Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 45 of 139  Not logged in ELOG logo
Entry  Monday, June 10, 2019, 16:22, Carla Babcock, Conditioning Station, Maintenance, TM4, No target, Ramping V on TM4, no HV cover in TH 

Ramped down the bias so David could remove the HV cover and lock out the target hall.

Ramped back up to BIAS / EL = 50kV / 26kV quickly with no sparks.

Monday, June 10, 2019, 15:35 : BIAS / EL = 52kV / 26kV

Monday, June 10, 2019, 15:45 : BIAS / EL = 54kV / 28.5kV. It seems that keeping the EL at 1/2 the bias voltage is right on the edge of what is acceptable - the HV seems to be sparking to the EL instead of to ground (either that or the EM interference from the sparks it producing a reaction in the EL...) I will run the EL higher and see if that helps.

Monday, June 10, 2019, 15:57 : Sat at 54kV for > 10mins, will continue up

Monday, June 10, 2019, 16:11 : At BIAS / EL = 55.8kV / 29kV got some sparks, some to EL and some to ground. Back at 55kV.

Monday, June 10, 2019, 16:24 : Sitting at 56kV for a couple mins

Monday, June 10, 2019, 16:37 : Sitting at 56.3kV bias, a spark tripped off the IG1S, which tripped the turbo and shut down all the HV. Back to zero!

Entry  Monday, June 10, 2019, 14:13, Travis Cave, Spent Target Vault, Standard Operation, , , Old TM#4 source tray moved 

 The old TM#4 source tray in the south hot cell was moved to the spent target vault. The tray had a low of 7.5mSv/hr to a high of 22.1mSv/hr though a 390 degree rotation.

Entry  Monday, June 10, 2019, 08:26, Carla Babcock, Conditioning Station, Maintenance, TM4, No target, Ramping voltage on TM4 w/o source tray 

TM4 in conditioning station with no source tray, extraction electrode set to HV bias. Brought up to 30kV over the weekend by ISAC ops with no issues.

BIAS=30kV

EL=15kV

IG1=9.4e-7T

 

Monday, June 10, 2019, 08:21 : At 32.4kV on bias, EL at 15kV, bias sparked to EL. Every bump of 100V on bias is accompanied by a small vacuum jump and often by a small current increase from ~60uA to 120uA.

* Conditioning station read back and set values are off by 2kV but archive values show this has always been the case. Which to trust? *

Monday, June 10, 2019, 08:54 : Spark while sitting at 38kV on bias, 19kV on EL. Seems to be a spark to EL.  Sitting at 38kV for ~10mins

Monday, June 10, 2019, 09:32 : Sat at 40kV for ~10mins or so, bumping up again.

Monday, June 10, 2019, 09:38 : Spark to EL while sitting at BIAS / EL = 42kV / 20.5kV

 

Monday, June 10, 2019, 13:57 : Ramped to BIAS / EL = 43 / 21.2. No problems other than what seems to be the usual conditioning station stuff.

 Monday, June 10, 2019, 14:17  : Couple sparks on the way to 48kV, seems to be to the EL.

Monday, June 10, 2019, 14:36 : Up to BIAS/EL = 51/25.5 with no big problems. Will stay here for a couple mins

 

Entry  Friday, June 07, 2019, 13:11, David Wang, Conditioning Station, Development, TM4, , TCS and TM4.  

TM4 has been connected at TCS for HV test. TCS water system and vacuum pumps are switched on.

Entry  Friday, June 07, 2019, 08:56, Travis Cave, Conditioning Station, Standard Operation, TM4, no target, Module move 

 TM#4 has been moved from the south hot cell to the conditioning station.

Entry  Thursday, June 06, 2019, 10:01, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, no source Tray, Electrical Check TM4_Electrical_Check_No_source_Tray_SHC_June_6_2019.pdf

 Results from the electrical check of TM#4 at the south hot cell with no source tray. R&U are shorted and when meggered A&P have a value of 193k ohms. See attached for details.

Entry  Tuesday, June 04, 2019, 08:46, David Wang, ITE, Standard Operation, TM2, , ITE water signal interlock check. 

ITE water signal interlock check is done. Everything is good. Coil 2   circuit no longer used in ITE . PQRU are looped as one circuit fro coil 1 circuit on Module since now.

Entry  Friday, May 24, 2019, 09:11, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, Module move 

 TM#4 has been moved from the south west silo to the south hot cell.

Entry  Thursday, May 23, 2019, 11:22, Travis Cave, South Hot-Cell, Maintenance, , , Removing garbage from the south hot cell. 

 A 55 Gal. drum was remotely lowered into the south hot cell. It was then filled with compressable waste. Then the drum was remotely removed from the south hot cell. The drum measured about 20microSv/hr upon removal from the south hot cell.

Entry  Thursday, May 23, 2019, 08:39, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, Module move 

 TM#1 has been moved from the south hot cell to the northwest silo.

Entry  Wednesday, May 22, 2019, 11:52, David Wang, Conditioning Station, Maintenance, TM1, , TM1 inpsection. 

TM1 shielding plates and their holding bolts are inspected. No corrosion.  TM1 is located at TCS now. Both TP1 and TP2 are started.

Entry  Wednesday, May 22, 2019, 11:50, David Wang, ITE, Standard Operation, TM4, , TM2 has been connected in ITE. Ta58#TM2ITE_2019_June_._Conenction_checklist.pdf

TM2 has been connected in ITE. high active water system and vacuum pumps are started. The pumping down on TM2 and ITE is good  so far.

See attachment for connection checklist.

Entry  Wednesday, May 22, 2019, 08:33, Travis Cave, Conditioning Station, Standard Operation, TM1, no target, Module move 

 TM#1 has been moved from the north west silo to the conditioning station for the day it will be moved back to the silo tomorrow morning.

Entry  Friday, May 17, 2019, 16:46, Adam Newsome, Safe Module Parking, Development, , , SMP Controls Installation Update IMG_20190417_100838.jpgIMG_20190417_100843.jpgIMG_20190517_162230.jpgIMG_20190517_162305.jpg

 

The following controls-related items were installed for the SMP project:

- Cable tray

- Main control panel

- Motor starter box

- Wiring from limit switches and rotation motor to main control panel

- Air fittings at supply (quick disconnect)

- Main air supply hose from supply to control panel (quick disconnect)

- Air tubing from lid control valve at control panel to lid cylinders

 

Air fittings stem off existing air supply lines on the South wall, below a manual shutoff valve. A quick disconnect was installed. When SMP is not in use, manual shutoff valve should be left off.

 

Main control panel and motor starter box were mounted on the North wall. Wire duct runs from the main control panel to the grated floor. Cabling/air runs underneath the mezzanine platform, along existing and new cable tray, to the SMP.

 

Cable tray was installed on the South wall, from the corner to the SMP module. A cutout was made to accommodate for existing tubing. An additional ~1 ft. of tray will be added to the end, near the corner, at a future time.

 

Remainder of installation work to be done before commissioning:

- Mount and install new Opto-22 module
- Chain new Opto-22 module to existing one (power, comms) below mezzanine on North wall

Entry  Friday, May 17, 2019, 10:47, Travis Cave, ITE, Standard Operation, TM2, Ta#58, Module move 

 TM#2 with Ta#58 has been moved from the south hot cell to the east target station.

Entry  Thursday, May 16, 2019, 14:35, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#58, Electrical Check Ta#58_TM2_SHC_electrical_chk_May_16_2019.pdfElectrical_Chk_TM2_no_target_May_15_2019_SHC.pdf

 Results of the electrical check of TM#2 without target and with the new Ta#58 target.

Entry  Thursday, May 16, 2019, 12:31, chad fisher, South Hot-Cell, Standard Operation, TM2, Ta#58, Ta #58 installed 

Ta #58 has been installed onto TM2. All new silver plated high current fasteners. All torqued to 130 in lbs.

Entry  Wednesday, May 15, 2019, 16:06, Isaac Earle, Safe Module Parking, Development, , , SMP module support flange installed and leak checked 20190515_094730.jpg20190515_094740.jpg20190515_103253.jpg20190515_103824.jpg

The SMP module support flange sub-assembly (IRH1755) was installed today according to drawing IRH1683.  Dow Corning 111 sealing compound was used to keep the o-ring adhered to the lower groove during transportation and installation.  The TCS shield plug (IRH1646) was then installed on the SMP module flange which has vacuum connections for leak checking.  Vacuum was pulled on the SMP vessel using the Varian 979 leak detector.  After approximately 3.5 hours of pumping the test port pressure was at 2.4E-2 Torr and leak rate was 7.9E-8atm*cc/s.  Helium was configured with the regulator set at 10psi and flow rate of >10 bubbles per second in Windex and then applied slowly around the perimeter of the vacuum flange (IRH1686) and it's mating components on both  the top and the bottom.  There was no response on the leak detector indicating the seals on both sides of the module flange are leak tight.

 

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20190515_094740.jpg

 

20190515_103253.jpg

 

20190515_103824.jpg

 

 

 

 

 

Entry  Monday, May 13, 2019, 11:22, David Wang, ITW, Repair, , , ITW entrance module has been connnected. 

Entrance module has been connected back to ITW. Everything is normal.

Entry  Monday, May 13, 2019, 09:55, Travis Cave, ITW, Standard Operation, , , Entrance module move 

 The West Entrance module has been moved from the south hot cell to the west target station.

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