Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  Evaporator_2, Page 33 of 34  Not logged in ELOG logo
  ID Date Author Target Material Target Oven W.O# Source Status Subject
  39   Friday, August 10, 2012, 19:57 Nikita Bernier   DoneSintering Ta foil with TaO coating

 Friday, August 10, 2012, 19:54

 

Target boat with TaC coating, inside covered with a 0.002 inches thick Ta foil, wrapped with a 0.002 inches thick Ta foil, contains a Ta foil with TaO coating.

See John's Ipad for their recipes.

Evaporator #2 is now auto-ramping overnight at 0.2 A/min, up to 830 A, with the maximum voltage limited at 14 V, between 2.00e-05 (Good vacuum) and 3.00e-05 Torr (Bad vacuum).

 

  38   Monday, July 30, 2012, 15:42 John Wong   ProblemsChiller maybe leaky

Monday, July 30, 2012, 15:38

The evaporator was used for the processing the NiO target for 8 days and it was discovered today that there was a puddle of water underneath the chiller. 

The cover of the chiller was removed and some water around the plumbing was found (see attachment #1). 

Will continue to keep running the chiller to see if there is more water leaking out...


 

Attachment 1: chiller.jpg
chiller.jpg
  37   Sunday, July 22, 2012, 20:51 John WongNiO38481-7HP-FEBIADDoneSintering NiO#1

 Sunday, July 22, 2012, 20:30

The NiO target materials were loaded into the container today.  

Total discs = 500, (10 discs/pack) 


length (after loaded) = 9.0cm 

Target container is wrapped with Ta-heat shields, and will be removed after the sintering process. 

One regular end cap is inserted (with Ni-foil inserted as a divider).  The caps, however, are very loose (tried 2 caps and still loose).  Hopefully the thermo diffusion bonding will seal the cap... 

The other end is inserted with a D-cap for out-gassing proposes, and will be replaced with the regular end-cap after the process. 

(see attachment#1)


Sunday, July 22, 2012, 20:48 

The camber has been pumped down and currently IG1=1.3e-6 Torr.

The HS cooling water was turned on and no leaks were detected.  

TGHT and TBHT were stepped up to 50A. 

Auto-ramping is initiated at 0.2A/min for TGHT max = 250A, TBHT max = 230A. 


 Thursday, July 26, 2012, 23:31

TGHT and TBHT have reached to 250A (local @ 242A/2.88V) and 230A, respectively, and have stayed for ~4hrs (see attachment#2)  

Currently, IGP1 = 4.9e-7 Torr, IGP2 = 3.5e-7 Torr, CG1B = 13mTorr. 

Initiating auto-cool down at 2A/min.  


 Monday, July 30, 2012, 15:11

The chamber was vented and the target was removed.

There was significant condensation oily fluid coated Cu-heatshield lid and around the ionizer opening.

Overall, the target looks very good.  The NiO target material was nicely sintered.  No shrinkage or loose particles were observed (see attachment #3).

The endcap, however, was not properly fitted and it just fell off, (see attachment #4). 

Both ends of the target are currently opened; the expension tool for the endcap is in order and hopefully this will solve the problem.

The target is being stored in the fumehood


 

Attachment 1: NiO#1_sinteringevap2.png
NiO#1_sinteringevap2.png
Attachment 2: NIO#1_TGHT_TBHT_250_220.png
NIO#1_TGHT_TBHT_250_220.png
Attachment 3: Sintered_NiO.GIF
Sintered_NiO.GIF
Attachment 4: Endcap.GIF
Endcap.GIF
  36   Thursday, July 19, 2012, 17:05 John WongEmpty37918-3LP-FEBIADDoneCoating target oven /w TaC & sintering for UCx#5

Thursday, July 19, 2012, 16:58

The target container was coated with TaC. 

It's wrapped with 3 layers of Ta as the heat-shield, including the backblock.

TGHT will be ramped up to 580A at 0.2A/min.

TBHT will be ramped up to 230A at 0.2A/min.

Currently, IGP1 = 1.5e-6 Torr.  BP = 15mTorr


 Friday, July 20, 2012, 13:56

TGHT and TBHT reached to 580A & 230A, respectively, and stayed for ~ 2hrs. 

Measured temperature at the ionizer tube to be 1630C.

Cooling down in process at 2A/min...


 Sunday, July 22, 2012, 20:53

The chamber was vented earlier around 14:00hr.  

The target container looks good! 


 

  35   Tuesday, July 17, 2012, 16:00 John Wong targetboat (TaC coated) DoneSintering TaC coated regular- & D-endcaps

Tuesday, July 17, 2012, 15:45

Target boat is filled with TaC coated regular- and D-endcaps. 

The boat is wrapped with a Ta heat-shield. 

Chamber is being pumped down, currently at 5e-6 Torr.


Tuesday, July 17, 2012, 15:58

Heat-shield cooling water valve opened; no leaks detected.

Initiated TGHT auto-ramping at 0.5A/min, set TGHT max at 580A.


 Wednesday, July 18, 2012, 10:44

Yesterday evening, the target heater tripped off a few times due to high vacuum excursion.  The TGHT ramping rate was low to 0.2A/min.  The current was ramped up sturdily to 500A this morning.  


Wednesday, July 18, 2012, 10:46

Increased ramping rate to 2A/min.  Vacuum currently at 2.2e-6 Torr.


 Wednesday, July 18, 2012, 16:18

TGHt has reached to 580A and stayed for about 5 hrs. 

Cooling down in process...  2A/min for TGHT --> 0A.


 Thursday, July 19, 2012, 10:31

TGHT reached to 0A. 

Evaporator is off. 

Venting chamber... 


 

  34   Thursday, July 12, 2012, 17:55 John WongNiOtargetboat (TaC coated) Maintenance NiO development- test#2

Thursday, July 12, 2012, 17:29

NiO was sprayed on Ni foil.

Average/discs: mass= 0.075g, thickness=0.076mm, density = 7.023g/cm3.

4 set of samples were loaded onto the targetboat (coated/sintered with TaC).  A piece of Ta foil was used as the under layer (see attachment #1).

A 0.002" thick Ta foil was wrapped around the container as the heat-shield.

The chamber was pumped down to 5.0e-6 Torr before the cooling water valve was opened; no leaks was detected.

For this process, the target heater will only go up to 250A (~1100C), with auto-ramping rate at 0.5A/min.

The heater has been stepped up to 50A, local 32A/ 0.23V.  The vacuum reached to max 1.6e-5 Torr, and it's coming down.


Thursday, July 12, 2012, 17:51

Auto-ramping initiated...


 Friday, July 13, 2012, 09:42

TGHT reached to 250A and stayed for 6 hrs (see attachment #2).  At that current, the target wasn't glowing so the temperature could not be measured. 

Initiated auto-cooling at 2A/min. 


Friday, July 13, 2012, 11:00  

TGHT reached to 65A.  Stopped the auto-cooling process and manually tapped down the p/s to 0A.  

Vacuum is stable at 5.7e-7 Torr.  

In the next 30 min or so, the chamber will be vented and the NiO target material will be taken out for inspection. 


 

Attachment 1: NiO_spray.PNG
NiO_spray.PNG
Attachment 2: TGHT0-250A.png
TGHT0-250A.png
  33   Thursday, June 21, 2012, 18:13 John WongNiOTa target boat FailedNiO development - Container broke!

John Wong wrote:

Nikita Bernier wrote:

Wednesday, June 20, 2012, 17:23

New Target boat, with no coating, wrapped with a 0.002 inches thick Ta foil, contains NiO D-shape discs :

Sample,   # Disks,    Mass (g),    Thickness (mm)

1    12,  1.9396,  1.938

2    13,  0.9592,  0.847

3    25,  2.6675,  3.06

See John's Ipad for their recipes.

Evaporator #2 is now auto-ramping overnight at 0.5 A/min, up to 580 A, with the maximum voltage limited at 14 V, between 3.00e-05 (Good vacuum) and 4.00e-05 Torr (Bad vacuum).


 

Wednesday, June 20, 2012, 22:28

TGHT tripped off at 78A due to high out-gassing pressure.  The current was tapped down to 75A before it was turned back on. 

Changed ramping rate from 0.5A/min to 0.2A/min.  

Initiate auto-ramping... 


 Thursday, June 21, 2012, 08:35

Vacuum has come down to 7e-7 as TGHT is being ramped up at 0.2A/min. (see attachment#1).

Increase TGHT rate to 2A/min.

The temperature should be measured when the heater gets up to around 500A.


 

 Thursday, June 21, 2012, 17:37

The NiO discs were heated up to 1500C at 560A.  The target heater was lowered in steps and the temperature was measured.  At 320A, the target container was ~1110C.  (see attachment #1) 

There was a sign of resistant on the target container as the p/s voltage started to go up at a higher rate.  (see attachment#2, 3, 4 for the archived striptool).

Unfortunately, the target container was broken; it was most likely reacted with the Ni.  (see attachment#5)

So.... the possible solution?!  TRY coating the container with Ta2O5.  Will discuss more in the Friday Jun 22 meeting. 


 

Attachment 1: NiO_targets_temp.pdf
NiO_targets_temp.pdf
Attachment 2: TGHT_0-580A.GIF
TGHT_0-580A.GIF
Attachment 3: TGHT_200-580A.GIF
TGHT_200-580A.GIF
Attachment 4: TGHT_vs_VOL.GIF
TGHT_vs_VOL.GIF
Attachment 5: NiO_container_broke.png
NiO_container_broke.png
  32   Wednesday, June 20, 2012, 22:33 John WongNiOTa target boat DoneNiO development

Nikita Bernier wrote:

Wednesday, June 20, 2012, 17:23

New Target boat, with no coating, wrapped with a 0.002 inches thick Ta foil, contains NiO D-shape discs :

Sample,   # Disks,    Mass (g),    Thickness (mm)

1    12,  1.9396,  1.938

2    13,  0.9592,  0.847

3    25,  2.6675,  3.06

See John's Ipad for their recipes.

Evaporator #2 is now auto-ramping overnight at 0.5 A/min, up to 580 A, with the maximum voltage limited at 14 V, between 3.00e-05 (Good vacuum) and 4.00e-05 Torr (Bad vacuum).


 

Wednesday, June 20, 2012, 22:28

TGHT tripped off at 78A due to high out-gassing pressure.  The current was tapped down to 75A before it was turned back on. 

Changed ramping rate from 0.5A/min to 0.2A/min.  

Initiate auto-ramping... 


 Thursday, June 21, 2012, 08:35

Vacuum has come down to 7e-7 as TGHT is being ramped up at 0.2A/min. (see attachment#1).

Increase TGHT rate to 2A/min.

The temperature should be measured when the heater gets up to around 500A.


 

Attachment 1: Photo_2012-06-21_8_27_40_AM.png
Photo_2012-06-21_8_27_40_AM.png
  31   Wednesday, June 20, 2012, 17:29 Nikita BernierNiOTa target boat DoneNiO development

Wednesday, June 20, 2012, 17:23

New Target boat, with no coating, wrapped with a 0.002 inches thick Ta foil, contains 3 NiO pellets :

Sample,   # Disks,    Mass (g),    Thickness (mm)

1    12,  1.9396,  1.938

2    13,  0.9592,  0.847

3    25,  2.6675,  3.06

See John's Ipad for their recipes.

Evaporator #2 is now auto-ramping overnight at 0.5 A/min, up to 580 A, with the maximum voltage limited at 14 V, between 3.00e-05 (Good vacuum) and 4.00e-05 Torr (Bad vacuum).


Thursday, June 21, 2012, 18:14  

See attachment #1, 2 for the density measurements and the graph for the disc thickness  -JW 


 

Attachment 1: NiO_density_measurements.xlsx
Attachment 2: Casts_thickness.GIF
Casts_thickness.GIF
  30   Monday, June 11, 2012, 12:26 John WongSiC38481-2HP-SISProblemsEnd caps vaporized

John Wong wrote:

Nikita Bernier wrote:

John Wong wrote:

Nikita Bernier wrote:

John Wong wrote:

Tuesday, May 15, 2012, 12:24

The HP-SIS SiC target was made on Nov 03, 2010.  The target consists of 405 discs, 18.5cm in length.  It was sintered in the Evaporator#1. 

This target is going into Evap#2 for re-conditioning.  It is currently being pumped down. 


 

Friday, May 18, 2012, 12:19 

The target is wrapped with only one heat shield.

Evaporator #2 Target Heater is now auto-ramping at 0.5 A/min, up to 820 A, with the maximum voltage limited at 2 V, between 2.00e-05 (Good vacuum) and 3.00e-05 Torr (Bad vacuum). Tube Heater is auto-ramping at 0.5 A/min, up to 230 A, with the maximum voltage limited at 1 V. See attachments.

 Friday, May 18, 2012, 13:15

Increased TBHT voltage to 5V, and TGHT to 15V.  Currently, TBHT =83A, 0.986V, TGHT= 144A, 1.65V, IGP1 = 5.2e-7 Torr, IGP2 = 4.3e-7 Torr. 

Continue ramping up... 


 Tuesday, May 22, 2012, 12:02

TGHT and TBHT were ramped up to 830A/13.65V (local), and 235A/3.85V, respectively.  The target was conditioned over the long weekend.  


 

 Tuesday, May 22, 2012, 12:13

Initiating the cool-down process at 5 A/min.

See archive plots of the Target Heater (Attachment 1) and the Tube Heater (Attachment 2).

 Tuesday, May 22, 2012, 15:24

TGHT/TBHT were ramped down to 0A.  The target has cooled for about 45 min.  All pumps and chillers are off.  The chamber has been vented.


 

 Monday, June 11, 2012, 12:20

After the re-conditioning, the target's end-caps vaporized.  This is something happened before (see elog entries below):

https://elog.triumf.ca/TIS/Evaporator_1/20

https://elog.triumf.ca/TIS/Evaporator_1/22

The caps were removed and yellow crystals were observed. (see attachment#1).

The D-caps will be inserted in both ends and will be re-conditioned again to see if the yellow crystals can be removed at high temperature.


 

Attachment 1: Photo_2012-06-11_12_06_19_PM.jpg
Photo_2012-06-11_12_06_19_PM.jpg
  29   Tuesday, May 29, 2012, 15:43 Nikita BernierBeOTarget boat #2 FailedSintering BeO pellets #3

John Wong wrote:

Nikita Bernier wrote:

Nikita Bernier wrote:

Thursday, April 05, 2012, 16:31

Target boat contains 6 BeO pellets :

Sample,   Mass (g),   Thickness (mm),   Density (g/cm3)

1   1.2842,    5.406,        1.4647
2   1.2619,    5.150,        1.5108
3   1.2886,    5.316,        1.4946
4   1.2858,    5.310,        1.4931

5   1.3382,    5.520,        1.4948
6   1.3916,    5.650,        1.5187

 

Samples are made of BeO powder with 30% PVB which was treated at 400 RPM for 26 minutes. A ratio of 1:0.1 of mineral oil was added before another high speed treatment for 10 minutes. The powder was then pressed into pellets.

Pellets are loaded on a target boat coated/sintered with TaC. The target boat is wrapped with a Ta foil that is 0.002 inches thick.

**** Sintering is postponed until the situation with the ventilation in the lab06 is cleared. ****

 

 Tuesday, May 22, 2012, 16:44

Target chamber is currently being pumped down. Leak check will be done tomorrow by turning on the cooling water for the heat shield.

 Wednesday, May 23, 2012, 17:38

TGHT was stepped up to about 55A before the auto ramping was initiated.  The vacuum limit parameter was set for good vac at <4.0 e-5 Torr and bad vac at >5.0 e0-5 Torr. 

The pressure is coming close to the trip limit (8.5 e-5 Torr) (see attachment 1: strip tool over the past 5 hours).  Changed the vacuum limit parameter:  good vac =3.0e-5 Torr, bad vac= 4.0e-5 Torr. 


 Saturday, May 26, 2012, 10:44

TGHT is auto ramping up smoothly as the pressure is regulating between 1e-5 to 4 e-5 torr.  (See attachment 2, past 21 hr)


Sunday, May 27, 2012, 12:25  

There could be a power bump  early this morning at 06:30hr, and tripped off the TGHT power supply (see attachment #3).  The computer in the cold lab was found to be off expectedly, so the alarm handler running on that computer was also shut off (*Need a UPS on this computer!)  

Called the ISAC Ops, and  nothing about any power bump around that time was noticed.  

Turned on TGHT p/s and set TGHT at 318A, local at 315A/4.58V.  TGHT has been running for about 10 mins.  Currently vac at 4.2e-7 Torr.  


Sunday, May 27, 2012, 12:35

Initiating TGHT auto ramping... 


 Monday, May 28, 2012, 00:20

TGHT has reached to 600A and will remain at that current for the rest of the night.  The target oven temperature will be measured tomorrow.

See attachment#4 for the striptool over the past 10hr.


 Monday, May 28, 2012, 10:56

TGHT stayed at 600A for about 12 hours.  Pressure gradually came down to 7.6e-7 Torr. (See attachment #5). 

At TGHT=600A, The target boat temperature was measured at 1400C (with the pyrometer), and the Ta-heat shield (1-layer) was at 1050C. [Note: These temperature measurements are very closed to the measurements with an empty LP target (with not heat shield), TGHT @ 600A = 1360C].


Monday, May 28, 2012, 11:04

Due to the water leak from the Evap2 chiller, the system has to be shut off for inspection. 

TGHT was tapped down to 0A.  The target was cooled down for about 20min before the chiller was turned off.

Will continue with the process after the problem is solved...


 

 Tuesday, May 29, 2012, 15:30

Evap2 was vented out and the pellets were taken out of the boat and examined.

The six pellets are cracked and have a greyish colour. The cracking is probably caused by the instant cooling and reheating when the system tripped on Sunday morning.

The light grey colour and white spots suggest that the sintering process was not completed and so the shrinkage cannot be determined.

A new batch of BeO pellets will have to be prepared and sintered in order to determine the dimensions of the final die.

 

  28   Monday, May 28, 2012, 11:15 John Wong   ProblemsChiller is leaking water

Monday, May 28, 2012, 11:08

It was discovered this morning that the Evaporator #2 chiller was leaking water from the bottom (see attachment 1).  A puddle of water was formed and eventually found its way down to the Hotcell. 

The evaporator was running over the weekend for the BeO pellets process.  The TGHT is now off and the chiller will be inspected... 


 

Attachment 1: Chiller_leaky.jpg
Chiller_leaky.jpg
  27   Wednesday, May 23, 2012, 17:45 John WongBeOTarget boat #2 DoneSintering BeO pellets #3

Nikita Bernier wrote:

Nikita Bernier wrote:

Thursday, April 05, 2012, 16:31

Target boat contains 6 BeO pellets :

Sample,   Mass (g),   Thickness (mm),   Density (g/cm3)

1   1.2842,    5.406,        1.4647
2   1.2619,    5.150,        1.5108
3   1.2886,    5.316,        1.4946
4   1.2858,    5.310,        1.4931

5   1.3382,    5.520,        1.4948
6   1.3916,    5.650,        1.5187

 

Samples are made of BeO powder with 30% PVB which was treated at 400 RPM for 26 minutes. A ratio of 1:0.1 of mineral oil was added before another high speed treatment for 10 minutes. The powder was then pressed into pellets.

Pellets are loaded on a target boat coated/sintered with TaC. The target boat is wrapped with a Ta foil that is 0.002 inches thick.

**** Sintering is postponed until the situation with the ventilation in the lab06 is cleared. ****

 

 Tuesday, May 22, 2012, 16:44

Target chamber is currently being pumped down. Leak check will be done tomorrow by turning on the cooling water for the heat shield.

 Wednesday, May 23, 2012, 17:38

TGHT was stepped up to about 55A before the auto ramping was initiated.  The vacuum limit parameter was set for good vac at <4.0 e-5 Torr and bad vac at >5.0 e0-5 Torr. 

The pressure is coming close to the trip limit (8.5 e-5 Torr) (see attachment 1: strip tool over the past 5 hours).  Changed the vacuum limit parameter:  good vac =3.0e-5 Torr, bad vac= 4.0e-5 Torr. 


 Saturday, May 26, 2012, 10:44

TGHT is auto ramping up smoothly as the pressure is regulating between 1e-5 to 4 e-5 torr.  (See attachment 2, past 21 hr)


Sunday, May 27, 2012, 12:25  

There could be a power bump  early this morning at 06:30hr, and tripped off the TGHT power supply (see attachment #3).  The computer in the cold lab was found to be off expectedly, so the alarm handler running on that computer was also shut off (*Need a UPS on this computer!)  

Called the ISAC Ops, and  nothing about any power bump around that time was noticed.  

Turned on TGHT p/s and set TGHT at 318A, local at 315A/4.58V.  TGHT has been running for about 10 mins.  Currently vac at 4.2e-7 Torr.  


Sunday, May 27, 2012, 12:35

Initiating TGHT auto ramping... 


 Monday, May 28, 2012, 00:20

TGHT has reached to 600A and will remain at that current for the rest of the night.  The target oven temperature will be measured tomorrow.

See attachment#4 for the striptool over the past 10hr.


 Monday, May 28, 2012, 10:56

TGHT stayed at 600A for about 12 hours.  Pressure gradually came down to 7.6e-7 Torr. (See attachment #5). 

At TGHT=600A, The target boat temperature was measured at 1400C (with the pyrometer), and the Ta-heat shield (1-layer) was at 1050C. [Note: These temperature measurements are very closed to the measurements with an empty LP target (with not heat shield), TGHT @ 600A = 1360C].


Monday, May 28, 2012, 11:04

Due to the water leak from the Evap2 chiller, the system has to be shut off for inspection. 

TGHT was tapped down to 0A.  The target was cooled down for about 20min before the chiller was turned off.

Will continue with the process after the problem is solved...


 

Attachment 1: past_5_hrs.JPG
past_5_hrs.JPG
Attachment 2: past_21_hrs.png
past_21_hrs.png
Attachment 3: power_lost_2012-05-27_12_0630hr.png
power_lost_2012-05-27_12_0630hr.png
Attachment 4: TGHT_600A.png
TGHT_600A.png
Attachment 5: TGHT@600A_past_12hr.JPG
TGHT@600A_past_12hr.JPG
  26   Tuesday, May 22, 2012, 16:45 Nikita BernierBeOTarget boat #2 DoneSintering BeO pellets #3

Nikita Bernier wrote:

Thursday, April 05, 2012, 16:31

Target boat contains 6 BeO pellets :

Sample,   Mass (g),   Thickness (mm),   Density (g/cm3)

1   1.2842,    5.406,        1.4647
2   1.2619,    5.150,        1.5108
3   1.2886,    5.316,        1.4946
4   1.2858,    5.310,        1.4931

5   1.3382,    5.520,        1.4948
6   1.3916,    5.650,        1.5187

 

Samples are made of BeO powder with 30% PVB which was treated at 400 RPM for 26 minutes. A ratio of 1:0.1 of mineral oil was added before another high speed treatment for 10 minutes. The powder was then pressed into pellets.

Pellets are loaded on a target boat coated/sintered with TaC. The target boat is wrapped with a Ta foil that is 0.002 inches thick.

**** Sintering is postponed until the situation with the ventilation in the lab06 is cleared. ****

 

 Tuesday, May 22, 2012, 16:44

Target chamber is currently being pumped down. Leak check will be done tomorrow by turning on the cooling water for the heat shield.

  25   Tuesday, May 22, 2012, 15:26 John WongSiC38481-2HP-SISDoneRe-condition the HP-SIS SiC target

Nikita Bernier wrote:

John Wong wrote:

Nikita Bernier wrote:

John Wong wrote:

Tuesday, May 15, 2012, 12:24

The HP-SIS SiC target was made on Nov 03, 2010.  The target consists of 405 discs, 18.5cm in length.  It was sintered in the Evaporator#1. 

This target is going into Evap#2 for re-conditioning.  It is currently being pumped down. 


 

Friday, May 18, 2012, 12:19 

The target is wrapped with only one heat shield.

Evaporator #2 Target Heater is now auto-ramping at 0.5 A/min, up to 820 A, with the maximum voltage limited at 2 V, between 2.00e-05 (Good vacuum) and 3.00e-05 Torr (Bad vacuum). Tube Heater is auto-ramping at 0.5 A/min, up to 230 A, with the maximum voltage limited at 1 V. See attachments.

 Friday, May 18, 2012, 13:15

Increased TBHT voltage to 5V, and TGHT to 15V.  Currently, TBHT =83A, 0.986V, TGHT= 144A, 1.65V, IGP1 = 5.2e-7 Torr, IGP2 = 4.3e-7 Torr. 

Continue ramping up... 


 Tuesday, May 22, 2012, 12:02

TGHT and TBHT were ramped up to 830A/13.65V (local), and 235A/3.85V, respectively.  The target was conditioned over the long weekend.  


 

 Tuesday, May 22, 2012, 12:13

Initiating the cool-down process at 5 A/min.

See archive plots of the Target Heater (Attachment 1) and the Tube Heater (Attachment 2).

 Tuesday, May 22, 2012, 15:24

TGHT/TBHT were ramped down to 0A.  The target has cooled for about 45 min.  All pumps and chillers are off.  The chamber has been vented.


 

  24   Tuesday, May 22, 2012, 12:15 Nikita BernierSiC38481-2HP-SISDoneRe-condition the HP-SIS SiC target

John Wong wrote:

Nikita Bernier wrote:

John Wong wrote:

Tuesday, May 15, 2012, 12:24

The HP-SIS SiC target was made on Nov 03, 2010.  The target consists of 405 discs, 18.5cm in length.  It was sintered in the Evaporator#1. 

This target is going into Evap#2 for re-conditioning.  It is currently being pumped down. 


 

Friday, May 18, 2012, 12:19 

The target is wrapped with only one heat shield.

Evaporator #2 Target Heater is now auto-ramping at 0.5 A/min, up to 820 A, with the maximum voltage limited at 2 V, between 2.00e-05 (Good vacuum) and 3.00e-05 Torr (Bad vacuum). Tube Heater is auto-ramping at 0.5 A/min, up to 230 A, with the maximum voltage limited at 1 V. See attachments.

 Friday, May 18, 2012, 13:15

Increased TBHT voltage to 5V, and TGHT to 15V.  Currently, TBHT =83A, 0.986V, TGHT= 144A, 1.65V, IGP1 = 5.2e-7 Torr, IGP2 = 4.3e-7 Torr. 

Continue ramping up... 


 Tuesday, May 22, 2012, 12:02

TGHT and TBHT were ramped up to 830A/13.65V (local), and 235A/3.85V, respectively.  The target was conditioned over the long weekend.  


 

 Tuesday, May 22, 2012, 12:13

Initiating the cool-down process at 5 A/min.

See archive plots of the Target Heater (Attachment 1) and the Tube Heater (Attachment 2).

Attachment 1: TGHT-VAC1.JPG
TGHT-VAC1.JPG
Attachment 2: TBHT-VAC1.JPG
TBHT-VAC1.JPG
  23   Friday, May 18, 2012, 13:17 John WongSiC38481-2HP-SISDoneRe-condition the HP-SIS SiC target

Nikita Bernier wrote:

John Wong wrote:

Tuesday, May 15, 2012, 12:24

The HP-SIS SiC target was made on Nov 03, 2010.  The target consists of 405 discs, 18.5cm in length.  It was sintered in the Evaporator#1. 

This target is going into Evap#2 for re-conditioning.  It is currently being pumped down. 


 

Friday, May 18, 2012, 12:19 

The target is wrapped with only one heat shield.

Evaporator #2 Target Heater is now auto-ramping at 0.5 A/min, up to 820 A, with the maximum voltage limited at 2 V, between 2.00e-05 (Good vacuum) and 3.00e-05 Torr (Bad vacuum). Tube Heater is auto-ramping at 0.5 A/min, up to 230 A, with the maximum voltage limited at 1 V. See attachments.

 Friday, May 18, 2012, 13:15

Increased TBHT voltage to 5V, and TGHT to 15V.  Currently, TBHT =83A, 0.986V, TGHT= 144A, 1.65V, IGP1 = 5.2e-7 Torr, IGP2 = 4.3e-7 Torr. 

Continue ramping up... 


 Tuesday, May 22, 2012, 12:02

TGHT and TBHT were ramped up to 830A/13.65V (local), and 235A/3.85V, respectively.  The target was conditioned over the long weekend.  


 

  22   Friday, May 18, 2012, 12:19 Nikita BernierSiC38481-2HP-SISDoneRe-condition the HP-SIS SiC target

John Wong wrote:

Tuesday, May 15, 2012, 12:24

The HP-SIS SiC target was made on Nov 03, 2010.  The target consists of 405 discs, 18.5cm in length.  It was sintered in the Evaporator#1. 

This target is going into Evap#2 for re-conditioning.  It is currently being pumped down. 


 

Friday, May 18, 2012, 12:19 

The target is wrapped with only one heat shield.

Evaporator #2 Target Heater is now auto-ramping at 0.5 A/min, up to 820 A, with the maximum voltage limited at 2 V, between 2.00e-05 (Good vacuum) and 3.00e-05 Torr (Bad vacuum). Tube Heater is auto-ramping at 0.5 A/min, up to 230 A, with the maximum voltage limited at 1 V. See attachments.

Attachment 1: autoramp1.png
autoramp1.png
Attachment 2: ievap2autoheat1.png
ievap2autoheat1.png
  21   Wednesday, May 16, 2012, 14:04 John Wong   Problems resolvedTBHT cooling line leaky

John Wong wrote:

 Tuesday, May 15, 2012, 17:00

It was found that there were water droplets from the TBHT cooling line.  The joint is leaky.  (see attachment 1) 

A message has sent to Rick M. 


 

 Wednesday, May 16, 2012, 14:01

The connector was re-tighten.  The water valve was opened, and no water leaks were found.


 

  20   Tuesday, May 15, 2012, 17:06 John Wong   Problems resolvedTBHT power supply faulty

 Tuesday, May 15, 2012, 17:03

The tube heater power supply current readback and setpoint are not matching.  Ray Dube checked the power supply and confirmed that it is faulty.  He will replace a functional p/s tomorrow. 


 Friday, May 18, 2012, 13:24

The original p/s was replaced with a new one and there was still a discrepancy between the readback and the setpoint.  After checking with the drawings for the ITE/ITW tube heaters, it was confirmed that the connections for the Evap#2 tube heater control were wrong.  (see attachment 1).  The connections were corrected and the power supply is now operational. 


 

Attachment 1: tubeheater_control.png
tubeheater_control.png
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