Wednesday, May 21, 2014, 13:56, Travis Cave, Spent Target Vault, Standard Operation, , , Spent target assay
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All targets in the vault have been assayed and measured. Results will be posted soon.
Results of assay are now attached in a new layout. |
Wednesday, May 21, 2014, 13:56, Travis Cave, Spent Target Vault, Standard Operation, , , Spent target assay
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All targets in the vault have been assayed and measured. Results will be posted soon. |
Thursday, May 15, 2014, 14:38, David Wang, ITE, Repair, TM3, TM3, Bias short on ITE
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Anders and I opened the HV cover in ITE and did a visual check inside ITE HV cover and top of TM3.Bill was with us and took the pictures. There was nothing obviously wrong when we opened the HV cover in ITE. We disconnected TM3 high current cables from ITE. Then we did an electrical check on TM3.The TM3 was good and passed megga test (465Mohm at 500V). The module was good and was separated electrically from the ITE at that moment. Then, we went back to electrical room and measured the resistance between bias and ground with ground bar opened and power supply disconnect. It was still shorted at that moment .We thought the short is located inside HV chase between electrical room and ITE. Then, we went back to ITE again and reconnected TM3 back to ITE. We wiped two blue nylon insulators between bias and ground, and no obviously spark track or dirty on them. We put HV cover back in ITE locked area, and went back to electrical room again.We decided to do a final electrical check there. We thought the short should be still there and we just want to confirm it . But this time the short is gone. Everything goes back to normal. The short disappeared and We test bias to 5KV and the current looks normal now. |
Wednesday, May 14, 2014, 19:01, Grant Minor, ITE, Maintenance, TM3, , HV short inspection at ITE
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Friedhelm Ames commented to me that there appears to be a short between High Voltage and Ground at TM3 at ITE.
Friedhelm, Anders and I initiated a survey by Andrew from RPG, and entered the Target Hall at approximately 5pm to visually assess the HV cover at the MAA. There was no clear indication of a problem. We opted to wait for David to return as we weren't sure exactly what we were looking for.
Friedhelm and Anders confirmed in the Electrical Room that the short is in the Target Hall. |
Wednesday, May 07, 2014, 10:15, David Wang, ITE, Repair, TM3, , ITE TM3, entrance module and BL2A3 window flange seals leak check..
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ITE TM3, entrance module, and 2A3 window flange seals have been leak checked this morning after 2 new seals replacement.The LD base leak rate was 0.0xE-9 atm.cc/sec, base pressure was 0.0 XE-4 Torr. I sprayed lots helium around the TM3, entrance module and 2A3 flange seals. No any response had been found on LD during the spraying. All three flanges are sealed perfectly now. |
Wednesday, May 07, 2014, 10:08, David Wang, ITE, Repair, TM3, , ITE entrance module flange seal had been replaced. 7x
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ITE entrance module flange seal had been replaced yesterday.The flange and the seal groove were cleaned with Acetone before the new seal is installed. See pictures |
Tuesday, May 06, 2014, 14:05, Travis Cave, ITE, Standard Operation, , , module move
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The entrance module was out a new seal went in and then the entrance module went back, and then TM#3 went back. So all modules are now back in place in the east target station. |
Monday, May 05, 2014, 13:11, David Wang, ITE, Repair, TM3, , ITE Entrance module has been disconnected.
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ITE entrance module has been disconnected and the lifting yoke is installed for module move. See attached pictures. |
Monday, May 05, 2014, 13:05, David Wang, ITE, Repair, TM3, , ITE target module flange seal has been replaced.
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ITE target module flange seal has been replaced.The flan surface and the o-ring groove have been cleaned with Acetone before the new seal is installed. See attached picture. |
Monday, May 05, 2014, 10:40, Travis Cave, ITE, Standard Operation, TM3, TiC#4, module move
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TM#3 with TiC#4 has been moved from the east station to the south west silo. |
Wednesday, April 16, 2014, 17:08, Keith C Ng, ITE, Repair, , , 2a3 window - He leak check
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Helium leak checked 2a3 window after installing using remote line:
- There was a leak found between the target and entrance module at the target pit, rate of 9E-6 atm-cc/sec.
- One test performed with the remote helium line to the window. There was a response but the leak detector was located above the window access channel, drift cannot be ruled out.
- 3 more tests performed with vacuum group, with leak detector relocated farther away from ITE and isolated with plastic. 2 tests using remote line had no response. One test done with a wand through 2a3 wall penetration had a response of 3.2E-9 atm-cc/sec (not using remote line).
Vacuum group (D. Yosifov) comments that due to the much larger leak at the top of the tank he cannot say with confidence the response seen is a leak at the window (due to leak at top) but if there is, a tolerable leak rate. |
Friday, April 04, 2014, 16:59, Anders Mjos, ITW, Development, , , Flow meters installed on Heat Shield and Coil water return
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David W. has installed two SST Proteus flow meters, model OV7006FTA32, on ITW Heat Shield and Coil. The flow meters are connected to a power supply and a data logger in the electrical room.
The Heat Shield flow meter has SN 00278112 and is on the Black wire pairs and connected to CH3 & CH4 on the logger.
The Coil flow meter has SN 00278113 and is on the Green wire pairs and connected to CH1 & CH2 on the logger.
The first channel (CH1, CH3) is temperature in degrees Celcius and the second channel (CH2, CH4) is flow rate in liters per minute.
A camera has been placed on the logger.
Flow rates today (2014-04-04):
HS 8.2 - 8.3 lpm
COIL 8.0 - 8.1 lpm
Calibration sheets
UPDATE 2014-04-11: Corrected HS to CH3 & CH4. |
Wednesday, April 16, 2014, 10:16, Anders Mjos, ITW, Development, TM3, Ta#42, Flow meters installed on Heat Shield and Coil water return
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Anders Mjos wrote: |
David W. has installed two SST Proteus flow meters, model OV7006FTA32, on ITW Heat Shield and Coil. The flow meters are connected to a power supply and a data logger in the electrical room.
The Heat Shield flow meter has SN 00278112 and is on the Black wire pairs and connected to CH3 & CH4 on the logger.
The Coil flow meter has SN 00278113 and is on the Green wire pairs and connected to CH1 & CH2 on the logger.
The first channel (CH1, CH3) is temperature in degrees Celcius and the second channel (CH2, CH4) is flow rate in liters per minute.
A camera has been placed on the logger.
Flow rates today (2014-04-04):
HS 8.2 - 8.3 lpm
COIL 8.0 - 8.1 lpm
Calibration sheets
UPDATE 2014-04-11: Corrected HS to CH3 & CH4.
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PDFs of temperature and flow traces are available on DocuShare
Monday, April 28, 2014, 09:27. p+ off since 8:20
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Temp [C] |
Flow [lpm] |
HS |
28.3 |
8.38 |
COIL |
26.3 |
8.01 |
Tuesday, April 29, 2014, 09:28: p+ 30 uA
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Temp [C] |
Flow [lpm] |
HS |
31.7 |
8.40 |
COIL |
27.6 |
8.13 |
Monday, May 05, 2014, 10:49: p+ off since 8:39
(Downloaded data and updated traces on DocuShare)
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Temp [C] |
Flow [lpm] |
HS |
27.1 |
8.47 |
COIL |
26.6 |
8.11 |
Wednesday, May 14, 2014
(Downloaded data and updated traces on DocuShare)
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Temp [C] |
Flow [lpm] |
HS |
33.5 |
7.7 |
COIL |
29.0 |
7.5 |
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Tuesday, April 15, 2014, 08:53, Travis Cave, ITE, Standard Operation, TM3, TiC#4, module move
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TM#3 with TiC#4 has been moved from the conditioning station to the east target station. |
Monday, April 14, 2014, 13:58, David Wang, ITE, Repair, , , Reconnected ITE entrance module
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I reconnected the entrance module back to the ITE station. All diagnostic cables, turbo- pump, air lines, water lines on ITE entrance module and BL2A3 window are connected back. |
Monday, April 14, 2014, 11:57, Travis Cave, ITE, Standard Operation, , , entrance module move
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The East Entrance module has been moved from the south west silo to the east target station. The move went well. |
Friday, April 11, 2014, 18:17, Keith C Ng, ITE, Repair, , , 2a3 window - install
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Today:
1) Installed new cradle and shortened beam pipe section in wall penetration.
- Removed tank dust cover from flange and cleaned
- Held flange faces together from 2A tunnel side to check alignment, slightly biased to the East axially and a small gap present in the top when resting
2) Prepared new 2A window
- Connected preswaged (1/2 turn) swagelok nuts to the existing copper lines in the target hall, 1/4 turn from finger tight, 3/4 turns total
- Leak checked cooling lines with pressurized air at 75psi and snoop, no leaks were found at the joint
- Grooves were cleaned and helicoflex delta seals were installed with vacuum grease used in the periphery to hold ring in window, applied at 6 points every 60deg
3) Window installation
- Lowered window into position by cooling lines
- Window located into tank flange first then slid beam pipe towards it, capturing the window with seals
- Lowered clamp into place in hole
4) Clamp installation
- Lowered clamp into access hole and started closing clamp with steel RH drive bar
- torqued to 50 ft-lbs collar gap was still ~8"
- Increased torque to 60 ft-lbs then 70 ft-lbs stopped closing of clamp when the displacement did not change between the stop ring and clamp yoke
- It was decided not to continue to close this clamp, more assessment may be necessary
6) We will attempt to pump on the seal in its current configuration, tools have been removed. |
Friday, April 11, 2014, 11:35, David Wang, Conditioning Station, Standard Operation, TM3, , Helium pressure test on TM3 HS water line with new Ta target. at CS 6x
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The helium pressure test on TM3 HS water line with new Ta target is finished at CS. The circuit is leak tight.. No any response on LD. See pictures. |
Thursday, April 10, 2014, 14:03, Bevan Moss, Conditioning Station, Standard Operation, TM3, TiC#4, HV conditioning
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The TiC#4 target that is on TM3 was conditioned to 25kV today with the EINZEL lens at 12.5kV. There was one spark shortly after reaching 25kV that reset the bias PS and another one after the module sat at 25kV for ~30 minutes. Attached is the strip tool data and screen shot. Prior to starting the conditioning the power on the chiller needed to by cycled as the VFD on the fans had tripped due to a recurring inrush problem. |
Wednesday, April 09, 2014, 11:10, David Wang, South Hot-Cell, Standard Operation, TM3, , TM3 heat shield circuit leack check at SHC
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This Monday morning, Chad and I leak checked heat shielding circuit on TM3 with new target installed. The base LR on LD :0.0xE-9 atm.cc/sec, base pressure 0.0xE-4 torr. Chad sprayed helium twice on the VCR joints. No leak has been found. The circuit will be pressured with helium at CS. |
Tuesday, April 08, 2014, 09:05, Travis Cave, South Hot-Cell, Standard Operation, TM3, TiC#4, module move
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TM#3 with TiC#4 has been moved from the south hot cell to the conditioning station. |
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