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Entry  Tuesday, May 02, 2017, 18:33, Aurelia Laxdal, South Hot-Cell, Repair, TM3, no target, TM3 HV tests at atmosphere for Each Line(s) after the Fiber Glass removal May 2, 2017 

Today a HV test at atmosphere was performed for Each Line(s), while floating the other lines. THIS TEST AT ATMOSPHERE IS THE FIRST ONE AFTER THE FIBER GLASS WAS REMOVED.

Please note:

a). the Einzel Lens line (Y) was grounded.

b). after the fiber glass was removed the "R-U COIL" line and the "(F) Plasma" (which is the Anode line) were shorted to the BIAS voltage.

Tests performed:

1. Applied up to 32kV to "(A) OVEN -"

Sparks occurred at 32kV between the Extraction Electrode holder and the Ground Electrode.

2. Applied up to 33kV to "(B) OVEN +"

Sparks occurred at 33kV but we could not identify the spark location.

3. Applied up to 31kV to "(C) TUBE -"

Sparks occurred at 31kV between the Extraction Electrode holder and the Ground Electrode, at the top and the bottom.

4. Applied up to 30kV to "(D) TUBE +"

Sparks occurred at 30kV between the Extraction Electrode holder and the Ground Electrode, 2 spots at the bottom.

5. Applied up to 30kV to "(P-Q) COIL +"

Sparks occurred at 30kV between the Extraction Electrode holder and the Ground Electrode, all around.

6. Applied up to 30kV to "(R-U) COIL -", to "(F) Plasma" the Anode, to "(E) Cavity" or MSP, "(G) Gas", and  "(J) Heat Shield" - all these are "connected" together at the BIAS voltage.

Sparks occurred around 29-30kV at the Extraction Electrode holder and the Ground Electrode, at the bottom.

8. Applied up to 23kV to "(I) EE" - this is for the Extraction Electrode.

Sparks occurred at 23kV again at the same spot near the bottom, between the Extraction Electrode holder and the Ground Electrode.

 

Entry  Tuesday, May 02, 2017, 13:49, Travis Cave, Spent Target Vault, Standard Operation, , , Spent Targets moved Mini_Vault_Storage_May_2_2017.pdfVault_Storage_May_2_2017.pdf

Five spent targets have been moved from the target storage vault to the mini vault in preparation for Thursdays loading of the F-308s. See attached for the list of targets in the mini vault, and the new status of the storage vault.

Entry  Tuesday, May 02, 2017, 09:48, Isaac Earle, North Hot-Cell, Development, , , NHC polycarbonate window cover panel installed IMG_0066.JPGIMG_0068.JPGIMG_0071.JPGIMG_0074.JPGIMG_0076.JPG

 The window cover panel has been installed on the hot side of the NHC shielding window according to drawing IRH1638.  It was necessary to drill and tap a hole in the steel frame first to achieve proper grounding for stud welding.  The strength of all studs were checked by installing a nut on the stud tightened against a block up against the steel frame, which was then torqued to a minimum of 10 ft*lbs.  For the final installation the nuts were each torqued to approximately 3 ft*lbs.  Visibility from the cold side of the cell was checked before and after installation by Chad Fisher and Isaac Earle:  no distortion was caused by the new cover panel and with the in-cell work lights aimed in a similar direction to how the permanent lights will be installed (shining down from the roof, and also aimed south from the periphery of the window) there was no significant decrease in visibility of the work space.  A couple of small scratches are visible on the panel surface - these were already there when the panel arrived at TRIUMF.  The panel has been installed in an orientation that will minimize the visibility of these scratches during normal work.  When the work lights were aimed at the window many imperfections in the panel were visible, however this is not expected to occur during normal operation.  After the cell lighting has been installed the visibility will be re-evaluated and a new panel can be procured if necessary.  

 

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IMG_0071.JPG

 

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Entry  Monday, May 01, 2017, 13:11, David Wang, South Hot-Cell, Repair, TM3, , Electrical Check on TM3 after fibergalss is moved in SHC.  

RU( coil 1), F (anode), and 60kv bias(HS, Gasline, and MSP)  are shorted together. Other lines are good.  They are measured between  individual line each other  @500V. The megga showed OL. All of  them to ground are OL @500V as well. EL is grounded during check.

Entry  Monday, May 01, 2017, 12:32, David Wang, Crane, Repair, , , TH crane burning smell 

TH crane burning smell showed again this morning. It appeared after 1-1.5 hours of continuously using during the F308 flasks moving in TH.After a certain time of using I think the brake gap is reduced because of  thermal expansion. The main hoist and brakes work fine still. We knew these brakes gap are tight especially on west side. So, It is not surprised that this burning smell appeared again. It does not affect the safe of crane use in my view. But, The life of this brake assembly could be affected.  I would like everyone know this issue. We may need to consult Gordon crane as well. Maybe, The gap should be increased up a little bit.  On this Friday, I will use crane to transfer 30K lbs shielding blocks. It will be a good test on crane main hoist again. 

Entry  Monday, May 01, 2017, 08:53, chad fisher, South Hot-Cell, Repair, TM3, , Fiberglass removal 

Fiberglass, capton tape and tie straps have been removed from TM3.

Entry  Sunday, April 30, 2017, 20:57, Aurelia Laxdal, South Hot-Cell, Repair, TM3, no target, TM3 May 1-15, 2017 Tentative Schedule at the SHC and TCS May_2107_TM3_Schedule_at_the_South_Hot_Cell_and_TCS.docx

Please see attachment for TM3 May 1-15, 2017 Tentative Schedule at the SHC and TCS.

Entry  Friday, April 28, 2017, 12:04, Anders Mjos, Conditioning Station, Maintenance, , , MP1 problem 

TCS:MP1 was tripping of intermittently yesterday. It was found by Dave Morris that the current sensor was not set correctly causing the pump on status to flicker at times. Dave adjusted the settings yesterday. The system should be operational and is currently running normally.

Entry  Thursday, April 27, 2017, 19:59, Aurelia Laxdal, South Hot-Cell, Repair, TM3, no target, TM3 HV tests at atmosphere for Each Line(s) April 27, 2017 

Today a HV test at atmosphere was performed for Each Line(s), while floating the other lines.

Please note the Einzel Lens line (Y) was grounded.

Tests performed:

1. Applied up to 29kV to "(A) OVEN -"

Sparks occurred at 29kV at the Fiber Glass inside the Service Tray; and at the right side at the lines wrapped in Fiber Glass.

2. Applied up to 29kV to "(B) OVEN +"

Sparks occurred at 29kV at the Fiber Glass inside the Service Tray.

3. Applied up to 6-7kV to "(C) TUBE -"

Could not identify the sparks; it was a continuous discharge.

4. Applied up to 6-7kV to "(D) TUBE +"

Sparks/discharges occurred at 6-7kV at the Fiber Glass on the right side at the lines wrapped in Fiber Glass. We had to turn OFF the lights in the Hot Cell to identify the small sparks.

5. Applied up to 4kV to "(P-Q) COIL +"

Discharge occurred at 4kV. Could not identify it.

6. Applied up to 29kV to "(R-U) COIL -"

Sparks occurred around 27-29kV at the Fiber Glass inside the Service Tray; and at the right side at the lines wrapped in Fiber Glass.

Tom saw a spark at 27kV between the Extraction Electrode holder and the Ground Electrode.

Saw also a spark at the Ring Alumina insulator in the Service Tray, located on top of the second comb insulator with Epoxi.

7. Applied up to 27kV to "(E) Cavity or MSP, (G) Gas, (J) Heat Shield" - all these are connected together at the BIAS voltage.

Sparks occurred at 27kV at the Fiber Glass inside the Service Tray.

8. Applied up to 23kV to "(I) EE" - this is for the Extraction Electrode.

Sparks occurred at 23kV again at the same spot near the bottom screw hole, between the Extraction Electrode holder and the Ground Electrode.

9. Applied up to 27kV to "(F) Plasma"- this is for the Anode.

Sparks occurred at 26-27kV again at the same spot near the bottom screw hole, between the Extraction Electrode holder and the Ground Electrode.

Entry  Thursday, April 27, 2017, 16:58, Isaac Earle, North Hot-Cell, Development, , , Right side NHC manipulator installed IMG_0036.JPGIMG_0046.JPGIMG_0054.JPGCRLD-1046-B_rev_1_Installation_Removal_Manual_(July_2013).pdfManipulator_Cart_User_Manual__(CRLD-1003).pdf

 Installation of the NHC right side manipulator was completed yesterday.  The three piece manipulator was assembled in the module assembly area on the manipulator cart which was then craned through the hatch to the NHC service area (the slave end had to be removed for it to fit through the hatch).  The installation went relatively smoothly except for the second (cold side) piece of lead shielding around the thru tube which would not fit because the OD of the two halves were not concentric when assembled (arrived this way from CRL).  The shielding was removed and 0.070" was cut down on the lathe, after which installation could be completed.  The slave end lift bail and the pulley cover panel had to be removed for the manipulator to fit through the thru-tube.  Both these items were reinstalled after the manipulator was in the wall, and it was confirmed that the slave end lift bail aligns with the slave-end removal hatch in the NHC roof.  There was some difficulty getting the slave end to the horizontal position using the Y motion drive, also while preparing the manipulator for installation we noticed one of the Z motion tapes on the master side was sliding to the edge of one of the pulleys and rubbing - both these issues will be investigated at a later date.

We confirmed that it is possible to remove the master end using the manipulator cart.  We will practice doing this at some point before the cell is commissioned.  We will also do a run-through of slave end removal through the NHC roof.

Electronic copies of the Model-N installation and removal manual as well as the manipulator cart user manual are attached for future reference.

 

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Entry  Wednesday, April 26, 2017, 17:55, Aurelia Laxdal, South Hot-Cell, Repair, TM3, no target, TM3 Schedule updates at the South Hot Cell and CS April_–_May_2107_TM3_Updated_Schedule_at_the_SHC_and_TCS.docxApril_–_May_2107_TM3_Initial_Schedule_at_the_SHC_and_TCS.docx

Please see TM3's Updated Schedule (the current schedule) at the SHC and TCS.

For the record I am uploading TM3's Initial Schedule at the SHC and TCS.

Entry  Wednesday, April 26, 2017, 17:37, Aurelia Laxdal, South Hot-Cell, Repair, TM3, no target, TM3 HV tests at atmosphere Pictures from April 19-21, 2017 DSC_0950.JPGDSC_0899.JPGSparkMarkEETM3.jpg


Please see the first two pictures of the HV test at atmosphere done on April 19.

First picture shows a big spark between the Extraction Electrode mounting plate holder (at HV) to the Ground Electrode. Please note minimum gap between these electrodes is 7.8mm.

However the biggest visible spark was noticed at the bottom screw hole. (It is difficult to determine if at the 7.8mm gap were concomitant sparks occurring.)This spark started at 22kV and became stable above 24kV.

On April 20, 2017 Chad inspected this area with the Hot Cell camera and found a spark mark on the Extraction Electrode holder plate at the bottom screw hole. See the third picture.

Again it is very difficult with the existing Hot Cell cameras to inspect the areas where the gap is small (at 7.8mm gap between the conical surfaces of the Ground Electrode and Extraction Electrode holder)

In the second picture there are 2 small sparks: one on the top and another one on the right side at the lines wrapped in Fiber Glass. These sparks started at 20kV.

On April 21 the HV test was repeated with the Containment box ON and the sparks occurred again, at the same locations and at the same voltage.

Entry  Thursday, April 13, 2017, 10:32, chad fisher, South Hot-Cell, Repair, TM3, , TM3 Lower Service Tray Video Inspection 

A video inspection of the lower service tray was performed this morning. Camera was inserted upwards into the service tray/service chase from the containment box. One potential spark mark was identified as well as epoxy not flush with insulator. Fiberglass does not extend into service tray/chase much and does not look, from initial inspection that it will be too difficult to remove.

Video can be found in docushare Document-142295

    Reply  Wednesday, April 26, 2017, 16:52, Aurelia Laxdal, South Hot-Cell, Repair, TM3, , TM3 Lower Service Tray Video Inspection FiberGlassInST.tiff

chad fisher wrote:

A video inspection of the lower service tray was performed this morning. Camera was inserted upwards into the service tray/service chase from the containment box. One potential spark mark was identified as well as epoxy not flush with insulator. Fiberglass does not extend into service tray/chase much and does not look, from initial inspection that it will be too difficult to remove.

Video can be found in docushare Document-142295

 The attached picture is from the video: showing the fiber glass inside the Service Tray.

Entry  Wednesday, April 26, 2017, 13:35, chad fisher, South Hot-Cell, Repair, TM3, , TM3 containment box removed 

the containment box has been removed from TM3.

Entry  Wednesday, April 26, 2017, 10:40, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, Module move 

 TM#3 has been moved from the north east silo to the south hot cell.

Entry  Wednesday, April 26, 2017, 10:24, David Wang, ITW, Standard Operation, TM2, , TM2 ITW 

TM2 was moved and connected in ITW yesterday afternoon. After roughing down, ITW turbo pumps are started. ITW TP4 can not be started to full speed. ISAC ops kept it at low speed mode with less than 1.0A current draw on pump. ITW IG1s shows red as well. I will take a look on them today when beam is off.

 

Entry  Wednesday, April 26, 2017, 08:28, chad fisher, South Hot-Cell, Repair, TM3, , TM3 progress and manipulators 

containment box was re-installed onto TM3 on Monday, Left manipulator may be showing signs of eminent handle or tong cable failure.

Entry  Tuesday, April 25, 2017, 19:35, Grant Minor, Crane, Repair, , , ISAC Target Hall Crane - West Hoist Brake Rattle 

Below is a report on the ISAC Target Hall crane brake issue observed yesterday and addressed today:

 

- On April 13th, both the East and West hoist brake assemblies were replaced by Gordon Crane & Hoist, after David observed a burning smell

- The East assembly was replaced with a completely new brake assembly from Kone crane

- The West assembly was replaced with a refurbished assembly, which used the East assembly housing fitted with a rebuild kit by Gordon Crane

 

- Yesterday while preparing TM3 for a lift, David noticed a vibration / rattle sound coming from the West hoist brake

- This issue was only observed when starting the hoist from a complete stop, at the slowest possible upwards hoist speed

- Once the hoist speed increased, the sound went away, even after returning to a slower speed

 

- Tom from Gordon Crane & Hoist came in this morning at 7am and replaced the new West assembly with the original West assembly, which had at that point also been fitted with a rebuild kit at Gordon Crane’s shop

- Tom also inspected the East brake assembly again

- Tom commented that he had issues setting the right gap between the friction plates and the brake rotor – too close and the brake would not release properly, too far and the brake rattle issue would be observed

- He also commented that during this most recent repair of the West brake, he applied never seize to the shaft and spline to ensure that this friction point was not an issue

 

- After Tom finished his repair and inspection of the brakes, David attempted a test lift of an SEG block (10 ton) at the slowest lift speed

- The rattle noise coming from the West brake was still observed

- Travis also tested the slowest speed in Remote Test mode from the control room, with David and Grant present in the Target Hall, the rattle was also still observed

 

- Tom advised that the rattle would not affect the safety of the hoist, and no damage would be done to the brake assemblies by running the hoist normally with the rattle noise

- Tom ensured that he would consult with Aiden and they would likely order a brand new West brake assembly from Kone

- Tom called Aiden Gordon to confirm that it was ok to proceed

- Aiden called me around 1:30pm and left a message that the slow speed rattle sound was benign and that we could proceed with normal operations, but he would definitely address the problem moving forward, and we should standby for his report

 

Photos and video have been uploaded to Docushare.  The hoist noise before the repair and after the repair during the test lifts can be heard in the videos.

 

https://documents.triumf.ca/docushare/dsweb/View/Collection-19812

 

Thanks and regards,

 

Grant

 

--

Grant Minor, M.A.Sc., P.Eng.

TRIUMF Remote Handling Group Leader

Nuclear Engineer

4004 Wesbrook Mall, Vancouver

BC, Canada, V6T2A3

gminor@triumf.ca

(604) 222-7359

http://www.triumf.ca/profiles/4557

Entry  Monday, April 24, 2017, 16:11, David Wang, Conditioning Station, Standard Operation, TM2, , TCS TP1s is restarted. 

TCS IG1S  is switched on as well. The reason to start the pump is to prepare a possible extended TM2 conditioning at TCS caused by TH crane issue. TCS:TP1 and TP2 are not switched on for this.

Entry  Monday, April 24, 2017, 16:06, David Wang, South Hot-Cell, Repair, TM2, , Crane main hoist strane noise when lifting up TM2  

 When lifting up TM2 (20000lbs) this afternoon, TH crane has a strange noise on main hoist. The module was lift up less than 1 feet.when strange sound was noticed.  The module move was stopped right away,and module  was lowed back to SHC. The strange noise was confirmed later with SEG block six inches lifting up. Gordon crane technician will be here to tomorrow morning to investigate the problem.

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