Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 110 of 138  Not logged in ELOG logo
Entry  Monday, June 27, 2016, 13:45, David Wang, ITE, Standard Operation, , , 5 Shielding blocks have been transferred from ITW to ITE. 

ITE is configured to take proton beam.

Entry  Tuesday, June 28, 2016, 14:42, Travis Cave, Spent Target Vault, Standard Operation, , Many, Spent target assay. Vault_Storage_June_30_2016.pdfMini_Vault_Storage_June_30_2015.pdf

The spent target assay were finally started or re-started today. Four targets were done today.

June 29 2016 another four targets were done today.

June 30 2016 all targets have assayed and measured. see the attached PDFs for the results.

Entry  Thursday, June 30, 2016, 13:33, Dan McDonald, Spent Target Vault, Maintenance, , , F308's 

The five spent target F308  flasks where gone through in accordance with Nordion guidelines, the sixth spare is remains in the Hot Cell area. All flasks where in reasonable shape with two needing weld repairs on the pallets. I replaced all the 3/4" pallet to flask fasteners with new Grade 8 bolts nut and washer combo. Flasks have been moved into the Hot Cell area awaiting movement into the Target Hall.

Entry  Wednesday, July 06, 2016, 07:06, David Wang, Conditioning Station, Standard Operation, , , venting TCS with argon. 

I switched off the vacuum pumps and vented TCS with argon. The TCS will be ready to accept TM2 this afternoon.

Entry  Friday, July 08, 2016, 16:56, Anders Mjos, Conditioning Station, Repair, , , VFD21 OL1 fault on Chiller 

Plant Services group (Tony) will contact a service tech on Monday.

Water system will be switched off over the weekend.

Entry  Monday, July 11, 2016, 10:59, Travis Cave, Spent Target Vault, Standard Operation, , Ta#48, Spent Target move Vault_Storage_July_11_2016.pdf

The spent Ta#48 was moved from the south hot cell to the spent target vault. I was placed in pail 139 and is in spot 6C in the vault. It was 201mSv/hr when measured at the hot cell. See the attached PDF for the latest results.

Entry  Tuesday, July 12, 2016, 12:42, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule for beam schedule 130 (Apr- Sep) Target_Hall_shedule_130_Apr_to_Sep.pdfTarget_Hall_shedule_130_Apr_to_Sep.mpp

Update schedule weekly.Attachment 1,2

    Reply  Thursday, July 14, 2016, 13:25, Anders Mjos, Conditioning Station, Repair, , , VFD21 OL1 fault on Chiller 

Anders Mjos wrote:

Plant Services group (Tony) will contact a service tech on Monday.

Water system will be switched off over the weekend.

Thursday, July 14, 2016, 13:24: Claus from Daikin is on site to troubleshoot.

The VFD driven fan motor has failed. Temporarily blocked air-flow through failed fan to improve air-flow to radiator. A new motor will be ordered (Curtis).

Thursday, July 14, 2016, 15:39: Stopped cooling system for the day


Friday, July 15, 2016, 08:16: Cooling system started

Friday, July 15, 2016, 15:00; Cooling system stopped.

Entry  Tuesday, July 26, 2016, 11:22, chad fisher, South Hot-Cell, Maintenance, , , Soth Hot Cell Waste Storage Vault Tunnel 

The two 45 gal (m) drums of waste removed from the south hot cell in December 2015 and January 2016 were transferred from the north hot cell to the shaft of the east vault tunnel on Monday, July 25th 2016 and subsequently to the east tunnel bunker in the vault tunnel on Tuesday, July 26th, 2016.The first drum (removed from the hot cell in December) containing both activated and contaminated metals was measured at 900 uSv/hr @ .5 m and the second drum (removed from the hot cell in January 2016) containing compressible items such as tank suits and plastic was measured at 150 uSv/hr @ .5 m.

Items were filed for storage/disposal with RPG under item number 1395 on the radioactive storage form.

Drums were transported to the vault tunnel using the 500 Mev Shield Flask (Drawing E-7097) with some minor modifications, namely a 1/4" thick Aluminum plate with four holes that line up with the holes in the bottom flange of the flask. This plate provided a bottom for the flask so that a drum could be contained within the flask during craning. Holes in the plate where countersunk for a 1/2" flat head bolt. Four bolts were also modified to accept 3/16 hair pins. 3 plates with clearances holes for the bolts were also manufactured to act as washers.

Procedure was as follows: With plate, washers and pins installed onto the flask, a modified drum dolly (5" spacers added to the casters) was placed inside the flask. Drum was craned into the flask using the automatic drum lifter. Flask with drum loaded was moved to the Meson Hall loading bay then craned to the B2 level of the Meson hall. Hair pins were pulled from the flask and the flask was then craned up leaving the drum (which was on the dolly firstly installed into the flask) and the plate. Drum on dolly was rolled to vault access shaft where it was craned off the modified dolly using the automatic drum lifter and down the access shaft to the vault tunnel level.  A second drum dolly was waiting at the bottom level and drum lowered onto it. Procedure was repeated for the second drum

Was vault was open , drums were wheeled into the vault tunnel and into a bunker that had been modified to accept these drums. Drums were lifted off dollies and put in place in bunker which had blocks installed to cover the entrance provided for installation.

 

Pictures can be found on docushare http://documents.triumf.ca/docushare/dsweb/View/Collection-18072  (collection 18072)

 

 

Entry  Friday, July 29, 2016, 14:27, Isaac Earle, North Hot-Cell, Development, , , North Hot Cell Measurements & Cleanup 

 The North Hot Cell was accessed today via the Ante Room for inspection, measurements, and clean-up.  There were no modules in the SHC or TCS, and no spent targets in the SHC.  Under these conditions the maximum field in the NHC was approximately 2μSv/hr.  The inside of the cell was cleaned and swept, followed by a floor swipe to check for contamination (none found).  All areas of the ante room floor were also swiped:  no contamination found.

 


The following measurements were taken in the NHC for comparison with the Soldiworks model:

SHC/NHC feedthrough panel fastener size:  1/4"-20,  1/2" long
NHC west wall to east edge of SEG block:  33-1/4" on south side, 33" on north side
NHC west wall to furthest extent of TCS (IRH1170): 40"
NHC west wall to wall indentation for viewing window: 46-7/8"
NHC west wall to end of existing ventilation duct: 4-1/8"

 

Entry  Wednesday, August 03, 2016, 09:15, chad fisher, South Hot-Cell, Repair, , , Manipulator 

East manipulator on the south hot cell is showing signs of eminent wrist/tong cable failure. Some slight slippage was noted yesterday and confirmed by a snapping sound and more slippage tomorrow.

Entry  Wednesday, August 03, 2016, 09:56, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule for beam schedule 130 (Apr- Oct, 2016) Target_Hall_shedule_130_Apr_to_Sep.mppTarget_Hall_shedule_130_Apr_to_Sep.pdf

Update schedule weekly. See attachments 1,2

Entry  Thursday, August 04, 2016, 08:56, Travis Cave, Spent Target Vault, Standard Operation, , UC#16, Spent Target move Vault_Storage_August_3_2016.pdf

The spent UC #16 have been moved from the south hot cell to the storage vault see attached PDF for details.

Entry  Friday, August 05, 2016, 13:50, chad fisher, South Hot-Cell, Maintenance, , , Anteroom clean out 

Some items have been removed from the anteroom in preparation for painting. Items have been placed on plastic in the south hot cell service area. No contamination found so far.

Entry  Friday, August 05, 2016, 14:13, Isaac Earle, North Hot-Cell, Development, , , Preparations for NHC Ventilation Test 

A hole was drilled in the NHC exhaust duct in the east end of the target hall above the hatch to the Ante Room.  This will be used for measuring NHC exhaust flow rate with a thermal anemometer.  The hole was tapped and plugged with an NPT tap.

Flow was measured in the existing hole in the SHC exhaust duct in approximately the same location.  Flow velocity was measured to be 1415 ft/min with the lid on the SHC.  Using duct ID 7.75", and assuming the average flow velocity is 90% of the flow at duct center, the flow rate was found to be 417cfm.  We will attempt to match this figure for the NHC when the ventilation tests are performed.  The tests have been scheduled for the maintenance day on Tuesday August 9th.

The anemometer probe and SHC test port plug were checked for contamination: none found.

Entry  Monday, August 08, 2016, 11:24, chad fisher, South Hot-Cell, Maintenance, , , Anteroom Clean-up - Waveguide 

The wave guide from TM3 has been surveyed, swiped and removed from the anteroom and transported to rad waste for disposal. The wave guide has been stored in the anteroom since its removal.

Entry  Tuesday, August 09, 2016, 11:36, Anders Mjos, Conditioning Station, Maintenance, , , RGA and CG1S moved Old.JPGNew.JPG

 The locations (ports) for the RGA and CG1S was swapped today by Anders and Isaac to provide clearance for the North Hot Cell ventilation. Attached photos show old and new locations.

Entry  Wednesday, August 10, 2016, 12:18, chad fisher, South Hot-Cell, Maintenance, , , Anteroom clearing 

Black "radio active" materials cabinet has been emptied, items bagged and removed from the anteroom. Cabinet itself has been swiped inside and out and also been removed from the anteroom. Most items have been removed from the anteroom now save some cardboard, rolls of plastic etc.

Entry  Wednesday, August 10, 2016, 14:38, Isaac Earle, North Hot-Cell, Development, , , North Hot Cell Ventilation Test Results 

Testing was performed on August 9th on the ISAC nuclear ventilation system to determine if the existing ventilation system can achieve the required cell depressions for both SHC and NHC under all expected configurations and if a proposed modification to the DDC control system can provide acceptable stability and response time for the system.  The proposed control system observes the lower of the SHC depression or the NHC depression + 10% (to avoid stability issues), and adjusts the dampers to try to achieve 250Pa (1.00" WC) depression in the area it is observing.  With the proposed control system the SHC and NHC dampers are programmed to be at the same position, but can be tuned with a bias between them if required to achieve all ventilation requirements. The NHC and SHC dampers are programmed with a limit at 90% of the fully-open position.  There is a damper in the ducting system in the section of duct after the SHC and NHC legs join together;  this is set at 50% open, and was not adjusted during the the tests.  Test summary and results are listed below:

1.  Prior to switching to SHC+NHC control mode, the flow rate and depression of the SHC was measured with the lid on:  266Pa cell depression, damper 47% open, duct flow 417cfm.  The lid was opened and the measurements repeated:  35Pa, damper 90% open, duct flow 630cfm (results in 83ft/min, 0.42m/s average flow velocity across HC module opening)

2. The control system was switched to the new SHC+NHC single control loop system. Measurements were taken with both hot cell lids closed.  SHC:  246Pa, damper 72% open, 350cfm flow rate.  NHC: 257Pa, damper 72% open, 510cfm flow rate.  The ventilation fan speed was then increased from 53Hz to 57Hz (maximum speed is 60Hz).  Measurements were taken with both hot cell lids closed.  SHC:  257Pa, damper 51% open, 353cfm flow rate.  NHC: 257Pa, damper 51% open, 515cfm flow rate.

3. The SHC module port lid was opened and the NHC lid left closed.  SHC: 37Pa, damper 90% open, 462cfm (results in 61ft/min, 0.31m/s average flow velocity across HC module opening).  NHC: 249Pa, damper 90% open, 551cfm.

4. The NHC module port lid was opened and the SHC lid closed.  SHC: 203Pa, damper 90%, 360cfm.  NHC: 33Pa, damper 90%, 648cfm (results in 85ft/min, 0.44m/s average flow velocity across HC module opening).  The fan speed was then increased to 60Hz (max speed) to see if the depression setpoint for the SHC could be achieved in this configuration.  SHC: 231Pa, damper 90%, 389cfm.  NHC: 29Pa, damper 90%, 705cfm (results in 93ft/min, 0.47m/s average flow velocity across HC module opening)

5. Both SHC and NHC module port lids were opened and the fan was left at 60Hz.  SHC: 31Pa, damper 90%, 448cfm (results in 59ft/min, 0.30m/s average flow velocity across HC module opening).  NHC: 29Pa, 90% damper, 669cfm (results in 88ft/min, 0.45m/s average flow velocity across HC module opening)

 

For all tests the control system arrived at a stable depression value in less than 5 minutes, and thereafter exhibited only minor fluctuations.

It was observed that when the fan speed was increased to 57Hz, and for the duration of the tests, there was negligible change in the depression and damper positions for the mass separator room and target pit area.
 
The HEPA filter in the SHC leg of ducting has not been changed since commissioning of the facility (~15 years), and the SHC charcoal filters have not been changed since installation approximately 5 years ago.  The SHC pre-fitler located inside the cell was changed in January 2016.  When these are changed (which should be done before commissioning of the NHC ventilation system), the difference between SHC and NHC flow rates should decrease, and the SHC depression with NHC open should increase (likely up to the 250Pa setpoint).
 
Conclusion: The new SHC+NHC single control loop system effectively controls the system under all conditions tested.  The existing ventilation system achieved the required NHC depression (250Pa, from RS 50, Document #131915) with both cells closed, and with SHC open only.  The same depression for SHC with both cells closed was achieved with both cells closed, but only reached 231Pa w/ NHC open (203Pa at 57Hz fan speed).  It is expected that 250Pa can be easily achieved in the final system because the NHC will be better sealed than in its current condition, the damper in the shared SHC/NHC leg can be opened further, there will be greater flow through the SHC leg after changing the HEPA and charcoal filters, and the system can be tuned to better balance the SHC and NHC flow rates.  RS51 states "the ventilation system should maintain an average air flow velocity of 0.5m/s across the opening into the hot cell".  This is almost achieved with the NHC open, but SHC only had 0.3m/s average flow velocity.  It should be possible to increase both to > 0.5m/s by further opening the shared leg damper and tuning the system to have more balanced flow rates.  At the very least, both SHC and NHC should have > 0.42m/s average flow velocity to match what is currently achieved in SHC only mode (measured in test step #1), which to date has not allowed contamination to escape out the top of the hot cell.  Depending on what flow velocity is deemed acceptable, after commissioning it may be possible to have both the SHC and NHC open concurrently based on the results of Test 5.  At the time of commissioning, the SHC/NHC damper bias and NHC air inlet damper should both be tuned to achieve as similar depression and flow rate conditions as possible for both cells, and to meet all requirements in the RS document.

 

Notes:

Duct flow rate was calculated assuming that measured flow velocity at the center of the duct is 90% of average duct velocity.  The duct ID at the sample location is 7.75", the hot cell opening size used for SHC and NHC module opening flow velocity calculations was 33" x 33".

Duct flow velocity measurements were taken using a thermal anemometer (Model number: 9555-P, Serial number: 9555:1108059 Rev. 2.11.0, Last calibrated by Rob Walker on April 29, 2016).

After completion of the tests the system was restored to it's original configuration and the ISAC target hall was swiped for contamination: none found.  No EF12 trips occurred during these tests.

Entry  Friday, August 12, 2016, 09:58, chad fisher, South Hot-Cell, Maintenance, , , Manipulator Maitenance 

Disassembled the master side of the right manipulator this morning to check the wrist cable. The cable on the master side shows no sign of wear or fraying suggesting that the slave side cable may be the item that is wearing. during disassembly of the master I did notice some loose parts that could have been the source of the audible concern but should not have contributed to the slippage felt in the gripper. I will try and schedule Tuesday for entry into the hot cell to address the slave cable.

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