Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 20 of 140  Not logged in ELOG logo
Entry  Thursday, October 31, 2019, 08:49, Anders Mjos, Conditioning Station, Repair, , , Water leak on non-active cooling water circuit 
Yesterday a leak was discovered in the ISAC-I experimental hall. The leak appears to be at the connection between the evaporator and the return water
line. 1 in of water was lost from TCS:TK1. The water is currently valved off to prevent further leakage.
A fault reportt has been submitted to mechanical
Entry  Tuesday, May 22, 2018, 10:02, Anders Mjos, Conditioning Station, Repair, , , Water leak from TK1 over the weekend 2018-05-22_TCS_TK1_water_leak.pngBroken_Valve.jpg2018-05-22_TCS_TK1_water_leak_archiver.png
Link to e-log,
Link to efault
Tank level down from 76 to 55 in on TK1
    Reply  Monday, December 15, 2014, 09:41, Anders Mjos, Conditioning Station, Maintenance, TM2, , Water leak found at the isolation transforer 


    
        
            Anders Mjos wrote:
        
        
            
             The level dropped below 15 in over the weekend. MP2 stopped, but MP3 condtinued pumping.
Entry  Friday, March 08, 2019, 14:10, chad fisher, South Hot-Cell, Repair, TM2, , Water block polishing B_after_SB_(2).jpg
After trials with 2000 grid wet paper I have moved up to "red" scotch brite. This seems to have worked the best so far although it took two
minutes to remove the ring that the other materials could not remove (see picture).
I have moved to next circuit. Currently at 3 minutes and 30 seconds with scotch brite but significant ring remains.
Entry  Monday, February 25, 2019, 09:44, chad fisher, South Hot-Cell, Repair, TM2, , Water block jig 
module side water block jig has been removed in preparation for electrical checks.
Entry  Monday, March 11, 2019, 14:34, chad fisher, South Hot-Cell, Repair, TM2, , Water Block Polishing status 
Stage 1 polishing (water scale and at least 99% of visual indium removed) has been achieved on all 2 seal water blocks that will be used (Ground electrode
has not been polished). Process required 3-4 3minute cycles of the tool using scotch brite pads with the tool running at approximately 75 psi.
Entry  Tuesday, March 12, 2019, 09:13, chad fisher, South Hot-Cell, Repair, TM2, , Water Block Polishing status Blocks_Stage_1_Polish.jpg
Stage 1 polish has been achieved on all single seal water blocks using the single pad tool run at 75 psi, 2 3 minute cycles per block using red scotch
brite.
Entry  Thursday, March 14, 2019, 10:25, chad fisher, South Hot-Cell, Repair, TM2, , Water Block Polishing status Blocks_final_polished.jpg
Phase 2 (intermediate) and Phase 3 (Final) polishing is complete on all water blocks on TM2 (minus ground electrode circuit which has only had a cursory
cleaning). Phase 2 with 2000 grit wet sand paper and isopropynol for 1 minute with tool at 75 psi, Phase 3 with Veltex polishing cloth for 1 minute with
tool at 75 psi.
Entry  Thursday, May 09, 2013, 14:23, chad fisher, South Hot-Cell, Repair, TM3, , Water Block Jig Removal IMG_1059[1].JPG
The source tray side of the water block jig has been removed in preparation for moving the module to the  conditioning station for electrical tests.
Entry  Friday, April 26, 2013, 11:20, chad fisher, South Hot-Cell, Repair, TM3, , Water Block Jig (back half) 
The back half of the water block jig (services tray side) has been sucessfully located onto the module.
About 50% of the waterblocks have centered themselfs it their respective cups and the rest look good for concentricity but will require some gentle
wiggling to get them to seat.
Entry  Thursday, June 13, 2013, 09:21, chad fisher, South Hot-Cell, Development, , , Warm Cell Mock-up 20130613_084421[1].jpg20130613_084426[1].jpg
the warm cell mock-up has been inserted into the warm cell and final preparation for the remote test are being made.
Entry  Wednesday, March 01, 2023, 09:34, David Wang, Cooling, Maintenance, , , Visual inspection of HALCW for possible small water leak or drip.  
I visually inspected HALCW system including water station section, both target pits, and de-ionizer system.  No small leak and drip was found . 
The inspection in both target pits will be repeated after flow sensors are replaced. 
Entry  Friday, November 19, 2021, 12:48, Adam Newsome, South Hot-Cell, Development, , , Vertical motion limit switch installation PXL_20211119_172142852.jpg
A rotary limit switch was installed, attached to the shaft adjacent to the drive motor for the vertical drive system. This limit switch is not yet wired
to the control system and operational - this will be done at a future date and the e-log will be updated.
Relevant electrical drawings: IRH2083 to IRH2085
Entry  Monday, April 08, 2013, 16:16, Bevan Moss, Conditioning Station, Standard Operation, TM1, Ta #39, Venting with Argon 
 TM1 started venting at 4:15 pm with Argon. I will leave the valve open over night.
Entry  Tuesday, February 07, 2017, 15:57, Isaac Earle, North Hot-Cell, Development, , , Ventilation Ducting Gasket Installed 
 Lead gasket IRH1633 was installed today according to assembly drawing IRH1618 Rev B.
Entry  Monday, March 18, 2013, 15:28, Bevan Moss, Conditioning Station, Standard Operation, TM4, CS Test Target #1, Vented With Argon Vented_with_Argon.JPG
 The conditioning station has been vented with argon. Time taken is not known but it is less than 3 hours. See attached picture for convectron gauge
readings. CG1A is in air.
Entry  Monday, July 15, 2019, 13:29, David Wang, Conditioning Station, Development, TM4, , Vacuum surge when TM4 B line iwas supplied with water. vacuum_surge_on_B_line_with_water.png
Yesterday, TM4 B line was supplied with water at TCS for testing.  TCS: IG1 and IG2 had big response on it. See attachment. The water was disconnected
right away, and line was purged. Vacuum recovered after overnight pump. 
Entry  Friday, December 18, 2015, 11:42, Anders Mjos, Conditioning Station, Repair, , , Vacuum gauges not reading correctly 
 It was found that the conversion from voltage to vacuum (Torr) in EPICS is not correct for the XGS-600 controllers in use at the TCS. EPICS did
not correspond to local values displayed on the controller. An e-fault has been submitted.
    Reply  Monday, December 21, 2015, 13:27, Anders Mjos, Conditioning Station, Repair, , , Vacuum gauges not reading correctly 


    
        
            Anders Mjos wrote:
        
        
            
             It was found that the conversion from voltage to vacuum (Torr) in EPICS is not correct for the
Entry  Friday, September 11, 2015, 14:31, Anders Mjos, Conditioning Station, Maintenance, TM2, ZrC#7, Vacuum gauge and EPICS read back calibration 
The corelation betwenn the local value on the gauge controllers and the read back valiues in EPICS was compared. Data can be found in a previous  e-log
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