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ID |
Date |
Author |
Category |
Type |
Module |
Target/Number |
Subject |
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823
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Monday, December 15, 2014, 15:55 |
Grant Minor | Conditioning Station | Repair | | | Access to ISAC TCS TK2 Expansion Tank - Fall Arrest |
Hello all,
Access was required this morning to the TCS TK2 Expansion Tank to open a valve and re-fill the tank.
As the access path to this tank lacked any form of Fall Protection, Fall Arrest was employed.
Worksafe BC Part 11 Section 11.2 requires fall protection to be employed at elevations greater than 3 meters. The expansion tank is located at an elevation far exceeding this regulation.
http://www2.worksafebc.com/publications/ohsregulation/part11.asp
The worker, Allon Messenberg, was fitted with a harness, personal self-retracting lifeline / lanyard with shock-pack, and carried two steel rope ring-ended slings with him to tie off to the structural beams overhead. All products used were DBI-Sala safety products, which are kept in the Remote Handling machine shop Fall Protection Equipment lockers. Several RH group members have keys to this locker, including me.
Three configurations were required to gain access to the tank (photo attached):
Configuration 1: Traversing the section between the 2nd floor offices and the ventilation duct.
Configuration 2: Traversing the section between the ventilation duct and the "cross point" of the structural beams.
Configuration 3: Tied-off to the "cross point" of the structural beams and working within the reach limits of the personal SRL and shock-pack.
Transitions between the three configurations required brief moments of un-clipping from the harnesses. This will be solved in the future via the use of additional carabiners and lanyards.
Operations has advised me that they have observed either TRIUMF workers or contractors working in this area without wearing Fall Arrest equipment. My request is for staff and operations to stay vigilant in observing access to this area.
Any work performed in this area without the usage of fall arrest must be reported in an NCR.
I welcome any comments from those who have ideas for improving the safe method of access to this tank.
The cooling package is described in the TCS operating manual, Document-103881. Page 8 states clearly that Fall Arrest is required to access this valve.
Regards,
Grant |
Attachment 1: TK2_Expansion_Tank_Elevation_ISAC1_Exp_Hall_15Dec2014.JPG
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Attachment 2: TK2_Expansion_Tank_-_Fall_Arrest_Config_1_-_15Dec2014.JPG
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Attachment 3: TK2_Expansion_Tank_-_Fall_Arrest_Config_2_-_15Dec2014.JPG
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Attachment 4: TK2_Expansion_Tank_-_Fall_Arrest_Config_3_-_15Dec2014.JPG
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831
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Thursday, January 08, 2015, 10:34 |
chad fisher | South Hot-Cell | Standard Operation | | | TM2 Tray Build Status and Problems |
Final assembly of the source tray for TM2 was started this morning.
Sliding tray was received from keensert installation and cleaned.
Mounting plate/ionizer tube location jig was rechecked against assembly ITA3136...Mounting plate was loosened, jigs for centering the ceramic shields installed and fasteners re-torqued to 57 in lbs.
Upon attempted assemble of ITA3536 and 3537 (support frames) it was noticed that the countersinks were not deep enough...the heads of the screws protrude and would interfere with/damage the support insulators. These items have been given to Dan to have the counterbores adjusted...drawing should be changed to insure a small gap.
Also, one of the support frames has marks on its side that may be a high voltage issue.
Upon inspection of the components in question (ITA3540 & 3538) it was found that they have been made to spec and model; however the spec& model does not allow for adequate theoretical clearance given tolerances. Countersinks will be adjusted and changes documented.
"Pitting" will attempt to be lapped.
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Attachment 1: TM2_Tray_20150108_09.jpg
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Attachment 2: TM2_Tray_20150108_10.jpg
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Attachment 3: TM2_Tray_20150108_11.jpg
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Attachment 4: TM2_Tray_20150108_12.jpg
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840
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Friday, February 06, 2015, 08:06 |
David Wang | Crane | Repair | | | TH crane lost movement controls since last Friday. |
Last Friday, During the crane per use check, I found the main power supply to to crane was shut off. I was told Don and Travis shut off the main power before Triumf power outage. Travis restored crane main power and I could turn on the main relay on radio pedant in TH. But, I didnt have all crane main bridge movement controls on TH raido pedant except rotation. I still have all movement controls on small trolley from the radio pedant. When I operated radio pedant, Travis could hear the relay works in crane control room, but in TH no crane movements. It looks like a crane control problem so Dave Morris was contacted. Dave found one of battery on PLC board is dead and need to be replaced.He did order the battery right way. On this Wednesday, Dave noticed us we could temporarily run the crane. I went to T.H for checking. At the beginning, I found I cant not turn on the crane main relay from radio pedant in TH. Don was in crane control room. He switched the crane control from TH radio mode to control room pedant( big yellow control box laid on the ground, the mode switch is located on the up left corner of first main panel) and he turned on the main relay by doing this and got all movement controls from the big yellow pedant. After switching the mode back to TH radio mode I also got all the controls from TH radio pedant. Everything worked fine on crane so we moved the man lift into TH on Wednesday afternoon and arranged the TH crane inspection on Thursday. On Thursday morning, Gordon Crane guys came in TH and started their inspection. At the beginning, everything works fine. But after they did some operation and checks on crane, the crane main relay could not be switched on again (from TH raid box). The crane inspection job are suspended. RH group tried to active the main relay by switching the mode back to yellow pedant in crane control room just like we did on Wedsday, but it did not work this time. David Morris was contacted to check from his side if anything wrong. He checked and told us the program is working and everything is good from his side. A crane expert is needed to trouble shoot this problem. Neil Wong is going to bring Gordon crane guys and start to trouble shoot the problem this morning. |
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841
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Friday, February 06, 2015, 12:27 |
David Wang | Crane | Repair | | | TH crane troubleshoot |
Gordon crane technician started TH crane trouble shooting this morning. The problem is found that there is no 115VAC power supply to energize a main coil which is used to switch on 450V AC power supply to crane. He did a test and found the crane could be operated by big yellow pedant in control room when he manually gave the coil 115VAC power supply to energize it.. At that moment, the crane is set to big yellow pedant operating mode. But, he can not figure out why there is no 115VAC power to this coil.The wiring tracking back is not an easy job for him. The troubleshooting is stopped now. The job will be resumed on next week with more skilled technician involving in from Gordon crane. |
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842
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Wednesday, February 11, 2015, 13:13 |
chad fisher | South Hot-Cell | Maintenance | | | New gas bottle storage rack |
The new gas bottle storage rack has been installed by/for the south hot cell.
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Attachment 1: 20150211_115656.jpg
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844
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Monday, February 16, 2015, 11:57 |
David Wang | Crane | Repair | | | TH crane |
Dave.Morris installed a new battery on crane control PLC board and uploaded the program. Travis, Dan and I tested the crane in local, remote, and test mode. The crane works fine. Also, the TH lock up has been tested. Everything is good. |
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845
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Tuesday, February 17, 2015, 13:06 |
Anders Mjos | ITE | Development | | | Resistance measured of TGHT and TBHT lines to ITE |
The copper bars was installed by David and Anders. After the measurements were completed, the copper bars were removed.
See photo and attached spread sheet. |
Attachment 1: 002.JPG
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Attachment 2: Resistance_from_Electrical_Room_to_Target_Station.xlsx
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846
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Tuesday, February 17, 2015, 13:07 |
Anders Mjos | ITW | Development | | | Resistance measured of TGHT and TBHT lines to ITW |
See e-log entry for ITE for details. The copper bars have not been removed. They can be used for testing the new power supplies.
Local measurement was done by Ray with a voltmeter. The voltmeter was consistent with EPICS readback and local readback on the power supplies. A voltage drop of 0.137 V @ 580 A was measured across the bus bar from the TGHT power supply to the cooled transmission lines. |
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847
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Monday, February 23, 2015, 12:28 |
David Wang | ITE | Maintenance | | | 2015 shut down coils and pedal wheels replacement on ITE water flow sensors. |
Dan and I replaced pedal wheels and coils on ITE water flow sensors. It is a shut down job we did every two years. See attachment for detail. |
Attachment 1: 2015_shut_down_ITE_water_sensors__replacements.pdf
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848
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Wednesday, February 25, 2015, 10:44 |
David Wang | ITW | Maintenance | | | 2015 shut dwon ITW water sensor coils and pedal wheels replacement |
Dan and I replaced pedal wheels and coils on ITW water flow sensors. It is a shut down job we did every two years. See attachment for detail. |
Attachment 1: 2015_shut_down_ITW_water_sensors__replacements.pdf
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849
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Thursday, February 26, 2015, 09:22 |
David Wang | ITW | Standard Operation | | | TH Shut Down Activities Schedule Feb 23th- Mar 25th |
TH shut down activities schedule from Feb 23th-March 25th. The schedule will be updated each week. See attachment 1.
Feb-27-2015: Updated the schedule, and uploaded as PDF file. See attachment 2. |
Attachment 1: Target_Hall_shut_down_activities.mpp
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Attachment 2: Target_Hall_shut_down_activities.pdf
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850
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Friday, February 27, 2015, 09:34 |
chad fisher | South Hot-Cell | Maintenance | | | Hot cell Entry February 25 2015 |
See attached report.
Summary:
Radio problems just before entry to cell. Inspection afterwards revealed batteries charge but battery in one radio shorts out after a couple loads/cycles.
Fields in hot cell range from 630 uSv/h @ 1 m to 1.5mSv/h @ 1m. Contributing to the fields is the febiad coil line removed from TM4 in the south west corner of the hot cell.
Contamination/particulate on table as mostly black colored and of a fairly substantial size, but seamingly easy to collect. Distinquishable pieces of target material present.
Hot cell window show no sign of leaking on the inside of cell.
Pre-filter changed.
Manipulators lubricated.
Hot cell entry procedures appear to still be fairly successful in minimizing contamination migration from the hot cell.
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Attachment 1: ISAC_South_Hot_Cell_Entry.pdf
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853
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Thursday, March 05, 2015, 07:17 |
David Wang | ITW | Standard Operation | | | TH Shut Down Activities Schedule Feb 23th- Apr 15th update |
TH shut down jobs are processing as scheduled this week. Discussed with Don, and we think the jobs scheduled in next week should be processed as we planned. See attachments for updated schedule.
I updated the schedule today. See attachment 3, 4 for updating. 2015-Mar-10.
2013-Mar -13, I updated the schedule to show the jobs we finished this week. See attachment 5,6 |
Attachment 1: Target_Hall_shut_down_activities.pdf
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Attachment 2: Target_Hall_shut_down_activities.mpp
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Attachment 3: Target_Hall_shut_down_activities.pdf
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Attachment 4: Target_Hall_shut_down_activities.mpp
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Attachment 5: Target_Hall_shut_down_activities.pdf
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Attachment 6: Target_Hall_shut_down_activities.mpp
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854
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Thursday, March 05, 2015, 14:30 |
chad fisher | South Hot-Cell | Development | | | Dissection Box |
Box for dissecting targets almost complete. Should be done tomorrow. |
Attachment 1: 20150305_142144.jpg
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855
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Monday, March 09, 2015, 09:42 |
chad fisher | South Hot-Cell | Development | | | Hot Cell Table Swiping |
3 swipes of the south hot cell table were taken from the target hall through the roof hatch (2 standard, 1 alpha).
Initial results of the table swipes are pending however swipes of the pool tool and end effector are clean, 0 counts, booties, gloves clean.
Fall arrest equipment has a puzzling 6000 counts, and suit 500 counts.
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861
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Friday, March 13, 2015, 13:36 |
Travis Cave | Spent Target Vault | Standard Operation | | ThO#1 | Spent Target Move |
The ThO#1 has been placed in the storage vault placed in pail #122 in spot 2B of the vault. It was 6.2mSv/hr upon removal from the south hot cell. see attached PDF for details. |
Attachment 1: Storage_Vault_March_13_2015.pdf
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864
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Tuesday, March 17, 2015, 10:33 |
Travis Cave | Spent Target Vault | Standard Operation | | UC#11 | Spent Target Move |
The spent UC#11 has benn moved from the south hot cell to the spent target vault. See attached PDF for details. |
Attachment 1: Vault_Storage_March_17_2015.pdf
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865
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Friday, March 20, 2015, 13:37 |
chad fisher | South Hot-Cell | Development | | | TM2 Optics Tray |
Final assembly and alignment of TM2 optics tray continued today. Front section is "aligned". |
Attachment 1: 20150320_113132[2].jpg
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Attachment 2: 20150320_113018_1[1].jpg
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866
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Monday, March 23, 2015, 07:56 |
David Wang | ITE | Standard Operation | | | TH Shut Down Activities Schedule Feb 23th- Apr 15th update |
This schedule is following Dons schedule on module moves. See attachments for updating.
2015-03-27: Weekly update the schedule. The shut down job is close to the end. See attachment 3, 4. |
Attachment 1: Target_Hall_shut_down_activities.pdf
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Attachment 2: Target_Hall_shut_down_activities.mpp
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Attachment 3: Target_Hall_shut_down_activities.pdf
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Attachment 4: Target_Hall_shut_down_activities.mpp
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867
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Monday, March 23, 2015, 14:03 |
chad fisher | South Hot-Cell | Standard Operation | | Ta#45 | Ta#45 inserted into hot cell |
Ta#45 has been inserted into the hot cell. Swipe taken of inner tool port area: 100000 counts/min. |