Conditioning continues today with resistors removed from the HV cable
Tuesday, July 18, 2017, 16:53: BIAS / EZL 50 / 25 kV - no sparks
Tuesday, July 18, 2017, 16:56: BIAS / EZL 55 / 27.5 kV - one spark
TM3 remained at 55 kV over night. Turbo pumps tripped twice and was restarted and HV recovered by RIB ops. Last recovery brought EZL to 16 kV (not 27.5 kV)
About 25 sparks over 15 h. No sparks for the last 3 h
Wednesday, July 19, 2017, 08:12: EZL to 27.5 kV
Wednesday, July 19, 2017, 08:38: BIAS to 57 kV
Wednesday, July 19, 2017, 08:46: BIAS to 57.5 kV
Wednesday, July 19, 2017, 09:05: BIAS to 59 kV
Wednesday, July 19, 2017, 09:19: BIAS to 60 kV
Wednesday, July 19, 2017, 09:28: EZL to 30 kV
Wednesday, July 19, 2017, 12:25: Heavy sparking. Lowered BIAS to 30 kV
Wednesday, July 19, 2017, 12:37: Increased BIAS again towards 50 kV, but heavy sparking again between 45 and 50 kV. Lowered back to 30 kV
Wednesday, July 19, 2017, 12:40: BIAS at 46 kV
Wednesday, July 19, 2017, 12:42: BIAS at 47 kV
Wednesday, July 19, 2017, 12:44: BIAS at 48 kV
Wednesday, July 19, 2017, 12:48: BIAS at 50 kV
Wednesday, July 19, 2017, 14:50: BIAS at 55 kV after ~2h without sparking at 50 kV
Wednesday, July 19, 2017, 15:12: Sparking. Lowered to 40 kV
Wednesday, July 19, 2017, 16:39: BIAS at 55 kV
Friday, July 21, 2017
Observed top of module inside target hall during HV sparks using crane cameras. No sparks observed, but some faint sound could be heard. Module still sparks at 60 and 55 kV. Have to lower to 40 kV to stop sparking.
Friday, July 21, 2017, 13:25: BIAS / EZL at 50 / 25 kV for without sparking for the last 90 min |