climed to 3.3XE-9 atm.cc/sec and stabled there( 3minutes). base pressure no change. The leak is too small to be concern. We will run this target as this condition.

 

  1424   Thursday, January 19, 2017, 10:15 David WangConditioning StationStandard Operation  Target Hall schedule for 2017 winter shut down

Updated target hall schedule for 2017 winter shut down. See attachments 1,2

Update schedule after Febiad beam schedule changed to ITE. See attachments 3,4

  1423   Wednesday, January 18, 2017, 11:53 Isaac EarleNorth Hot-CellDevelopment  NHC partition wall installation complete

 The final panels of the partition wall were installed today as per drawing IRH1609.  Sealing, finishing, and painting of the NHC walls and floor can now commence.

 

IMG_7728.JPG

  1422   Wednesday, January 18, 2017, 09:55 David WangITEStandard OperationTM4 ITE and TM4 2017 winter shut down leak check.

ITE and TM4 2017 winter shut down leak check are finished. All ITE primary, secondary vacuum vessel and TM4 water lines are good. No any leak has been found.

  1421   Tuesday, January 17, 2017, 13:45 Isaac EarleNorth Hot-CellDevelopment  NHC ducting installed

 The new ducting section connecting the existing duct termination in the TCS space to the NHC partition wall has been installed by Smith Sheet Metal contractors.  The installation drawing is IRH1618.  There was not enough clearance between the duct pipe and the TCS vessel to butt weld the new ductwork as originally intended.  Instead a flange was welded to the existing pipe and also to the new section and the two were bolted together.  Drawings of the modifications have been provided by the contractor, and as-built drawings will be completed at a later date.  There was not time for the contractor to fabricate a gasket for the flanged joint, so one will be installed by TRIUMF at a later date and included in the as-built drawing package.

  1420   Monday, January 16, 2017, 09:32 David WangITWStandard OperationTM2 Helium pressure test on TM2 water llines at ITW

TM2 helium pressure test result at ITW. 70 psi helium 3 minutes on each circuit. LD base LR0.0XE-9atm.cc/sec  BP 0.0XE-4torr.  ITW IG1 1.22Xe-7 torr, ITW IG1S 1.31XE-7torr, ITW PNG4 2.66XE-6Torr(ITW TP4 off).

 

  2017-01-13 (atm.cc/sec) 2017 mini shut down
HS 0.0 x E-9  
Window 0.0 x E-9  
EE 2.7 x E-9  
Ta+ 2.2 x E-9  
Ta- 6.6 x E-9  
Tube- 1.3 x E-8  
Tube+ 2.8 x E-8  
Coil 2 2.8 x E-9  
coil 1 7.1 x E-9  
MSP 6.7 x E-8  
GE leak , no test  

All number are getting better comparing to last time check. All ITW vacuum readings are very good. ITW PNG4 was in low E-7 torr range also. At present, it is in low E-6 range due to ITW TP4 switching off.  The TM2  water line seals  are stable and reliable for 2017 beam run. The same check will be repeated  in 2017 mini shut down.

  1419   Thursday, January 12, 2017, 14:24 David WangITWStandard OperationTM2 ITW primary and secondary vacuum vessel winter shut down leak check.

TM2 is located in ITW for this leak check. Leak detector is installed between ITW BV2s as before. LD base leak rate 0.0XE-9atm.cc/sec, base pressure 0.0XE-4 Torr. First , I leak checked dump module top flange seal which a small leak was found in last year winter shut down. This time,all ITW  turbo-pumps cooling fans are switched off during the check. Lots helium are sprayed around the dump module top flange this time. I did not see any response on LD.  The check is repeated 3 times. The results are same. There is no leak has been found on ITW dump module top flange seal at this moment. The  further confirming check will be repeated  when TM2 is moved back to ITW with dummy Febiad target  at the end of this month. The rest check result:  1 small leak(1.2 xE-8 atm.cc/sec) is found on one TM2 blue nylon bottom o-ring. This o-ring will be replaced when module is moved out of ITW.  It will be an easy job. Another small leak( 1.1XE-8 atm.cc/sec) is found on exit module 1 service cap top plate to frame o-ring seal. Its location is on east-south side of the exit module 1.This side is close and parallel to exit module 2 west-south side. Vacu- seal sprayer is used to fix this problem.  After two times spray, the leak is disappeared. This is not a permanent fix. The big top plate o-ring replacement is a complicate and dose taking job. It need to be well planned. The leak rate is small, and the leak source is close to ITW TP3 so there is no rush to replace the big o-ring on exit 1 service cap top plate at this moment. But, we need to close watching on this issue and have a job plan for this o-ring replacement since it could get worse in the future. There is no leak has been found on big T tank seal this year as well. All other primary and secondary vacuum seals  in ITW are good. TM2 water lines helum pressurize will be fulfilled In ITW or at TCS later. I will update this e-log when further test are finished.

 2017-01-25:  The O-ring on 60KV bias blue nylon stand is replaced at TCS. I leak check it. It is perfectly good now.

  1418   Wednesday, January 04, 2017, 14:27 David WangConditioning StationStandard Operation  started TCS vacuum pump

TCS TP1S has been started.

2017-01-23 afternoon: Stopped TP1S. We will use TCS to take TM2 tomorrow afternoon.

  1417   Friday, December 09, 2016, 18:05 Aurelia LaxdalConditioning StationRepairTM3 TM3 vacuum system have been connected at TCS.

Aurelia Laxdal wrote:

David Wang wrote:

All water circuits are by passed on the top of TM3. Water pumps and vacuum turbo- pumps are started. Everything is ready for TM3 camera sparking check.

 Wednesday November 30st: <br>

- 3 cameras (1 UV and 2 regular cameras)  were installed in the Service cap and the module was pumped down.  1 UV and 1 regular were placed on the East side of the module, aiming to water lines entering the Service Tray; 1 regular camera was placed on the South side of the module, aiming at the bottom of the blue insulators.

- started pumping down. <br>

Thursday, December 1st: <br>

- 1st HV test done. TM3 started sparking above 20kV. The cameras responses were consistent with the sparks. However, the screens were flickering and it was not clear if the responses were due to electromagnetic interferences; or due to cameras' gain change caused by high intensity light due to sparking.<br>

- added helium using the regulating valve. same results were found; <br>

Friday, December 2nd: <br>

- vented the module. <br>

- shielded the cameras' cables with aluminum tape. <br>

- removed 2 blue insulator (EE and HS) and shortened them by 1". They were found too long: HS blue insulator touching the horizontal HV water line; and the EE blue insulator at 2-3mm far from the HV water line; re-installed both shortened blue insulators.<br>

- changes the location of the cameras: 1 regular camera taped to the UV camera were placed South, aiming at the bottom of the blue insulators; 1 regular camera was kept on the East side of the module, also aiming at the bottom of the blue insulators. <br>

- started pumping down. <br>

Saturday, December 3rd: <br>

- 2nd HV test was done, with cameras' installed as mentioned above. results were consistent with the first test results. <br>

- added helium. results were the same. <br>

- vented and changed the location of the cameras: 1 regular camera taped to the UV camera were placed at the top of the Service Tray (South-West corner) aiming down the Service Tray; 1 regular camera was kept (its setup was not touched at all) on the East side of the module, aiming at the bottom of the blue insulators. <br>

- attempted to pump down, but the module was leaking. reopened the flanges, cleaned them, attempted again to pump down, but it showed a bigger leak. <br>

Sunday, December 4th: <br>

- the third attempt to pump down was successful (without reopening the module!). <br>

Monday, December 5th: <br>

- did the 3rd HV test with the cameras installed as described on December 3rd. same results as before were seen. <br>

- again helium was added and same results were noticed. <br>

- stopped pumps and prepared for venting to relocate the cameras lower in the Service Tray.

 

 

 

 Monday, December 5th (Con't): <br>

- vented and changed the location of the cameras;<br>

- the UV camera was placed (tapped on an aluminum spacer and on the grounded water lines) at the middle of the Service Tray (right below the first Mykroy insulator-plate) aiming down the Service Tray (at the second Mykroy insulator-plate and water lines) ; <br>

- 1 regular camera was placed right below the UV camera, also using a spacer (taped with the camera on grounded water lines) and also aiming down the Service Tray (at the second Mykroy insulator-plate and water lines);  The spacer for this camera had 300counts on it after it was removed from TM3, after the test;<br>

- NOTE: when installing the 1st regular camera: dropped a small allen key in the Service Tray. It landed on last insulator with the epoxi and water lines, between the first HV line and the wall of the grounded Service Tray.  This insulator is down below in the Service tray. Used a magnet stick to recuperate the allen key. <br>

- the 2nd regular camera was placed at the top of the Service Tray (tapped on the grounded water lines) looking down at the first Mykroy insulator-plate and water lines. NOTE: this camera had a filter applied to its lens. <br>

- pumped down <br>

Tuesday, December 6th:<br>

- did the 4th HV test with the cameras installed as described on December 5rd Tuesday morning very early . Same results as before were seen, except that the top camera (2nd regular camera) with the filter applied to its lens was flickering less than the other 2 cameras, and for small sparks this camera was not reacting at all. <br>

- vented shortly after the 4th test and relocated the cameras for the 5th HV test (last test); <br>

- placed only 2 regular cameras in the Service Tray;<br>

- 1 regular camera was placed right below the 2nd Mykroy insulator-plate, aiming down the Service Tray at the last insulator with the epoxi and water lines (this insulator is down below in the Service tray); <br>

- the 1st regular camera was placed a level up in the Service Tray, right below the 1st Mykroy insulator-plate, aiming down the Service Tray at the 2nd Mykroy insulator-plate; <br>

- NOTE: no spacers were used<br>

- pumped down and did the 5th HV test with the cameras installed as described above in the evening; <br>

- again same results as before were seen: the camera with the filter applied to its lens was flickering less than the other camera, and for small sparks this camera was not reacting at all. <br>

- NOTE: for this last test heard sparks outside (at atmosphere) when the HV was pushed at 26kV; <br>

Wednesday, December 7th:<br>

- vented and removed the cameras from TM3. No contamination was found on the cameras and wires. <br>

- TM3 was moved to the silo.<br>

  1416   Friday, December 09, 2016, 14:58 Isaac EarleNorth Hot-CellDevelopment  NHC service area floor and top of roof block painted

 The concrete floor in the North Hot Cell service area and the top of the NHC roof block in the target hall have been painted with Macropoxy 646 oil based epoxy paint, colour Flint Grey.  Two coats were used for the NHC roof, and one for the service area floor.

 

NHC_SA_before_and_after.jpg

 

NHC_roof_before_and_after.jpg

  1415   Monday, December 05, 2016, 10:10 David WangITWStandard OperationTM2 Five shielding blocks have been transferred from ITE to ITW.

The ITW is configured to take proton beam.

  1414   Monday, December 05, 2016, 10:04 Aurelia LaxdalConditioning StationRepairTM3 TM3 vacuum system have been connected at TCS.

David Wang wrote:

All water circuits are by passed on the top of TM3. Water pumps and vacuum turbo- pumps are started. Everything is ready for TM3 camera sparking check.

 Wednesday November 30st: <br>

- 3 cameras (1 UV and 2 regular cameras)  were installed in the Service cap and the module was pumped down.  1 UV and 1 regular were placed on the East side of the module, aiming to water lines entering the Service Tray; 1 regular camera was placed on the South side of the module, aiming at the bottom of the blue insulators.

- started pumping down. <br>

Thursday, December 1st: <br>

- 1st HV test done. TM3 started sparking above 20kV. The cameras responses were consistent with the sparks. However, the screens were flickering and it was not clear if the responses were due to electromagnetic interferences; or due to cameras' gain change caused by high intensity light due to sparking.<br>

- added helium using the regulating valve. same results were found; <br>

Friday, December 2nd: <br>

- vented the module. <br>

- shielded the cameras' cables with aluminum tape. <br>

- removed 2 blue insulator (EE and HS) and shortened them by 1". They were found too long: HS blue insulator touching the horizontal HV water line; and the EE blue insulator at 2-3mm far from the HV water line; re-installed both shortened blue insulators.<br>

- changes the location of the cameras: 1 regular camera taped to the UV camera were placed South, aiming at the bottom of the blue insulators; 1 regular camera was kept on the East side of the module, also aiming at the bottom of the blue insulators. <br>

- started pumping down. <br>

Saturday, December 3rd: <br>

- 2nd HV test was done, with cameras' installed as mentioned above. results were consistent with the first test results. <br>

- added helium. results were the same. <br>

- vented and changed the location of the cameras: 1 regular camera taped to the UV camera were placed at the top of the Service Tray (South-West corner) aiming down the Service Tray; 1 regular camera was kept (its setup was not touched at all) on the East side of the module, aiming at the bottom of the blue insulators. <br>

- attempted to pump down, but the module was leaking. reopened the flanges, cleaned them, attempted again to pump down, but it showed a bigger leak. <br>

Sunday, December 4th: <br>

- the third attempt to pump down was successful (without reopening the module!). <br>

Monday, December 5th: <br>

- did the 3rd HV test with the cameras installed as described on December 3rd. same results as before were seen. <br>

- again helium was added and same results were noticed. <br>

- stopped pumps and prepared for venting to relocate the cameras lower in the Service Tray.

 

 

 

  1413   Saturday, December 03, 2016, 10:01 David WangITWRepairTM2 venting ITW and TM2 with argon.

A short between TM2 EE and bias is produced yesterday during tube heater ramp up.  Alex asked for an argon venting on ITW to see if the problem could be solved by venting and pumping down yesterday.  I set up argon venting system in electrical room and started the venting at 8:30 AM this morning.  It will take 5 hours to vent the ITW to 760 torr(mechanical gauge reading).  The venting system pressure is set as 2 torr. A pressure relieve valve is installed into ITW venting line to prevent station over venting. The argon bottle  valve in electrical room will be closed by isac opps after 5 hours venting.

  1412   Wednesday, November 30, 2016, 16:31 David WangConditioning StationRepairTM3 TM3 vacuum system have been connected at TCS.

All water circuits are by passed on the top of TM3. Water pumps and vacuum turbo- pumps are started. Everything is ready for TM3 camera sparking check.

  1411   Tuesday, November 29, 2016, 14:50 Travis CaveITWStandard OperationTM2UC#18module moved

TM#2 with UC#18 has been moved to ITW from the conditioning station.

  1410   Tuesday, November 29, 2016, 12:57 David WangITWStandard OperationTM2 TM2 is connected in ITW

All turbo pumps are started. Water system and water signals have been checked. Pumping down on ITW and TM2 is good so far.

  1409   Tuesday, November 29, 2016, 07:50 David WangConditioning StationStandard OperationTM2 TM2 is disconnected at TCS.

Argon venting is done.

ELOG V2.9.2-2455