Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 106 of 138  Not logged in ELOG logo
ID Date Author Category Type Module Target/Numberdown Subject
  1459   Thursday, March 23, 2017, 11:22 Grant MinorCraneMaintenance  Target Hall crane 20 ton hoist noise / smell - inspection by Gordon Crane & Hoist

Strange noise and a burning brake type smell was observed yesterday by David and Anders when running the main 20 ton hoist locally.  A service call was arranged today with Gordon Crane.  No major issues were found.  A more detailed summary is in the attached e-mail correspondence.  Gordon Crane will issue a formal report, but they recommend replacing both sets of brake disks and brake calipers. - Grant

Attachment 1: Target_Hall_crane_main_hoist_problem_-_A_Mjos_-_22_Mar_2017.pdf
Target_Hall_crane_main_hoist_problem_-_A_Mjos_-_22_Mar_2017.pdf
Attachment 2: Update_-_Target_Hall_20T_Hoist_Inspection_-_G_Minor_-_23_Mar_2017.pdf
Update_-_Target_Hall_20T_Hoist_Inspection_-_G_Minor_-_23_Mar_2017.pdf Update_-_Target_Hall_20T_Hoist_Inspection_-_G_Minor_-_23_Mar_2017.pdf Update_-_Target_Hall_20T_Hoist_Inspection_-_G_Minor_-_23_Mar_2017.pdf
Attachment 3: Re__Update__Target_Hall_20T_Hoist_Inspection_-_David_Wang_-_23_mar_2017.pdf
Re__Update__Target_Hall_20T_Hoist_Inspection_-_David_Wang_-_23_mar_2017.pdf Re__Update__Target_Hall_20T_Hoist_Inspection_-_David_Wang_-_23_mar_2017.pdf Re__Update__Target_Hall_20T_Hoist_Inspection_-_David_Wang_-_23_mar_2017.pdf Re__Update__Target_Hall_20T_Hoist_Inspection_-_David_Wang_-_23_mar_2017.pdf
  1460   Thursday, March 23, 2017, 11:42 David WangConditioning StationMaintenanceTM4 TM4 Sevice cap rust are cleaned out.

TM4 service cap rust are cleaned out at TCS. All top surface of TM4 are wiped and cleaned . The module looks good now. see attachments

Attachment 1: TM4_clean_up_at_TCS_006.JPG
TM4_clean_up_at_TCS_006.JPG
Attachment 2: TM4_clean_up_at_TCS_007.JPG
TM4_clean_up_at_TCS_007.JPG
Attachment 3: TM4_clean_up_at_TCS_002.JPG
TM4_clean_up_at_TCS_002.JPG
Attachment 4: TM4_clean_up_at_TCS_008.JPG
TM4_clean_up_at_TCS_008.JPG
Attachment 5: TM4_clean_up_at_TCS_005.JPG
TM4_clean_up_at_TCS_005.JPG
  1461   Friday, March 24, 2017, 11:12 Keith C NgSpent Target VaultStandard Operation  2A window transfer

Transfered the 2A window from the ISAC Storage Vault to the Cyclotron Vault Tunnel Storage area. RPG storage form attached.

Attachment 1: 2017mar24_vault_tunnel_storage_form(1).pdf
2017mar24_vault_tunnel_storage_form(1).pdf
  1464   Monday, March 27, 2017, 06:33 David WangITEStandard Operation  ITE clean up

ITE clean up is done.  HV cage inside is wiped.

  1465   Monday, March 27, 2017, 12:55 David WangSpent Target VaultRepair  S/W silo rust clean up

Rust on S/W silo and cover plate stored at silo area are cleaned up.

Attachment 1: rust_removal_at_sw_silo_001.JPG
rust_removal_at_sw_silo_001.JPG
Attachment 2: rust_removal_at_sw_silo_002.JPG
rust_removal_at_sw_silo_002.JPG
Attachment 3: rust_removal_at_sw_silo_003.JPG
rust_removal_at_sw_silo_003.JPG
Attachment 4: rust_removal_at_sw_silo_004.JPG
rust_removal_at_sw_silo_004.JPG
Attachment 5: rust_removal_at_sw_silo_005.JPG
rust_removal_at_sw_silo_005.JPG
  1471   Wednesday, March 29, 2017, 14:11 David WangConditioning StationStandard OperationTM4 small leak on TM4 Ta(-) water line.

A small leak has been found on TM4 Ta(-) which is marked as "B" on terminal blocks. The LD base Leak rate is 1.2XE-8 atm.cc/sec. 70psi helium has been applied to Ta(-) water line for 3minutes. The leak rate went up to 2.5xE-6 atm.cc/sec and stabilized there. Anders found a helium response on RGA helium reading during the same time. This confirms the leak is real. Other lines are leak checked today also. They are good still. All TM4 water lines were leak checked in ITE in 2017 January. They  were all good at 0.0 X E-9 atm.cc/sec. See attachment e-log.

Attachment 1: TM4_2017_leak_check_in_ITE.png
TM4_2017_leak_check_in_ITE.png
  1472   Thursday, March 30, 2017, 11:21 David WangConditioning StationRepairTM4 Leak check on TM4 Ta(-) water lines in service cap

Leak check on TM4 Ta(-) water lines in service cap is done. LD base LR after 50minutes pumping down:0.0xE-9 atm.cc/sec. base pressure: 0.0XE-4 torr. I sprayed lots helium on welding stems on Ta(-) line in service cap including stems in blue nylon insulator and stems to service tray.  no any response has been foun on LD. The Ta(-) line in service cap is leak free.

 Totally panel open and leak check time is about 12minutes. Argon vented TCS before leak check this morning. 

  1474   Tuesday, April 04, 2017, 10:23 David WangConditioning StationStandard OperationTM4 Helium pressure leak check on TM4 Ta(-) water lines

This morning, The helium pressure leak check on TM4 Ta(-) is done after TM4 finished conditioning yesterday.  LD base LR:8.0XE-9 atm.cc/sec, base pressure: 0.0XE-4 torr. Applied 70 psi helium to TM4 TA(-) water line. The LR slowly climbed to 2.2XE-7 atm.cc/sec, and stopped there. Waited for 5 minutes and change at 2.2 X E-7 atm.cc/sec.

  1475   Tuesday, April 04, 2017, 10:24 David WangConditioning StationStandard OperationTM4 Stopped TCS pumps this morning

 Argon vented TCS and TM4 after pumps are stopped.

  1476   Tuesday, April 04, 2017, 14:39 David WangCraneStandard Operation  Crane check main hoist on jogging with shielding plug lifted.

Today, I checked TH crane main hoist  when shielding plug is installed into ITE pit. I did  some jogging actions on main hoist during the operation. Everything looks fine. No burning smell, no strange noise. An outside crane expert suggest that jogging is the worst working situation for crane. We have to use jogging actions during our crane operation. But, we could try to use less jogging when operate the crane.

  1477   Tuesday, April 04, 2017, 14:40 David WangITEStandard OperationTM4 TM4 has been connected in ITE

all turbo-pumps are started. Everything looks fine so far.

  1479   Wednesday, April 05, 2017, 11:57 David WangITEMaintenance  ITE target module flange o-ring repalcement

ITE target module tank flange o-ring was replaced yesterday before TM4 moving. ITE: IG1S reading looks fine so far. 

  1480   Wednesday, April 05, 2017, 14:13 David WangConditioning StationMaintenanceTM1 TM1 and TCS vacuum system are connected together

I started two turbo-pumps on TM1 and one small TP on TCS. They are work fine. 

  1481   Thursday, April 06, 2017, 12:33 David WangConditioning StationRepairTM1 TM1 rust inpsection and removal

TM1 inside service cap surface and shielding plug surface are visually inspected yesterday. No rust has been found. I cleaned all rust on top of TM1  today.  Rust on TM1 silo  top plate are cleaned as well.

  1482   Thursday, April 06, 2017, 15:11 Grant MinorCraneMaintenance  Target Hall Crane 20 ton hoist - Report by Gordon Crane 5-Apr-2017

-------- Forwarded Message --------

Subject:

ISAC Hoist Brake Repair

Date:

Wed, 05 Apr 2017 20:42:49 -0700

From:

Aidan C. Gordon <aidan@gordoncrane.com>

To:

Curtis Ballard <ballard@triumf.ca>, Neil Wong <nwong@triumf.ca>

CC:

Peter Neumann <peter@gordoncrane.com>, Shelley Cherkowski <Shelley@gordoncrane.com>

 

Hi Curtis

 

Further to the emergency service call at the Isac Target Hall on Thursday March 23rd, we advise as follows:

 

It was reported that the hoist was making an unusual noise and that there was a strong brake odour during operation.

The lift was completed using the auxiliary hoist.

 

A man-lift was arranged and Senior Service Technician Tom Kauss attended site the next morning to troubleshoot.

He determined that one of two hoist brakes (walkway side) had a strong odour and on closer examination it appeared that the 

brake lining material was breaking down and particulate lining material was getting caught between the lining and the discs.

These lining fragments were rubbing and burning off during the hoist operation.

The end cover of the brake had an accumulation of brake lining fragments 

The lining was not overly worn, but appears to be becoming friable, perhaps with age or exposure to radiation.

 

The brake was cleaned with compressed air to remove the friable material and thoroughly tested. 

A test load of approximately 10 tons was lifted and the hoist handled the load without issue

The brake fragment issue did not recur while we on site and the hoist was recommissioned for use.

 

To guard against the likely recurrence of this condition on this critical application crane, and as both brakes have seen identical conditions in operation, 

we recommend that both brake assemblies be replaced.

The brake assembly would include the brake coil, friction discs, steel brake discs and the brake springs

TRIUMF does not have a spare brake on hand, therefore one of the removed brakes could be rebuilt and kept on hand. 

 

Two (2) each  XL-60009637 Complete Brake Assemblies   $ 5,706.00  Each

 

One (1) only XL-60009674 Brake Repair Kit $ 2,435.00

            For Rebuild

 

One (1) only XL-52272125 Brake Spring Kit $     59.72 For Rebuild

Installation & Testing of New Brakes estimated at: $ 1,250.00 Lot

We have one brake in stock in our Vancouver Service Depot. A second brake is available Ex-Ontario

FOB Site

Applicable Taxes Extra

Quote Valid for 30 days, subject to prior sale.

 

We are available next week to perform this work on site.

Please let us know if you have any questions or if you would like us to proceed.

 

Best Regards

          Aidan

 

------------------

Aidan C. Gordon

General Manager

aidan@gordoncrane.com

Gordon Crane & Hoist Inc.

Celebrating 34 years of Excellence (1983-2017)


www.gordoncrane.com

Toll Free 1-866-HOIST-IT

              (1-866-464-7848)

Tel:  (604) 324-2441

105-8475 Ontario St

Vancouver BC  V5X 3E8


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  1483   Thursday, April 06, 2017, 15:16 Anders MjosConditioning StationMaintenance  Installation of new break out box to accommodate both ITM:MP2 and TCS:MP1

Installation by Marshall. Dave M from controls adjusted circuitry to get TCS:MP1 to start.

Work is being done in preparation for the Module Move Ventilation SAS project

  1488   Tuesday, April 11, 2017, 14:06 David WangConditioning StationStandard OperationTM4 SHC, TM2 leak check on HS line.

Chad and I did leak check on TM1 HS line at SHC. 0.0XE-9 atm.cc/sec.  No leak.

  1489   Wednesday, April 12, 2017, 07:26 David WangConditioning StationStandard OperationTM2 TM2 and TCS vacuum system has been connected.

Roughing down overnight. Turbo pumps are started this morning. Everything looks good so far.

  1491   Wednesday, April 12, 2017, 12:51 David WangSouth Hot-CellRepairTM3 TM3 Ram readings @ SHC

 We have a ram installed on SHC pole which is 0.5 meter to  module shielding block surface. the readings we got today during TM3 move:
at containment box center (highest reading): 3.14 msv/hr.
at bottom  of shielding blocks: 960 usv/hr.
at 1/4  of  shielding blocks height from  bottom :700usv/hr.
at 1/2 of shielding blocks height from bottom: 340usv/hr.
at 3/4 of shielding blocks height from bottom:140u/sv/hr.
   The Ram is behind the pole and measured the surface which is 90 degree right side of that opened service tray side. 

  1494   Thursday, April 13, 2017, 10:32 chad fisherSouth Hot-CellRepairTM3 TM3 Lower Service Tray Video Inspection

A video inspection of the lower service tray was performed this morning. Camera was inserted upwards into the service tray/service chase from the containment box. One potential spark mark was identified as well as epoxy not flush with insulator. Fiberglass does not extend into service tray/chase much and does not look, from initial inspection that it will be too difficult to remove.

Video can be found in docushare Document-142295

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