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  RH-ISAC, Page 34 of 138  Not logged in ELOG logo
ID Date Author Categorydown Type Module Target/Number Subject
  1131   Tuesday, November 24, 2015, 14:02 chad fisherSouth Hot-CellRepair  Left Manip repair

electronics package on left manip died completely yesterday (it has been going for a while).

Disconnected entire package and replaced with package from "spare" manipulator.

everything is back up and working.

  1132   Tuesday, November 24, 2015, 14:03 chad fisherSouth Hot-CellStandard OperationTM4 Ta#46

Ta#46 has been removed from TM4.

  1133   Wednesday, November 25, 2015, 11:52 Travis CaveSouth Hot-CellStandard OperationTM4Ta#46Module moved

Yesterday TM#4 with Ta#46 was moved from the east station to the south hot cell.

  1135   Wednesday, November 25, 2015, 14:13 chad fisherSouth Hot-CellStandard OperationTM4UC#14UCx#14

UCx#14 installed onto TM4. High current fasteners torqued to 130 in lbs.

  1136   Wednesday, November 25, 2015, 14:16 chad fisherSouth Hot-CellRepair  Cell Decon

Cell (table) was systematically cleaned with a swiffer and resulting piles of contaminated waste placed in pail with spent Ta target.

Attachment 1: 20151125_100512.jpg
20151125_100512.jpg
Attachment 2: 20151125_101620.jpg
20151125_101620.jpg
  1147   Wednesday, December 02, 2015, 10:41 chad fisherSouth Hot-CellRepair  Drum Clean-up #2

Another drum of waste was removed from the south hot cell this morning. This drum contained one 5 gal steel pail (damaged), two sodium light bulbs, airlines, and tank suits. Upon removal the drum was/is 1.5 mSv/h on contact. there was 200 counts of contamination found on the lid...easily removed. It will be moved to the north hot cell at 11am.

  1151   Friday, January 08, 2016, 09:29 chad fisherSouth Hot-CellRepair  Window Decon

Entered the hot cell to perform final decon on the window. Initial swipes this morning were 11000 c.p.m. on 44-2. After decon approximately 100 counts.

  1153   Friday, January 22, 2016, 14:24 David WangSouth Hot-CellStandard Operation  2016 Winter Shut Down Target Hall Schedule (sketch)

Post a sketch of 2016 winter shut down target hall schedule. see attachment 1,2

 UPDATE THE SCHEDULE ACCORDING TO CYCLOTRON SIDE JOB. SEE ATTACHMENTS 3,4

Attachment 1: 2016_winter_shut_down__target_hall_schedule.pdf
2016_winter_shut_down__target_hall_schedule.pdf
Attachment 2: 2016_winter_shut_down__target_hall_schedule.mpp
Attachment 3: 2016_winter_shut_down__target_hall_schedule.pdf
2016_winter_shut_down__target_hall_schedule.pdf
Attachment 4: 2016_winter_shut_down__target_hall_schedule.mpp
  1167   Wednesday, March 16, 2016, 14:23 chad fisherSouth Hot-CellStandard OperationTM2SiC#32SiC#32 removal Target Module Inspection

SiC#32 has been removed from TM2. Quick inspection shows some troubling discoloration on the water cooled connection blocks of C and D as well as the left target heater A.

As for the target, both legs are broken and is has the normal "charge up" marks on the 9 pin connector.

Attachment 1: 20160316_141127.jpg
20160316_141127.jpg
Attachment 2: 20160316_141146.jpg
20160316_141146.jpg
  1168   Thursday, March 17, 2016, 14:57 David WangSouth Hot-CellRepairTM2 TM2 first round leak check in SHC

Chad and I finished the first round check on Tm2 water lines. The lines and spots checked are: Target oven + and - (front side braze joints) , Tube heater+and -(front side braze joints and water blocks), coil2 and coil 1(front side braze joints and area close to water blocks),. No leak has been found on all above of them.  The last, we checked   the GE which has the biggest leak so far. The leak detector base leak rate only can get to 4XE-9 atm.cc/sec. Chad sprayed helium very close to GE water block, and I got a quick response on leak detector. The leak rate climbed from 4Xe-9 atm.cc/sec to 1.4 atm.cc/sec. We confirmed the GE is leaking now. The exact location need to be pinpointed later once the containment box is out after the module is back to SHC. The module will be moved to TCS tomorrow morning and pressurized again there. Anders will use RGA to monitor the helium response during the check.  

  1172   Friday, March 18, 2016, 11:43 chad fisherSouth Hot-CellStandard Operation  SiC#32 dissection

SiC#32 has been open for inspection.

Attachment 1: 20160318_105519_1.jpg
20160318_105519_1.jpg
Attachment 2: 20160318_105311.jpg
20160318_105311.jpg
Attachment 3: 20160318_105248.jpg
20160318_105248.jpg
Attachment 4: 20160318_105428.jpg
20160318_105428.jpg
  1178   Wednesday, March 23, 2016, 11:00 Travis CaveSouth Hot-CellStandard OperationTM2no targetmodule moved

TM#2 was moved into the south hot cell by 08:30.

  1179   Wednesday, March 23, 2016, 11:32 David WangSouth Hot-CellRepairTM2 TM2 Helium spray leak check on GE and MSP lines at SHC

  Chad and I did the helium spray leak check on TM2 GE and MSP water lines at SHC this morning. We confirmed the GE leak on water blocks. We can not found the MSP leak by using the helium spray since its leak rate in TCS is much smaller than GE leak.  The leak check process are as below:
Leak detector are calibrated before the check.
GE lines : Base leak rate 0.0 X E-9 atm.cc/sec, base pressure 0.0 XE-4 torr.
Chad sprayed 5 psi helium to GE lines soldering joints  for 5 second, no response on leak detector.
Chad sprayed 5 psi helium to GE lines water blocks( between blocks seal surface) for 5 seconds, Leak detector response to 8 XE-9 atm.cc/sec right away.
Chad sprayed  5 psi helium to GE lines soldering joints for 5 seconds again, No response on leak detector.
Chad sprayed 5 psi helium around the source tray and to vacuum duct for 5 seconds more, No response on leak detector.
MSP lines: Base leak rate 0.0X E-9 atm.cc/sec, base pressure 0.0 X E-4 torr.  Chad did same thing as he did on GE lines. no response on LD. Chad repeated the test and prolonged the spray time to 10 seconds, No response.
The conclusion: It is pretty clear we have a leak on GE line water blocks seal.  MSP lines leak could not be found by helium spray in SHC since it is a small leak.
 

  1186   Friday, April 01, 2016, 11:41 Travis CaveSouth Hot-CellStandard OperationTM1UC#15Electrical Check

Electrical check of the target on TM#1, target in question is UC#15. See PDF for details.

Attachment 1: TM1_elec_chk_UC#15_SHC.PDF
TM1_elec_chk_UC#15_SHC.PDF
  1194   Wednesday, April 06, 2016, 09:37 Travis CaveSouth Hot-CellStandard OperationTM4UC#14module moved

TM#4 with UC#14 has been moved from the east target station to the south hot cell.

  1195   Wednesday, April 06, 2016, 14:03 chad fisherSouth Hot-CellStandard OperationTM4Ta#47UCx#14 removed Ta#47 installed

UCx#14 has been removed from TM4 and Ta#47 installed. No marks on 9 pin connector on UCx#14.

  1196   Wednesday, April 06, 2016, 14:52 Travis CaveSouth Hot-CellStandard OperationTM4UC#14, No Target, Ta#47Electrical Check

Various electrical checks done on TM#4, one of post beam UC#14, of no target and with Ta#47. See PDFs for details.

Attachment 1: TM4_elec_chk_notgt_SHC.PDF
TM4_elec_chk_notgt_SHC.PDF
Attachment 2: TM4_elec_chk_Ta47_SHC.PDF
TM4_elec_chk_Ta47_SHC.PDF
Attachment 3: TM4_elec_chk_UC14_SHC_postbeam.PDF
TM4_elec_chk_UC14_SHC_postbeam.PDF
  1224   Monday, May 09, 2016, 10:13 Travis CaveSouth Hot-CellStandard OperationTM2no targetmodule moved

TM#3 was moved from the conditioning station to the NE Silo. TM#2 was moved from the SW Silo to the South hot cell.

  1225   Tuesday, May 10, 2016, 13:37 chad fisherSouth Hot-CellStandard OperationTM2Ta#48Ta#48 Installation

Ta#48 has been installed onto TM2. Also new window gaskets were installed.

High current fasteners were torqued to 130 in lbs. Shutter side of the containment box recieved new fasteners.

  1226   Tuesday, May 10, 2016, 13:54 David WangSouth Hot-CellStandard OperationTM2 SHC, TM2 leak check on window line and HS line.

Chad and I leak checked the TM2 HS and window lines after new target installation.  The window line was very easy pumped down on LD. But, The HS line only could pumped to 2-3 torr at first. Chad changed the VCR gaskets on HS line(target). It solved the problem. The LD could pumped  both of Window and HS lines to the bottom scale. Chad sprayed lots helium around the VCR joints.  No leak has been found. WE will do helium pressurizing test on them at TCS.

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