ID |
Date |
Author |
Category |
Type |
Module |
Target/Number |
Subject |
1903
|
Monday, April 01, 2019, 14:56 |
Isaac Earle | Safe Module Parking | Development | | | SMP shield box and vacuum vessel installed in final location |
Last week drilling of the additional required holes in the SMP shield box was completed in the Target Hall. This morning the shield box (IRH1675) was moved to its final installation position in the silo area on the B2 level. The vacuum vessel (IRH1806) was then installed inside the shield box. The center of the vacuum vessel is 2-3" north of the south travel limit of the crane. Photos as well as measurements of the final position are attached below.




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1904
|
Thursday, April 04, 2019, 14:49 |
Isaac Earle | Safe Module Parking | Development | | | SMP vacuum vessel support roller friction check |
With the SMP vacuum vessel now installed inside the shield box, a test was performed to measure the torque required to rotate the vessel. At a moment arm distance of 2.0m a force of 89N was required to rotate the vessel (with no module installed) resulting in a torque of 178Nm. Based on this, the coefficient of rolling resistance (CRR) was calculated to be 0.007; This is fairly close to available data for similar applications such as cast iron wheels on steel rail (https://en.wikipedia.org/wiki/Rolling_resistance). The CRR used for design of the SMP drivetrain was 0.054 which was based on empirical data for a similar product. Because this is significantly higher than the friction of the as-built system the drive-train components are stronger than required and should have no problem rotating the vessel when loaded with a module.
Further details and calculations included in the attached PDF. |
1905
|
Friday, April 05, 2019, 13:44 |
chad fisher | Spent Target Vault | Development | | | 2019 Pail drop tests |
- Drop test performed January 8, 2019 with 25 lb target, UN pail and lug cover. Drop failed. Lug cover half removed. Pictures and video in docushare collection 24626.
- Second test January8, 2019 UN pail, "new" dish cover, old lock lever ring, 25 lb target. Single drop from 1.2m onto latch, no sealant. No leaks 24 hours later. Pictures in docushare collection 24626
- Drop test performed April 2, 2019 repeat of previous test using until that was loaded in north hot cell test. Target punctured can. Pictures in docushare collection 24626.
- Drop test performed April 5, 2019 repeat of previous test with the addition of a aluminum sleeve (0.05" thick) inside the pail between pail and target.
New UN rated pail with 9.55 kg target, 1.2 kg 16 gauge Al sleeve (10.75 OD x 14.75" tall), 3 liters of water with red food coloring no sealant on gasket.
First drop standard drop test from 1.2m onto latch
Second drop test 1.2m onto bottom of pail
Third drop 1.2m onto side of pail
Drops 4-6 1.2m onto lid
Pail was left inverted for an hour after the first three drops with no leaks after 1 hour.
No leaks after the remaining 3 drops .Bottom very damaged suggesting need for protective disc in bottom of pail.
Pictures can be found in docushare Collection-24627
- Drop tests performed May 2, 2019 with 9.7 kg target, 1.346 kg of mixed module and target components, sleeve and disc. First drop on latch from 1.2m, no leak, second drop straight on bottom from 1.2m, no leak, third drop on side from 1.2m leak. Drop test described in more detail in document drop test witness document on docushare. Pictures and video in docushare collection 24626.
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1906
|
Friday, April 12, 2019, 11:44 |
chad fisher | South Hot-Cell | Standard Operation | | | Pail transfer |
Pail transfer was undertaken in the south hot cell. went very well except near the end the master tong cable of the right hand manipulator broke. Not entirely a surprise due to the amount of use it has seen lately. |
1907
|
Wednesday, April 17, 2019, 12:03 |
chad fisher | South Hot-Cell | Repair | | | Manipulator repair |
Broken handle cable of east manipulator has been replaced and manipulator is operational again. |
1908
|
Thursday, April 18, 2019, 10:04 |
Travis Cave | South Hot-Cell | Maintenance | | Ta#50, SiC#34, Ta#46, Ta#47, and Ta#45 | Target transfer from old pail to new pail. |
Targets Ta#50 and SiC#34 have been transferred from their old pails to new ones. Ta#50 was done on April 12th 2019 it was moved from pail #148 to pail #200 and a new field measurement was done and found to be 3.57mSv/hr. SiC#34 was done on April 18th 2019 it was moved from pail #143 to pail # 206 and a new field measurement was done and found to be 2.20mSv/hr. Both measurements were done by the RAM that is mounted at the south hot cell.
April 24 2019
Target Ta#46 has now been transferred to a new pail with a number 207 from pail 143 it was 3.62 mSv/hr when removed from the south hot cell.
April 25 2019
Target Ta#47 has now been transferred to a new pail with a number 201 from pail 137 it was 2.25mSv/hr when removed from the south hot cell. The bag that the target was in has shown signs of degradation.
Target Ta#45 has now been transferred to a new pail with a number 202 from pail 124 it was 1.45mSv/hr when removed from the south hot cell. The bag that the target was in was destroyed. Also in the pail was a shutter, IMG Gauge, some altem parts, wire and bolts.
The extraction electrode from Ta#47 was added to this pail as it was left behind from last transfer. |
1909
|
Monday, April 29, 2019, 07:56 |
chad fisher | South Hot-Cell | Development | | | Pail transfers |
Two pail transfers took place April 25th.
Ta#47 transfered from pail 137 to pail 201. existing plastic bag from 137 showed many areas of typical age/rad damage related failure.
Ta#45 in pail 124 was transfered to pail 202. Pail 124 also contained the shutter and "roof mounted" img gauge from TM2 that were removed in 2015 in addition to a bunch of fasteners, heat shrink tubing (from lock lever rings from an previous methods of spent target packaging) etc. The original plastic bag in pail 124 had completely failed and shredded and flaky. The shutter and extraction electrode from Ta#47 were put in pail 202 with Ta#45...cabling of the shutter being completely intertwined with the target. |
1910
|
Monday, April 29, 2019, 09:32 |
Travis Cave | Spent Target Vault | Standard Operation | | SiC#31,32 and UC#19,20,21 | Spent targets moved to mini vault. |
The following targets have been moved from the spent target vault to the mini vault:
#127 - SiC#31 (front)
#132 - SiC#32
#145 - UC#19
#150 - UC#20
#159 - UC#21 (back) |
1916
|
Thursday, May 02, 2019, 09:37 |
Travis Cave | Spent Target Vault | Standard Operation | | UC#26 | Spent Target Move |
The spent UC#26 target was moved from the south hot cell to the spent target vault. It was place in pail #209 and put in spot 1A in the vault and was 2.42mSv/hr upon removal from the south hot cell. |
1917
|
Wednesday, May 08, 2019, 10:29 |
Travis Cave | South Hot-Cell | Standard Operation | | | Entrance module move |
The entrance module has been moved from the west station to the south hot cell. |
1918
|
Friday, May 10, 2019, 10:23 |
chad fisher | South Hot-Cell | Repair | | | West Entrance module wire scanner replacement |
West entrance module - visible broken or disconnected wire visible on old/existing wire scanner. Wire scanner removed, new one installed. |
1919
|
Monday, May 13, 2019, 09:55 |
Travis Cave | ITW | Standard Operation | | | Entrance module move |
The West Entrance module has been moved from the south hot cell to the west target station. |
1920
|
Monday, May 13, 2019, 11:22 |
David Wang | ITW | Repair | | | ITW entrance module has been connnected. |
Entrance module has been connected back to ITW. Everything is normal. |
1921
|
Wednesday, May 15, 2019, 16:06 |
Isaac Earle | Safe Module Parking | Development | | | SMP module support flange installed and leak checked |
The SMP module support flange sub-assembly (IRH1755) was installed today according to drawing IRH1683. Dow Corning 111 sealing compound was used to keep the o-ring adhered to the lower groove during transportation and installation. The TCS shield plug (IRH1646) was then installed on the SMP module flange which has vacuum connections for leak checking. Vacuum was pulled on the SMP vessel using the Varian 979 leak detector. After approximately 3.5 hours of pumping the test port pressure was at 2.4E-2 Torr and leak rate was 7.9E-8atm*cc/s. Helium was configured with the regulator set at 10psi and flow rate of >10 bubbles per second in Windex and then applied slowly around the perimeter of the vacuum flange (IRH1686) and it's mating components on both the top and the bottom. There was no response on the leak detector indicating the seals on both sides of the module flange are leak tight.




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1925
|
Friday, May 17, 2019, 16:46 |
Adam Newsome | Safe Module Parking | Development | | | SMP Controls Installation Update |
The following controls-related items were installed for the SMP project:
- Cable tray
- Main control panel
- Motor starter box
- Wiring from limit switches and rotation motor to main control panel
- Air fittings at supply (quick disconnect)
- Main air supply hose from supply to control panel (quick disconnect)
- Air tubing from lid control valve at control panel to lid cylinders
Air fittings stem off existing air supply lines on the South wall, below a manual shutoff valve. A quick disconnect was installed. When SMP is not in use, manual shutoff valve should be left off.
Main control panel and motor starter box were mounted on the North wall. Wire duct runs from the main control panel to the grated floor. Cabling/air runs underneath the mezzanine platform, along existing and new cable tray, to the SMP.
Cable tray was installed on the South wall, from the corner to the SMP module. A cutout was made to accommodate for existing tubing. An additional ~1 ft. of tray will be added to the end, near the corner, at a future time.
Remainder of installation work to be done before commissioning:
- Mount and install new Opto-22 module
- Chain new Opto-22 module to existing one (power, comms) below mezzanine on North wall |
1930
|
Thursday, May 23, 2019, 11:22 |
Travis Cave | South Hot-Cell | Maintenance | | | Removing garbage from the south hot cell. |
A 55 Gal. drum was remotely lowered into the south hot cell. It was then filled with compressable waste. Then the drum was remotely removed from the south hot cell. The drum measured about 20microSv/hr upon removal from the south hot cell. |
1937
|
Monday, June 10, 2019, 14:13 |
Travis Cave | Spent Target Vault | Standard Operation | | | Old TM#4 source tray moved |
The old TM#4 source tray in the south hot cell was moved to the spent target vault. The tray had a low of 7.5mSv/hr to a high of 22.1mSv/hr though a 390 degree rotation. |
1944
|
Thursday, June 20, 2019, 15:09 |
Isaac Earle | Safe Module Parking | Development | | | SMP motor wiring inspected by electrician |
The AC wiring for the SMP motor was inspected by Randy Boehm (TRIUMF electrician) as recommended by Franco Mammarella (TRIUMF electrical engineer). After inspecting the system Randy required the following changes:
- AC wiring inside the control panel be increased to 16awg minimum (14awg preferred)
- Wiring between the control panel and motor control box be increased to 14awg
- Power cable to the motor be increased to 14awg
- Current rating for MS connectors be checked and replaced if below 10A
- Prefer that motor control box components be relocated to the control panel to reduce number of AC wires and connections (preferred but not mandatory)
- A dedicated ground wire is required in the cable going to the motor (if not already in place)
After these changes have been made the inspection will be repeated.
July 31, 2019 update:
Items 1, 2, 3, and 6 from above were completed. 14awg wiring was used for wiring inside the control panel (Item 1). Current rating for the MS connectors was checked and is over 10A (Item 4). Motor control box components were not relocated to the control panel at this time (Item 5).
Randy repeated his inspection today, and approved of the updated 120V wiring.
Adam updated the SMP electrical and control schematics (IRH1868-1874) |
1946
|
Thursday, July 04, 2019, 08:57 |
Isaac Earle | Safe Module Parking | Development | | | SMP vacuum system installed |
July 3:
- Assembled exhaust line flexible hose and fittings as per ISK0529 Rev D then leak checked: 1.4E-1 Torr test port pressure, 1.1E-7 atm-cc/s leak rate, no response to helium spray at both ends of flexible line (all vacuum fittings purchased from Kurt Lesker under Requisition #1046936)
- Connected exhaust of SMP vacuum pump to nuclear ventilation duct using flexible hose assembly as per ISK0529 Rev D
- Installed convectron gauges at pump inlet as per ISK0529 Rev D
- Installed TCS plug block (IRH1646) in SMP
- Connected plug block vacuum port to SMP pump using flexible corrugated hose
- Connected SMP:CG1 to portable pressure display: ~700Torr
- Turned on SMP:MP1 at 4:17pm, after approximately 25 minutes was down to 75 Torr, at 1hr 40 minutes was 90mTorr, left pumping over night
July 4:
- Pressure at 4mTorr at 8am, will leave pumping longer to see if it gets any lower
- Submitted Work Request #5239 to PLC Controls for wiring of the pump and convectron gauges and integrations with EPICS
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1955
|
Friday, July 26, 2019, 15:43 |
Isaac Earle | Safe Module Parking | Development | | | SMP vacuum control system completed |
The SMP vacuum control system has been wired and setup to be controlled from EPICS. Backing valve control (SMP:BV1) was tested by connecting to the turbo pump solenoid on TM3 located in the silo directly north of the SMP. The SMP pump (SMP:MP1) was turned on and off through the EPICS interface and responded as expected. Both convectron gauges (SMP:CG1 and SMP:CG2) responded as expected when the pump was turned on. The readings from the two gauges were consistent throughout the mili-Torr range.
The work was done by Ray Mendoza under WP I2019-07-24-4 (work request #5239).

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