Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 101 of 138  Not logged in ELOG logo
  ID Date Author Category Type Moduledown Target/Number Subject
  390   Thursday, June 27, 2013, 14:27 chad fisherSouth Hot-CellDevelopment  Polishing Cleaning tool - Water blocks

The polishing/cleaning tool prototype is now finished and appers to work great.

Thanks to Dan and Maico for the great job making my design a reality.

Attachment 1: 20130626_144941.jpg
20130626_144941.jpg
  393   Wednesday, July 03, 2013, 08:43 chad fisherSouth Hot-CellStandard Operation  Ta#39 Transfered to spent target storage vault
  394   Wednesday, July 03, 2013, 08:44 chad fisher, Travis CaveSouth Hot-CellStandard Operation  Ta#39 Transfered to spent target storage vault

Ta#39 has been transferred to spent target storage vault. Ta#39 was placed into pail #106 and placed into spot of 4C of the spent target vault. The pail measured 95.8mSv/hr upon removal from the hot cell. See attached PDF for details.

Attachment 1: Vault_Storage_July_3_2013.pdf
Vault_Storage_July_3_2013.pdf Vault_Storage_July_3_2013.pdf Vault_Storage_July_3_2013.pdf Vault_Storage_July_3_2013.pdf
  412   Friday, July 26, 2013, 11:06 David WangSouth Hot-CellStandard Operation  The steel shielding plug has been put on theSHC top in target hall

to reduce the radioactive shining from  SHC Ta# 40 target.

  413   Monday, July 29, 2013, 14:32 Travis CaveSpent Target VaultStandard Operation Ta#40Spent target move

Spent target Ta#40 has been placed into storage. The target was placed in pail #107 and was put into slot 5A of the vault. It had a field of 224mSv/hr upon removal from the south hot cell. See attached PDF for more details.

Attachment 1: Vault_Storage_July_29_2013.pdf
Vault_Storage_July_29_2013.pdf Vault_Storage_July_29_2013.pdf Vault_Storage_July_29_2013.pdf Vault_Storage_July_29_2013.pdf
  416   Wednesday, July 31, 2013, 11:13 Travis CaveSpent Target VaultStandard Operation  Spent target move

Five spent targets have been removed from the storage vault and placed into the mini storage. The target placed into the mini storage are UO#3, UC#'s  3,4,5 and SIC#23. See attached PDFs for vault details.

Attachment 1: Vault_Storage_July_31_2013.pdf
Vault_Storage_July_31_2013.pdf Vault_Storage_July_31_2013.pdf Vault_Storage_July_31_2013.pdf Vault_Storage_July_31_2013.pdf
Attachment 2: Mini_Vault_Storage_July_31_2013.pdf
Mini_Vault_Storage_July_31_2013.pdf Mini_Vault_Storage_July_31_2013.pdf Mini_Vault_Storage_July_31_2013.pdf Mini_Vault_Storage_July_31_2013.pdf
  417   Wednesday, August 07, 2013, 06:47 maicodallavalleSpent Target VaultMaintenance  F-308

All the F-308's have been torqued up  and the locks installed. Ready to be moved.

  432   Wednesday, August 28, 2013, 14:17 Travis CaveSouth Hot-CellStandard Operation UC#6Spent target move

Spent target move, UC#6 has been moved from the south hot cell to the target storage. The target is in pail 108 and in slot 8C of the vault. See attached PDF for details.

Attachment 1: Vault_Storage_August_28_2013.pdf
Vault_Storage_August_28_2013.pdf Vault_Storage_August_28_2013.pdf Vault_Storage_August_28_2013.pdf Vault_Storage_August_28_2013.pdf
  462   Tuesday, September 24, 2013, 14:46 Bevan MossSouth Hot-CellRepair  Right manipulator repair

 The right manipulator A-9885 Handle Cable Assembly has been repaired by Maico and myself. We repaired the manipulator following some verbal instructions from Chad on the modified repair strategy. This allows the repair to be completed without going into the hot cell. The instructions in the repair manual are very vague and can actually cause problems. For example it is best to pin the manipulator before completing any work. Other than that the work went smoothly with the exception that the counter weight hangs up on the manipulator occasionally and can cause the cable to come off of the pulley. Also it appears that the left manipulator has had the cable installed incorrectly as it rides on the housing of the wrist.

  497   Tuesday, October 08, 2013, 13:11 Travis CaveSpent Target VaultStandard Operation SiC#29Spent target move

SiC#29 has been moved to the spent target vault. The target was placed in Pail #109 and placed into slot 2B it was 24.7mS/hr upon removal from the south hot cell. See attached PDF of the vault details.

Attachment 1: Vault_Storage_October_8_2013.pdf
Vault_Storage_October_8_2013.pdf Vault_Storage_October_8_2013.pdf Vault_Storage_October_8_2013.pdf Vault_Storage_October_8_2013.pdf
  499   Tuesday, October 08, 2013, 14:58 Anders MjosSouth Hot-CellStandard Operation SiC#29Target to Heat Shield electrical short

The SiC#29 CTL target has been taken apart with the help of Isaac and Chad. Electrical measurements were done between Target and Heat Shield as the target was disassembled. Work was done on October 2nd, 4th, 7th and 8th.

The megger showed about 30kOhm at 50V with the following changes

  • Bolts for CTL block loosened
  • Above bolts removed
  • CTL block pulled away from Heat Shield
  • CTL block removed
  • Heat Shield lid removed
  • Bolts for target removed
  • Shims between target and insulators

The megger showed about 50kOhm at 100V with the following changes

  • Target removed. Measured between cathode restraint and HS.

The megger showed OL at 540V with No 3 insulator removed. A measurement on No 3 insulator while it was sitting on the HS showed 70kOhm at 120V confirming that the insulator can no longer hold voltage.

While taking off the coil retainer plate, Chad noticed that all bolts were not tight.

Photos are available on DocuShare.

  503   Tuesday, October 15, 2013, 16:44 Grant MinorCraneRepair  Target Hall Crane - operational with temporary thermal sensor bypass

E-mail correspondence on the Target Hall crane fault diagnosis between October 11th and 15th:

On 15/10/2013 3:34 PM, Grant Minor wrote:

Hello all,

Mike Smith from Norelco arrived this morning and spent some time with Travis from RH and Mike Rowe from Controls group examining the crane controls and electrical schematics.  A common understanding of the wiring and control signal scheme for the thermal sensor circuits was reached.  A scanned copy of Norelco / Seattle Crane drawing E5 - 1/1 with markups by Dave Morris (Oct 11th) and Mike Smith (Oct 15th) is attached.

The group then worked on top of the crane bridge to systematically isolate the thermistor circuits in each drive motor.  The thermistor readings were all normal / as-expected (about 180 Ohms for 3 in series), i.e. there was no indication of failure in any of the motor thermistors.  Fall arrest equipment was used to access the motors where required.

Next, the shunt circuit in each temperature sensor module was measured (terminals T1 and T2 on each module, on drawing E5 - 1/1).  The shunt in the operational module was measured at 500 kOhms.  The shunt in the suspected faulty module was measured at 79 kOhms.

It was concluded that there is most likely a fault in the module with the low shunt resistance.  The suspect module was left wired in bypass (shorted from terminals 14 to 11).  Mike Smith advised at that point that it would be safe to operate the crane in this mode temporarily until a replacement module can be installed.  I discussed this with him and Don Dale, and we agreed the risk is low, as we have not ever experienced a motor overheat scenario in the operating lifetime of the crane.

Mike Smith called me around 1pm to advise that he has located a replacement unit from their supplier in the US and I asked him to order 2 units on expedited overnight.  Mike expects the components to arrive Friday this week or Monday next week latest, factoring in delays at customs and local delivery times.  The units will be sent to Norelco first, then to TRIUMF locally.

Remote Handling is now continuing with Target Hall operations, using the crane as normal with the thermal module bypassed until the replacement module arrives.

Thanks to Dave Morris / Mike Lowe for their assistance in diagnosing this fault.

Here is a short summary of the Fault:

Cause of fault
- Most likely a failed thermal sensor module for one of the two pairs of bridge drive motors

Diagnosis
- Crane company (Norelco) consulted, with on-site inspections by tech Mike Smith on October 9th and October 15th
- Controls group / Mike Smith measured resistances in motor thermistors and sensors to systematically isolate fault to thermal sensor

Remedy actions taken

- Thermal sensor bypassed to temporarily restore crane function
- Risk of operating without sensor determined to be low through discussions with Norelco / Don Dale / Grant Minor
- Replacement thermal sensor + 1 spare (~ $300 ea + shipping) ordered from parts supplier through Norelco - expected delivery Monday October 21st

How could this fault have been prevented?
- Cause of failure within thermal sensor module unknown at this time
- Annual crane inspection performed by Norelco in March 2013 did not indicate any problems with this sensor (crane drive system functioned as normal)
- Suggested for future: routine inspection of sensor module shunt resistance to determine if there are any long-term signs of slow degradation

What can be done to prevent the fault in the future?
- The ISAC crane controls were designed in the late 1990's by Norelco sub-contractor Seattle Crane (now defunct)
- The crane is supposed to have two pairs of independent motors with separate thermal sensors, each capable of driving the crane if the other fails due to thermal trip
- My understanding is that the controls logic design should have been designed so that failure of one pair of motors does not prevent crane operation... it does not seem to be the case with the current design
- The design of the control logic related to these sensors could be re-evaluated and modified so that a trip from one thermal module does not prevent operation of the bridge if the other module is OK
- This is a project that will require some time and some controls and engineering resources
- In the interim, if the same failure occurs again, it may be possible to jumper the thermal sensor from the crane control room and continue operating normally - I will confirm with controls group / Norelco
- However, this is not advisable as it would be difficult in some cases to determine if the trip was due to a faulty thermal module, or an actual motor overheat scenario
- I will discuss further actions with Don Dale

Thanks and best regards,

Grant


On 11/10/2013 4:29 PM, Grant Minor wrote:

Hello all,

I spoke with the Norelco tech Mike Smith this afternoon regarding the failed thermal sensor component / circuit.  He will call Kone on holiday Monday (their office is not closed for Canadian Thanksgiving) and determine if they have a replacement module.

I explained (to the best of my understanding) the diagnosis performed by Dave Morris / controls group and the test that was done to isolate the thermal sensor unit.  Unfortunately, Mike Smith's drawings from Seattle crane contain notes and revisions that don't match the drawing that Dave Morris provided me (Seattle Crane dwg E5 - 1/1 revision 1 02-10-99), and he was unable to confirm in his opinion whether the bypass performed by Dave Morris has correctly isolated the problem components.  In addition, he believes that the bypass he performed on Wednesday isolated portions of circuitry that are inconsistent with this thermal sensor circuit.

Mike Smith will return Tuesday morning to review the bypass and schematics.  He recommended not operating the crane until he has a chance to confirm this thermal sensor issue.

From the drawings I have in hand and from discussions with Dave Morris, the failed component might be the thermistor sets inside the motor housing which are in series with the suspect module, or the module itself.  My understanding is that the crane is designed with two pairs of motors for the bridge drive, and each pair is protected by one of these thermal modules (thus there are two modules total).  Both modules would be the same age and both might be susceptible to the same failure mode.

As it is unclear to me the exact nature of the drive system failure, and I have a recommendation from Norelco to hold on operation of the crane, I must unfortunately state that the crane should not be used and we will have to wait until Tuesday to gather more information.

I am not so concerned about temporary loss of the thermal protection circuitry, as we have not had an overheating scenario in those motors in the lifetime of the crane (to my knowledge).  I am more concerned about getting 100% confirmation that we have addressed the problem.  If we attempt to use the crane and experience another failure during a lift that prevents us from placing the load down safely with the crane stuck in position over a target station, then we would be in much deeper trouble.

My apologies for this situation.

Best regards and have a good weekend,

Grant


On 11/10/2013 1:28 PM, Grant Minor wrote:
Thanks Dave,

I've contacted Norelco, Mike Smith and I are planning a path forward for further diagnosis and repair.

The crane MUST NOT be used to carry a load until it is identified whether the module or the sensors have failed, the reason for the failure, and the functionality of the thermal sensors has been restored.

Without the thermal sensor circuit we lose protection from motor overheat, an event which could have much more serious failure implications to the crane.

Cheers,

Grant

On 11/10/2013 1:04 PM, David Morris wrote:
The fault has been identified in the Target Hall Crane as a failed motor temperature module, or motor temperature sensor, on the East-West motion. The status contact in the module was bypassed allowing crane motion. There was no fault with the controls.

Dave

Attachment 1: ISAC_THall_Crane_elec_E5_1slash1_15Oct2013.pdf
ISAC_THall_Crane_elec_E5_1slash1_15Oct2013.pdf
  505   Wednesday, October 16, 2013, 18:53 Grant MinorITERepair  ITE Harp 9 Removed & Blanked-Off - blocks NOT YET replaced

The blocks above the pre-separator section of the ISAC beam lines were removed today in the Target Hall by Bevan Moss and Chad Fisher with Lynne LeMessurier present from RPG.

The two blocks in the layer below the top layer above the pre-separator were damaged on removal (see attached photos).  This was due to an attempt to lift them in the incorrect sequence caused by misinterpretation of the labeling / numbering system drawn on the top of the blocks.  The blocks are labelled for the replacement sequence, but not for the removal sequence.  An attempt was made to lift a block that had an overlap with an adjacent block that was not visible, causing damage to two blocks.  A note was added in black marker to the critical block to indicate that it should be removed last (shown in attached photo).  The block replacement sequence will be photographed and a procedure document will be written by Bevan, with a bound copy of the procedure provided in the Target Hall, in order to prevent such an incident from occurring again.  Broken pieces of the blocks were collected and placed in a 5-gallon pail.

The removal of all of the blocks caused the depression in the target station to fluctuate around the trip point (17 inches of water column), which caused the ventilation alarm to trip on and off constantly.  Operations contacted me to ask if this could be remedied.  Bevan closed the damper to ITW, which brought the depression to a low enough value so that the alarm could be defeated properly.  This was around 2pm.

Preliminary co-ordination of the ITE Harp 9 removal job was discussed by Scott Kellogg and Ron Kuramoto around lunch time.  Keith Ng (RH) and Scott searched for the blank-off that was used during the last Harp 9 repair (removed from B/L in March 2013) but they could not locate it.  I was later able to find the blank-off bagged in a grey rubbermaid bin at the bottom of the stairs in the target storage vault pit (under the SHC / NHC ventilation and filters).  The blank-off was found bagged and tagged as surveyed at 100 counts @ 0.5m on March 27, 2013.  I gathered Scott, Ron Kuramoto, and Danka Krsmanovic to co-ordinate the Harp 9 removal and blank-off installation, starting at around 2:30 pm.

For the Target Hall Harp work, Ron Kuramoto and Scott prepared the required tools and plastic coverings / bags.  I acted as crane operator.  Danka was the surveyor present.  Anders Mjos joined the group for photos and moral support.

Scott disconnected services from the Harp device, and prepared it for lift.  I called operations to confirm that the section of B/L had been vented.  Ron and Scott used the RH tools to disconnect the 2 vacuum flange bullet bolts.  Ron directed the crane with signals and I lowered the chain rigging to the Harp, it was connected and removed from the BL with the main hoist.  (I made the mistake of directing the rigging of the harp to the main 20T hoist, when in fact the 3T Aux hoist should have been used, as the main hoist can't reach to the vacuum / storage pit on the west side of the hall.)

Danka performed several swipes and measurements of the Harp after removal.  Alpha contamination was discovered on the bottom of the Harp flange.

Ron and Scott installed the blank-off flange, then I called operations to indicate that pumping should start.

Ron and Scott retrieved the vacuum test flask jig / support structure from the West storage pit and brought it down to the pre-separator pit.  I lowered the Harp into this flask jig, and Scott used the side-wall location bolts from the top of the harp assembly to fasten the flanges of the Harp and the jig.

I had trouble at first activating the Aux hoist but soon realized that it's necessary to press the Aux pendant "ON" button down for several seconds before the power actually turns on to this hoist.

We then removed the main hoist hook and attached the Aux hoist to the Harp / flask.  The assembly was transported to the West storage pit.

Some of the handrails had to be removed to facilitate initial movements of the Harp assembly.  These handrails should be replaced tomorrow morning.

Scott also submitted a Work Order for a back-up blank-off today, job number 40303.

The pre-separator blocks have NOT been replaced yet, we will do this tomorrow morning.

It was a busy day, thanks to all for their efforts and for staying a bit late to get the blank-off installed.

Best regards,

Grant

Attachment 1: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013.JPG
Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013.JPG
Attachment 2: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-001.JPG
Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-001.JPG
Attachment 3: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-002.JPG
Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-002.JPG
Attachment 4: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-004.JPG
Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-004.JPG
Attachment 5: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-007.JPG
Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-007.JPG
Attachment 6: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-009.JPG
Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-009.JPG
Attachment 7: Closing_Damper_for_ITE_16Oct2013.JPG
Closing_Damper_for_ITE_16Oct2013.JPG
Attachment 8: ITE_Harp_9_Remove_and_Blank_16Oct2013-012.JPG
ITE_Harp_9_Remove_and_Blank_16Oct2013-012.JPG
Attachment 9: ITE_Harp_9_Remove_and_Blank_16Oct2013-021.JPG
ITE_Harp_9_Remove_and_Blank_16Oct2013-021.JPG
Attachment 10: ITE_Harp_9_Remove_and_Blank_16Oct2013-031.JPG
ITE_Harp_9_Remove_and_Blank_16Oct2013-031.JPG
Attachment 11: ITE_Harp_9_Remove_and_Blank_16Oct2013-038.JPG
ITE_Harp_9_Remove_and_Blank_16Oct2013-038.JPG
  507   Thursday, October 17, 2013, 17:16 Grant MinorITERepair  Pre-Separator-area (ITE Harp 9) Blocks Replaced

The pre-separator-area blocks were replaced today by Bevan and Travis, with Grant present for photos and observation.

Photos are attached of each block replacement.

Some difficulty was encountered in replacing the "Layer #3" blocks (photo 9 attached).  An interference occurred between the outside of the west "Layer #3" block and an aluminum channel directly beside the rubber pad that supports the block.  The block was initially resting on this channel but slipped off, breaking off some concrete at the edge.   See photo 12 attached and notice crumbled concrete inside this channel around the area where the interference occurred. Photo 14 shows the damaged block edge.

It should be noted that when these two blocks are resting flat, there should be a gap between them (i.e. they should NOT be touching as shown in photo 9).

 

Attachment 1: PreSeparatorHarp9Blocks_17Oct2013.JPG
PreSeparatorHarp9Blocks_17Oct2013.JPG
Attachment 2: PreSeparatorHarp9Blocks_17Oct2013-008.JPG
PreSeparatorHarp9Blocks_17Oct2013-008.JPG
Attachment 3: PreSeparatorHarp9Blocks_17Oct2013-009.JPG
PreSeparatorHarp9Blocks_17Oct2013-009.JPG
Attachment 4: PreSeparatorHarp9Blocks_17Oct2013-012.JPG
PreSeparatorHarp9Blocks_17Oct2013-012.JPG
Attachment 5: PreSeparatorHarp9Blocks_17Oct2013-017.JPG
PreSeparatorHarp9Blocks_17Oct2013-017.JPG
Attachment 6: PreSeparatorHarp9Blocks_17Oct2013-020.JPG
PreSeparatorHarp9Blocks_17Oct2013-020.JPG
Attachment 7: PreSeparatorHarp9Blocks_17Oct2013-021.JPG
PreSeparatorHarp9Blocks_17Oct2013-021.JPG
Attachment 8: PreSeparatorHarp9Blocks_17Oct2013-014.JPG
PreSeparatorHarp9Blocks_17Oct2013-014.JPG
  508   Friday, October 18, 2013, 10:17 Bevan MossITWRepair  Paddle Wheel

 Yesterday I visually inspected the paddle wheel and noticed that it was spinning freely and constant. As the signal was intermittent replaced the coil at the back of the wheel only. This does not require access to the high active water. With the coil replaced the signal looked strong. I asked operations to keep and eye on it and advise if the problem has been resolved. I also discussed with David this morning and he informed me that this is the same procedure he would have followed.

  518   Tuesday, October 22, 2013, 16:52 Bevan MossConditioning StationRepair  Canbus base card for BIAS

 The base card in the canbus BIAS module was determined to be faulty. Dave Morris removed a card VECC to repair the conditioning station. 

  520   Tuesday, October 22, 2013, 17:07 Bevan MossConditioning StationStandard Operation  services shut down

 The turbo pump, roughing pump, have been turned off and the valves for venting opened. The cooling package has also been turned off.

  523   Thursday, October 24, 2013, 11:31 Travis CaveSpent Target VaultStandard Operation UC#7Spent target move

UC #7 has been moved from the south hot cell to the spent target vault, it was placed in pail #110 and put in slot 8B of the vault, it was 22.6mSv/hr upon removal from the hot cell. See attached PDF for vault details.

Attachment 1: Vault_Storage_October_24_2013.pdf
Vault_Storage_October_24_2013.pdf Vault_Storage_October_24_2013.pdf Vault_Storage_October_24_2013.pdf Vault_Storage_October_24_2013.pdf
  541   Tuesday, November 12, 2013, 14:33 Bevan MossConditioning StationRepair  Cooling manifold returned

 The cooling manifold for the conditioning station high power water cooled lines has been returned. The cooling package can once again be operated

  547   Monday, November 18, 2013, 16:44 Bevan MossConditioning StationStandard Operation  Testing of cooling package

 I have tested all of the compressors for TCS. All are operational and cycled as they should. 

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