Saturday, October 05, 2013, 14:45, Friedhelm Ames, Conditioning Station, Standard Operation, TM3, NiO#2, vacuum readings
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IG1 8.0 e-7 T
IG1S 2.5 e-6 T
IG2 4.3 e-6 T
I will start the high voltage now
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Sunday, October 06, 2013, 00:17, Friedhelm Ames, Conditioning Station, Standard Operation, TM3, NiO#2, high voltage conditioning
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high voltage conditioning was carried out over the day up to 24 kV. i will leave it at 20 kV over night. Current is at 22 micro Amps, heaters off.
vacuum: IG1 7.7e-7
IG2 4.07 e-6
IG1sS 2.2 e-6
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Sunday, October 06, 2013, 15:39, Friedhelm Ames, Conditioning Station, Standard Operation, TM3, NiO#2, HEATERS STARTED
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The high voltage was sparking several times during the night. It may be correlated with the cycling of the cooling water temperature and conductance.
vacuum levels at 11:00
IG1 7.5e-7 T
IG2 3.9e-6 T
IG1s 2.0 e-6 T
heaters have been ramped up to TGH 580 A, TBHT 250 A,
anode 100 V 5.3 mA, coil 50 A Faraday cup 50 nA bias 20 kV EL 6 kV
vacuum
IG1 7.9e-7
IG2 4.5e-6
IG1s 2.2e-6 |
Sunday, October 06, 2013, 17:08, Friedhelm Ames, Conditioning Station, Development, TM3, NiO#2, trip of all power supplies
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All power supplies tripped on high conductivity of the cooling water < 5 MOhm, It is not clear if this was caused by a spark or vice versa. According to the strip tool for this signal the resistance of the water went up. There might be a fault in this signal. I do not have permission to force this signal so I keep the heaters off. We should revisit the interlock conditions, this signal should not be included in the interlocks for the heaters. Both target and tube seem to be still o.k. As I do not want to destroy the target I keep the heaters off and restart the high voltage only. |
Sunday, October 06, 2013, 20:28, Friedhelm Ames, Conditioning Station, Standard Operation, TM3, NiO#2, turbo pumps stopped
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vacuum readings before stopping
IG1: 7.4e-7 T
IG2 3.8 e-6 T
IG1S 1.95 e-6 T |
Monday, October 07, 2013, 12:06, Travis Cave, ITE, Standard Operation, TM3, NiO#2, module move
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TM#3 has been moved from the conditioning station to the east target station, move went well. |
Tuesday, October 15, 2013, 15:34, Bevan Moss, ITE, Standard Operation, TM3, , Blocks moved from ITW to ITE
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Blocks 1-4 have been moved from ITW to ITE. Block 5 was moved to a storage area as it will be in the way of the harp repair. Danka took air samples and found 200 counts of alpha on the air samples but nothing on the swipes. It is recommended that resporators be worn while blocks are being lifted and lowered. She will check the monitor tomorrow to confirm it is behaving as it should. |
Tuesday, October 22, 2013, 14:23, Anders Mjos, ITE, Standard Operation, TM3, NiO#2, Padlle wheel frequency measurements
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as measured today in the electrical room by David and Anders |
Friday, October 25, 2013, 13:39, Anders Mjos, ITE, Standard Operation, TM3, NiO#2, Padlle wheel frequency measurements
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with TM4 in ITW as measured today in the electrical room by David and Anders.
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Thursday, October 31, 2013, 11:38, Anders Mjos, ITE, Standard Operation, TM3, NiO#2, Padlle wheel frequency measurements
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with TM4 in ITW as measured today in the electrical room by David and Anders. |
Tuesday, November 12, 2013, 09:51, David Wang, ITE, Standard Operation, TM3, , TM3 disconnection
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TM3 has been disconnected this morning and purged all HV water lines. I found the power plug for all turbo pump fans wasnt connected during the last run. That maybe the one of the reason on that ITE TP3 failure. |
Tuesday, November 19, 2013, 10:52, Travis Cave, South Hot-Cell, Standard Operation, TM3, NiO#2, module move
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TM#3 with NiO#2 moved from ITE to the south hot cell. |
Wednesday, November 20, 2013, 08:50, chad fisher, South Hot-Cell, Standard Operation, TM3, NiO#2, NiO#2 removed
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NiO#2 has been removed from TM3 |
Wednesday, November 20, 2013, 09:52, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module move
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TM#3 with no target has been moved from the south hot cell to the north east silo. |
Thursday, November 21, 2013, 12:12, Anders Mjos, South Hot-Cell, Standard Operation, TM3, NiO#2, End of beam target inspection - ANODE does not hold 250V
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The target was inspected by Chad and Anders in the Hot Cell. Electrical megger tests were done during the assembly. It was found that Insulators No 3 (ITD0311) and No 2 (ITD0310) failed to hold voltage after the run.
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[V] |
[kOhm] |
ANODE - HS |
40 |
21 |
ANODE - TGT |
100 |
55 |
HS - TGT |
100 |
55 |
Lid removed |
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ANODE - HS |
40 |
21 |
ANODE - TGT |
90 |
41 |
HS - TGT |
100 |
55 |
Target removed |
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ANODE - HS |
245 |
139 |
No 3 Ins - TBHT |
0 |
0 |
No 2 Ins |
110 |
64 |
No 2 Ins removed |
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ANODE - HS |
540 |
OL |
EE to HS was measured OL at 1000 V.
Photos can be found on DocuShare
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Monday, November 25, 2013, 11:48, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module move
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TM#3 with no target has been moved from the north east silo to the south hot cell. |
Wednesday, November 27, 2013, 12:50, Bevan Moss, South Hot-Cell, Standard Operation, TM3, , Ground devices wiring check
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Travis and I completed an electrical check on the wiring harness for the devices on the ground plane. All lines passed 500V with the megger except for PNG and the BTM steerer. Those devices had a short to ground. of ~1.4ohm. |
Wednesday, November 27, 2013, 15:24, Bevan Moss, South Hot-Cell, Maintenance, TM3, , Wiring Harness Electrical Test
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Maico removed the containment box today allow Travis and I to further test the wiring harness. I disconnected the junction block and Travis and I repeated the test from yesterday. The all lines except the PNG tested OL. The module was then lowered and the twisted pair connected to the pin that corresponds to the steerer labeled BTM (it is likely this is not labeled correctly). This testing showed showed that the source of the short found yesterday is in the wiring harness or the source tray. The PNG gauge was then tested again. When beeping out the harness to find the location of the pin it was found that the short had gone away. This circuit was then tested with the megger at 500V and showed OL. Don Jackson has suggested looking at the SHV feed through. It is difficult to determine where the source of the problem is as it is intermittent. The source tray side wiring harness for the steerers was then disconnected from the steerers and tested to OL. Finally the connections on the source tray were tested. It was determined that the third socket down (see attached picture) has a short somewhere to ground. When Chad returns on Friday I will have him complete a visual inspection and if the source can be found we may be able to deflect the line. Failing that to repair this connection a new steerer cone assembly will need to be installed. |
Friday, November 29, 2013, 11:54, chad fisher, South Hot-Cell, Repair, TM3, , Steerer short investegation
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Using in cell camera and transit the suspect line on the steerers was inspected as best as possible. An existing photo of the complete steerers before installation was used for comparison. The wiring and beading inspected today showed no obvious problems, breaks or spots where there may be a short. In comparison to the photo from construction, what we could see of the steerers looked identical to the original installation. |
Friday, November 29, 2013, 11:57, Bevan Moss, South Hot-Cell, Repair, TM3, , Steerer short investegation
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chad fisher wrote: |
Using in cell camera and transit the suspect line on the steerers was inspected as best as possible. An existing photo of the complete steerers before installation was used for comparison. The wiring and beading inspected today showed no obvious problems, breaks or spots where there may be a short. In comparison to the photo from construction, what we could see of the steerers looked identical to the original installation.
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The test was repeated to confirm that there was a short. |
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