Monday, June 29, 2015, 10:51, David Wang, Conditioning Station, Repair, TM2, , leak on TM2 side panel
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There is an air to vacuum leak on TM2 service cap side panel which we moved out during the TM2 wiring job. The CS pumps are stopped now. The CS will be vented soon. The seal on this panel has to been changed.
2016-06-30. The o-ring seal on this panel(PNG1 and steerers) is replaced and leak checked. No leak now. |
Tuesday, June 30, 2015, 15:53, David Wang, Conditioning Station, Development, TM2, , leak on TM2 at CS  
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I leak checked TM2 at CS this afternoon which including air to vacuum check on service cap and helium pressure test on water lines. There is a small leak on water line R ,U (COIL1) during the helium pressure test.. Below 20 psi helium, there is no leak on it. But , once the helium pressure is increased over 20 psi, it showed up on Leak Detector. At 60 psi helium, the leak rate is 9.4xE-9 atm.cc/sec. For detail information, See attachment. All other water lines and air to vacuum seals are good. |
Thursday, July 02, 2015, 10:22, Anders Mjos, Conditioning Station, Maintenance, TM2, , TP1S failed
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See e-fault 8233. Edi assisted in diagnosing the problem. The pump will have to be replaced. |
Friday, July 03, 2015, 09:11, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module moved
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TM#2 has been moved from the conditioning station to the south hot cell. |
Friday, July 03, 2015, 09:41, David Wang, Conditioning Station, Standard Operation, TM2, , Target Hall Scheduled Activities April 07 - July 24 2015   
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Updated the schedule before the weekend 2015-07-03. See attachment 1,2
Updated the schedule according to present TM2 refurbishment process. See attachment 3,4 |
Friday, July 03, 2015, 11:33, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Coil Leak Progress 
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First thing this morning the hot cell was "cleaned up" in preparation for the return of TM2 for attempted verification and locating of leak on R/U coil circuit.
Containment box has been removed and front cover reinstalled to provide some modicum of shielding form the entrance and exit windows. Box was placed at an angle in the corner to try and minimize line-of-sight with potential worker(s).
Did notice some funny discoloration of both sides of coil water block "R" as seen in attached picture. |
Friday, July 03, 2015, 13:29, chad fisher, South Hot-Cell, Repair, TM2, , Hot Cell/ Module Fields
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Field measured at block "R" through tool port with pole monitor is 6.65 mSv/H.
There are three air hoods and two air lines currently available. |
Wednesday, July 08, 2015, 12:18, chad fisher, South Hot-Cell, Repair, TM2, , R U Coil line Removal
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R U coil line removal started at 11:30. Water block jig installed and coil line disconnected from module. |
Wednesday, July 08, 2015, 14:05, David Wang, South Hot-Cell, Repair, TM2, , leak check coil line(R,U) on TM2 at SHC
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Chad and I leak checked coil line(R,U) on TM2 at SHC yesterday. The leak detector was pumped down to 0.0Xe-9 atm.cc/sec before the check. Chad sprayed helium on the soldering joints connecting the cooling copper lines to the small holding blocks for the coil terminal(R,U). After sprayed helium 2 seconds, I saw the leak rate on LD started to climbed up. The highest leak rate is 4.0xE-8 atm.cc/sec. It is a very positive response. We waited the leak detector pumped back to 0.0xE-9am.cc/sec, and tested again on the same joints. The result is same. Chad also sprayed helium on the R,U water blocks to check the C-seal. I saw a delayed tiny response on LD ( from 0.0 to 1.3xE-9atm.cc/sec). We think this tiny response is caused by the helium drifting to the leak soldering joint, but not a real C seal leak. |
Wednesday, July 08, 2015, 14:24, David Wang, South Hot-Cell, Repair, TM2, , TM2 pressure bubble test on RU water blocks.
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July-06, 2015. Chad , Grant and I did the bubble test on R,U water blocks. We suspected the leak on the R,U circuit is from C seals on the water blocks so we did this test first. I applied both air and helium to R,U circuit , Chad applied snoop soap on the R,U water blocks.The air and helium pressure was increased from 40 psi to 90 psi Max step by step.Chad did not see any bubbles on the water blocks during the test. Since we did not find the leak source, we decided to do vacuum helium check on the all joints and c-seals of the R,U lines later. Finally, We found the leak by vacuum helium spray the day after this bubble test. See other e-log. |
Wednesday, July 08, 2015, 14:48, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Status
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Water block jig has been removed. Stuck source tray side water block jig component has been removed. An attempt was made to connect the gas lines to there bracket however they contact/interfer with the tube heater lines...Anders is looking into a solution.
Containment box and front cover have been replaced and TM2 is ready to move to the silo. |
Thursday, July 09, 2015, 09:55, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module moved
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TM#2 has been moved from the south hot to the north east silo. TM#1 has been moved from the south west silo to the conditioning station. |
Thursday, July 09, 2015, 13:51, chad fisher, South Hot-Cell, Repair, TM2, , Coil line removal hot cell
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coil line has been removed from the hot cell. Initial decon was performed...after it still appears to have approximately 200 counts. It will now be transfered to the rad waste decon facility for further decon. |
Friday, July 10, 2015, 09:33, chad fisher, South Hot-Cell, Repair, TM2, , Coil Line Decon
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Coil line has been in RPG's ultrasonic decon over night. Initial swipes this morning picked up 5000 counts. It has been decontaminated to the point no more contamination is being found and nothing can be found with the frisker...so...it's ready for Maico and Dan? |
Tuesday, July 14, 2015, 08:42, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module moved
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TM#2, no target, has been moved from the north east silo to the south hot cell. |
Tuesday, July 14, 2015, 12:56, chad fisher, South Hot-Cell, Repair, TM2, , TM2 containment box removed
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Containment box was removed from Tm2 this morning in preparation for installation of coil line and all the trimmings. |
Wednesday, July 15, 2015, 09:44, chad fisher, South Hot-Cell, Repair, TM2, , Coil Line replacement 
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water block jig installed, module side sealing surfaces re-polished and cleaned. Coil line inserted into the hot cell and installed onto the module. Bolts torqued to 90 in.lbs. Received .13mSv. |
Wednesday, July 15, 2015, 11:02, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Coil Line Vacuum Leak Check
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TM2 coil line R,U has been vacuum leaked check at the hot cell and has passed with no response from the leak detector. |
Wednesday, July 15, 2015, 11:18, David Wang, South Hot-Cell, Repair, TM2, , leak check coil line(R,U) on TM2 at SHC 
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Chad and I leak checked the coil 1 circuit(R,U) after rebuilt coil line is installed on TM2 source tray. The pumping down on the circuit is very quick and smooth. The LD base lake rate 0.0xE-9 atm.cc/sec. Base pressure0.0xE-4 torr.
Chad sprayed lots helium on the R( coil 1+)and U(coil 1 -) water blocks. During 1 minute waiting time, there is no any response on LD. The R and U water blocks and C-seals are leak tight. |
Thursday, July 16, 2015, 14:36, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Status 
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IMG gauge, clip for ground to window lines and gas line extensions were installed today.
David and I also tried to locate the short between the coil line and MSP/Heat Shield...it went away for a bit...but is back. |
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