ID |
Date |
Author |
Category |
Type |
Module |
Target/Number |
Subject |
1494
|
Thursday, April 13, 2017, 10:32 |
chad fisher | South Hot-Cell | Repair | TM3 | | TM3 Lower Service Tray Video Inspection |
A video inspection of the lower service tray was performed this morning. Camera was inserted upwards into the service tray/service chase from the containment box. One potential spark mark was identified as well as epoxy not flush with insulator. Fiberglass does not extend into service tray/chase much and does not look, from initial inspection that it will be too difficult to remove.
Video can be found in docushare Document-142295 |
1493
|
Wednesday, April 12, 2017, 16:39 |
Aurelia Laxdal | South Hot-Cell | Repair | TM3 | no target | TM3 Inspection at the South Hot Cell |
Found spark signs on TM3's containment on the side of the water blocks. They may be OLD or/and NEW sparking signs, but this in not determined at this moment. Please see picture: first attachment. First and second attachment show the profiles of water block and HV lines. |
Attachment 1: DSC_0886.JPG
|
|
Attachment 2: DSC_0883.JPG
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|
1492
|
Wednesday, April 12, 2017, 13:03 |
Travis Cave | South Hot-Cell | Standard Operation | TM3 | no target | Electrical Check |
Electrical check of TM#3 with no target at the south hot cell |
Attachment 1: TM3_elec_chk_no_tgt.PDF
|
|
1491
|
Wednesday, April 12, 2017, 12:51 |
David Wang | South Hot-Cell | Repair | TM3 | | TM3 Ram readings @ SHC |
We have a ram installed on SHC pole which is 0.5 meter to module shielding block surface. the readings we got today during TM3 move:
at containment box center (highest reading): 3.14 msv/hr.
at bottom of shielding blocks: 960 usv/hr.
at 1/4 of shielding blocks height from bottom :700usv/hr.
at 1/2 of shielding blocks height from bottom: 340usv/hr.
at 3/4 of shielding blocks height from bottom:140u/sv/hr.
The Ram is behind the pole and measured the surface which is 90 degree right side of that opened service tray side. |
1490
|
Wednesday, April 12, 2017, 09:20 |
Travis Cave | South Hot-Cell | Repair | TM3 | no target | Module move |
TM#3 is now in the south hot cell. |
1489
|
Wednesday, April 12, 2017, 07:26 |
David Wang | Conditioning Station | Standard Operation | TM2 | | TM2 and TCS vacuum system has been connected. |
Roughing down overnight. Turbo pumps are started this morning. Everything looks good so far. |
1488
|
Tuesday, April 11, 2017, 14:06 |
David Wang | Conditioning Station | Standard Operation | TM4 | | SHC, TM2 leak check on HS line. |
Chad and I did leak check on TM1 HS line at SHC. 0.0XE-9 atm.cc/sec. No leak. |
1487
|
Tuesday, April 11, 2017, 14:02 |
Travis Cave | Conditioning Station | Standard Operation | TM2 | Ta#51 | module moved |
TM#2 with Ta#51 has been moved from the south hot cell to the conditioning station. |
1486
|
Tuesday, April 11, 2017, 11:30 |
Travis Cave | South Hot-Cell | Standard Operation | TM2 | Ta#51 | Electrical Check |
Electrical check performed on TM#2 with Ta#51, see attached PDF. |
Attachment 1: TM2_Ta51_SHC_elec_chk.PDF
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|
1485
|
Monday, April 10, 2017, 11:23 |
Travis Cave | Conditioning Station | Standard Operation | TM1 | no target | Module move |
TM#1 has been moved from the conditioning station to the north west silo. There was a slight delay in the move as the limits for the hoist drum got way out of whack and had to be adjusted. |
1484
|
Friday, April 07, 2017, 09:53 |
Travis Cave | Conditioning Station | Maintenance | TM1 | no target | Electrical Check and TM1 other checks |
Results of an electrical check on TM#1 with no target attached to it.
I use this e-log entry for TM1 notes as well 1. TM1 IG1 is a dual filament gauge . Its filament is very close to grid now. It shorted one time during the pumping down. It still works fine so far . But, we may need to change it if we use this module in TS again.
TCS 1G1 and 1G1S are pumped to 5Xe-6 torr. IG2 stayed at 2.5XE-5 torr. Since no target is installed on module , I capped top of HS water line. Maybe, the small o-ring seal in cap is too old, I found a big leak on this seal when i use LD check it. That is the reason IG2 stayed too high. Still, Leak check and helium presuure test are fulfilled on TM1. Leak detector BLR 5XE-7 atm.cc/sec, BP 0.0XE-4 torr9. Back up pressure is 51 mtorr which is high because of leak on HS line cap seal so LD BLR is high. At this level, Ta+-, Tube +-, MSP, EE are good. Other air to vacuum seal are good as well at this leak rate. I will check and change small o-ring seal in HS cap. The TM1 is functional basically. |
Attachment 1: TM1_elec_chk_no_tgt.PDF
|
|
1483
|
Thursday, April 06, 2017, 15:16 |
Anders Mjos | Conditioning Station | Maintenance | | | Installation of new break out box to accommodate both ITM:MP2 and TCS:MP1 |
Installation by Marshall. Dave M from controls adjusted circuitry to get TCS:MP1 to start.
Work is being done in preparation for the Module Move Ventilation SAS project |
1482
|
Thursday, April 06, 2017, 15:11 |
Grant Minor | Crane | Maintenance | | | Target Hall Crane 20 ton hoist - Report by Gordon Crane 5-Apr-2017 |
-------- Forwarded Message --------
Hi Curtis
Further to the emergency service call at the Isac Target Hall on Thursday March 23rd, we advise as follows:
It was reported that the hoist was making an unusual noise and that there was a strong brake odour during operation.
The lift was completed using the auxiliary hoist.
A man-lift was arranged and Senior Service Technician Tom Kauss attended site the next morning to troubleshoot.
He determined that one of two hoist brakes (walkway side) had a strong odour and on closer examination it appeared that the
brake lining material was breaking down and particulate lining material was getting caught between the lining and the discs.
These lining fragments were rubbing and burning off during the hoist operation.
The end cover of the brake had an accumulation of brake lining fragments
The lining was not overly worn, but appears to be becoming friable, perhaps with age or exposure to radiation.
The brake was cleaned with compressed air to remove the friable material and thoroughly tested.
A test load of approximately 10 tons was lifted and the hoist handled the load without issue
The brake fragment issue did not recur while we on site and the hoist was recommissioned for use.
To guard against the likely recurrence of this condition on this critical application crane, and as both brakes have seen identical conditions in operation,
we recommend that both brake assemblies be replaced.
The brake assembly would include the brake coil, friction discs, steel brake discs and the brake springs
TRIUMF does not have a spare brake on hand, therefore one of the removed brakes could be rebuilt and kept on hand.
Two (2) each XL-60009637 Complete Brake Assemblies $ 5,706.00 Each
One (1) only XL-60009674 Brake Repair Kit $ 2,435.00
For Rebuild
One (1) only XL-52272125 Brake Spring Kit $ 59.72 For Rebuild
Installation & Testing of New Brakes estimated at: $ 1,250.00 Lot
We have one brake in stock in our Vancouver Service Depot. A second brake is available Ex-Ontario
FOB Site
Applicable Taxes Extra
Quote Valid for 30 days, subject to prior sale.
We are available next week to perform this work on site.
Please let us know if you have any questions or if you would like us to proceed.
Best Regards
Aidan
------------------
Aidan C. Gordon
General Manager
aidan@gordoncrane.com
Gordon Crane & Hoist Inc.
Celebrating 34 years of Excellence (1983-2017)
www.gordoncrane.com
Toll Free 1-866-HOIST-IT
(1-866-464-7848)
Tel: (604) 324-2441
105-8475 Ontario St
Vancouver BC V5X 3E8
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|
1481
|
Thursday, April 06, 2017, 12:33 |
David Wang | Conditioning Station | Repair | TM1 | | TM1 rust inpsection and removal |
TM1 inside service cap surface and shielding plug surface are visually inspected yesterday. No rust has been found. I cleaned all rust on top of TM1 today. Rust on TM1 silo top plate are cleaned as well. |
1480
|
Wednesday, April 05, 2017, 14:13 |
David Wang | Conditioning Station | Maintenance | TM1 | | TM1 and TCS vacuum system are connected together |
I started two turbo-pumps on TM1 and one small TP on TCS. They are work fine. |
1479
|
Wednesday, April 05, 2017, 11:57 |
David Wang | ITE | Maintenance | | | ITE target module flange o-ring repalcement |
ITE target module tank flange o-ring was replaced yesterday before TM4 moving. ITE: IG1S reading looks fine so far. |
1478
|
Wednesday, April 05, 2017, 09:46 |
Travis Cave | Conditioning Station | Standard Operation | TM1 | no target | module moved |
TM#1 has been moved from the North West silo to the conditioning station. |
1477
|
Tuesday, April 04, 2017, 14:40 |
David Wang | ITE | Standard Operation | TM4 | | TM4 has been connected in ITE |
all turbo-pumps are started. Everything looks fine so far. |
1476
|
Tuesday, April 04, 2017, 14:39 |
David Wang | Crane | Standard Operation | | | Crane check main hoist on jogging with shielding plug lifted. |
Today, I checked TH crane main hoist when shielding plug is installed into ITE pit. I did some jogging actions on main hoist during the operation. Everything looks fine. No burning smell, no strange noise. An outside crane expert suggest that jogging is the worst working situation for crane. We have to use jogging actions during our crane operation. But, we could try to use less jogging when operate the crane. |
1475
|
Tuesday, April 04, 2017, 10:24 |
David Wang | Conditioning Station | Standard Operation | TM4 | | Stopped TCS pumps this morning |
Argon vented TCS and TM4 after pumps are stopped. |