Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 78 of 138  Not logged in ELOG logo
Entry  Tuesday, July 07, 2020, 17:43, Carla Babcock, ITE, Development, TM4, , RF tests on new IG-LIS wiring 

Tested RF from RF driver into new IGLIS wires at ITE. Used 5V, 1MHz (2MHz setting because of internal halving issue).

As expected there was a very slight mismatch visible (original cable ~ 68 Ohms, new cable ~ 53 Ohms).

The matching resistor will be changed and it will be retested.

Entry  Wednesday, July 08, 2015, 12:18, chad fisher, South Hot-Cell, Repair, TM2, , R U Coil line Removal TM2_20150708_coil_line_leak.jpg

R U coil line removal started at 11:30. Water block jig installed and coil line disconnected from module.

Entry  Monday, May 27, 2013, 10:35, Bevan Moss, Conditioning Station, Standard Operation, TM4, Ta #40, Pumps Started HV testing to follow 

The pumps have been turned on at ~9:30 this morning. Current values are 6.61 Mohm TCS:DIC1 @19.4 C. HV testing will start momentarily.

Entry  Tuesday, January 02, 2018, 14:47, Anders Mjos, Conditioning Station, Standard Operation, , , Pumping on secondary vacuum 

Tuesday, January 02, 2018, 14:45: TP1S started

Entry  Thursday, August 18, 2011, 16:07, Bevan Moss, Conditioning Station, Standard Operation, TM1, UCx#2, Pump Down 

 Pump down in the conditioning station started at ~2:40 for rough down. The turbo pumps were turned on at ~3:30 and at 3:52 the pressures were reading as follows:

IMG in the containment box 9.2 x 10^-5 T

IMG in the secondary 2.0 x 10^-3 T

ION in the service cap 4.6 x 10^-5 T

Note that the cross has been installed on the vacuum vessel which now includes a turbo pump and the IMG 100.

Leak check will occur tomorrow.

Entry  Thursday, May 23, 2013, 14:12, Bevan Moss, Conditioning Station, Maintenance, , , Primary Circuit Drained and Flushed 

 Rob Walker has drained the primary side of the conditioning station. It will be flushed, filled  and chemically treated. It was desired to chemically treat the primary side before before but it took so long that sediment was found (things started to grow).

Entry  Friday, August 05, 2016, 14:13, Isaac Earle, North Hot-Cell, Development, , , Preparations for NHC Ventilation Test 

A hole was drilled in the NHC exhaust duct in the east end of the target hall above the hatch to the Ante Room.  This will be used for measuring NHC exhaust flow rate with a thermal anemometer.  The hole was tapped and plugged with an NPT tap.

Flow was measured in the existing hole in the SHC exhaust duct in approximately the same location.  Flow velocity was measured to be 1415 ft/min with the lid on the SHC.  Using duct ID 7.75", and assuming the average flow velocity is 90% of the flow at duct center, the flow rate was found to be 417cfm.  We will attempt to match this figure for the NHC when the ventilation tests are performed.  The tests have been scheduled for the maintenance day on Tuesday August 9th.

The anemometer probe and SHC test port plug were checked for contamination: none found.

Entry  Thursday, March 30, 2023, 14:29, Frank Song, ITE/ITW, Development, , , Preparation of target stations for FEBIAD runs 1_(5).png1_(2).png

Helium cylinder and  Argon cylinder are installed in both ITE/ITW faraday cages , regulator for outlet pressure are not set yet.

 

TO ITE :  Argon bottle size 14"L x 4"D with SV2 connected at pressure 900 Psi ( 70 bar )

               Helium bottle size 18"L x 7"D with SV1 connected at pressure 2000 Psi ( 130 bar )

TO ITW: Argon bottle size 15"L x 2"D with SV2 connected at pressure 1000 Psi ( 80 bar )

              Helium bottle size 18"L x 7"D with SV1 connected at pressure 2000 Psi ( 130 bar )

An Neon cylinder size 20"L x 6"D  at less than 100 psi ( <10 bar ) pressure stored in the cabinet of ITW cage without connection

two gas line connection pictures are attached here for reference.

Entry  Wednesday, May 15, 2013, 10:17, Bevan Moss, Conditioning Station, Standard Operation, TM3, No Source Tray, Preliminary Results from HV testing module_hv_test_0KV.rgaMODULE_hv_test_42kv.rgaTM3_13052013_no_source_tray.xlsx

 Testing on TM3 without a source tray was completed on 13/05.2013. All items were tied to common and the water blocks were left open at the bottom of the module. They were left with the quick connections at the top. The vacuum was in the low 10^-6T range so this was deemed acceptable. The cooling lines withing the cage in the target hall were shorted so flow could continue. As you will see from the results a maximum of 44kV was achieved before a major spark turned the power supply off. I will be compiling all the the data so it can be compared. Also attached is the archiver data, strip tool data, and RGA data.

Entry  Thursday, March 07, 2019, 12:20, chad fisher, South Hot-Cell, Repair, TM2, , Pre-polishing pictures 

Pictures of the water blocks before polishing can be found on docushare, collection 24400

Entry  Thursday, October 17, 2013, 17:16, Grant Minor, ITE, Repair, , , Pre-Separator-area (ITE Harp 9) Blocks Replaced 8x

The pre-separator-area blocks were replaced today by Bevan and Travis, with Grant present for photos and observation.

Photos are attached of each block replacement.

Some difficulty was encountered in replacing the "Layer #3" blocks (photo 9 attached).  An interference occurred between the outside of the west "Layer #3" block and an aluminum channel directly beside the rubber pad that supports the block.  The block was initially resting on this channel but slipped off, breaking off some concrete at the edge.   See photo 12 attached and notice crumbled concrete inside this channel around the area where the interference occurred. Photo 14 shows the damaged block edge.

It should be noted that when these two blocks are resting flat, there should be a gap between them (i.e. they should NOT be touching as shown in photo 9).

 

Entry  Thursday, December 21, 2017, 15:11, Anders Mjos, Conditioning Station, Maintenance, , , Powered down devices 

Powered down mechanical pumps in ISAC-I Experimental hall, vacuum gauge and turbo pump controllers in ISAC-I B2 North Hot Cell service area

Entry  Thursday, August 03, 2017, 17:08, Anders Mjos, Conditioning Station, Repair, TM2, , Power bump 

 Thursday, August 03, 2017, 17:08: Restarting vacuum and water system

Entry  Thursday, November 03, 2022, 16:41, Carla Babcock, North Hot-Cell, Standard Operation, , UCx#39, Post irradiation inspection UCx#39 

Did the PIE on UCx#39-IGLIS on Thursday Nov. 2 2022, couple pictures uploaded to docushare. Did not remove the target, just the heat shield cover.

Final electrical check on the module showed a dead short from TGHT/TBHT to HV common, which we did not see online. Seems like it must have occurred after ramp down? It persisted on the target after we removed it from the module. We couldn't find any obvious contact points, because it seems it did not happen while current was running in the target. Possible locations are the bottom support leg for the TBHT and the top of the right side target leg, though it was difficult to confirm with the camera.

Otherwise the only thing to note was a blacker-than-usual spot on the inside of the Cu heat shield, downstream in the proton direction.

 

Entry  Thursday, December 01, 2022, 13:45, Carla Babcock, North Hot-Cell, Standard Operation, TM4, C#4, Post irradiation inspection C#4 20221122_152435.jpg20221122_153033.jpg20221122_152407.jpg

Post irradiation inspection of C#4 which was running in TM4/ITE was conducted at the NHC on Nov. 22 2022.

The yields from this target had been dropping and its behaviour was erratic, with the voltages on the tube and target jumping all over the place sometimes. The ion current on the FCs followed the voltages. We took this to mean the target container was breaking down.

Upon inspection we found the container looked pretty damaged - highly crystallized and distorted. The container had gone banana-shaped, but not in the usual direction. It had curved  in the direction of the ion source (see photos). The heat shield and other surrounding components were super clean, no deposits or marks at all.

Entry  Thursday, June 29, 2017, 11:12, Anders Mjos, South Hot-Cell, Standard Operation, TM4, UC#20, Post Irradiation Examination (PIE) 

The target was inspected by Chad and Anders. Photos are available on DocuShare. It was noticed that the target tube heater terminals had lifted up from the insulator on the target assembly as seen in this Photo. This has later been detemined to be from the assembly, where additional clearance was required and achieved by installing washers.

Entry  Monday, September 24, 2018, 10:21, Anders Mjos, South Hot-Cell, Standard Operation, TM2, UC#23, Post Irradiation Examination (PIE) 20180924_161322929_iOS.jpg

UC#23 experienced short between target and heat shield as it was heated during operation. The inspection of the target after irradiation revealed that the left target leg was close to the heat shield opening and likely the cause of the short. Marks could be seen on the leg indicating contact. See attached photo. More photos are available on DocuShare

Entry  Tuesday, August 23, 2016, 08:05, chad fisher, South Hot-Cell, Maintenance, , , Post Hot Cell Entry Clean-up 

Plastic has been removed from the floor and any known active items in the hot cell moved to the south east corner in an attempt to shield the anteroom. Fields at the aluminum panel were reduced from 66 uSv/h to 58.8uSv\h. No contamination found on walls, floor, tacky mats, or standard aluminum cover. The aluminum cover with breathable air line hole did have 400 counts on 44-2, 1200 on ludlum.

 

Entry  Thursday, February 24, 2022, 13:23, David Wang, ITE/ITW, Maintenance, , , Polyurethane water cooling lines replacement in ITE and ITW.  

Polyurethane  water cooling lines in ITE and ITW  HV shroud are replaced.  Both stations Ta, Tu, MSP, HS, Coil , EE in HV shroud are new lines.

Entry  Thursday, June 27, 2013, 14:27, chad fisher, South Hot-Cell, Development, , , Polishing Cleaning tool - Water blocks 20130626_144941.jpg

The polishing/cleaning tool prototype is now finished and appers to work great.

Thanks to Dan and Maico for the great job making my design a reality.

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