Tuesday, April 04, 2017, 14:40, David Wang, ITE, Standard Operation, TM4, , TM4 has been connected in ITE
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all turbo-pumps are started. Everything looks fine so far. |
Wednesday, April 05, 2017, 11:57, David Wang, ITE, Maintenance, , , ITE target module flange o-ring repalcement
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ITE target module tank flange o-ring was replaced yesterday before TM4 moving. ITE: IG1S reading looks fine so far. |
Wednesday, April 05, 2017, 14:13, David Wang, Conditioning Station, Maintenance, TM1, , TM1 and TCS vacuum system are connected together
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I started two turbo-pumps on TM1 and one small TP on TCS. They are work fine. |
Thursday, April 06, 2017, 12:33, David Wang, Conditioning Station, Repair, TM1, , TM1 rust inpsection and removal
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TM1 inside service cap surface and shielding plug surface are visually inspected yesterday. No rust has been found. I cleaned all rust on top of TM1
today. Rust on TM1 silo top plate are cleaned as well. |
Thursday, April 06, 2017, 15:11, Grant Minor, Crane, Maintenance, , , Target Hall Crane 20 ton hoist - Report by Gordon Crane 5-Apr-2017
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v\:* {behavior:url(#default#VML);}
o\:* {behavior:url(#default#VML);}
w\:* {behavior:url(#default#VML);}
.shape {behavior:url(#default#VML);}
Normal
0
false
false
false
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Thursday, April 06, 2017, 15:16, Anders Mjos, Conditioning Station, Maintenance, , , Installation of new break out box to accommodate both ITM:MP2 and TCS:MP1
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Installation by Marshall. Dave M from controls adjusted circuitry to get TCS:MP1 to start.
Work is being done in preparation for the Module Move Ventilation SAS project |
Tuesday, April 11, 2017, 14:06, David Wang, Conditioning Station, Standard Operation, TM4, , SHC, TM2 leak check on HS line.
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Chad and I did leak check on TM1 HS line at SHC. 0.0XE-9 atm.cc/sec. No leak. |
Wednesday, April 12, 2017, 07:26, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 and TCS vacuum system has been connected.
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Roughing down overnight. Turbo pumps are started this morning. Everything looks good so far. |
Wednesday, April 12, 2017, 12:51, David Wang, South Hot-Cell, Repair, TM3, , TM3 Ram readings @ SHC
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We have a ram installed on SHC pole which is 0.5 meter to module shielding block surface. the readings we got today during TM3 move:
at containment box center (highest reading): 3.14 msv/hr.
at bottom of shielding blocks: 960 usv/hr. |
Thursday, April 13, 2017, 10:32, chad fisher, South Hot-Cell, Repair, TM3, , TM3 Lower Service Tray Video Inspection
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A video inspection of the lower service tray was performed this morning. Camera was inserted upwards into the service tray/service chase from the containment
box. One potential spark mark was identified as well as epoxy not flush with insulator. Fiberglass does not extend into service tray/chase much and does
not look, from initial inspection that it will be too difficult to remove. |
Thursday, April 13, 2017, 11:33, David Wang, Conditioning Station, Standard Operation, TM2, , Helium pressure test on TM2 water llines at TCS.
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LD BLR :0.0 X E-9 atm.cc/sec. BP:0.0XE-4 torr. helium 70 psi. 3 minutes on each circuit
HS
1.8XE-7 ATM.CC/SEC
TA+
1.4 XE-7
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Thursday, April 13, 2017, 14:16, David Wang, Crane, Repair, , , TH crane: east side main hoist brake assembly is replaced.
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Gordon Crane technician Tom Kauss finished the replacement of the east side main hoist brake assembly. A new set up is installed. he adjusted gap too
close during first time try. So, the smell appeared when operate the brake. He increased the gap to a proper distance then. It looks like everything works
fine now. Still, The brake need to be tested with 10K lBS load on it. We will do the load test on next Thursday when he come here to replace west side |
Wednesday, April 19, 2017, 08:29, David Wang, Conditioning Station, Standard Operation, , , TH schedule 132 update in first beam week 
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Update schedule to show job process in TH. See attachment 1,2. |
Friday, April 21, 2017, 08:19, David Wang, Conditioning Station, Repair, , , Low frequency on TCS TGHT flow sensor.  
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Anders and I found a low frequency issue(13hz only) on TCS TGHT flow sensor when doing TM4 conditioning. By trouble shooting, We found the module water
lines are good. the restriction cause this problem in on TCS supply or return water lines to TGHT. I switched TGHT lines with MSP water lines. The
wheel frequency on TGHT is 67.0hz which is pretty high. Now, MSP is using the original TGHT water line(flow sensor frequency 13hz). Flow sensors and |
Monday, April 24, 2017, 09:52, David Wang, Conditioning Station, Standard Operation, TM2, , Switch off TCS water system and vacuums
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The TCS bias was turn off before that. The TM2 and TCS are still under vacuum now. |
Monday, April 24, 2017, 16:06, David Wang, South Hot-Cell, Repair, TM2, , Crane main hoist strane noise when lifting up TM2
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When lifting up TM2 (20000lbs) this afternoon, TH crane has a strange noise on main hoist. The module was lift up less than 1 feet.when strange
sound was noticed. The module move was stopped right away,and module was lowed back to SHC. The strange noise was confirmed later with SEG
block six inches lifting up. Gordon crane technician will be here to tomorrow morning to investigate the problem. |
Monday, April 24, 2017, 16:11, David Wang, Conditioning Station, Standard Operation, TM2, , TCS TP1s is restarted.
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TCS IG1S is switched on as well. The reason to start the pump is to prepare a possible extended TM2 conditioning at TCS caused by TH crane issue.
TCS:TP1 and TP2 are not switched on for this. |
Tuesday, April 25, 2017, 19:35, Grant Minor, Crane, Repair, , , ISAC Target Hall Crane - West Hoist Brake Rattle
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Normal
0
false
false
false
EN-US
X-NONE
X-NONE
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Wednesday, April 26, 2017, 08:28, chad fisher, South Hot-Cell, Repair, TM3, , TM3 progress and manipulators
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containment box was re-installed onto TM3 on Monday, Left manipulator may be showing signs of eminent handle or tong cable failure. |
Wednesday, April 26, 2017, 10:24, David Wang, ITW, Standard Operation, TM2, , TM2 ITW
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TM2 was moved and connected in ITW yesterday afternoon. After roughing down, ITW turbo pumps are started. ITW TP4 can not be started to full speed. ISAC
ops kept it at low speed mode with less than 1.0A current draw on pump. ITW IG1s shows red as well. I will take a look on them today when beam is off.
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