|
ID |
Date |
Author |
Category |
Type |
Module |
Target/Number |
Subject |
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999
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Thursday, July 16, 2015, 07:38 |
David Wang | ITE | Standard Operation | | | Target Hall Scheduled Activities April 07 - August 07 2015 |
Update the TH schedule according to present TM2 refurbishment process. See attachments 1,2
2015-07-20 , Update the TH schedule after some changes on TM2 and TM4 arrangement. See attachments 3,4 |
Attachment 1: Target_Hall_Scheduled_Activities__Apr_07_to_Aug_07.pdf
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Attachment 2: Target_Hall_Scheduled_Activities__Apr_07_to_Aug_07.mpp
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Attachment 3: Target_Hall_Scheduled_Activities__Apr_07_to_Aug_19.pdf
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Attachment 4: Target_Hall_Scheduled_Activities__Apr_07_to_Aug_19.mpp
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1010
|
Thursday, July 23, 2015, 10:23 |
David Wang | ITE | Standard Operation | | | Target Hall Scheduled Activities April 07 - August 019 2015 |
Update Target Hall schedule after the changing on TM2 process. See attachment 1,2 |
Attachment 1: Target_Hall_Scheduled_Activities__Apr_07_to_Aug_19.pdf
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Attachment 2: Target_Hall_Scheduled_Activities__Apr_07_to_Aug_19.mpp
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1028
|
Friday, July 31, 2015, 09:47 |
David Wang | ITE | Standard Operation | | | Target Hall Scheduled Activities April 07 - August 019 2015 |
Weekly update of Target Hall schedule after so many jobs have been finished in this week. See attachment 1, 2 |
Attachment 1: Target_Hall_Scheduled_Activities__Apr_07_to_Aug_19.pdf
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Attachment 2: Target_Hall_Scheduled_Activities__Apr_07_to_Aug_19.mpp
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1031
|
Friday, August 07, 2015, 10:01 |
David Wang | ITE | Standard Operation | | | Target Hall Scheduled Activities April 07 - August 19 2015 |
Weekly update target hall schedule and activities. See attachment 1,2
Update and extend Target Hall schedule to Sep 08. See attachment 3,4 |
Attachment 1: Target_Hall_Scheduled_Activities__Apr_07_to_Aug_19.pdf
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Attachment 2: Target_Hall_Scheduled_Activities__Apr_07_to_Aug_19.mpp
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Attachment 3: Target_Hall_Scheduled_Activities__Apr_07_to_Sep_08.mpp
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Attachment 4: Target_Hall_Scheduled_Activities__Apr_07_to_Sep_08.pdf
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2505
|
Thursday, November 23, 2023, 11:15 |
Adam Newsome | Crane | Repair | | | Target Hall Crane: CW/CCW rotation mechanism failure [tripped breaker] |
It is reported that the crane's hook rotation is not working currently. It was working yesterday (Nov 22). Investigation to follow, and this e-log will be updated.
Edit [2023-11-23]: the issue was a result of a tripped circuit breaker. Perhaps the motor became overloaded. It is advised to monitor the rotation mechanism over the new few operations, and rotate the hook CW and CCW prior to performing any critical operation to confirm it is working. |
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501
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Wednesday, October 09, 2013, 19:33 |
Grant Minor | Crane | Repair | TM4 | | Target Hall Crane not operational - likely controls / PLC hardware failure (not stuck wheel) |
Grant Minor wrote:
|
Grant Minor wrote this e-mail today:
***
Hello all,
During our planned operation of transporting TM4 from a storage silo to the Hot Cell, we had a problem with the East-West bridge drive on the Target Hall crane. The crane bridge is currently stuck in position over the silo area. We were unable to complete the transport operation. TM4 has been placed back down into the silo and the crane hook block has been disconnected from the module lifting yoke.
We have been on the phone with Norelco this afternoon and have determined the likely cause of the problem. There is a splice joint in the crane rails at this position, where a small gap exists between the rail sections. If the crane bridge is stopped during operation such that the wheel comes to rests in this gap, the crane motors have insufficient torque for the wheel to overcome the gap and ride back onto the rail. The Norelco tech Mike Smith remembers encountering this problem several years ago (before my time) but cannot remember how it was overcome. The fix likely involved moving the wheel out of the gap with pry bars.
Target Hall Survey Needed at or before 7:00 am, Wednesday Oct 9th (Lynne, Fiona, Danka, Max or Dano?)
Mike Smith and possibly a few others from Norelco will come tomorrow morning at 7:00am, and require access to the Target Hall. Since we have opened the Hot Cell in preparation for the module move, we will need a survey as early as possible to allow Mike and his crew to enter the hall without a suit and respirator.
Most of the Remote Handling group will be off-site for a Division meeting, but Travis and Maico will stay for the day to accompany the Norelco guys and help with the problem assessment.
Travis: Please take Mike to the control room when he arrives, one of the cameras is currently zoomed in on the wheel and problem rail section.
Maico: Scaffolding may be required to get access to the crane rail. Unfortunately we don't have an operational crane to transport a man-lift into the hall ;) Please see what you can do to get this ready in case we need it. Max's leak check might have to go on hold until we get this resolved. Please take responsibility for ensuring correct Fall Protection procedures are followed. This means that nobody should be walking up on the crane rail unless they are tied in with harnesses, or there is scaffolding directly under them.
I can be reached on my cell phone at 778-319-4612. The Division meeting is on UBC campus so I can return to TRIUMF fairly quickly if needed.
Thank you all for your assistance,
Grant
***
A photo of the THall camera view of the bridge wheel at the rail splice is attached, as well as Mike Smith's crane inspection report from March 2013.
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E-mail from today:
Hello Dave, Jane, Franco, Michael, Don (controls + Franco), Remy,
We have lost the East-West bridge drive control functionality of the ISAC Target Hall crane, and unfortunately this very much prevents us from operating the ISAC facility.
The problem was originally thought to be a stuck bridge wheel but this was not actually the case.
Mike Smith from Norelco was on-site for most of today working with Michael Rowe in an attempt to diagnose the problem.
Mike believes the problem to be one of the following three items:
- input PLC board on the crane bridge
- output PLC board in the interface panel in B1 level Room 5 (ISAC remote crane control room)
- communication between the two boards (festooning hardware)
We are in a pretty dire situation without the ISAC target hall crane, and we lack the expertise within the Remote Handling group in PLC hardware to diagnose this on our own. I need to ask for somebody's help from the controls group in diagnosing and repairing this problem.
I have notes from my telephone conversation with Mike Smith which I can discuss with a controls representative in the morning. There is a pretty muddled history of the design and implementation of these controls but essentially Norelco outsourced the PLCs and festooning to a third party contractor, Seattle Crane in the US, which no longer exists anymore. Neither Kone, Seattle Crane, or Norelco made appropriate as-built drawings of the wiring of the PLCs. Mike Smith at Norelco had a stack of hand-written notes about the as-built configuration he made at the time of installation in the late 1990's but these notes have not been located yet.
The PLCs appear to be Allan Bradley but the modules are from approximately 1997 and we're not sure if spare units are available.
Mike Smith says the easiest thing to do at this point is install replacement PLC modules on the crane bridge and in the control room that have confirmed functionality. If control is not restored then the problem is likely in the festooning.
Control of the crane bridge was temporarily attained by bypassing the controls (speed control / end limits, etc.) and sending drive signal directly to the drive motor controller in order to return the bridge to its home position at the access ladder. This mode of operation is not safe as the crane has no speed reduction / limits to prevent driving the bridge into the walls at max speed.
Jane / Remy / Franco: please let me know who I should correspond with on the controls side and I will talk with them tomorrow morning.
Thanks,
Grant |
|
500
|
Tuesday, October 08, 2013, 18:12 |
Grant Minor | Crane | Repair | TM4 | | Target Hall Crane Stuck in East-West Direction - Update |
Grant Minor wrote this e-mail today:
***
Hello all,
During our planned operation of transporting TM4 from a storage silo to the Hot Cell, we had a problem with the East-West bridge drive on the Target Hall crane. The crane bridge is currently stuck in position over the silo area. We were unable to complete the transport operation. TM4 has been placed back down into the silo and the crane hook block has been disconnected from the module lifting yoke.
We have been on the phone with Norelco this afternoon and have determined the likely cause of the problem. There is a splice joint in the crane rails at this position, where a small gap exists between the rail sections. If the crane bridge is stopped during operation such that the wheel comes to rests in this gap, the crane motors have insufficient torque for the wheel to overcome the gap and ride back onto the rail. The Norelco tech Mike Smith remembers encountering this problem several years ago (before my time) but cannot remember how it was overcome. The fix likely involved moving the wheel out of the gap with pry bars.
Target Hall Survey Needed at or before 7:00 am, Wednesday Oct 9th (Lynne, Fiona, Danka, Max or Dano?)
Mike Smith and possibly a few others from Norelco will come tomorrow morning at 7:00am, and require access to the Target Hall. Since we have opened the Hot Cell in preparation for the module move, we will need a survey as early as possible to allow Mike and his crew to enter the hall without a suit and respirator.
Most of the Remote Handling group will be off-site for a Division meeting, but Travis and Maico will stay for the day to accompany the Norelco guys and help with the problem assessment.
Travis: Please take Mike to the control room when he arrives, one of the cameras is currently zoomed in on the wheel and problem rail section.
Maico: Scaffolding may be required to get access to the crane rail. Unfortunately we don't have an operational crane to transport a man-lift into the hall ;) Please see what you can do to get this ready in case we need it. Max's leak check might have to go on hold until we get this resolved. Please take responsibility for ensuring correct Fall Protection procedures are followed. This means that nobody should be walking up on the crane rail unless they are tied in with harnesses, or there is scaffolding directly under them.
I can be reached on my cell phone at 778-319-4612. The Division meeting is on UBC campus so I can return to TRIUMF fairly quickly if needed.
Thank you all for your assistance,
Grant
***
A photo of the THall camera view of the bridge wheel at the rail splice is attached, as well as Mike Smith's crane inspection report from March 2013. |
Attachment 1: THall_Crane_Bridge_Wheel_at_South_Rail_Splice_8Oct2013.JPG
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Attachment 2: NORELCO_inv13045_joMS-064_31March2013.pdf
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2040
|
Friday, January 03, 2020, 13:15 |
Adam Newsome | Crane | Repair | | | Target Hall Crane PLC Module/Battery Replacement |
The Target Hall Crane bridge and trolley motion was lost after a period of the crane having power disconnected over winter holidays. This is reported in the following e-log: https://elog.triumf.ca/TIS/RH-ISAC/2039. This issue is a duplicate of what happened in 2019 at this time: https://elog.triumf.ca/TIS/RH-ISAC/1845
It was determined from troubleshooting via PLC indicator lights that the memory battery had died during the power-off time, and because of this, the program stored was lost. Note that this is an anomaly - the battery should have lasted much longer than the shutoff duration of ~2 weeks.
The SLC500 module was replaced with a spare, which contained a new battery. The old SLC500 module is still functioning but the battery has been removed (spares will be ordered) - this module is stored in a cabinet drawer in the control room. It will need to be re-programmed if re-installed as the program was lost. The original program titled TargetHallCrane.RSS was downloaded to the module. The crane was tested in local mode and determined to be functioning.
The following links are resources for resolving this issue:
https://isaccontrols.wiki.triumf.ca/index.php/ISAC_Target_Hall_Crane
https://isaccontrols.wiki.triumf.ca/index.php/SHUTDOWN_2015_Tasks#ISAC_Target_Hall_Crane_Controls_DM_-_Completed
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|
1482
|
Thursday, April 06, 2017, 15:11 |
Grant Minor | Crane | Maintenance | | | Target Hall Crane 20 ton hoist - Report by Gordon Crane 5-Apr-2017 |
-------- Forwarded Message --------
Hi Curtis
Further to the emergency service call at the Isac Target Hall on Thursday March 23rd, we advise as follows:
It was reported that the hoist was making an unusual noise and that there was a strong brake odour during operation.
The lift was completed using the auxiliary hoist.
A man-lift was arranged and Senior Service Technician Tom Kauss attended site the next morning to troubleshoot.
He determined that one of two hoist brakes (walkway side) had a strong odour and on closer examination it appeared that the
brake lining material was breaking down and particulate lining material was getting caught between the lining and the discs.
These lining fragments were rubbing and burning off during the hoist operation.
The end cover of the brake had an accumulation of brake lining fragments
The lining was not overly worn, but appears to be becoming friable, perhaps with age or exposure to radiation.
The brake was cleaned with compressed air to remove the friable material and thoroughly tested.
A test load of approximately 10 tons was lifted and the hoist handled the load without issue
The brake fragment issue did not recur while we on site and the hoist was recommissioned for use.
To guard against the likely recurrence of this condition on this critical application crane, and as both brakes have seen identical conditions in operation,
we recommend that both brake assemblies be replaced.
The brake assembly would include the brake coil, friction discs, steel brake discs and the brake springs
TRIUMF does not have a spare brake on hand, therefore one of the removed brakes could be rebuilt and kept on hand.
Two (2) each XL-60009637 Complete Brake Assemblies $ 5,706.00 Each
One (1) only XL-60009674 Brake Repair Kit $ 2,435.00
For Rebuild
One (1) only XL-52272125 Brake Spring Kit $ 59.72 For Rebuild
Installation & Testing of New Brakes estimated at: $ 1,250.00 Lot
We have one brake in stock in our Vancouver Service Depot. A second brake is available Ex-Ontario
FOB Site
Applicable Taxes Extra
Quote Valid for 30 days, subject to prior sale.
We are available next week to perform this work on site.
Please let us know if you have any questions or if you would like us to proceed.
Best Regards
Aidan
------------------
Aidan C. Gordon
General Manager
aidan@gordoncrane.com
Gordon Crane & Hoist Inc.
Celebrating 34 years of Excellence (1983-2017)
www.gordoncrane.com
Toll Free 1-866-HOIST-IT
(1-866-464-7848)
Tel: (604) 324-2441
105-8475 Ontario St
Vancouver BC V5X 3E8
Privilege and Confidentiality Notice
The information in this email is intended for the named recipients only. It may contain privileged and confidential information. If you have received this email in error, any use, copying or dissemination of its contents is prohibited. Please notify the sender immediately by telephone at the number indicated on this page to arrange destruction and/or return of the email. Your co-operation is appreciated. Thank you.
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503
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Tuesday, October 15, 2013, 16:44 |
Grant Minor | Crane | Repair | | | Target Hall Crane - operational with temporary thermal sensor bypass |
E-mail correspondence on the Target Hall crane fault diagnosis between October 11th and 15th:
On 15/10/2013 3:34 PM, Grant Minor wrote:
Hello all,
Mike Smith from Norelco arrived this morning and spent some time with Travis from RH and Mike Rowe from Controls group examining the crane controls and electrical schematics. A common understanding of the wiring and control signal scheme for the thermal sensor circuits was reached. A scanned copy of Norelco / Seattle Crane drawing E5 - 1/1 with markups by Dave Morris (Oct 11th) and Mike Smith (Oct 15th) is attached.
The group then worked on top of the crane bridge to systematically isolate the thermistor circuits in each drive motor. The thermistor readings were all normal / as-expected (about 180 Ohms for 3 in series), i.e. there was no indication of failure in any of the motor thermistors. Fall arrest equipment was used to access the motors where required.
Next, the shunt circuit in each temperature sensor module was measured (terminals T1 and T2 on each module, on drawing E5 - 1/1). The shunt in the operational module was measured at 500 kOhms. The shunt in the suspected faulty module was measured at 79 kOhms.
It was concluded that there is most likely a fault in the module with the low shunt resistance. The suspect module was left wired in bypass (shorted from terminals 14 to 11). Mike Smith advised at that point that it would be safe to operate the crane in this mode temporarily until a replacement module can be installed. I discussed this with him and Don Dale, and we agreed the risk is low, as we have not ever experienced a motor overheat scenario in the operating lifetime of the crane.
Mike Smith called me around 1pm to advise that he has located a replacement unit from their supplier in the US and I asked him to order 2 units on expedited overnight. Mike expects the components to arrive Friday this week or Monday next week latest, factoring in delays at customs and local delivery times. The units will be sent to Norelco first, then to TRIUMF locally.
Remote Handling is now continuing with Target Hall operations, using the crane as normal with the thermal module bypassed until the replacement module arrives.
Thanks to Dave Morris / Mike Lowe for their assistance in diagnosing this fault.
Here is a short summary of the Fault:
Cause of fault
- Most likely a failed thermal sensor module for one of the two pairs of bridge drive motors
Diagnosis
- Crane company (Norelco) consulted, with on-site inspections by tech Mike Smith on October 9th and October 15th
- Controls group / Mike Smith measured resistances in motor thermistors and sensors to systematically isolate fault to thermal sensor
Remedy actions taken
- Thermal sensor bypassed to temporarily restore crane function
- Risk of operating without sensor determined to be low through discussions with Norelco / Don Dale / Grant Minor
- Replacement thermal sensor + 1 spare (~ $300 ea + shipping) ordered from parts supplier through Norelco - expected delivery Monday October 21st
How could this fault have been prevented?
- Cause of failure within thermal sensor module unknown at this time
- Annual crane inspection performed by Norelco in March 2013 did not indicate any problems with this sensor (crane drive system functioned as normal)
- Suggested for future: routine inspection of sensor module shunt resistance to determine if there are any long-term signs of slow degradation
What can be done to prevent the fault in the future?
- The ISAC crane controls were designed in the late 1990's by Norelco sub-contractor Seattle Crane (now defunct)
- The crane is supposed to have two pairs of independent motors with separate thermal sensors, each capable of driving the crane if the other fails due to thermal trip
- My understanding is that the controls logic design should have been designed so that failure of one pair of motors does not prevent crane operation... it does not seem to be the case with the current design
- The design of the control logic related to these sensors could be re-evaluated and modified so that a trip from one thermal module does not prevent operation of the bridge if the other module is OK
- This is a project that will require some time and some controls and engineering resources
- In the interim, if the same failure occurs again, it may be possible to jumper the thermal sensor from the crane control room and continue operating normally - I will confirm with controls group / Norelco
- However, this is not advisable as it would be difficult in some cases to determine if the trip was due to a faulty thermal module, or an actual motor overheat scenario
- I will discuss further actions with Don Dale
Thanks and best regards,
Grant
On 11/10/2013 4:29 PM, Grant Minor wrote:
Hello all,
I spoke with the Norelco tech Mike Smith this afternoon regarding the failed thermal sensor component / circuit. He will call Kone on holiday Monday (their office is not closed for Canadian Thanksgiving) and determine if they have a replacement module.
I explained (to the best of my understanding) the diagnosis performed by Dave Morris / controls group and the test that was done to isolate the thermal sensor unit. Unfortunately, Mike Smith's drawings from Seattle crane contain notes and revisions that don't match the drawing that Dave Morris provided me (Seattle Crane dwg E5 - 1/1 revision 1 02-10-99), and he was unable to confirm in his opinion whether the bypass performed by Dave Morris has correctly isolated the problem components. In addition, he believes that the bypass he performed on Wednesday isolated portions of circuitry that are inconsistent with this thermal sensor circuit.
Mike Smith will return Tuesday morning to review the bypass and schematics. He recommended not operating the crane until he has a chance to confirm this thermal sensor issue.
From the drawings I have in hand and from discussions with Dave Morris, the failed component might be the thermistor sets inside the motor housing which are in series with the suspect module, or the module itself. My understanding is that the crane is designed with two pairs of motors for the bridge drive, and each pair is protected by one of these thermal modules (thus there are two modules total). Both modules would be the same age and both might be susceptible to the same failure mode.
As it is unclear to me the exact nature of the drive system failure, and I have a recommendation from Norelco to hold on operation of the crane, I must unfortunately state that the crane should not be used and we will have to wait until Tuesday to gather more information.
I am not so concerned about temporary loss of the thermal protection circuitry, as we have not had an overheating scenario in those motors in the lifetime of the crane (to my knowledge). I am more concerned about getting 100% confirmation that we have addressed the problem. If we attempt to use the crane and experience another failure during a lift that prevents us from placing the load down safely with the crane stuck in position over a target station, then we would be in much deeper trouble.
My apologies for this situation.
Best regards and have a good weekend,
Grant
On 11/10/2013 1:28 PM, Grant Minor wrote:
Thanks Dave,
I've contacted Norelco, Mike Smith and I are planning a path forward for further diagnosis and repair.
The crane MUST NOT be used to carry a load until it is identified whether the module or the sensors have failed, the reason for the failure, and the functionality of the thermal sensors has been restored.
Without the thermal sensor circuit we lose protection from motor overheat, an event which could have much more serious failure implications to the crane.
Cheers,
Grant
On 11/10/2013 1:04 PM, David Morris wrote:
The fault has been identified in the Target Hall Crane as a failed motor temperature module, or motor temperature sensor, on the East-West motion. The status contact in the module was bypassed allowing crane motion. There was no fault with the controls.
Dave |
Attachment 1: ISAC_THall_Crane_elec_E5_1slash1_15Oct2013.pdf
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2659
|
Wednesday, August 14, 2024, 11:29 |
Aaron Tam | Waste Package/Ship | Standard Operation | | SiC#46 | Target Disposal and visual check |
SiC#46 loaded into pail 293 successfully along with other hotcell waste
Upon visual inspection of the target, a spark-sign was spotted on the perimeter of the extraction electrode. Metallic looking material also found built up between the extraction electrode and the backing plate of the target
Photo attached |
Attachment 1: SiC46.jfif
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118
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Wednesday, June 06, 2012, 13:36 |
chad fisher | South Hot-Cell | Standard Operation | TM1 | Ta#38 | Target Change Nb#6 - Ta#38 |
Nb#6 was removed from TM1...it looked very clean.
Ta#38 was installed onto TM1...fit well.
Isaac Earle did this change with supervision in an effort to cross train.
TM1 containment box was checked for damage from the "bump" it got during yesterday's move. There was new scratches on the shutter side panel. Picture to follow.
The front containment box panel was "difficult" to remove...it required a good pull to get off.
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2295
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Wednesday, January 19, 2022, 13:36 |
David Wang | Crane | Standard Operation | | | Targe hall crane below hook attachment pins and plates annual inspection. |
Tom Kauss inspected target hall crane below hook attachment pins and plates ITA6550-01. He certified the use of these pins and plates. The inspection of these pins and plates was in Target hall crane annual check list. It was issued as a calibration index by Isaac Earle in 2022-Feb-08. After inspection, The inspection tag was issued and attached to pin. Tom has an inspection record on this job. See attachments. |
Attachment 1: 2022-01-19_174.jpg
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Attachment 2: 2022-01-19_172.jpg
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52
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Wednesday, November 16, 2011, 07:44 |
chad fisher | South Hot-Cell | Standard Operation | TM1 | TaC#1 | TaC#1 Removal and inspection |
November 15, 2011 removed TaC#1 from TM1 and inspected TM1 for any obivous signs of trouble (Problems with EE at end of run).
Upon starting removal of the high current conductor fastener on A+ (Left oven leg) it became clear right away that the oven of the target was broken as the leg moved as soon as the fasten was loosened.
Inspection of TM1 with the target removed yeilded no obvious signs of trouble, save a piece of capton tape found on the sliding tray directly below the service tray.
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2675
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Friday, September 06, 2024, 14:28 |
Aaron Tam | South Hot-Cell | Standard Operation | | Ta#68(Spare) | Ta#68(Spare) removed from TM4 and into Anteroom |
September 5, 2024 -AT
- Plastic and clean target tray added to SHC
- TM4 moved to SHC
- TM4 containment box cover removed
September 6, 2024 - AT
- Ta#68(Spare) removed from TM4 onto clean tray
- top left mounting bolt fell under source tray in containment box - unretrievable
- Ta#68(Spare) moved out of SHC via toolport door
- SHC lift table was lower than tool port tunnel by 2". Target-on-Tray slipped back onto lift table when trying to drag it up to the tool port. Target bounced out of one locating pin, but stayed within boundaries of the tray
- Water also leaked out from the VCR fitting and on to the SHC lift table, and toolport.
- Target-on-tray slid into a clean plastic bag, and then into a plastic box.
September 9, 2024 - AT
- Ta#68(Spare) taken out of plastic bag and water drained from waterlines
- Target was rotated in every direction several times until no more water poured out from the VCR joints
- Ta#68(Spare) put back in box without the bag (to promote evaporation)
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2698
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Tuesday, October 08, 2024, 11:20 |
Aaron Tam | South Hot-Cell | Standard Operation | TM2 | Ta#68 | Ta#68 install onto TM2, w/ Troubleshooting |
October 7, 2024 - Aaron Tam
Ta#68 HP-SIS checks performed at B1 lab, moved to anteroom, and inserted into SHC via tool port w/ Aaron Schmidt.
Ta#68 fixed to source tray with 4 mounting bolts in order of: Right manip. holding, Top left, Right manip. removed, Bottom right, Top right, bottom left. w/ Aaron Schmidt and Brady Borrmann
- Motion was smooth, no resistance when positioning onto pins
VCR fittings done up with ample force, leak check passed
Conductor bolts installed in order of: 2 Target electrode conductors (Checked washers), 3 target Inner and outer conductors.
All bolts checked for full contact with mirror and binos.
Electrical check failed: Dead short (look for David's ELOG for more detail when available)
Troubleshooting while David is checking resistance: w/ Ferran
- Intermittent success with heavy manipulation of water lines
- Loosening off Waterline bracket-to-source-tray
- Loosening off Bracket to water line bolts 5/32 hex's
- Rotating bracket towards operator (effectively raising waterlines in the back upwards) seems to yield more intermittent success, but never passing megger @ 250V
- Tube was inadvertently dented when handling the tube in a wrenching motion with manip tong. counterclockwise
- Target removed while David is still on the multimeter (calling for any sign of success)
- Starting to remove Target in order of: Tightening back waterline-to-bracket 5/32 hex screws, loosening off waterline bracket, loosening off VCR nuts, 2 Target electrode conductor bolts, 3 Target inner and outer conductor bolts, Fixing bolts Top left (dropped below source tray), Bottom right...
- (At this time David called with some success with electrical check)
- Reversing course to verify fault has passed, target was reassembled, only finger loose on the VCR nuts.
- Faults no longer present
- Target removed
- As target was being pulled off source tray locating pins, a piece of ceramic fell onto the source tray just behind window waterlines.
Target taken out of Hotcell by Ferran. New VCR gaskets installed. Target reinserted
Target installed no issues. Used fixing bolt used to replace dropped one.
Leak check passed, Electrical check passed
- Notably don't have a photo of reinstalled target or source tray before 2nd install attempt.
Containment cover reinstalled
Ceramic piece moved into Pail #285 (suspect this is a very hot piece)
TM2 ready for move to ITE |
Attachment 1: 1st_Install_Leak_check_passed.jfif
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Attachment 2: 1st_Install_Complete_waiting_for_electrical_check.jfif
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Attachment 3: Troubleshooting_1st_install_(dent_in_tube_visible).jfif
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Attachment 4: Water_Line_Dent_Face.jfif
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Attachment 5: Water_Line_Dent_profile.jfif
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Attachment 6: Waterline_alignment_after_removing_VCR_connection.jfif
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Attachment 7: Ceramic_piece_fell_untouched_position.jfif
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Attachment 8: Ceramic_Piece.jfif
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Attachment 9: 285_Pail_location.jfif
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Attachment 10: Closer_look_Below_Target_between_electrodes.jfif
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Attachment 11: Closer_Look_Taget_Electrode_Conductor_LEFT_(2).jfif
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Attachment 12: Closer_Look_Taget_Electrode_Conductor_LEFT.jfif
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Attachment 13: Closer_Look_Taget_Electrode_Conductor_RIGHT_(2).jfif
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Attachment 14: Closer_Look_Taget_Electrode_Conductor_RIGHT.jfif
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Attachment 15: Closer_Look_Target_Inner_and_Outer_conductors.jfif
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Attachment 16: Closer_Look_waterline_bracket_after_manipulation.jfif
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Attachment 17: TM2_Cover_Closed_completed_ready_for_move.jfif
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2728
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Tuesday, December 03, 2024, 15:53 |
Aaron Tam | South Hot-Cell | Standard Operation | TM2 | Ta#68 | Ta#68 Removal |
Note: Ta#68 had a difficult install. See E-log ID# 2698 for more info
First look:
- Containment box cover looks the same as previous (See:ID: 2697)
- Target shows large amount of soot-like deposits (See photos for locations)
- Deposits seem to have been left on parts of the service tray as well ie.: Multipin connector
Removal:
- Removal was smooth
- Water-line bracket fixing bolts seemed loose even before I put a tool to them
Eyes of sides:
- Better photos of where deposits are
- Everything else seems normal
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Attachment 1: Containment_Cover_Internal.jpg
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Attachment 2: First_Look.jpg
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Attachment 3: First_look_Water_Lines_and_bracket.jpg
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Attachment 4: First_look_Water_Lines_and_bracket.jpg
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Attachment 5: First_Look_water_line_bracket_closer.jpg
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Attachment 6: First_Look_Triplet_Conductos.jpg
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Attachment 7: Triplet_conductors_2.jpg
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Attachment 8: Multi_Pin.jpg
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Attachment 9: Top.jpg
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Attachment 10: Top_Closer.jpg
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Attachment 11: Top_Closer_(2).jpg
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Attachment 12: Right.jpg
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Attachment 13: Left.jpg
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Attachment 14: Bottom.jpg
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Attachment 15: Bottom_Closer.jpg
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Attachment 16: Extraction_electrode.jpg
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Attachment 17: Extraction_electrode2.jpg
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Attachment 18: Extraction_electrode3.jpg
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Attachment 19: Extraction_electrode4.jpg
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Attachment 20: Deposit.jpg
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Attachment 21: Deposit2.jpg
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Attachment 22: Deposit_3.jpg
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2732
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Wednesday, December 04, 2024, 14:30 |
Aaron Tam | South Hot-Cell | Standard Operation | | Ta#68 | Ta#68 PIE |
Abstract:
This target has seen some irregular beam patterns
Possibility that the beam hit the walls of the target tube or even the cooling fins
This PIE we want to investigate how the irregular beam physically affected the target
Related ELOGS:
ID: 2728
ID: 2698
PIE was performed by Aaron Tam, Directed by Aurelia Laxdal, Observed by Lucas Backes, Special help from Chad Fisher
External views:
- Windows are clear of any irregularities
- More pictures of this can be found in RH-ISAC E-log 2728
Internal Views:
- Heatshield internal
- Some discolouration from heat and soot deposits.
- This seems to be fairly clean to normal amounts - not concerning
- Target tube
- tube is bent with the middle higher than the sides
- Target tube was not removed 9/64ths allen wrench could not be located for this operation
- Target tube Exit
- Heatshield windows were punctured to reveal the target tube entraces/exits
- Entrance is waterline side (ITE)
- Extraction electrode parts were removed from the back off the target
- These parts look normal
- some of the extraction electrode would not pull out due to tight fitting parts and the investigation stopped here.
Conclusion: Target physical condition is normal as far as we could investigate |
Attachment 1: Waterline_disconnect.jpg
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Attachment 2: Heatshield_inside.jpg
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Attachment 3: Target_tube_first_look.jpg
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Attachment 4: Heatshield2.jpg
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Attachment 5: Heatshield3.jpg
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Attachment 6: Target_tube_2.jpg
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Attachment 7: Target_tube_3.jpg
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Attachment 8: Couldn't_undo_this_bolt.jpg
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Attachment 9: Exit_tube.jpg
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Attachment 10: Exit_tube2.jpg
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Attachment 11: Exit_tube3.jpg
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Attachment 12: Exit_tube4.jpg
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Attachment 13: Exit_tube5.jpg
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Attachment 14: Exit_tube6.jpg
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Attachment 15: Exit_tube7.jpg
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Attachment 16: Exit_tube8.jpg
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Attachment 17: Exit_tube9.jpg
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Attachment 18: Exit_tube10.jpg
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Attachment 19: entrance_tube.jpg
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Attachment 20: entrance_tube2.jpg
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Attachment 21: entrance_tube3.jpg
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Attachment 22: entrance_tube4.jpg
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Attachment 23: Exit_tube5.jpg
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Attachment 24: entrance_tube6.jpg
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Attachment 25: entrance_tube7.jpg
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Attachment 26: entrance_tube8.jpg
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Attachment 27: entrance_tube9.jpg
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Attachment 28: entrance_tube10.jpg
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Attachment 29: entrance_tube11.jpg
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Attachment 30: Extraction_electrode.jpg
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Attachment 31: entrance_tube1.jpg
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Attachment 32: Extraction_electrode2.jpg
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2702
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Thursday, October 10, 2024, 10:24 |
Aaron Tam | South Hot-Cell | Standard Operation | TM2 | Ta#67 | Ta#67 PIE |
Post Irradiation Examination
October 9, 2024 - Aaron Tam w/ Chad Fisher, Aurelia Laxdal, and Lucas Backes
PIE conducted by Chad with direction from Aurelia. Aaron and Lucas observing/documenting
Goal: Thin foil target material is somewhat novel, and we should characterize the differences if there are any.
Photos of the pre-examined target can be seen on ELOG 2697 on Tuesday October 1, 2024, when the target was removed from TM2
Notes:
- Right most inner/outer target conductor bolts was sitting proud and had threads showing, photo attached
- Some Black deposit was found on the inside of the heatshield directly below the extraction tube, and loose in powder form inside the heatshield.
- Target tube seems to have more of a crystalline texture than previous examinations.
- When Target tube was being removed, one of the target electrode conductors broke off
- some dimple texture was found on the target tube windows and this was further explored by prying a channel through the length of one side of the tube to get a better look
Target pieces were placed loosely back within the heatshield, and the lid loosely placed back on.
Awaiting pail loading, and move to storage vault
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Attachment 1: Black_deposit_loose_inside_heatshield_(2).jfif
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Attachment 2: Black_deposit_loose_inside_heatshield.jfif
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Attachment 3: Black_Deposit_on_heatshield_(2).jfif
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Attachment 4: Black_Deposit_on_heatshield.jfif
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Attachment 5: Closer_Look_at_Broken_off_Conductor_piece.jfif
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Attachment 6: Closer_look_Dimple_texture_on_target_tube_window_ENTRANCE_(2).jfif
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Attachment 7: Closer_look_Dimple_texture_on_target_tube_window_ENTRANCE_(4).jfif
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Attachment 8: Closer_look_Dimple_texture_on_target_tube_window_ENTRANCE.jfif
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Attachment 9: Closer_look_Dimple_texture_on_target_tube_window_EXIT_(2).jfif
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Attachment 10: Closer_look_Dimple_texture_on_target_tube_window_EXIT.jfif
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Attachment 11: Conductor_Screw_sitting_proud_(1).jfif
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Attachment 12: Conductor_Screw_sitting_proud.jfif
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Attachment 13: Copper_Colour_Pattern_(2).jfif
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Attachment 14: Copper_Colour_pattern.jfif
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Attachment 15: Crystalline_Texture_on_target_tube_(1).jfif
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Attachment 16: Crystalline_Texture_on_target_tube.jfif
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Attachment 17: Entrance_Window_inside_heatshield.jfif
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Attachment 18: Entrance_Window_outside_Heatshield.jfif
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Attachment 19: Exit_Window_inside_Heatshield.jfif
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Attachment 20: Exit_window_outside_heatshield.jfif
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Attachment 21: f8ccf123-0d03-47b8-86c9-27ae5b29c70d.jfif
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Attachment 22: f5747a26-1431-4506-8127-e30b1e829339.jfif
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Attachment 23: fbcb86a1-2d48-46a9-a64f-f5bcb01959fa.jfif
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Attachment 24: Open_Target_tube_dimple_feature.jfif
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Attachment 25: Operation_Target_Tube_removal_(2).jfif
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Attachment 26: Operation_Target_Tube_removal.jfif
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Attachment 27: Procedure_Ripping_into_target_tube_(2).jfif
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Attachment 28: Procedure_Ripping_into_target_tube_(4).jfif
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Attachment 29: Procedure_Ripping_into_target_tube_(5).jfif
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Attachment 30: Procedure_Ripping_into_target_tube_(6).jfif
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Attachment 31: Procedure_Ripping_into_target_tube.jfif
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Attachment 32: Target_Electrode_Conductor_removed.jfif
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Attachment 33: Target_Tube_Window_ENTRANCE.jfif
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Attachment 34: Target_window_ENTRANCE.jfif
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Attachment 35: Target_window_EXIT.jfif
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2523
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Friday, January 12, 2024, 11:25 |
David Wang | South Hot-Cell | Standard Operation | TM2 | Ta#66 | Ta#66 post operation electrical check at SHC |
Ta#66 post operation electrical check was done at SHC this Monday. See attachment. |
Attachment 1: TM2_Ta66_post__oeration_electrical_check.pdf
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