Tuesday, June 16, 2015, 14:28, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Source Tray Installation/Water Block Sealing Surface Clean
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Today cleaning and polishing pads were inserted into the hot cell.
Module side waterblock jig installation was attempted however one of the locking tabs/latches (ITA2405?) came undone/fell off. Luckily, I had old,
obsolete jigs in the hot cell so I was able to remove parts I needed from an old one and rebuild the current one. |
Wednesday, June 17, 2015, 14:21, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Waterblock Clean Polish
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Fiberglass that fell out yesterday was put back in place (as well as possible).
Cleaning took place this morning with excellent results. Cleaning was performed with red scotch brite on the cleaning tool, air pressure at 40
psi while running, with one 60 second cycle. Three blocks (EE, HS and Window) needed a second pass to remove the indium. |
Thursday, June 18, 2015, 08:03, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Optics Tray Transfer
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The TM2 optics tray has been transferred from the source tray to the transfer fixture in preparation for installation of the source tray into the module. |
Friday, June 19, 2015, 11:57, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Source Tray Progress
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Window waterline has been successfully connected using 1 1/2 inch long non-blunt start 1/4-28 bolts.
All bolt torques have been checked with dial torque wrench and are confirmed to be tight to 90 in lbs. |
Friday, June 19, 2015, 13:00, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Source Tray Install Status
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Left manipulator now broken. Master side however, so repair can take place Monday or Tuesday. |
Tuesday, June 23, 2015, 10:55, chad fisher, South Hot-Cell, Repair, , , Left Manipulator Repair
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The master wrist/tong cable has been replaced on the left manipulator. Everything appears to function well so far. |
Tuesday, June 23, 2015, 14:19, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Water Block Jigs Removed
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Both halves of the water block jigs have been removed and the module is now ready for base vacuum leak and electrical checks.
During removal of the jigs the fiberglass that had been "shoved" by hand in between two of the lines in the early 2000's fell out again. |
Wednesday, June 24, 2015, 10:16, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Vacuum Leak Check
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The following circuits have been vacuum leak checked and have not registered any leaks:
Circuit D, C, B, A, Coil2, EE, Ground Electrode, Mounting Support plate, Coil 1.
Left are Heat Shield and Window circuits which will be checked after blank offs are installed on the vcr terminations. |
Friday, June 26, 2015, 09:44, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Retrofit Status
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On June 25th the following work was completed:
Optics tray was installed into TM2. The lower fastener on the vertical cable tray (IRH1585) needed to be removed and vertical cable tray rotated
upwards as optics tray would not clear cable tray. Optics tray was intstaled, cable tray repositioned and screw re-inserted. |
Friday, June 26, 2015, 09:45, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Status
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Containment box window waterlines have been connected and leak checked and new containment box cover installed.
Module ready for transport just before 9am. |
Tuesday, June 30, 2015, 09:47, chad fisher, South Hot-Cell, Repair, , , manipulator repair
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The right hand manipulator has been repaired. It took 43 minutes and I received ~ 0.56 mSv |
Tuesday, June 30, 2015, 12:37, chad fisher, South Hot-Cell, Standard Operation, TM1, UCx#12, UCx #12 Removal
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UCx#12 has been removed from TM1 and placed in a pail with argon.
Right leg (B) of target is clearly broken.
Containment Box cover re-installed and module ready to move. |
Friday, July 03, 2015, 11:33, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Coil Leak Progress
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First thing this morning the hot cell was "cleaned up" in preparation for the return of TM2 for attempted verification and locating of leak
on R/U coil circuit.
Containment box has been removed and front cover reinstalled to provide some modicum of shielding form the entrance and exit windows. Box was placed |
Friday, July 03, 2015, 13:29, chad fisher, South Hot-Cell, Repair, TM2, , Hot Cell/ Module Fields
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Field measured at block "R" through tool port with pole monitor is 6.65 mSv/H.
There are three air hoods and two air lines currently available. |
Wednesday, July 08, 2015, 12:18, chad fisher, South Hot-Cell, Repair, TM2, , R U Coil line Removal
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R U coil line removal started at 11:30. Water block jig installed and coil line disconnected from module. |
Wednesday, July 08, 2015, 14:48, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Status
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Water block jig has been removed. Stuck source tray side water block jig component has been removed. An attempt was made to connect the gas lines to
there bracket however they contact/interfer with the tube heater lines...Anders is looking into a solution.
Containment box and front cover have been replaced and TM2 is ready to move to the silo. |
Thursday, July 09, 2015, 13:51, chad fisher, South Hot-Cell, Repair, TM2, , Coil line removal hot cell
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coil line has been removed from the hot cell. Initial decon was performed...after it still appears to have approximately 200 counts. It will now be transfered
to the rad waste decon facility for further decon. |
Friday, July 10, 2015, 09:33, chad fisher, South Hot-Cell, Repair, TM2, , Coil Line Decon
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Coil line has been in RPG's ultrasonic decon over night. Initial swipes this morning picked up 5000 counts. It has been decontaminated to the point no
more contamination is being found and nothing can be found with the frisker...so...it's ready for Maico and Dan? |
Tuesday, July 14, 2015, 12:56, chad fisher, South Hot-Cell, Repair, TM2, , TM2 containment box removed
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Containment box was removed from Tm2 this morning in preparation for installation of coil line and all the trimmings. |
Wednesday, July 15, 2015, 09:44, chad fisher, South Hot-Cell, Repair, TM2, , Coil Line replacement
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water block jig installed, module side sealing surfaces re-polished and cleaned. Coil line inserted into the hot cell and installed onto the module.
Bolts torqued to 90 in.lbs. Received .13mSv. |
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