Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 57 of 141  Not logged in ELOG logo
  ID Date Author Category Type Moduledown Target/Number Subject
  601   Monday, February 17, 2014, 09:32 David WangConditioning StationRepairTM2 helium pressure test on TM2 tube heater +(D) water line.

I did the helium pressure test on Tube heater+ line this morning. The vacuum on CS and TM2 are very good. The base lake rate on leak detector was 1.7xE-7 atm.cc/sec. Base pressure was 0.0xE-4torr.  I applied helium to the "D"line .The test started from 30psi up to 80psi on both side "D" line.The base leak rate slightly changed to 1.9xE-7 atm.cc/sec during the test,but not base pressure. At this base leak rate level, No obvious leak had been found . See attachment pictures. The test will be repeated later when the base leak rate could be pumped into E -8 or E-9(the best) range.            

Attachment 1: 002.JPG
002.JPG
Attachment 2: 003.JPG
003.JPG
Attachment 3: 004.JPG
004.JPG
Attachment 4: 012.JPG
012.JPG
Attachment 5: 016.JPG
016.JPG
Attachment 6: 018.JPG
018.JPG
  602   Tuesday, February 18, 2014, 11:26 David WangConditioning StationRepairTM2 I stopped turbo pumps and disconnected vacuum system on TM 2 and CS

I stopped turbo pumps and disconnected vacuum system on TM2 and CS. The TM2 will be moved to SHC for C seal installation on "D" water block.

  603   Thursday, February 20, 2014, 09:45 Travis CaveConditioning StationStandard OperationTM2no targetmodule move

TM#2 has been moved from the conditioning station to the south hot cell.

  604   Thursday, February 20, 2014, 11:04 chad fisherSouth Hot-CellRepairTM2 Readying TM2 for C-Seal Leak Check

Containment box has been removed and water block jig installed.

Attachment 1: TM2_20140220_01.jpg
TM2_20140220_01.jpg
  605   Monday, February 24, 2014, 11:05 chad fisherSouth Hot-CellRepairTM2 Circuit D blank off

The blank off with the o-ring has been removed, manipulator fixed, circuit D water block sealinhg surfaces cleaned and blank off with c-seals installed and torqued. Leak check will occur shortly.

  606   Monday, February 24, 2014, 12:09 chad fisherSouth Hot-CellRepairTM2 C-seal blank off test

Circuit D has passed the vacuum leak check. Jig has been removed and containment box re-installed for move to conditioning station.

Attachment 1: TM2_20140224_1.jpg
TM2_20140224_1.jpg
  607   Monday, February 24, 2014, 13:52 Travis CaveSouth Hot-CellStandard OperationTM2no targetmodule move

TM#2 moved from the south hot cell to the conditioning station.

  608   Tuesday, February 25, 2014, 06:53 David WangSouth Hot-CellRepairTM2 Leak check on TM2 tube heater (+) water line with blank off(C-seal) installed on WB.

Chad and I did the leak check   on TM2 tube heater (+) water line  with blank off and C-seal  installed on  WB at South Hot Cell.The line was easy to pump down to 0.0xE-9atm.cc/sec and 0.0XE-4 torr on leak detector. Chad flushed lot helium around the water block (10 sec spray). No response had been found on leak detector.

  609   Tuesday, February 25, 2014, 10:00 David WangConditioning StationRepairTM2 helium pressure test on TM2 tube heater (+) water line with blank off(C-seal) installed on WB.

I did the helium pressure  test  on TM2 tube heater (+) water line  with blank off(C-seal) installed on  water block at CS.The leak detector was hooked directly to the top of the module this time. So base leak rate and base pressure were at the bottom scale on LD. 30 -80 psi helium was applied to the D lines(both side)  with10 psi   increasing each time. There is no any tiny response hasbeen found during the test. The lines are perfectly sealed. Also i sprayed the helium on the top of the service cap .All  air to vacuum seals on the top are good either. See attachment pictures.

Attachment 1: 004.JPG
004.JPG
Attachment 2: 005.JPG
005.JPG
Attachment 3: 006.JPG
006.JPG
Attachment 4: 007.JPG
007.JPG
Attachment 5: 008.JPG
008.JPG
Attachment 6: 009.JPG
009.JPG
Attachment 7: 010.JPG
010.JPG
Attachment 8: 011.JPG
011.JPG
Attachment 9: 017.JPG
017.JPG
Attachment 10: 019.JPG
019.JPG
  611   Wednesday, March 05, 2014, 10:07 Travis CaveConditioning StationStandard OperationTM2no targetmodule move

TM#2 with no target or source tray has been moved from the conditioning station to the north east silo. TM#1 with no target has been moved into the conditioning station.

  713   Thursday, July 24, 2014, 09:10 Travis CaveSouth Hot-CellStandard OperationTM2no targetmodule move

TM#2 has been moved to the hot cell from the north east silo.

  714   Thursday, July 24, 2014, 18:21 Grant MinorSouth Hot-CellRepairTM2No target / no source trayLeak check on TM2 ionizer tube cooling lines C and D - module side

Target Ionizer tube cooling lines "C" and "D" in Target Module 2 were both leak checked at the Hot Cell.  The lines were both blanked-off.

Bill Paley was present with David Wang in the Target Hall, operating the leak detector.  Grant Minor and Anders Mjos were present with Chad Fisher at the Hot Cell.

The "D" circuit was already blanked off with a copper blank containing silver brazed stainless steel inserts and indium plated inconel c-seals.

The "C" circuit was already blanked off with an aluminum blank and rubber o-rings.

The cooling lines are indicated in the attached screencapture from ITA6021 Rev .14, and are also labelled in the attached photo.

The "D" circuit was checked first, starting at around 12pm.

1.  The helium flow was tested by blowing dust on the work table.

2. The base leak rate on the Varian leak detector was confirmed in the "D" circuit to be stable at 10^-9 atm cc / sec and the pressure was 10^-4 Torr.

3. Each soldered joint on the "D" circuit was sprayed with a 2-second blast of helium - no response at the Varian.

4. The joint between the module-half of the water block and the copper blank-off was sprayed with a 2-second burst - no response.

5. A general area flood of helium sprayed for 10 seconds was applied all around both the "D" and "C" blocks - no response.

It was concluded that the "D" circuit had passed this leak check.  The "C" circuit was checked next.  The detector was changed to the "C" circuit and the circuit was pumped down.  At around 2pm the leak check resumed.

6. The base leak rate on the Varian leak detector was confirmed in the "C" circuit to be stable at 10^-9 atm cc / sec and the pressure was 10^-4 Torr.

7. The solder joint area on the "C" circuit was sprayed with an 8-second burst of helium - no response.

8. The joint between the two halves of the water blocks was sprayed with a 6-second helium burst - no response.

It was concluded that the "C" circuit had passed this leak check.

The electrical continuity of the "C" and "D" circuits were confirmed in the Target Hall at the service cap, and in the module at the Hot Cell, to double check that the correct lines has been pumped and leak checked - this was OK.

The ionizer tube heater lines appear to be leak tight at the Hot Cell.

 

 

 

 

Attachment 1: ITA6021_Rev_14_screencapture_cooling_lines_24July2014.jpg
ITA6021_Rev_14_screencapture_cooling_lines_24July2014.jpg
Attachment 2: TM2_hot_cell_leak_check_tube_heater_C_D_24July2014_small2.jpg
TM2_hot_cell_leak_check_tube_heater_C_D_24July2014_small2.jpg
Attachment 3: TM2_hot_cell_leak_check_no_source_tray_24july2014.JPG
TM2_hot_cell_leak_check_no_source_tray_24july2014.JPG
  715   Monday, July 28, 2014, 09:29 Travis CaveConditioning StationStandard OperationTM2no targetmodule move

TM#2 has been moved from the south hot cell to the conditioning station.

  716   Monday, July 28, 2014, 14:37 David WangConditioning StationDevelopmentTM2 helium pressure test on TM2 tube heater +(D)and -(C)water lines.
  • TM2 installed in Conditioning Station
  • Varian Leak detector connected directly to Target Module 2 Service cap.
  • Vacuum draw in Target Station with both module turbo pumps
  • Leak detector baseline normal (10^-4 Torr, 10^-9 Std cc/s He)
  • Since no Source tray is installed, and tube heater supply conductor is blanked off in target enclosure, it was necessary to test both supply and return points.
  • For each line tested, 80 psi He was connected, and waited ~2 min to for a response on the leak detector.
  • Lines tested:
    • conductor D (tube heater), Supply -> no He response
    • conductor D (tube heater), Return -> no He response
    • conductor C (tube heater), Supply -> no He response
    • conductor C (tube heater), Return -> no He response
  • Based on this leak testing, both supply and return lines of conductors C & D are leak tight under 95 psi He (80 psig He supply to vacuum)

 

Attachment 1: 011.JPG
011.JPG
Attachment 2: 012.JPG
012.JPG
Attachment 3: 013.JPG
013.JPG
Attachment 4: 014.JPG
014.JPG
Attachment 5: 015.JPG
015.JPG
Attachment 6: 017.JPG
017.JPG
Attachment 7: 018.JPG
018.JPG
  717   Monday, July 28, 2014, 14:45 David WangConditioning StationDevelopmentTM2 turned off TM2 and CS turbo pumps.

I turned off TM2 and CS turbo-pumps. TM2 will be moved from CS to silo tomorrow morning.

  803   Friday, November 28, 2014, 13:06 Travis CaveSouth Hot-CellStandard OperationTM2no targetmodule move

TM#2 with no target or source tray has been moved from the north east silo to the south hot cell.

  805   Monday, December 01, 2014, 14:06 chad fisherSouth Hot-CellRepairTM2 TM2 REFURB. WATER LOOP TEST

Some issues with the turntable and having to wait for a decision on whether to remove TM2 from the hot cell so that TM4 with dead UCx target could be put in this morning.

Progress on TM2:

  • Containment box has been removed from TM2.
  • Water block jig has been installed.
  • Existing blank off has been removed.
  • Sealing surfaces have been inspected.
  • First stage of sealing surface cleaning has been performed.

Tomorrow:

  • Polish of sealing surfaces.
  • Installation of loop.
  • Vacuum/helium leak check of loop.

TM2_20141201_03 - sealing surfaces before cleaning...kind of dirty

TM2_20141201_05AC - sealing surfaces after cleaning...looks good!

Attachment 1: TM2_20141201_01.JPG
TM2_20141201_01.JPG
Attachment 2: TM2_20141201_02.JPG
TM2_20141201_02.JPG
Attachment 3: TM2_20141201_03.JPG
TM2_20141201_03.JPG
Attachment 4: TM2_20141201_04.JPG
TM2_20141201_04.JPG
Attachment 5: TM2_20141201_05AC.jpg
TM2_20141201_05AC.jpg
  807   Tuesday, December 02, 2014, 10:15 chad fisherSouth Hot-CellRepairTM2 TM2 Reburb. Loop Install

Final polish, clean with methanol and clean compressed air.

Loop installed and torqued to 90 in lbs.

Minimum of approximately 1"  between loop and containment box at closest point.

Attachment 1: TM2_20141202_01.jpg
TM2_20141202_01.jpg
Attachment 2: 20141203_142215.jpg
20141203_142215.jpg
Attachment 3: 20141203_143530.jpg
20141203_143530.jpg
  808   Tuesday, December 02, 2014, 13:33 David WangSouth Hot-CellDevelopmentTM2 Leak check on TM2 tube heater +(D) at SHC

Chad and I leak checked TM2 tube heater+(D) circuit at SHC with water bypass loop and new seals installed on the water block. The LD base LR 0.0xE-9 atm.cc/sec,base pressure0.0xE-4 torr. Chad sprayed helium on the leak check area in SHC for 5 seconds. No any response has been found on LD during 1minutes waiting time. The test was repeated again and the result is same. NO LEAK at this stage!  After the TM2 is moved to CS , The D line will be pressured with 80 psi helium for helium pressure leak test before any hot water is circuited through it.  

Attachment 1: 2014-12-02_003.JPG
2014-12-02_003.JPG
Attachment 2: 2014-12-02_001.JPG
2014-12-02_001.JPG
Attachment 3: 2014-12-02_004.JPG
2014-12-02_004.JPG
  809   Thursday, December 04, 2014, 09:49 Travis CaveConditioning StationStandard OperationTM2no targetmodule move

TM#2 has been moved from the south hot cell to the conditioning station.

ELOG V2.9.2-2455