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  RH-ISAC, Page 43 of 138  Not logged in ELOG logo
New entries since:Wed Dec 31 16:00:00 1969
Entry  Tuesday, November 27, 2018, 11:05, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#57, Module move 

 TM#4 with Ta#57 has been moved from the east target station to the south hot cell.

Entry  Tuesday, November 27, 2018, 13:31, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#57, Ta#57 removal 

Ta#57 has been removed from TM4.

Entry  Wednesday, November 28, 2018, 11:31, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#57 and UC#26, Electrical Check Elec_Chk_Ta57_Post_Beam_SHC_11-28-28.pdfElec_Chk_TM4_no_tgt_SHC_11-28-18.pdfElec_Chk_UC26_SHC_11-28-18.pdfElec_Chk_UC26_IGLIS_part_SHC_11-28-18.pdf

 Electrical check of TM#4 with the old Ta#57, no target and with new IG-LIS UC#26 target. See attached PDF for details.

Entry  Thursday, November 29, 2018, 06:38, David Wang, South Hot-Cell, Standard Operation, TM4, , Leak check TM4 UCx 26 at SHC. 

Chad and I did a leak check on TM4 HS line with UCx 26# installed . Base LR 0.0X E-9 atm.cc/sec. Base pressure 0.0XE-4 torr.  No response on leak detector during leak check.

Entry  Wednesday, January 09, 2019, 10:47, Travis Cave, South Hot-Cell, Standard Operation, TM2, UC#25, Module move 

 TM#4 with UC#25 has been moved from ITW to the south hot cell.

Entry  Wednesday, January 09, 2019, 13:08, Travis Cave, South Hot-Cell, Standard Operation, TM2, UC#25, Electrical Check Electrical_Chk_TM#2_UC#25_post_beam_Jan-09-2019.pdf

 Electrical check of the target module with the UC#25 attached after the beam run.

Entry  Thursday, February 14, 2019, 14:02, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module move 

 TM#2 has been moved from the conditioning station to the south hot cell.

Entry  Tuesday, February 19, 2019, 10:20, chad fisher, South Hot-Cell, Repair, TM2, , Containment box removed 

Containment box has been removed from TM2 in preparation for source tray removal. I will walk Aaron through removal of the optics tray today also.

Entry  Tuesday, February 19, 2019, 11:56, chad fisher, South Hot-Cell, Repair, TM2, , Optics tray removal 

Aaron has removed the optics tray in TM2 in preparation for source tray removal.

Entry  Wednesday, February 20, 2019, 09:07, chad fisher, South Hot-Cell, Repair, TM2, , Module side waterblock jig 

I have installed the module side water block jig.

Entry  Friday, February 22, 2019, 10:31, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Source tray removal 6x

The source tray has been removed from TM2.

Entry  Monday, February 25, 2019, 09:44, chad fisher, South Hot-Cell, Repair, TM2, , Water block jig 

module side water block jig has been removed in preparation for electrical checks.

Entry  Tuesday, February 26, 2019, 08:51, chad fisher, South Hot-Cell, Repair, TM2, , TM2 containment box 

The containment box has been reinstalled onto TM2 in prepatation for testing in the conditioning station.

Entry  Friday, March 01, 2019, 09:57, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Source tray removal 20190228_095131.jpg20190228_143718.jpg20190301_074849.jpg20190301_092907.jpg

TM4 optics tray was installed onto the old TM2 source tray yesterday and tray filled with non-active metal scrap. Tray inserted into transfer frame 95% yesterday. During insertion the ball nut of the transfer jig became unfastened from its drive plate. This will have to be fixed before the jig can be used reliably again however we were able to finish the job...the transfer jig is 20 years old now so it is not entirely suprising that it needs some attention.

Today the Tm2 tray final install into the transport tray occurred by driving the tray drive screw and bringing the tray into the transfer frame the last inch 1/2 or so. "Feet" (ITA2380) had to be removed from sliding tray assembly to fit in the box however upon attempting this is was immediately clear that one of the screws was stuck and must have been cross threaded during assembly. As as result the entire drive bracket (ITA2375) had to be removed form the source tray to allow final insertion into the box.

11 handles from spent target transfers, 1 plastic bin box, Ta LP test target TRI coil, 1 aluminum box, sockets and extensions from spent target transfers and 5 obsolete legs from previous source tray replacements were amoung the items disposed of with the spent source tray.

Entry  Tuesday, March 05, 2019, 09:38, chad fisher, South Hot-Cell, Repair, , , Transfer Fixture Repair 20190305_092228.jpg20190305_092231.jpg20190305_092326.jpg20190305_092558.jpg

Transfer fixture has been remotely disassembled to the point where the ball nut lock plate assembly can be inserted into the tool port and the plate replaced by hand in the tool port without having to enter the hot cell. Straight head screws will be replaced with SHCS to facilitate easier re-assembly and future disassembly.

Entry  Tuesday, March 05, 2019, 14:29, chad fisher, South Hot-Cell, Repair, , , Tray Transfer Fixture Repair Complete 20190305_130312.jpg20190305_132303.jpg20190305_133800.jpg20190305_141346.jpg

Repair of the tray transfer fixture is complete (minus testing).

A distorted ball nut lock plate was replaced and thread loc added. to the ball nut/plate assembly. Testing will take place tomorrow once the thread lock has a chance to cure.

Entry  Thursday, March 07, 2019, 12:02, chad fisher, South Hot-Cell, Repair, TM2, , Box Off water block jig on 20190307_113548.jpg

The containment box has been removed from TM2 and the water block jig installed in preparation for water block polishing.

Entry  Thursday, March 07, 2019, 12:20, chad fisher, South Hot-Cell, Repair, TM2, , Pre-polishing pictures 

Pictures of the water blocks before polishing can be found on docushare, collection 24400

Entry  Thursday, March 07, 2019, 13:59, chad fisher, South Hot-Cell, Repair, TM2, , Polishing 

Polishing of the water block sealing surfaces has commenced. First attempt was on block B with low nap brown polishing pad (the least aggressive pad prepared) and isopropyl for 30 seconds. This cleaned a little but did not remove the "ring" which I believe is water scale. I will step up to 2000 grit wet sand paper and iso next.

Entry  Friday, March 08, 2019, 14:10, chad fisher, South Hot-Cell, Repair, TM2, , Water block polishing B_after_SB_(2).jpg

After trials with 2000 grid wet paper I have moved up to "red" scotch brite. This seems to have worked the best so far although it took two minutes to remove the ring that the other materials could not remove (see picture).

I have moved to next circuit. Currently at 3 minutes and 30 seconds with scotch brite but significant ring remains.

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