Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 121 of 139  Not logged in ELOG logo
ID Date Author Category Type Module Target/Numberdown Subject
  1989   Monday, September 23, 2019, 13:21 Travis CaveSpent Target VaultStandard Operation  Repacking of the targets.

 All targets in the mini vault have been repackaged and are now ready to be loaded into F-308s. All the target pails have new numbers see attached sheet for details.

Attachment 1: Target_Index_2019-09-23_Mini_Vault.pdf
Target_Index_2019-09-23_Mini_Vault.pdf Target_Index_2019-09-23_Mini_Vault.pdf
  1990   Monday, September 30, 2019, 11:27 Isaac EarleSafe Module ParkingDevelopment  SMP vacuum vessel modifications completed

The SMP vacuum vessel welds were reinforced to match the specifications on IRH1710 Rev D.  In addition a tube stub was added on the side of the vessel for installation of a PRV.  The relief valve installed was Accu-Glass 113150, with 2psi setpoint (not the MDC 420036 model specified on IRH1710 Rev D).  The drawing will be updated to reflect this.

Welding was performed in the TRIUMF machine shop.  A larger capacity forklift was rented to move the vessel back and forth between the shop and the Meson Hall loading bay where the main crane was used to flip the vessel between welds.

After welding the vessel was leak checked using a blank-off plate (helium leak tight).  The vessel was then returned to the Target Hall, the top flange IRH1755 was re-installed, and the TCS shield plug was installed on the flange.  The vessel was pumped down over the weekend using the SMP vacuum pump, and reached 8mTorr by Monday morning.  A helium leak check was performed in the Target Hall:  baseline leak rate 0.0E-9 atm-cc/sec, 0.0E-4Torr port pressure, no response to generous helium spray on PRV and around both seal locations for the top flange.

Remaining re-assembly of the SMP will now proceed.

  2000   Friday, October 04, 2019, 16:43 David WangConditioning StationStandard OperationTM2 TM2 has been connected at TCS.

TM2 has been connected at TCS this morning. helium pressure test on Tm2 HS line is done. No leak.

  2001   Friday, October 04, 2019, 16:50 David WangSouth Hot-CellStandard OperationTM4 UCx 28 target with TM4 SHC leak check and electrical check.

TM4 HS Leak check result is good . No leak. electrical check after target installation: Bias to chassis 550 Mohm. Coils are shorted each other and shorted to 60 KV bias. ABCD to 60KV bias 500V Megga measurement are 100M at least which is good. EE to bias are OL at 500V. The electrical check result is good.

  2006   Thursday, October 10, 2019, 16:17 Adam NewsomeSafe Module ParkingDevelopment  SMP Main Panel: Relay Addition for E-Stop Circut

An update was made for the E-stop and power supply system in the SMP main panel. Upon testing remote control, it was determined that the Opto 22 AC module was not sufficiently rated to handle the current draw of the motor (5A fuse versus motor 5.7A current draw). The design was modified so that the E-stop chain, which supplies 120 VAC line voltage through the main panel E-stop then the remote module (or local pendant when plugged in), will now activate a relay rather than run directly to the motor and 24 VDC PSU. This means that this E-stop chain will not carry the current draw of the entire system. Rather, the relay that is toggled when the E-stop circuit is closed will supply the system with power - this relay is rated for 15 A so the main 10 A fuse will blow before the relay fails in the event of a current spike. The new relay was installed on Oct 9, 2019. The local pendant was tested at this time and worked as expected (motion control, E-stops). On Oct 10, 2019, remote control was tested again and is working as expected (motion control, E-stops). In the attached schematic screenshot, the modification is CR7. In the image of the panel, this relay is located in the top left.

 

Edit: TRIUMF electrician Joel Semilla has seen the design change and verified it is acceptable.

Attachment 1: Changes_to_IRH1869.JPG
Changes_to_IRH1869.JPG
Attachment 2: IMG_20191009_153336_-_new_relay_for_E-stop.jpg
IMG_20191009_153336_-_new_relay_for_E-stop.jpg
  2007   Tuesday, October 15, 2019, 16:42 Isaac EarleSafe Module ParkingDevelopment  SMP flange alignment tested using shield plug

 As a preliminary test in preparation for SMP commissioning, one of the steel module shield plugs was installed into the SMP to check the positional and rotational alignment procedures.  The following is a summary of the steps performed:

  1. Shield plug lifted with crane and rotated to an arbitrary (non-orthogonal) position
  2. Using the crane pendant the shield plug was roughly aligned over the SMP and lowered until the base was within 15cm of the top of the flange
  3. The SMP flange was rotated to roughly match the orientation of the shield plug 
  4. Precise positioning of module achieved visually from within the Target Hall using crane for NESW position and SMP for rotation
  5. Module lowered into SMP vessel (not resting on base of vessel)
  6. Target Hall crane was then set to "Test Mode" and operated from the crane control room
  7. Crane position with the module centered in the SMP vessel was recorded as E-W: 18.5495m,  N-S: 4.9065m
  8. The shield plug was lifted from the SMP, moved to an arbitrary location in the Target Hall, and set to a different arbitrary rotational position
  9. The SMP flange was returned to the "centered" position
  10. The shield plug was moved to the previously recorded location over the SMP and lowered to within 15cm of the top of the flange (using cameras)
  11. Steps 3-5 were repeated using only camera views to achieve alignment (SMP rotation was controlled using the pendant with instructions by phone from the crane room operator because the module for remote control currently requires a part to be changed)

Official commissioning of the SMP will now be planned as per the commissioning plan Document-170404

 

 smp1.jpg

 

smp2.jpg

 

smp3.jpg

 

smp4.jpg

  2010   Tuesday, October 22, 2019, 16:26 Isaac EarleSafe Module ParkingDevelopment  SMP shield box grounding

A braided grounding strap was attached to the aluminum gear box support on the SMP shield box structure, and grounded by attaching it to the exterior of an electrical conduit located in the south-west corner of the B2 area at the top of the silo in that corner.  The braiding was also connected to the stainless steel support structure for the SMP vacuum pump.

  2014   Friday, October 25, 2019, 06:43 David WangSafe Module ParkingDevelopmentTM3 SMP vacuum

TM3 was moved into SMP Oct 25 morning.  After two nights pumping down, SMP CG1 read 30mtorr this morning.  The pump is stopped. SMP will be vented soon for TM3 moving back to silo. 

  2016   Monday, October 28, 2019, 12:00 Isaac EarleSafe Module ParkingDevelopment  SMP shielding attenuation measured & compared to theoretical values

The attenuation of the SMP shielding was measured as part of SMP commissioning (Document-170404, R1, Section 4, Test #8)

The field on the shutter side of TM3 was measured without any shielding as it was removed from a storage silo.  At 0.5m from the edge of the module the maximum field was 5.00mSv.  After installation into the SMP the maximum field outside the SMP shielding at 0.5m from the edge of the module was found to be 27uSv/hr. The resulting attenuation is 185x

Expected attenuation was calculated by Joe Mildenberger assuming that the majority of the activated components in that module are either copper or aluminum.  With 6" of steel shielding (SMP shield vessel plus vacuum vessel), the attenuation factors were found for the following isotopes: 

 

Na-22 (created in Al): 115

Co-60 (created in steel (Fe) or Cu): 70

Mn-54: (created in steel (Fe) or Cu): 200

 

Based on these figures, the measured result of 185 seems to be reasonable.

  2017   Tuesday, October 29, 2019, 10:00 Adam NewsomeSafe Module ParkingDevelopment  SMP Updates to E-stop circuit and feedback signals

The SMP main control panel and remote control module were updated in order to implement the following items which were deemed desirable during commissioning:
 

  •     24 VDC line added to E-stop circuit:

    Previously the E-stop relay cut power to only 120 VAC. This means that the lid rotation motor would stop instantly, but since the lid open/close valve is powered by 24 VDC which comes from a power supply unit, there would be a short delay while the unit powers off in which the valve was still active. This could result in a situation in which, for example, someone is operating the pendant to close the lid and another person recognizes a hazard and presses the E-stop on the main panel, but the lid does not stop closing for approximately 3 seconds while the operator is still holding the "close" button down.

    To rectify this issue, the 24 VDC line was routed through a NO contact of the same E-stop relay that controls the entire 120 VAC supply to the system. This was tested on Oct. 25, 2019 - working.

     
  • Status feedback signals to remote control room:

    Previously status signals for "Lid raised", "Lid Centred", "CW Limit", and "CCW Limit" were only displayed as light indicators on the main control panel. It was determined during remote operation that it would be helpful to have these signals sent back to the software interface so that an operator does not need to use a camera to look at the light indicators.


    Electrical drawings and cable schedule have been updated to reflect these changes. The SMP will be tested again using the commissioning plan checklist to confirm no there were no inadvertent effects on the rest of the same from these changes.

 

  2019   Thursday, October 31, 2019, 08:49 Anders MjosConditioning StationRepair  Water leak on non-active cooling water circuit

Yesterday a leak was discovered in the ISAC-I experimental hall. The leak appears to be at the connection between the evaporator and the return water line. 1 in of water was lost from TCS:TK1. The water is currently valved off to prevent further leakage.

A fault reportt has been submitted to mechanical services - awaiting response.


Friday, November 01, 2019

Leak repaired by Mechanical Services. A brass fitting had cracked and was replaced with a galvanized fitting.

  2020   Thursday, October 31, 2019, 10:17 David WangAssembly/Bench TestMaintenanceTM2 Febiad target gas line leak check.

Feibiad gas line for ITE and its adapter fittings for TM2 are tested today by installing them on a dummy water stem. No leak on VCO fitting, adapter o-rings, and all Swagelock fittings of this assembly. Manual valve on gas line works fine.  The positional check on gas line between TM2 and ITW will be fulfilled next Tuesday during module disconnection. 

  2037   Thursday, December 12, 2019, 14:39 Isaac EarleSafe Module ParkingDevelopment  SMP assembly shifted 1.0" north

The SMP assembly was shifted approximately 1.0" north today by pushing it, braced against the south wall, using a 100 Ton capacity air lifting bag supplied by Beamlines Group.  The move was one of the action items identified at the Gate 4A/4B close-out review.  During commissioning of the SMP, TM3 was installed into the vacuum vessel, which required the crane to be all the way at its south limit, so the move is to provide some margin for future use, particularly if TM1 is put in the SMP as the extent of its shielding is slightly larger than the other modules.

 

One of the air fittings for the lid actuation cylinder on the north side was damaged during the move.  It was replaced and correct functionality of lid actuation was then confirmed.

  2038   Thursday, January 02, 2020, 09:55 David WangCoolingStandard Operation  I turned on HALC water pump MP2.

HALCW MP2 is switched onnow. There is a small amount of air trapped in system. The pump works fine.  Water level and system resistivity will be monitored for a while.

LALCW P5 and P6 are switched on  for cooling HALCW.  HALCW MP2 is in operation now.

  2039   Thursday, January 02, 2020, 10:10 David WangCraneStandard Operation  TH crane issue.

Target hall crane does not work properly after TH crane main power is switched off during Christmas time in control room. I switched the main power back this morning. The only movement could be operated is crane rotation. Power is supplied crane. The control  on N-S, E-W and up-down movements do not work. We had the same problem last year. After trouble shooting, It was pointed to a PLC battery issue. Control group changed the battery and reloaded the program. I guess  the battery is drained out very fast for some reason. So, We face the same problem again this year.

Adam checked control room main power supply. I checked in TH crane again. The problem is still there. We can confirm this is the same issue like last year. 

  2040   Friday, January 03, 2020, 13:15 Adam NewsomeCraneRepair  Target Hall Crane PLC Module/Battery Replacement
The Target Hall Crane bridge and trolley motion was lost after a period of the crane having power disconnected over winter holidays. This is reported in the following e-log: https://elog.triumf.ca/TIS/RH-ISAC/2039. This issue is a duplicate of what happened in 2019 at this time: https://elog.triumf.ca/TIS/RH-ISAC/1845

It was determined from troubleshooting via PLC indicator lights that the memory battery had died during the power-off time, and because of this, the program stored was lost. Note that this is an anomaly - the battery should have lasted much longer than the shutoff duration of ~2 weeks.

The SLC500 module was replaced with a spare, which contained a new battery. The old SLC500 module is still functioning but the battery has been removed (spares will be ordered) - this module is stored in a cabinet drawer in the control room. It will need to be re-programmed if re-installed as the program was lost. The original program titled TargetHallCrane.RSS was downloaded to the module. The crane was tested in local mode and determined to be functioning.

The following links are resources for resolving this issue:
https://isaccontrols.wiki.triumf.ca/index.php/ISAC_Target_Hall_Crane
https://isaccontrols.wiki.triumf.ca/index.php/SHUTDOWN_2015_Tasks#ISAC_Target_Hall_Crane_Controls_DM_-_Completed
  2041   Tuesday, January 07, 2020, 08:02 David WangCoolingStandard Operation  Switch on HALCW MP2

HALCW MP2 is switched on this morning after yesterday cooling tower maintenance. LALCW P5 and P6 pumps are started by isac operator  as well. The system is good so far.

  2042   Tuesday, January 07, 2020, 09:37 David WangITWStandard Operation  5 shielding blocks are moved out of ITW top.

5 shielding blocks are moved out of itw top.

  2043   Wednesday, January 08, 2020, 10:34 David WangAssembly/Bench TestDevelopment  Module lifting assembly ITA0490

The second module lifting assembly ITA0490 is moved into TH and installed onto TM3 . It will stay with TM3. I adjusted the  CofG on the assembly. It is same to the first lifting assembly we are using now. After adjustment, The installation of assembly on TM3 are smooth. 

  2045   Thursday, January 09, 2020, 14:14 David WangConditioning StationStandard OperationTM3 Start of TCS roughing pump for TM3.

I started TCS roughing pump. TM3 TP1 and TP2 will be started tomorrow morning.

ELOG V2.9.2-2455