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Entry  Tuesday, September 10, 2019, 08:25, David Wang, Conditioning Station, Standard Operation, TM4, UCx27, Argan vent TCS. 

TCS is argon vented. TM4 is disconnected at TCS.

Entry  Wednesday, April 15, 2015, 09:01, Anders Mjos, Conditioning Station, Development, , , Archiver variables added by Controls 

 

 

 

 

 

 

 

 

 

 

The following variable have been added to the archiver (as per work request)

TCS:TS5:RDTEMP 
TCS:TCM1:EE:RDTEMP 
TCS:TCM1:COIL1:RDTEMP 
TCS:TCM1:TBHT:RDTEMP 
TCS:TCM1:TGHT:RDTEMP 
TCS:TCM1:MSP:RDTEMP 
TCS:TCM1:HVC1:RDTEMP 
TCS:TCM1:HS:RDTEMP 
TCS:FC:SCALECUR 
TCS:COL:SCALECUR 
TCS:TK2:RDLEVEL 
TCS:TK2:RDLEVEL 
TCS:DIF1:RDFLOW 
TCS:CHILL:RDHRS

The archiver was restarted.

 

 

Entry  Wednesday, August 10, 2016, 12:18, chad fisher, South Hot-Cell, Maintenance, , , Anteroom clearing 

Black "radio active" materials cabinet has been emptied, items bagged and removed from the anteroom. Cabinet itself has been swiped inside and out and also been removed from the anteroom. Most items have been removed from the anteroom now save some cardboard, rolls of plastic etc.

Entry  Friday, August 05, 2016, 13:50, chad fisher, South Hot-Cell, Maintenance, , , Anteroom clean out 

Some items have been removed from the anteroom in preparation for painting. Items have been placed on plastic in the south hot cell service area. No contamination found so far.

Entry  Monday, August 08, 2016, 11:24, chad fisher, South Hot-Cell, Maintenance, , , Anteroom Clean-up - Waveguide 

The wave guide from TM3 has been surveyed, swiped and removed from the anteroom and transported to rad waste for disposal. The wave guide has been stored in the anteroom since its removal.

Entry  Wednesday, August 24, 2016, 09:19, chad fisher, South Hot-Cell, Maintenance, , , Anteroom Clean -up paint prep 

Remaining items from anteroom have been bagged and removed (save the boot boxes, 1 garbage can and 1 coverall garbage can).

Room is ready to be surveyed so it can be deemed a non-boot box area for painting.

Entry  Wednesday, September 04, 2013, 12:21, Bevan Moss, South Hot-Cell, Repair, TM3, , Ante-room work IMG_0983.JPG

 September 3rd

David Wang and myself lowered the leak testing cart into the Ante room and prepared the ante-room for the leak testing of TM3s line. David and Grant then entered the anteroom and inspected the old c-seal and leak tested the the heat shield line. The line pumped down to the lower limits of the leak detector and there was no response from the cart. A presentation with the results of the C-seal inspection results was completed by Grant Minor and email for a design review held on the 4th.

September 4th

David Wang and myself removed the leak detector and surveyed the anteroom and cart. The following results were found with the high spec gamma detector.

Leak Detector body and cart 0 

Leak Detector wheels 200 cpm

Floor off of plastic 300 cpm (there was contamination before)

Plastic in front of HC opening 2000 cpm

Working table after plastic was removed < 50 cpm

Tool box < 50 cpm

First tacky mat 2500 cpm

Second tacky mat 200 cpm

outside of door tacky mats 0 cpm

David then laid fresh plastic on the floor around the HC opening and covered the exposed floor as well.

Following this Travis and David measured the lengths of the wiring and attempted to separate the wiring harness from the Ultem block. It was found that the block was pinned and could not be separated, a new block will need to be made. The measured the following lengths:

Steerering - 26" to 27"

Collimator - 32" - 33"

PNG - 60"

 

Entry  Thursday, October 15, 2015, 14:17, chad fisher, South Hot-Cell, Repair, TM2, , Anode Connector Install and adjustment 20151015_085914.jpg

The TM2 containment box was removed this morning for installation of the 9 pin connector...connection.

The 9 pin connector copper tube connection was made and Anders advised on routing of the cable to the banana plug water block connection.

Short was diagnosed (short disappeared when water block was pushed slightly towards center of module) and thicker Ultem spacer installed and tested again. All good.

Entry  Wednesday, June 21, 2023, 14:39, Adam Newsome, Safe Module Parking, Maintenance, , , Annual electrical and mechanical inspection of Safe Module Parking PXL_20230621_210144119.MP.jpgPXL_20230621_210546559.jpgPXL_20230621_210146892.jpg

An annual electrical and mechanical inspection was performed on the SMP today by Adam Newsome, Travis Cave, Eric Lahe, Maico Dalla Valle, Antoniette Yap, and Jason Zhang as per Work Permit I2023-06-21-4. The following items were checked:

  • Check condition of wiring for physical/radiation/UV damage
    • OK, no signs of significant damage
  • Check for cable tray debris or damage
    • There were multiple items in the cable tray which do not belong there - misc. pieces of wood and metal... these items were not disposed of but should be in the near future
  • Check inside control panel: components and wiring, labeling
    • Labeling intact, components in good condition
    • Misc. random wires pulled to check... one ground wire was loose - it was tightened
  • Verify camera views
    • This was not inspected in detail but signal status was checked, and is checked prior to remote operation
  • Check connectors for damage
    • All connectors OK
  • Check pendant for damage and verify labeling intact
    • Pendant OK
  • Lid open/close test
    • Lid was opened and close multiple times - smooth operation, no concern
    • Lid close logic was checked - OK
  • Vessel rotation and limit switch check
    • Both CW and CCW limits were checked, functioning
    • No concern on rotation - chain drive, rotary limit switch, and cable reel all functioning normally
  • Lubricate chains
    • Not done - should be done next year
  • Inspect tensioners
    • Done - OK
  • Tighten fasteners
    • Not all fasteners were checked - washers will be replaced soon so this was not deemed necessary
    • Approximately 50 washers are missing for socket head screws in slotted parts. Not safety critical but they should be replaced soon.
  • Visual inspection
    • All OK

Overall the inspection was successful.

Entry  Wednesday, May 08, 2024, 14:01, Frank Song, ITW, Maintenance, , , Annual clean up for ITW Faraday cage  

The ITW Faraday Cage has been cleaned, this is part of Winter Shut Down job happens in ISAC-1 Electric maintenance room annually.

Entry  Monday, July 04, 2022, 11:44, Nadia Jorgenson, Safe Module Parking, Standard Operation, , , Annual Inspection of Safe Module Parking - Mechanical  SMP_Missing_Washers_1.jpgSMP_Missing_Washers_2.jpgSMP_Missing_shims.jpg

 

An annual mechanical inspection was performed on the SMP today by Dan McDonald and Nadia Jorgenson. The following items were checked:

 

  • Lubricate chains
    • Not needed
  • Inspect tensioners
    • No issues found
  • Tighten fasteners
    • A few slightly loose, most are in need of washers, see attached pictures
    • Could use some shims in a few places, see attached picture
  • Inspect components during rotation - chain drive, rotary limit switch, and cable reel etc.
    • No issues
Entry  Thursday, June 30, 2022, 14:28, Nadia Jorgenson, Safe Module Parking, Standard Operation, , , Annual Inspection of Safe Module Parking - Electrical  

 

An annual electrical inspection was performed on the SMP today by Travis Cave and Nadia Jorgenson as per Work Permit I2022-06-30-2. The following items were checked:

 

Electrical Inspection of Safe Module Parking:

  • Check condition of wiring for physical/radiation/UV damage
    • OK, no signs of damage
  • Check for cable tray debris or damage
    • Some objects stored in the cable tray but nothing concerning, no damage noted
  • Check inside control panel: components and wiring, labeling
    • Labeling intact, components in good condition
    • Wiring in good condition
  • Verify camera views
    • Checked, no issues
  • Check connectors for damage
    • All connectors OK
  • Check pendant for damage and verify labeling intact
    • Pendant OK
  • Lid open/close test
    • Lid was opened and close multiple times - smooth operation, no concern
    • Lid close logic was checked - OK
  • Vessel rotation and limit switch check
    • Centre, CW and CCW limits were checked, functioning

 

Still to be done – Mechanical Inspection:

  • Lubricate chains
  • Inspect tensioners
  • Tighten fasteners
  • Inspect components during rotation - chain drive, rotary limit switch, and cable reel etc.
Entry  Friday, May 06, 2022, 10:12, Adam Newsome, Spent Target Vault, Maintenance, , , Annual Inspection of Mini-Storage Vault 

The annual inspection of the mini-storage vault was performed today. The following items were checked:

  • Cabling and cable management
  • Connectors
  • Controls box - internal wiring and components, functionality
  • Limit switches - functionality, wiring, mounting
  • Motor
  • Bearings
  • Set screws
  • Miscellaneous fasteners (some loose, but were tightened)

Everything appears to be in good working order.

Note: in the near future, the bearings should be greased. This is planned to take place during the next inspection of the main storage vault.

Entry  Thursday, May 02, 2024, 09:00, David Wang, ITW, Standard Operation, TM4, , Annual ITW water signal interlock check has been done.  

Annual ITW water signal interlock check has been done. Renee helped me on it. Everything works fine.

Entry  Wednesday, May 25, 2022, 13:23, David Wang, ITE, Standard Operation, TM4, , Annual ITE water signal interlocks. 

Annual ITE water signal interlocks check is done with Rob Shank. All ITE water signal  interlocks work fine.

Entry  Wednesday, July 07, 2021, 11:59, Adam Newsome, Safe Module Parking, Maintenance, , , Annual Electrical and Mechanical Inspection Capture.PNGPXL_20210707_162143876.jpgPXL_20210707_162918257.jpg

An annual electrical and mechanical inspection was performed on the SMP today by Adam Newsome, Dan McDonald, and Jason Zhang as per Work Permit I2021-07-07-3. The following items were checked:

  • Check condition of wiring for physical/radiation/UV damage
    • OK, no signs of significant damage
  • Check for cable tray debris or damage
    • There were multiple shards of plastic in the cable tray - they were removed and disposed of
  • Check inside control panel: components and wiring, labeling
    • Labeling intact, components in good condition
    • One COM wire for the relay array was loose - it was tightened
  • Verify camera views
    • This was not inspected but has recently been checked, and is checked prior to remote operation
  • Check connectors for damage
    • All connectors OK
  • Check pendant for damage and verify labeling intact
    • Pendant OK
  • Lid open/close test
    • Lid was opened and close multiple times - smooth operation, no concern
    • Lid close logic was checked - OK
  • Vessel rotation and limit switch check
    • Both CW and CCW limits were checked, functioning
    • No concern on rotation - chain drive, rotary limit switch, and cable reel all functioning normally
  • Lubricate chains
    • Done
  • Inspect tensioners
    • Done - OK
  • Tighten fasteners
    • Done - OK
    • Note: some concern over socket head screws in slotted parts - they should have washers. Not a critical issue but worth checking into.
  • Visual inspection
    • All OK

Overall the inspection was successful.

Entry  Thursday, August 25, 2016, 08:43, David Wang, Conditioning Station, Standard Operation, TM2, , All TM2 connections to TCS are done. 

The HV cover is installed. The Faraday cage at B2 level is locked also.The TCS and TM2 are still pumping down. Everything is good so far.

Entry  Tuesday, November 10, 2015, 10:23, Anders Mjos, Conditioning Station, Maintenance, TM3, , Air to vacuum leak on service cap TM3_Service_Cap_Leak.pdf

Conducted a more thorough leak check this morning with Edi. He found a leak on the base of the  blue F/T insulator for the multi-pin connector (see attachment). I discovered that all the bolts could rotate freely in the threads as they were too small. The bolts were replaced. The leak rate was reduced but still significant. The o-ring will likely need to be replaced.

Tuesday, November 10, 2015, 17:00: Could not find new o-ring. Cleaned groove and o-ring and applied o-ring grease. Re-attached F/T.

    Reply  Thursday, November 12, 2015, 10:18, Anders Mjos, Conditioning Station, Maintenance, TM3, , Air to vacuum leak on service cap 

Anders Mjos wrote:

Conducted a more thorough leak check this morning with Edi. He found a leak on the base of the  blue F/T insulator for the multi-pin connector (see attachment). I discovered that all the bolts could rotate freely in the threads as they were too small. The bolts were replaced. The leak rate was reduced but still significant. The o-ring will likely need to be replaced.

Tuesday, November 10, 2015, 17:00: Could not find new o-ring. Cleaned groove and o-ring and applied o-ring grease. Re-attached F/T.

Tuesday

Steerer wire had disconnected again. See DocuShare for photos.


Thursday, November 12, 2015

Leak checked the fixed F/T and the panel for steeerers. No leaks found.

Entry  Friday, October 07, 2022, 14:46, Adam Newsome, South Hot-Cell, Development, , , Addition of lift table to E-stop circuit ISAC_SHC_Lift_Schematic_updated_20221007.jpgPXL_20221007_185635660.MP.jpgPXL_20221007_185649720.jpg

A modification was made to integrate the hot cell's lift table into the E-stop circuit. See work permit I2022-10-07-1

The E-stop mounted on the right side of the small enclosure adjacent to the operator station will now serve to stop the lift table's up and down motion, as well as the turntables up/down and CW/CCW motions. Functionality was checked by B. Webster (electrical services) and A. Newsome.

 

Note: it is recommended next time there is a hot cell entry to inspect whether or not the limit switch specified in the schematic is actually installed. The schematic should be updated to match the drawing.

 

Redlined electrical drawing photo attached to this e-log, and the paper drawing is left inside the lift table's control box. The schematic will be revised based on the redline updates, likes as part of work request #6342 (to integrate this drawing into the turntable controls drawing package).

ELOG V2.9.2-2455